Alaska Logo
Department of Commerce, Community, and Economic Development
Alaska Oil and Gas Conservation
Commission
Loading...
HomeMy WebLinkAboutKRU CPF 1+2+3 - ConocoPhillips Alaska, Inc.State of Alaska AOGCC Gas Disposition Files Year: 2017 Facility: KRU CPF 1 + CPF 2 + CPF 3 Operator: ConocoPhillips Alaska, Inc.   CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (f) STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION CPF1 CPF2 CONFIDENTIAL pursuant to: AS 43.05.230. AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (f) Caelus Gas Usage Total Pilot and Purge 1,822 Flare Less than 1 hour 337 Flare Greater than 1 hour 30 Fuel 50,798 Asset Gas 165,916 MakeUp Gas 0 Return Gas 618,453 Total Production 837.356 FLARING OR VENTING EVENTS GREATER THAN 1 HOUR DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME Electrical Breaker Cubicle panel CC -103 lost power due 12:13:00 to a potential faulty Reboiler Production wells were shut-in AM- breaker causing utility loss and until power was restored to CC - 01:40:00 shutodwn of C Gas Lift 103 and C Gas Lift Compressor 1/1/2017 AM 30 Compressor. N restarted. DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME 0 CPF3 DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME 0 CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (t) STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION CPF1 CPF2 CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (1) Caelus Gas Usage Total Pilot and Purge 1,642 Flare Less than 1 hour 175 Flare Greater than 1 hour 0 Fuel 45,080 Asset Gas 294,691 MakeUp Gas 0 Return Gas 420,482 Total Production 762,070 FLARING OR VENTING EVENTS GREATER THAN 1 HOUR DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME CPF3 DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME 0 CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (f) STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION CONFIDENTIAL pursuant to: AS 43.05.230, AS 40 25.10. AS 38.05.035 (a)(6), and AS 36.05.036 (f) Caelus Gas Usage Total Pilot and Purge 1,750 Flare Less than 1 hour 246 Flare Greater than 1 hour 0 Fuel 47,216 Asset Gas 227,313 MakeUp Gas 0 Return Gas 480,375 Total Production 756,900 FLARING OR VENTING EVENTS GREATER THAN 1 HOUR CPF1 DESCRIPTION OF ACTION TAKEN TO DATE TIME VOLUME MSCF FLARING EVENT UNPLANNED MINIMIZE VOLUME 0 CPF2 DESCRIPTION OF ACTION TAKEN TO DATE TIME VOLUME MSCF FLARING EVENT UNPLANNED MINIMIZE VOLUME 0 CPF3 DESCRIPTION OF ACTION TAKEN TO DATE TIME VOLUME MSCF FLARING EVENT UNPLANNED MINIMIZE VOLUME 0 CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (t) STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (0 Caelus Gas Usage Total Pilot and Purge 1,736 Flare Less than 1 hour 228 Flare Greater than 1 hour 0 Fuel 45,225 Asset Gas 262,146 MakeUp Gas 0 Return Gas 575,289 Total Production 884,624 FLARING OR VENTING EVENTS GREATER THAN 1 HOUR CPF1 DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME CPF2 DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME 0 CPF3 DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME U CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (1) STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION CPF1 CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (f) Caelus Gas Usage Total Pilot and Purge 1,578 Flare Less than 1 hour 297 Flare Greater than 1 hour 2 Fuel 40,370 Asset Gas 108,675 MakeUp Gas 706 Return Gas 566,033 Total Production 716,955 FLARING OR VENTING EVENTS GREATER THAN 1 HOUR DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME 1C/1B water injection line was depressured after displacing water with gas for upcoming 5/13/2017 01:28:00 P 2 1C/1B WI piping depressure Y internal pipe coating project. CPF2 DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME 0 CPF3 DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME 0 CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.038 (1) STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (1) Caelus Gas Usage Total Pilot and Purge 1,411 Flare Less than 1 hour 443 Flare Greater than 1 hour 10 Fuel 36,341 Asset Gas 356,591 MakeUp Gas - 0 Return Gas 332,009 Total Production 726,805 FLARING OR VENTING EVENTS GREATER THAN 1 HOUR CPF1 DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME CPF2 DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE TIME VOLUME MSCF EVENT UNPLANNED VOLUME CPF3 DESCRIPTION OF FLARING ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF EVENT UNPLANNED VOLUME 6/23/2017 03:33:00 P 4 Ambient temp. Continued to cuN Reduced/increased inlet gas rates 6/24/2017 01:02:00 P 6 High ambient temperatures N Reduced/increased inlet gas rates CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (f) STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (f) Caelus Gas Usage Total Pilot and Purge 1,351 Flare Less than 1 hour 525 Flare Greater than 1 hour 218 Fuel 32,807 Asset Gas 430,206 Makeup Gas 0 Return Gas 259,955 Total Production 725,062 FLARING OR VENTING EVENTS GREATER THAN 1 HOUR CPF1 ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF DESCRIPTION OF FLARING EVENT UNPLANNED VOLUME 7/18/2017 05:30:00 PM - 07:51:00 PM 59 Electrical/Instrumental Malfunction 4160 breaker tripped for unknown reasons shutting down "A" GLC and other equipment. Reduced/Increased inlet gas rates. CPF2 ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF DESCRIPTION OF FLARING EVENT UNPLANNED VOLUME Ambient temps took a spike and "B" GLC was unable to move any gas through the plant. Stabilized facility 7/6/2017 11:38:00 PM - 12:53:00 AM 10 Excessive/insufficient inlet gas rates into facility N process and operation. All three turbine drivel GLC's unloaded due to high ambient temp. Recuded inlet gas rates and stabilized facility process and 7/28/2017 10:30:00 AM -12:05:00 PM 67 Process upset in A/B/C GLC section of facility N operation. CPF3 ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF DESCRIPTION OF FLARING EVENT UNPLANNED VOLUME Cut gas, called tech to come help 7/5/2017 09:42:00 PM - 10:57:00 PM 71 High ambeint temps caused both GLC to slow rpms. N determine cause of trip. Reducedlncreased inlet gas rates. 7/6/2017 12:51:00 PM - 02:45:00 PM 11 High ambeint temps caused B GLC to recycle N Shut in wells. CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (1) STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (f) Caelus Gas Usage Total Pilot and Purge 1,476 Flare Less than 1 hour 204 Flare Greater than 1 hour 3 Fuel 39,872 Asset Gas 479,389 MakeUp Gas 0 Return Gas 289,371 Total Production 810,315 FLARING OR VENTING EVENTS GREATER THAN 1 HOUR CPF7 ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF DESCRIPTION OF FLARING EVENT UNPLANNED VOLUME CPF2 ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF DESCRIPTION OF FLARING EVENT UNPLANNED VOLUME CPF3 ACTION TAKEN TO MINIMIZE DATE TIME VOLUME MSCF DESCRIPTION OF FLARING EVENT UNPLANNED VOLUME Reduced compressor efficiency due to having after coolers out of service 8/15/2017 11:52:00 AM - 12:52:00 PM 3 Excessive/insufficient inlet gas rates into facility N for repairs CONFIDENTIAL pursuant to: AS 43.05.230, AS 40.25.100, AS 38.05.035 (a)(8), and AS 38.05.036 (f)