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Alaska Oil and Gas Conservation Commission
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HomeMy WebLinkAboutPBU FS 1 - BP Exploration (Alaska) Inc.State of Alaska AOGCC
Gas Disposition Files
Year: 2016
Facility: PBU FS 1
Operator: BP EXPLORATION (ALASKA) INC.
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PROni lf%=n cne
Form 10-422 Rev. 512009 INSTRUCTIONS ON REVERSE SIDE
yr 1--
2�/z,q //L
Submit in Duplicate
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT- FS -1
GAS FLARING INCIDENT REPORT
January 2016
Events less than or equal to
Not required for unplanned events <= 1 hr
TOTAL 0
1/9/2016
0820-1419
1,994 See attachments
TOTAL
1,994
nned Events Less Than or Equal 1 Hour AND <= 5,000 mcf
DATETIME
exceeding 5,000 MCF
VOLUME DESCRIPTION OF IN(
1/16/2016
1059-1111
129 See attachments
1/27/2016
0015-0020
138
Assist
TOTAL
267
See attachments
TOTAL 0
Not required for unplanned events <= 1 hr
See attachments
See attachments
See attachments
Page 3
2/12/2016
2:27 PM
TOTAL0
Unplanned Events < 1 Hour
Unplanned Events > 1 Hour
1,994
Planned Events < i hour and not
exceeding 5,000 MCF
267
Planned Events > 1 hour or
exceeding 5,000 MCF
0
Pilot Purge
11,465
Assist
18,105
TOTAL FLARED VOLUME
31,831
Not required for unplanned events <= 1 hr
See attachments
See attachments
See attachments
Page 3
2/12/2016
2:27 PM
1/19/2016 Flaring Event at FSI
Reply Reply All Forward
Flaring Event at FS1
AK, OPS PCC EOC TL [AKOPSPCCEOCTL@bp.com]
10 AOGCC Reporting (DOA sponsored)
Cc: Loepp, Victoria T (DOA); Benson, Gary A [Gary.Benson@bp.com]; Arthur, Gregory [Gregory.Arthur@bp.com];
AK, OPS GC3&PCC OSM [AK0PSGC3PCC0SM@BP.com]; Martin, Nelson D [Nelson. Martin@bp.com];
AK, HSSEE Env Adv East [AKHSSEEEnvAdvEast@bp.com]; AK, OPS FS1 Facility OTL [AK0PSFS1Facility0TL@bp.com];
Sunday, January 10, 2016 3:49 PM
To: AOGCC Reporting CC: Victoria Loepp, AOGCC
aoocc. reporti nolo alas ka.aov
From: Jennifer Blake, GPB Production Optimization Team Leader
A flaring event occurred at FS1 starting at 01/09/2016 08:20 and stopping at 01/09/2016 14:19 with a volume of 1994
(MSCF). The event lasted for 359 minutes and was due to a shutdown of STV -IP 1825 due to a problem associated
with the fire & gas PMs. The event stopped when the STV -IP 1825 was restarted.
Thanks,
Jennifer Blake
PCC/EOC Production Optimization Team Lead (alt David Spall)
Office (907) 659-4472
Cell (907) 830-6204
Jennifer.blake@bo.com
https:/Iwebmaila.alaska.gov/mat?ae=Item &a=Open&t=IPM.Note&id=RgAAAABKLne2zgP4SoMkepOhCxbSBwBUvQ964rjQTgYgn3632GdlAAAAhhLyAABUv... 1/1
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number2.
0290000028
Facility Name
PBU FS 1
3. Field
PBU - EOA
4. Operator
BP
5. MonthNear of Disposition
I February -2016
Disposition
Volume MCF
20. Forproduction from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name Pool Code Percent
7. Reinjected
Q
PRUDHOE 640150 100.00%
8. Flared or vented t hour or less
1,035
9. Flared or vented more than 1 hour (see instr.)
0
10. Pilot and Purge
11,370
11. Assist Gas
18,199
12. Fuel gas used in lease operations.
545,579
13. Other (see instructions)
0
Official Use Only
Authorization>i hr:
Safety
MCF
14. TOTAL VOLUME (ITEMS 6-12)
576,183
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
D
Waste:
MCF
17. Transferred from: CGF
172,874
18. Transferred to: (Express as a negative #) CGF &CCP
-75,019,209
Commissioner Date
19. Remarks:
I hereby certify that the foregoing is true and correct to the best of my knowledge.
///�} In �� Note: All volumes must be corrected
Signature al�K.r'f a Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psla and to a
temperature of 60o F. Authority 20
Printed Name Diane Colley Phone (907) 564-5775 Date / AAC25.235.
Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - FS -1
GAS FLARING INCIDENT REPORT
February 2016
2/5/2016 2053-2134 285 Not required for unplanned events <= 1 hr
TOTAL 285
Not required for unplanned events <= 1 hr
Unplanned Events greater than 1 hour
TOTAL
Unplanned Events < 1 Hour
DATE TIME VOLUME
DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
Planned Events < 1 hour and not
See attachments
See attachments
TOTAL 0
Planned Events> 1 hour or
0
Planned Events Less Than or Equal 1 Hour AND <= 5,000 mcf
DATE TIME VOLUME
DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
2/8/2016 1650-1750 612
See attachments
See attachments
2/27/2016 0717-0722 138
TOTAL 750
Planned Events Exceeding 1 Hour OR > 5,000 mcf
DATE TIME VOLUME
DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
See attachments
See attachments
TOTAL 0
Page 4
3/11/2016
3:27 PM
TOTAL
Unplanned Events < 1 Hour
285
Unplanned Events > 1 Hour
0
Planned Events < 1 hour and not
750
exceeding 5,000 MCF
Planned Events> 1 hour or
0
exceeding 5,000 MCF
Pilot Purge
11,370
Assist
18,199
TOTAL FLARED VOLUME
30,604
Page 4
3/11/2016
3:27 PM
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number2. Facility Name
0290000028 PBU FS 1
Disposition
3. Field
PBU - EOA
Volume MCF
4. Operator 5. Month/Vear of Disposition
BP March -2016
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
Pool Name Pool Code Percent
7. Reinjected
0
PRUDHOE 640150 100.00°/
8. Flared or vented 1 hour or less
12,444
9. Flared or vented more than 1 hour (see instr.)
0
10. Pilot and Purge
12,111
11. Assist Gas
21,238
12. Fuel gas used in lease operations.
647,840
13. Other (see instructions)
Official Use Only
Authorization >1 hr:
Safety
MCF
14. TOTAL VOLUME (ITEMS 6-12)
693,633
ease Use
MCF
15. NGL Gas Equivalent
p
Conservation
MCF
16. Purchased gas
Waste:
MCF
17. Transferred from: CGF
204,068
18. Transferred to: (Express as a negative #) CGF 8 CCP
-78,539,922
Commissioner Date
19. Remarks:
I hereby certify that the foregoing is true and correct to the best of my knowledge.
/ Note: All volumes must be corrected
Signature ( ���"""✓✓✓""���222"'fff��� Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
Printed Name Diane Colley Phone (907) 564-5775 Date ( / AAC25.235.
=6
Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate
3/11/2016 1419-1518
TOTAL
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - FS -1
GAS FLARING INCIDENT REPORT
March 2016
12,444 Not required for unplanned events <= 1 hr
12,444
See attachments
TOTAL 0
Planned events less than or equal to 1 hour
See attachments
TOTAL 0
See attachments
TOTAL 0
Not required for unplanned events <= 1 hr
See attachments
See attachments
See attachments
Page 3
4/14/2016
1:52 PM
TOTAL
Unplanned Events < 1 Hour
12,444
Unplanned Events> 1 Hour
0
Planned Events < 1 hour and not
0
exceeding 5,000 MCF
Planned Events > 1 hour or
0
exceeding 5,000 MCF
Pilot Purge
12,111
Assist
21,238
TOTAL FLARED VOLUME
45,793
Not required for unplanned events <= 1 hr
See attachments
See attachments
See attachments
Page 3
4/14/2016
1:52 PM
Link, Liz M (DOA)
From:
AK, OPS PCC EOC TL <AKOPSPCCEOCTL@bp.com>
Sent:
Sunday, March 13, 2016 7:46 PM
To:
AOGCC Reporting (DOA sponsored)
Cc:
Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; AK, OPS GC3&PCC OSM;
Martin, Nelson D; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL, AK, OPS FS1 OSM;
Glover, Robin; Kain, Rachel B
Subject:
Flaring Event at FS1
To: AOGCC Reporting CC: Victoria Loepp, AOGCC
aoqcc. reporting (Walaska.gov
From: David Spall, GPB Production Optimization Team Leader
A flaring event occurred at FS1 starting at 03/11/2016 14:19 and stopping at 03/11/2016 15:18 with a volume of 12444
(MSCF). The event lasted for 59 minutes and was due to High gas transit line pressure caused by CGF power failure. The
event stopped when many wells across GPB were Shut-in and choked back to reduce the transit gas line pressure.
Thanks,
David Spall
PCC/EOC Production Optimization Team Lead (Alt Jennifer Blake)
Office 907-659-4472
Cell 219-689-4036
David.spall@bp.com
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number
0290000028
2. Facility Name
PBU FS 1
3. Field
PBU - EOA
4. Operator
BP
5. MonthNear of Disposition
Aril -2016
Disposition
Volume MCF
20. Forproduction from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name Pool Code Percent
7. Reinjected
O
PRUDHOE 640150 100.00%
8. Flared or vented 1 hour or less
2,096
9. Flared or vented more than 1 hour (see instr.)
16,644
10. Pilot and Purge
16,399
11. Assist Gas
44,147
12. Fuel gas used in lease operations.
559,687
13. Other (see instructions)
ctions)
0
Use Only
Authorization >1 hr:
Safety
�t-6lft}.
MCF
&!`/
14. TOTAL VOLUME (ITEMS 6-12)
638,973
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste:
MCF
17. Transferred from: CGF
185,495
_/
18. Transferred to: (Express as a negative #) CGF &CCP
-58,755,200
Commissioner Date
19. Remarks:
I hereby certity that the foregoing is true and correct to the best of my knowledge.
n�� %jn/f�j q Note: All volumes must be corrected
Signature i / l�t1S�(/f Tin- Manager Production Taxes and Ro alties Alaska t0 pressure Of 14.65 psie and to a
tl temperature of 60o F. Authority 20
Printed Name Diane Colley Phone (907) 564-5775 Date AAC25.235.
In
Form 10-422 Rev. 512009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT- FS -1
GAS FLARING INCIDENT REPORT
April 2016
jUnplanned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
4/24/2016 0635-0705 2,048 Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr
TOTAL 2,048
4/25/2016
4/25/2016
4/26/2016
TIME
0100-0500
1810-1930
1030-2359
TOTAL
7E DESCRIPTION OF IN
4,044 See attachments
8,667
16,644
ACTION TAKEN TO E
See attachments
4/16/2016 1058-1104 8 See attachments See attachments
4/23/2016 0043-0049 40
TOTAL 48
Planned events greater than 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
See attachments See attachments
TOTAL
Unplanned Events < 1 Hour
Unplanned Events > 1 Hour
Planned Events < 1 hour and not
exceeding 5,000 MCF
Planned Events > 1 hour or
exceeding 5,000 MCF
Pilot Purge
Assist
TOTAL FLARED VOLUME
7
TOTAL
2,048
16,644
48
0
16,399
44,147
79,286
Page 6
5/16/2016
3:44 PM
Link, Liz M (DOA)
From: AK, OPS PCC EOC TL <AKOPSPCCEOCTL@bp.com>
Sent: Tuesday, April 26, 2016 6:24 AM
To: AOGCC Reporting (DOA sponsored)
Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; AK, OPS GC3&PCC OSM;
Martin, Nelson D; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FSI OSM;
Glover, Robin; Kain, Rachel B; Wieliczkiewicz, Ed J; Croghan, Shawn K; Digert, Scott A
Subject: Flaring Event at FS1
To: AOGCC Reporting CC: Victoria Loepp, AOGCC
aoaca. reporti ng(a(<7a laska. gov
From: Jennifer Blake, GPB Production Optimization Team Leader
A flaring event occurred at FSI starting at 04/25/2016 01:00 and stopping at 04/25/2016 05:00 with a volume of 111
(MSCF). The event lasted for 240 minutes. The event had a volume greater than 5000 (MSCF) and was due to FS1 Old
and Annex systems shutdown because of a problem associated with slope wide power outage. The event stopped when
FS1 was shutdown.
A flaring event occurred at FS1 starting at 04/25/2016 18:10 and stopping at 04/25/2016 19:30 with a volume of 8667
(MSCF). The event lasted for 80 minutes. The event had a volume greater than 5000 (MSCF) and was due to T\C 1804
unloading unknown reason. The event stopped when 1804 T/C was reloaded.
A flaring event occurred at FS1 starting at 04/26/2016 10:30 and stopping at 04/26/2016 23:59 with a volume of 3933
(MSCF). The event lasted for 809 minutes and was due to Flaring off STV/IP gas, TC8125 SO due to CPS power supply
issues. The event will be ongoing with the CPS Power issues.
Thanks,
Jennifer Blake
PCC/EOC Production Optimization Team Lead (alt David Spall)
Office (907) 659-4472
Cell (907) 830-6204
Jennifer.blake@bp.com
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number
0290000028
2. Facility Name
PBU FS 1
3. Field
PBU - EOA
4. Operator
BP
5. MonthNear of Disposition
I May -2016
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name Pool Code Percent
7. Reinjected
O
PRUDHOE 640150 100.00%
8. Flared or vented t hour or less
1,370
9. Flared or vented more than 1 hour (see instr.)
326
10. Pilot and Purge
16,853
11. Assist Gas
35,117
12. Fuel gas used in lease operations.
445,173
13. Other (see instructions)
0
Official Use Only�
Authorization >t he
Safety
Z /
10
MCF
14. TOTAL VOLUME (ITEMS 6-12)
498,839
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste:
MCF
17. Transferred from: CGF
188,661
n
-+~--
Commissioner Date
18. Transferred to: (Express as a negative #) CGF 8 CCP
-70,829,904
19. Remarks:
I hereby certify that th foregoing is true and correct to the best of my knowledge.
vA Note: All volumes must be corrected
SignatureyV Title Manager Production Taxes and Ro aloes Alaska to pressure of 14.65 psi8 and to a
/ temperature of 60o F. Authority 20
Printed Name Diane Colley Phone (907) 564-5775 Date441 AAC25.235.
V71-
Form
TL
Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT- FS -1
GAS FLARING INCIDENT REPORT
May 2016
Unplanned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE - ACTION TAKEN TO ELIMINATE CAUSE
5/5/2016 0253-0300 1,370 Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr
TOTAL 1,370
See attachments
See attachments
TOTAL
0
Planned events less than or equal to 1 hour
DATE TIME
VOLUME
DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
See attachments
See attachments
TOTAL
0
Planned events greater than 1 hour
DATE TIME
VOLUME
DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
5/31/2016 0124-0500
326
See attachments
See attachments
TOTAL
326
TOTAL
Unplanned Events < 1 Hour
1,370
Unplanned Events> 1 Hour
0
Planned Events < 1 hour and not
0
exceeding 5,000 MCF
Planned Events > 1 hour or
326
exceeding 5,000 MCF
Pilot Purge
16,853
Assist
35,117
TOTAL FLARED VOLUME
53,666
Page 4
6/15/2016
2:44 PM
Link, Liz M (DOA)
From: AK, OPS PCC EOC TL <AKOPSPCCEOCTL@bp.com>
Sent: Friday, June 10, 2016 1:06 PM
To: AOGCC Reporting (DOA sponsored)
Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; AK, OPS GC3&PCC OSM;
Martin, Nelson D; AK, HSSEE Env Adv East; AK, OPS FSI Facility OTL; AK, OPS FS1 OSM;
Glover, Robin; Buckbee, Rachel A
Subject: Flaring Event at FS1
To: AOGCC Reporting CC: Victoria Loepp, AOGCC
aogcc.reporting cDalaska.gov
From: Jennifer Blake, GPB Production Optimization Team Leader
A flaring event occurred at FS1 starting at 05/31/2016 01:24 and stopping at 05/31/2016 05:00 with a volume of 326
(MSCF). The event lasted for 216 minutes and was due to depressurizing the HP separator for maintenance. The event
stopped when depressurization was completed.
A flaring event occurred at FS1 starting at 06/05/2016 00:45 and stopping at 06/05/2016 04:00 with a volume of 1500
(MSCF). The event lasted for 195 minutes and was due to the 1804 turbine spin cool for a planned water wash. The event
stopped when the spin cool was completed.
A flaring event occurred at FS1 starting at 06/10/2016 10:30 and stopping at 06/10/2016 12:00 with a volume of 107
(MSCF). The event lasted for 90 minutes and was due to Drill Site 5 depressurizing to the plant flare system for drill site
work. The event stopped when the DS5 depressurization was completed.
Thanks,
Jennifer Blake
PCC/EOC Production Optimization Team Lead (alt David Spall)
Office (907) 659-4472
Cell(907)830-6204
Jennifer.blake@bp.com
Flare StartDate 05/01/2016
Flare End Date 05/31/2016
FSI Flare Report Total Volume (MSCF) 1696
Report
Numbs System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
16-178 Flare Relief 05/31/2016 1:24:00 am 5:00:00 am 215 min No
Determination Cause Depressure HP Separator for maintenanoe
Action Taken Completed depressudng.
No Yes BP1\HOGUERC 326
Daily Volume (MSCF) 326
Total Volume (MSCF) 1696
Generated 06/07/2016 4:33:28PM Page 4 of 9
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number 2. Facility Name
0290000028 PBU FS 1
Disposition
3. Field
PBU - EOA
Volume MCF
4. Operator 5. MonthNear of Disposition
BP June -2016
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name Pool Code Percent
7. Reinjected
0
PRUDHOE 640150 100.00%
8. Flared or vented 1 hour or less
735
9. Flared or vented more than 1 hour (see instr.)
1,607
10. Pilot and Purge
16,197
11. Assist Gas
25,423
12. Fuel gas used in lease operations.
562,714
13. Other (see instructions)
Official Use Only
Authorization >1 hr:
Safety
L/ O
MCF
C�'/ 3 l
14. TOTAL VOLUME (ITEMS 6-12)
606,676
Lease Use
MCF
15, NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste
MCF
17. Transferred from: CGF
165,473
Commissioner Date
18. Transferred to: (Express as a negative #) CGF & CCP-
58,591,526
19, Remarks:
I hereby certify (hat the foregoing is true and correct to the best of my knowledge.
Note: All volumes must be corrected
SignatL Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psia and to a
Primed Name Diane Colle / temperature of 60o F. Authority 20
Y Phone (907) 564-5775 Date b AAC25.235.
Form 10-422 Rev. 512009 INSTRUCTIONS ON REVERSE SIDE
Submit in Duplicate
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - FS -1
GAS FLARING INCIDENT REPORT
June 2016
jUnplanned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr
TOTAL 0
See attachments
See attachments
TOTAL
0
Planned events less than or equal to 1 hour
1030-1200
DATE TIME VOLUME
DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
6/2/2016 1153-1243
381 See attachments See attachments
6/6/2016 1600-1700
59
6/25/2016 1050-1121
295
TOTAL
735
6/5/2016
0045-0400
6/10/2016
1030-1200
TOTAL
Unplanned Events < 1 Hour
Unplanned Events> 1 Hour
Planned Events < 1 hour and not
exceeding 5,000 MCF
Planned Events > 1 hour or
exceeding 5,000 MCF
Pilot Purge
Assist
TOTAL FLARED VOLUME
1,500 See attachments
107
1,607
TOTAL
0
0
735
1,607
16,197
25,423
43,962
See attachments
Page 4
7/18/2016
341 PM
Flare Start Date 06/01/2016
Flare End Date 06/30/2016
FSI Flare Report Total Volume (MSCF) 2342
Report
Numbs System
Date StartTime Stop Time Duration
Intermittent Black Smoke
Planned Reported By
Volume
16-179 Flare Relief 06/02/2016 11:53:00 am 12:43:00 pm 50 min
No No
Yes BPi\LYLEPE
381
Determination Cause
Depressure C HP Separator, Scrubber and Liquid Pot for maintenance.
Action Taken
Completed depressunng.
Daily Volume (MSCF)
381
16-184 Flare Relief 06/05/2016 12:45:00 am 40000 am 195 min
No No
Yes BP1\LYLEPE
1500
Determination Cause
1804 Spin Cool for water wash.
Action Taken
Completed spin cool.
Daily Volume (MSCF)
1500
16-186 Flare Relief 06/06/2016 4:00:00 pm 5:00:00 pm 60 min
No No
Yes BP1\WATKINT
59
Determination Cause
T/C 1804 and associated piping depressured forwaterwash and various train work.
Action Taken
Completed depressurization of 1804 compressor train.
Daily Volume (MSCF)
59
16-193 Flare Relief 06/10/2016 10:30:00 am 12:00:00 pm 90 min
No No
Yes BPlWCCADJ
107
Determination Cause
DS5 De pressured to plant flare system for drill site work.
Action Taken
DS5 de pressured to flare header pressure.
Daily Volume (MSCF)
107
16-219 Flare Relief 06/25/2016 10:50:00 am 11:21:00 am 31 min
No No
Yes BP1\LYLEPE
295
Determination Cause
Flare down DS1 for Drill site shut in work.
Action Taken
Depressured,
Daily Volume (MSCF)
295
Total Volume (MSCF)
2342
Generated 07/06/2016 1:44:03PM Page 5 of 11
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number
0290000028
2. Facility Name
PBU FS 1
3. Field
PBU - EOA
4. Operator
BP
5. MonthNear of Disposition
I July -2016
Disposition
Volume MCF
20. Forproduction from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name PoolCode Percent
7. Reinjected
0
PRUDHOE 640150 100.00%
B. Flared or vented 1 hour or less
0
9. Flared or vented more than 1 hour (see instr.)
0
10. Pilot and Purge
16,315
11. Assist Gas
30,312
12. Fuel gas used in lease operations.
587,974
13. Other (see instructions)
U
Official Use Only
Authorization >1 hr:
Safety
MCF
14. TOTAL VOLUME (ITEMS 5-12)
634,601
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste:
MCF
17. Transferred from: CGF
157,899
18. Transferred to: (Express as a negative #) CGF &CCP
-6$,595,854
Commissioner Date
19. Remarks:
I hereby certify that the foregoing is true and correct to the best of my knowledge.
/�/j/�/) Note: All volumes must be corrected
Signature�0 l ,(�'/1/�, Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psia and to a
/ temperature of 60o F. Authority 20
Printed Name Diane ColleyPhone (907) 564-5775 Date 6 AAC25.235.
Form 10-422 Rev. 512009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate
events
or equal to
TOTAL 0
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT- FS -1
GAS FLARING INCIDENT REPORT
July 2016
Not required for unplanned events <= 1 hr
Not required for unplanned events <= 1 hr
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
See attachments See attachments
TOTAL 0
Planned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
See attachments See attachments
TOTAL 0
TOTAL
Unplanned Events < 1 Hour
Unplanned Events > 1 Hour
Planned Events < 1 hour and not
exceeding 5,000 WE
Planned Events > 1 hour or
exceeding 5,000 MCF
Pilot Purge
Assist
TOTAL FLARED VOLUME
See attachments
0
TOTAL
0
0
0
0
16,315
30,312
46,627
See attachments
Page 3
8/11/2016
9:46 AM
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number
0290000028
2. Facility Name
PBU FS 1
3. Field
PBU - EOA
4. Operator
BP
5. Month/Year of Disposition
I August -2016
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name Pool Code Percent
7. Reinjected
O
PRUDHOE 640150 100.00%
8. Flared or vented 1 hour or less
0
9. Flared or vented more than 1 hour (see instr.)
1 728
--
10. Pilot and Purge
18,474
11. Assist Gas
30,654
12. Fuel gas used in lease operations.
582,068
13. Other (see instructions)
0
Official Use Only
Authotlzation>1 hr:
Safety
MCF
l
14. TOTAL VOLUME (ITEMS 6-12)
632,924
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
UMCF
Waste:
17. Transferred from: CGF
139,617
(
18. Transferred to: (Express as a negative #) CGF &CCP
-75,208,866
Commissioner Date
19. Remarks:
foregoing is true and correct to the best of my knowledge.
I hereby certify th5,w� C&ANote: All volumes must be corrected
Signature Title Manager Production Taxes and R alties Alaska to pressure of 14.65 psia and to a
Punted Name Diane Colleytemperature of 60o F. Authority 20 Phone (907) 564-5775 Date AAC25.235.
Form 10-422 Rev. 512009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate
events less than or equal
TOTAL
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT- FS -1
GAS FLARING INCIDENT REPORT
August 2016
Not required for unplanned events <= 1 hr
0
Not required for unplanned events <= 1 hr
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
8/26/2016 0030-0930 850 See attachments See attachments
8/26/2016 0930-2000 878
TOTAL 1,728
Planned events less than Or equal to 1 hour
See attachments See attachments
TOTAL 0
Planned events greater than 1 hour
TOTAL
See attachments
0
ACTION TAKEN TO I
See attachments
Page 3
9/12/2016
9:44 AM
TOTAL
Unplanned Events < 1 Hour
0
Unplanned Events> 1 Hour
1,728
Planned Events < 1 hour and not
0
exceeding 5,000 MCF
Planned Events> 1 hour or
0
exceeding 5,000 MCF
Pilot Purge
18,474
Assist
30,654
TOTAL FLARED VOLUME
50,856
ACTION TAKEN TO I
See attachments
Page 3
9/12/2016
9:44 AM
Flare StartDate 08/01/2016
Flare End Date 08/31/2016
FSI Flare Report Total Volume (MSCF) 1728
Report
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
16-275 Flare Relief 08/26/2016 12:30:00 am 9:30:00 am 540 min No
Determination Cause Depressurizing EOA artificial lift distribution system for repairs.
Action Taken Completed blowdown.
16-275 Flare Relief 08/26/2016 9:30:00 am 8:00:00 pm 630 min No
Determination Cause Depressurizing common lines 12-C and 12-B for DS12 shut down.
Action Taken Completed blowalmn.
Generated 09/01/2016 3:47:14PM
No No BP1\CALHOUJ 850
No No BP1NCALHOUJ 878
Daily Volume (MSCF) 1728
Total Volume (MSCF) 1728
Page 3 of 9
Link, Liz M (DOA)
From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com>
Sent: Monday, August 29, 2016 12:10 PM
To: AOGCC Reporting (DOA sponsored)
Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; Schinagl, Werner; Fortenberry,
Christopher; AK, HSSEE Env Adv East, AK, OPS FSI Facility OTL, AK, OPS FS1 CSM;
Glover, Robin; Buckbee, Rachel A
Subject: Flaring Event at FS1
To: AOGCC Reporting CC: Victoria Loepp, AOGCC
aogcc. reporting(@alaska.gov
From: Jennifer Blake, GPB Production Team Leader
A flaring event occurred at FS1 starting at 08/26/2016 00:30 and stopping at 08/26/2016 20:00 with a volume of 1728
(MSCF). The event lasted for 1170 minutes and was due to FS1 assisting the EOA Artificial Lift (AIL) line depressurizing.
The event stopped when depressurization was completed.
Thanks,
Jennifer Blake
EOC Production Optimization Team Lead
Office (907) 564-5926
Cell (907) 830-6204
Jennifer.blake@bosom
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number
0290000028
2. Facility Name
IPBU FS 1
3. Field
PBU - ECA
4. Operator
BP
5. Monthlyear of Disposition
I September -2016
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6, Sold
0
Pool Name Pool Code Percent
7. Reinjected
O
PRUDHOE 640150 100.00%
8. Flared or vented 1 hour or less
275
9. Flared or vented more than 1 hour (see instr.)
0
10. Pilot and Purge
19,474
11, Assist Gas
36,017
12. Fuel gas used in lease operations.
574,442
13. Other (see instructions)
0Official
Use Only
Authorization >7 h[
Safety
MCF
14. TOTAL VOLUME (ITEMS 6-12)
630,208
Lease Use
MCF
15, NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste:
MCF
17. Transferred from: CGF
140,164
Commissioner Date
18. Transferred to: (Express as a negative #) CGF &CCP
-71,357,137
19, Remarks:
I hereby certify that the foregoing is true and correct to the best of my knowledge.
Note: All volumes must be corrected
Signature Tin. Title Mana er Production Taxes and Ro allies Alaska to pressure of 14.65 psis and to a
temperature of 60o F. Authority 20
ColI
Printed Name Diane ley Phone (907) 564-5775 Date t AAC25.235.
_J16
Form 10-422 Rev. 512009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT- FS -1
GAS FLARING INCIDENT REPORT
September 2016
events less than or equal to 1
TIME V
Not required for unplanned events <= 1 hr
TOTAL 0
Not required for unplanned events <= 1 hr
VUWNIE DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
See attachments See attachments
TOTAL 0
Planned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
9/16/2016 2059-2130 275 See attachments See attachments
TOTAL 275
Planned events greater than 1 hour
TOTAL
Unplanned Events < 1 Hour
Unplanned Events> 1 Hour
Planned Events < 1 hour and not
exceeding 5,000 MCF
Planned Events > 1 hour or
exceeding 5,000 MCF
Pilot Purge
Assist
TOTAL FLARED VOLUME
See attachments
0
TOTAL
0
0
275
0
19,474
36,017
55,766
See attachments
Page 3
10/14/2016
1:31 PM
Flare Start Date 09/01/2016
Flare End Date 09/30/2016
FS1 Flare Report
Total Volume (MSCF) 275
Report
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
16-305 Controlled Blowdown 09/16/2016 859:00 pm 9:30:00 pm 31 min No No Yes BP1\MOOREM 275
Determination Cause De pressured C train HP Separator for piping replacement downstream of L-14 control valve.
Action Taken Completed de pressure of C HP Separator
Daily Volume (MSCF) 275
Total Volume (MSCF) 275
Generated 10/04/2016 2.32.30PM Page 2 of 10
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number
0290000028
2. Facility Name
IPBU FS 1
3. Field
PBU - EOA
4. Operator
BP
5. MonthNear of Disposition
I October -2016
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent o/
Total Volume.
6. Sold
O
Pool Name Pool Code Percent
7. Reinjected
0
PRUDHOE 640150 100.00%
B. Flared or vented 1 hour or less
916
9. Flared or vented more than 1 hour (see instr.)
2,932
10. Pilot and Purge
22,364
11. Assist Gas
56,581
12. Fuel gas used in lease operations.
604,251
13. Other (see instructions)
0
Official Use Only
Authorization>1 hr:
Safety
Z f3Z
MCF
14. TOTAL VOLUME (ITEMS 6-12)
687,044
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0MCF
Waste :
17. Transferred from: CGF
157,617
0
Z -bra
18. Transferred to: (Express as a negative #) CGF & CCP
-75,020,620
Commissioner Date
19. Remarks:
I hereby certify that the foregoing is true and correct to the best of my knowledge.
Note: All volumes must be corrected
Signature Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
Printed Name Diane Colley Phone (907) 564-5775 Date /)�14 AAC25.235.
V T-1--
2- )
-1--
2-/ /G /k7
Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate
h7aV 4
TOTAL 0
Unplanned events greater than 1 hour
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT- FS -1
GAS FLARING INCIDENT REPORT
October 2016
DESCRIPTION OF INCIDENT & CAUSE
Not required for unplanned events <= 1 hr
Not required for unplanned events <= 1 hr
VAIL
TIME VOLUME
DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
10/8/2016 0130-0445
1,727
See attachments
See attachments
TOTAL 0
Unplanned Events < 1 Hour
0
Unplanned Events > 1 Hour
0
Planned Events < 1 hour and not
Planned events less than or equal to 1 hour
exceeding 5,000 MCF
DATE
TIME VOLUME
DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
10/7/2016
1630-1730 458
See attachments
See attachments
10/8/2016
1630-1730 458
TOTAL 916
VAIL TIME
VOLUME DESCRIPTION OF INi
10/7/2016 0000-0300
1,205 See attachments
10/8/2016 0130-0445
1,727
TOTAL
2,932
TOTAL
Unplanned Events < 1 Hour
0
Unplanned Events > 1 Hour
0
Planned Events < 1 hour and not
916
exceeding 5,000 MCF
Planned Events> 1 hour or
2,932
exceeding 5,000 MCF
Pilot Purge
22,364
Assist
56,581
TOTAL FLARED VOLUME
82,793
See attachments
Page 5
11/16/2016
5:13 PM
Flare Start Date 10/01/2016
Flare End Date 10/31/2016
FS1 Flare Report
Total Volume (MSCF)
3848
Report
Numbs System Date StartTime Stop Time
Duration Intermittent
Black Smoke
Planned Reported By
Volume
16-344 Controlletl Blowdown 10/07/2016 120000 am 3:00:00 am
180 min No
No
Yes BP1\MOOREM
1205
Determination Cause Spin cooling 1803T/C for water wash.
Action Taken Completed spin cooling.
16-344 Controlled Slowdown 10/07/2016 4:30:00 pm 5:30:00 pm
60 min No
No
Yes BPIXMCCADJ
458
Determination Cause Mater wash spin cycle
Action Taken Stop water wash spin cycle
Daily Volume (MSCF)
1663
16-346 Controlled Blowdown 10/08/2016 1:30:00 am 4:45:00 am
195 min No
No
Yes BPIIMOOREM
1727
Determination Cause Spin cooling 1804T/C for water wash.
Action Taken Completed spin cooling.
16-346 Controlled Blowdown 10/08/2016 4:30:00 pm 5:30:00 pm
60 min No
No
Yes BPI IMCCADJ
458
Determination Cause Water wash spin cycle
Action Taken Stop water wash spin cycle
Dally Volume (MSCF)
2165
Total Volume (MSCF)
3848
Generated 11/02/2016 4:05:39PM Page 6 of 12
Link_ Liz M (DOA) nC ` ] 7'
From:
AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com>
Sent:
Monday, October 10, 2016 4:01 PM
To:
AOGCC Reporting (DOA sponsored)
Cc:
Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; Schinagl, Werner; Fortenberry,
Christopher; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM;
Glover, Robin; Buckbee, Rachel A
Subject:
Flaring Event at FS1
To: AOGCC Reporting CC: Victoria Loepp, AOGCC
aogcc. reporting(c)alaska.gov
From: Jennifer Blake, GPB Production Team Leader
A flaring event occurred at FSI starting at 10/07/2016 00:00 and stopping at 10/07/2016 03:00 with a volume of 1205
(MSCF). The event lasted for 180 minutes and was due to spin cooling Turbine Compressor 1803 for water wash. The
event stopped when spin cooling was completed.
A flaring event occurred at FS1 starting at 10/08/2016 01:30 and stopping at 10/08/2016 04:45 with a volume of 1727
(MSCF). The event lasted for 195 minutes and was due to spin cooling Turbine Compressor 1804 for water wash. The
event stopped when spin cooling was completed.
Thanks,
Jennifer Blake
EOC Production Optimization Team Lead
Office (907) 564-5926
Cell (907) 830-6204
Jennifer.blake@bp.com
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DIRPORITinN
1. Facility Number
0290000028
2. Facility Name
PBU FS 1
3. Field
PBU - EOA
4. Operator .. •
BP
5. Month/Year of Disposition
November -2016
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
total Volume.
6. Sold
0
Pool Name Pool Code Percent
7. Reinjected
0
PRUDHOE 640150 100.00%
8. Flared or vented 1 hour or less
375
9. Flared or vented more than 1 hour (see instr.)
990
10. Pilot and Purge
19,635
11. Assist Gas
52,029
12. Fuel gas used in lease operations.
606,897
13. Other (see instructions)
0
Official Use Only
Authorization>1 hr
Safety
//
MCF-`
14. TOTAL VOLUME (ITEMS 6-12)
679,926
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste:
MCF
17. Transferred from: CGF
167,206
3-/7-/
Commissioner Date
18. Transferred to: (Express as a negative #) CGF & CCP
-72 790 620
19. Remarks:
I hereby certify that the foregoing is true and correct to the best of my knowledge.
Signature O/M �/J/t Note: All volumes must be corrected
r vt, Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
Printed Name Diane Colley Phone (907) 564-5775 Date 1,96114 AAC25.235.
a
Form 10-422 Rev. 512009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate
events less than or equal to
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - FS -1
GAS FLARING INCIDENT REPORT
November 2016
DESCRIPTION OF INCIDENT & CAUSE
Not required for unplanned events <= 1 hr
Not required for unplanned events <= 1 hr
TOTAL
0
Unplanned events greater than 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
11/4/2016 1100-1300
990 See attachments
See attachments
TOTAL
990
Planned events less than or equal to 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
11/10/2016 1500-1600
375 See attachments
See attachments
TOTAL
375
Planned events greater than 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
See attachments
See attachments
TOTAL
0
TOTAL
Unplanned Events < 1 Hour
0
Unplanned Events > 1 Hour
990
Planned Events < 1 hour and not
375
exceeding 5,000 MCF
Planned Events > 1 hour or
0
exceeding 5,000 MCF
Pilot Purge
19,635
Assist
52,029
TOTAL FLARED VOLUME
73,029
Page 4
12/15/2016
12:31 PM
Flare Start Date 11/01/2016
Flare End Date 1113012016
FS1 Flare Report Total Volume (MSCF) 1365
Report
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
16-397 Flare Relief 11!04/2016 11:00:00 am 2:00:00 pm 160 min No
Determination Cause 1825 compressor shut down due to work on FSl transformer.
Action Taken Re set tripped breakers and used normal start up procedure.
16-411 Other 11/10/2016 3:00:00 pm 4:00:00 pm 60 min No
Determination Cause T\C 1625 shutdown for planned maintenance
Action Taken Loaded STV/IP TIC.
Generated 12/15/2016 2:11:57PM
No No BP1 WCCADJ 990
Daily Volume (MSCF) 990
No Yes BPI\HUNTL2 375
Daily Volume (MSCF) 375
Total Volume (MSCF) 1365
Page 4 of 12
Link, Liz M (DOA)
From: AKOpsProcIEOCTL <AKOPSPCCEOCTL@bp.com>
Sent: Tuesday, November 15, 2016 12:42 PM
To: AOGCC Reporting (DOA sponsored)
Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; Schinagl, Werner; Fortenberry,
Christopher; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM;
Glover, Robin; Buckbee, Rachel A
Subject: Flaring Event at FS1
To: AOGCC Reporting CC: Victoria Loepp, AOGCC
aogcc.reoorting(oDa I aska.gov
From: Jennifer Blake, GPB Production Team Leader
A flaring event occurred at FS1 starting at 11/04/2016 11:00 and stopping at 11/04/2016 14:00 with a volume of 990
(MSCF). The event lasted for 180 minutes and was due to shutting down the1825 compressor to do work on the FS1
transformer. The event stopped when the tripped breakers were reset and the compressor was restarted.
Thanks,
Jennifer Blake
EOC Production Optimization Team Lead
Office (907) 564-5926
Cell (907) 830-6204
Jennifer.blake@bp.com
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DiSPOSiTinN
1. Facility Number
0290000028
2. Facility Name
PBU FS 1
3. Field
PBU - EOA
4. Operator ... •5.
BP
MonthNear of Disposition
I December -2016
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
fi. Sold
Pool Name Pool Code Percent
7. Reinjected
0
PRUDHOE 640150 100.00%
8. Flared or vented 1 hour or less
5,754
9. Flared or vented more than 1 hour (see instr.)
4,062
10. Pilot and Purge
19,607
11. Assist Gas
55,498
12. Fuel gas used in lease operations.
655,177
13. Other (see instructions)
0
Official Use Only
Authorization>t hr:
Safety
MCF
T�
14. TOTAL VOLUME (ITEMS 6-12)
740,098
Lease Use
M
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste:
MCF
17. Transferred from: CGF
186,255
18. Transferred to: (Express as a negative #) CGF & CCP
-74 773 618
Commissioner Date
19, Remarks:
I hereby certify that the foregoing is true and correct to the best of my knowledge.
J�n�� Note: All volumes must be corrected
Signature Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psis and to a
/ j temperature of 60o F. Authority 20
Printed Name Diane Colley Phone (907) 564-5775 Date / AAC25.235.
Form 10-422 Rev. 512009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate
BP EXPLORATION (ALASKA( INC.
PRUDHOE BAY UNIT- FS -1
GAS FLARING INCIDENT REPORT
December 2016
Unplanned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
12/26/2016 2300-2400 5,208 Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr
12/27/2016 0001-0015 486
TOTAL 5,694
Unplanned events Rreater than 1 hour
TOTAL
finned events less than or equal to
DATE TIME
12/5/2016 0430-0515
TOTAL
Inned events greater than 1 hour
DATE TIME
utbLKIPTION OF INCIDENT
See attachments
M
60 See attachments
60
12/18/2016 0500-0350 4,062 See attachments
TOTAL 4,062
Unplanned Events < 1 Hour
Unplanned Events > 1 Hour
Planned Events < 1 hour and not
exceeding 5,000 MCF
Planned Events > 1 hour or
exceeding 5,000 MCF
Pilot Purge
Assist
TOTAL FLARED VOLUME
TOTAL
5,694
0
60
4,062
19,607
55,498
84,921
See attachments
See attachments
See attachments
Page 4
1/1212017
2 11 PM
Link, Liz M (DOA)
From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com>
Sent: Wednesday, January 04, 2017 11:59 AM
To: AOGCC Reporting (DOA sponsored)
Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory, Schinagl, Werner; Fortenberry,
Christopher, AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FSI OSM;
Glover, Robin; Buckbee, Rachel A
Subject: Flaring Events at FS1
To: AOGCC Reporting CC: Victoria Loepp, AOGCC
a oacc. reoorti na Cada las ka. aov
From: Jennifer Blake, GPB Production Team Leader
A flaring event occurred at FS1 starting at 12/18/2016 05:00 and stopping at 12/18/2016 15:50 with a volume of 4062
(MSCF). The event lasted for 650 minutes and was due to a STV/IP compressor 1825 shutdown for planned PSV
maintenance. The event stopped when the STV/IP Compressor was reloaded.
A flaring event occurred at FS1 starting at 12/26/2016 23:00 and stopping at 00:00 12/27/2016 with a volume of 5208
(MSCF). The event had a volume greater than 5000 (MSCF) and was due to an LPS Compressor 1803 shutdown caused
by a problem associated with the seal oil system. The event stopped when LP wells were shut in.
A flaring event occurred at FS1 starting at 01/02/2017 03:15 and stopping at 01/02/2017 04:52 with a volume of 18861
(MSCF). The event lasted for 97 minutes and was due to high gas transit line pressure caused by CGF's 1&2 booster
compressors tripping offline. The event stopped when transit gas line pressure was lowered.
A flaring event occurred at FS1 starting at 01/02/2017 21:11 and stopping at 01/02/2017 23:24 with a volume of 27708
(MSCF). The event lasted for 133 minutes and was due to high gas transit line pressure caused by CGF's 1&2 booster
compressors tripping offline. The event stopped when rates were cut and the transit gas line pressure was lowered.
Thanks,
Jennifer Blake
EOC Production Optimization Team Lead
Office (907) 564-5926
Cell(907)830-6204
Jennifer.blakePbp.com
Flare Start Date 12/012016
Flare End Date 12/312016
FS1 Flare Report Total Volume (MSCF) 9816
Report
Numbs System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
11-14 Hare Relief 12/05/2016 4:30:00 am 5:15:00 am 45 min No
Determination Cause De -pressure 1-B CL from 160# to flare for maintenance.
Action Taken i -B CL de -pressured. Blocked in.
16-466 Flare Relief 12/18/2016 5:00:00 am 3:50:00 pm 650 min No
Determination Cause TIC 1825 shutdown for planned maintenance PSV PM,
Action Taken Loaded STV/IP TIC.
No Yes BPIRICHNEG 60
Daily Volume (MSCF) 60
No Yes BP1\HUNTL2 4062
Daily Volume (MSCF) 4062
Total Volume (MSCF) 9816
Generated 01/05/2017 1:53:26PM Page 4 of 10