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HomeMy WebLinkAboutPBU FS 1 - BP Exploration (Alaska), Inc.State of Alaska AOGCC Gas Disposition Files Year: 2017 Facility: PBU FS 1 Operator: BP EXPLORATION (ALASKA) INC.     STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number2. 0290000028 Facility Name PBU FS 1 3. Field PBU - EOA 4. Operator BP 5. MonthNear of Disposition I January -2017 Disposition Volume MCF 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold 0 Pool Name Pool Code Percent 7. Reinjected 0 PRUDHOE 640150 100.00% 8. Flared or vented 1 hour or less 4,722 9. Flared or vented more than 1 hour (see instr.) 46,569 10. Pilot and Purge 21,458 11. Assist Gas 54,933 12. Fuel gas used in lease operations. 661,646 13. Other (see instructions) 0 Official Use Only Authorization >1 hr: Safety / Slv v MCF 14. TOTAL VOLUME (ITEMS 6-12) 789,328 Lease Use MCF 15. NGL Gas Equivalent 0 Conservation MCF 16. Purchased gas Q Waste: MCF 17. Transferred from: CGF 183,751 •~/—[.`- 18. Transferred to: (Express as a negative #) CGF 8 CCP -71,197,812 Commissioner Date 19. Remarks: I hereby certify that the foregoing is true and correct to the best of my knowledge. //� l Y�L Note: All volumes must be corrected Signature Title Manager Production Taxes and Ro allies Alaska to pressure of 14.65 psis and to a _ temperature of 60o F. Authority 20 Printed Name Diane Colle Phone (907) 564-5775 Date AAC25.235. v'T1-- .3/2f/ 1,4 -- Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate -^•� IvULUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 1/2/2017 0315-0452 18,861 See attachments See attachments 1/2/2017 2111-2324 27,708 TOTAL 46,569 Planned events less than or equal to 1 hour See attachments TOTAL 0 See attachments TOTAL 0 BP EXPLORATION (ALASKA) INC. Unplanned Events < 1 Hour PRUDHOE BAY UNIT - FS -1 Unplanned Events> 1 Hour GAS FLARING INCIDENT REPORT Planned Events < 1 hour and not January 2017 Unplanned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 1/23/2017 1820-1854 4,722 Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr TOTAL 4,722 21,458 -^•� IvULUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 1/2/2017 0315-0452 18,861 See attachments See attachments 1/2/2017 2111-2324 27,708 TOTAL 46,569 Planned events less than or equal to 1 hour See attachments TOTAL 0 See attachments TOTAL 0 See attachments See attachments Page 3 2/12/2017 5:13 PM TOTAL Unplanned Events < 1 Hour 4,722 Unplanned Events> 1 Hour 46,569 Planned Events < 1 hour and not 0 exceeding 5,000 MCF Planned Events> 1 hour or 0 exceeding 5,000 MCF Pilot Purge 21,458 Assist 54,933 TOTAL FLARED VOLUME 127,682 See attachments See attachments Page 3 2/12/2017 5:13 PM Flare StartDate 01101/2017 Flare End Date 01/31/2017 FS1 Flare Report Total Volume (MSCF) 51291 Report Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume 17-3 Flare Relief 01/02/2017 3:15:00 am 4:52:00 am 97 min No No No BPt\BUTLRM 18861 Determination Cause High gas transit line pressure caused by CGF compressor problems due to 182 booster. Action Taken Flared off P149V at 300M rate. 17-3 Flare Relief 01102/2017 9:11:00 pm 11:24:00 pm 133 min No No No BP1\BUTLRM 27708 Determination Cause High gas transit line pressure caused by CGF compressor problems due to booster 182 shutdown. Action Taken Shut in wells,18-7, 18-13, 2-12, 2-7, 2-35, 2-18 and Flared off P149V at 300MM Daily Volume (MSCF) 46569 Total Volume (MSCF) 51291 Generated 02/02/2017 11:09:42AM Page 3 of 8 Link, Liz M (DOA) From: AKOpsProcIEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Wednesday, January 04, 2017 11:59 AM To: AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; Schinagl, Werner; Fortenberry, Christopher; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A Subject: Flaring Events at FS1 To: AOGCC Reporting CC: Victoria Loepp, AOGCC aogcc.reoorting(a alaska.gov From: Jennifer Blake, GPB Production Team Leader A la�nrr grad a F�S1 starting at 12/18/2016 05:00 and stopping at 12/18/2016 15:50 with avo ume of 4062 (MSCF). The event lasted for 65D-minrrt�s..anndd was due to a STV/IP compressorIB25-shutdown-ffor planned PSV maintenance. The event stopped when the STV/ P -Co r -v a -loaded. A flaring event occurred at FS a 12/26/2016 23:00 and stopping at 00:00 1212712016 with a volume of 5208 (MSCF). The a volume greater than 5000 (MSCF) and was due to an LPS Compressor Ma-shutdcwn caused b� em associated with the seal oil system. The event stopped when LP wells were shut in. A flaring event occurred at FS1 starting at 01/02/2017 03:15 and stopping at 01/02/2017 04:52 with a volume of 18861 (MSCF). The event lasted for 97 minutes and was due to high gas transit line pressure caused by CGF's 1&2 booster compressors tripping offline. The event stopped when transit gas line pressure was lowered. A flaring event occurred at FS1 starting at 01/02/2017 21:11 and stopping at 01/02/2017 23:24 with a volume of 27708 (MSCF). The event lasted for 133 minutes and was due to high gas transit line pressure caused by CGF's 1&2 booster compressors tripping offline. The event stopped when rates were cut and the transit gas line pressure was lowered. Thanks, Jennifer Blake EOC Production Optimization Team Lead Office (907) 564-5926 Cell (907) 830-6204 Jennifer.blake@bp.com STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCFn [,nS n1cPnc1T1nA1 -- 1, Facility Number 2. Facility Name 0290000028 PBU FS 1 Disposition --------- 3. Field PBU - EOA Volume MCF --.- -.V. VV...V.. 4. Operator 5. MonthNear of Disposition BP February -2017 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold 0 Pool Name Pool Code Percent 7. Reinjected 0 PRUDHOE 640150 100.00% 8. Flared or vented 1 hour or less 6,805 9. Flared or vented more than 1 hour (see instr.) 0 10. Pilot and Purge 32,552 11, Assist Gas 49,569 12. Fuel gas used in lease operations. 588,594 13. Other (see instructions) 0 Official Use Only Authorization 71 hr: Safety MCF 14. TOTAL VOLUME (ITEMS 6-12) 677,520 Lease Use MCF 15. NGL Gas Equivalent 0 Conservation MCF 16. Purchased gas 0 Waste: MCF 17. Transferred from: CGF 171,057 18. Transferred to: (Express as a negative #) CGF & CCP -62,868,197 Commissioner Date 19, Remarks: I hereby certify that the foregoing is true and correct to the best of my knowledge. u� Note: All volumes must be corrected Signature Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psis and to a 7 temperature of 60o F. Authority 20 Printed Name Diane Colley Phone (907) 564-5775 Date..td AAC25.235. Form 10-422 Rev, 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT- FS -1 GAS FLARING INCIDENT REPORT February 2017 unplanned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 2/15/2017 1512-1545 4,583 Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr 2/17/2017 0709-0725 2,222 TOTAL 6,805 DATE See attachments See attachments TOTAL 0 Planned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE See attachments See attachments TOTAL 0 Planned events greater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE See attachments See attachments TOTAL 0 Unplanned Events < 1 Hour Unplanned Events > 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events > 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME TOTAL 6,805 0 0 0 32,552 49,569 88,926 Page 5 3/15/2017 10:10 AM STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 0290000028 2. Facility Name PBU FS 1 3. Field PBU - EOA 4. Operator BP 5. MonthNear of Disposition March -2017 Disposition Volume MCF 20. Forproduchon from multiple pools, list contribution of each pool as a percent of Total Volume. 6. SoldO Pool Name Pool Code Percent 7. Reinjected 0 PRUDHOE 640150 100.00% 8. Flared or vented 1 hour or less 3,621 9. Flared or vented more than 1 hour (see instr.) 7,914 10. Pilot and Purge 34,278 11. Assist Gas 66,241 12. Fuel gas used in lease operations. 659,271 13. Other (see instructions) Official Use Only Authorization>t hr: Safety GVT � / `� MCF -5—/u9 14. TOTAL VOLUME (ITEMS 6-12) 771,325 Lease Use MCF 15. NGL Gas Equivalent 0 Conservation MCF 16. Purchased gas 0 Waste: MCF IT Transferred from: CGF 189,983 S- 'l — 18. Transferred to: (Express as a negative #) CGF & CCP -73,106,791 Commissioner Date 19. Remarks: I hereby certify that the foregoing is true and correct to the best of my knowledge. //ry �q Note: All volumes must be corrected Signature t(;el tX �,���. Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 Printed Name Diane Colley Phone (907) 564-5775 Dale AAC25.235. r� Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - FS -1 GAS FLARING INCIDENT REPORT March 2017 junplanned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 3/21/2017 1420-1445 336 Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr 3/21/2017 1440-1452 2,916 TOTAL 3,252 CAUSE See attachments ACTION TAKEN TO I See attachments TOTAL 0 Planned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 3/21/2017 0214-0245 369 See attachments See attachments TOTAL 369 3/20-21/17 0352-0025 TOTAL Unplanned Events < 1 Hour Unplanned Events > 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events > 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME 7,914 See attachments 7,914 TOTAL 3,252 0 369 7,914 34,278 66,241 112,054 ACTION TAKEN TO I See attachments Page 4 4/13/2017 10:32 AM Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Monday, April 10, 2017 11:21 AM To: AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; Schinagl, Werner; Fortenberry, Christopher; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A Subject: Flaring Event at FSI To: AOGCC Reporting CC: Victoria Loepp, AOGCC aogcc.reporting Qalaska.gov From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 03/20/2017 03:52 and stopping at 03/20/2017 23:59 with a volume of 7753 (MSCF). The event lasted for 1207 minutes and was due to a STWIP compressor (1825) shutdown for planned maintenance. The event stopped when the STV/IP Compressor was reloaded shortly after midnight. Thanks, Jennifer Blake EOC Production Optimization Team Lead Office (907) 564-5926 Cell (907) 830-6204 Jennifer.blake@bp.com STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCFn rnS nicpnc1T1nk1 i. facility Numder 2. Facility Name 0290000028 PBU FS 1 Disposition 3. Field PBU - EOA Volume MCF P — — w w • • v • 4. O tor 5 MomhKear of Disposition BPeraAril-2017 20. Forproduchon from multiple pools, list contribution of each pod as a percent of Total Volume 6. Sold 0 Pool Nam' Pool Code Percent 7. Reinjected 0 PRUDHOE 640150 100.00% B. Hared or vented 1 hour or less 8,333 9. Flared or vented more than 1 hour (see inso.) 4,020 10. Pilot and Purge 23,025 11. Assist Gas 93,838 12. Fuel gas used in lease operations. 622,928 13. Other (see instructions) 0 Official Use OnlyAulhori2ation >1 hr: Safety /�, MCF1 .7_, :__ 14. TOTAL VOLUME (ITEMS 6-12) 752,144 Lease Use q gjy7e� MCF(�_I 15. NGL Gas Equivalent 0 Conservation MCF 18. Purchased gas 0 Waste: MCF 17. Transferred from: COT 176.770 18 Transferred to. (Express as a negative 0) CGF 8 CCP -64,298,842 Commissioner Date 19 Remarks: 10 I hereby certify that the foregoing is true and correct to the test of my knowledge. ^ ' Note: All volumes must be corrected SignatureTitle Mana er Production Taxes and Ro allies Alaska to pressure of 14.65 psia and to a Printed Name Diane ColleyPhone (907) 564-5775 Date �))/'L} temperature of 60o F. Authority 20AAC25-235. 2F7v—1 Form 10-422 Rev. 512009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate TOTAL n BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - FS-1 GAS FLARING INCIDENT REPORT April 2017 Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr 4/14/2017 0730-1000 ----' -- - 1,187 See attachments n�I mlv Inp[IY ILl eLIWI[NAIL LAUSE 4/17/2017 1330-2200 2,833 See attachments TOTAL 4,020 Planned events less than or equal to 1 hour DATE TIME 4;10/2017 VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 1750-1825 8,333 See attachments See attachments TOTAL 8,333 Planned events greater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE See attachments See attachments TOTAL 0 TOTAL Unplanned Events<1 Hour 0 Unplanned Events > 1 Hour 4,020 Planned Events < 1 hour and not 8,333 exceeding 5,000 MCF Planned Events> i hour or 0 exceeding 5,DO0 MCF Pilot Purge 23,025 Assist 93,838 TOTAL FLARED VOLUME 129,216 Page 4 5/14/2017 2:06 PM Flare Start Date 04101/2017 Flare End Date 04,30/2017 FS1 Flare Report Total Volume (MSCF) 12353 Report Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume -. nmc.cener u41IW2017 5.50:00pm 6.25O0 on 35mm No No Yes BP1lGR(MDO 8333 Determination Cause Flare for field and CGF TC maintenance Action Taken Closed Flare valve after maintenance completed. Daily Volume (MSCF) 8333 17-117 Controlled Blcwdown 04/14/2017 7.30O0 am 1000ocam 150mm No No No BP1X8ELLZ0 1187 Determination Cause Bow down of DS2 and associated common lines to FS1 Bare. Action Taken Depressurization of DS2 and asscosted common lines complete Daily Volume (MSCF) 1187 17-124 Other 04117M17 1.3000 pm 1000:00 pm 510 min No No No 8P14GRIMD0 2533 Determination Cause STV-M 1825 Shutdown due to a problem associated with IP21 not oommunlCabng with Honeywell. Problem with Bridgemaster. Action Taken Loaded STVlIP 1825. Daily Volume (MSCF) 2833 Total Volume (MSCF) 12353 1 1636PM Page 6of 10 Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Monday, June 12, 2017 4:56 PM To: AKOpsProdEOCTL, AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; Schinagl, Werner; Fortenberry, Christopher; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A Subject: CORRECTION: Flaring Event at FS1 CORRECTION: I had a template copy/paste error in my 04/14/2017 flare report (carry over from the 03/20/2017 report submitted on 04/10/2017). Please see the revision in below. Thank you, Jennifer From: AKOpsProdEOCTL Sent: Thursday, May 04, 2017 7:18 AM To: 'aogcc.reporting@alaska.gov' Cc: 'Loepp, Victoria T (DOA) (victoria.loepp@alaska.gov)'; Benson, Gary A; Arthur, Gregory; Schinagl, Werner; Fortenberry, Christopher; AK, HSSEE Env Adv East; AK, OPS FSl Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A Subject: Flaring Event at FS1 To: AOGCC Reporting CC: Victoria Loepp. AOGCC aOgC. reROftt;M1q lCLaIa9ka.00J From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 04/10/2017 17:50 and stopping at 04/10/2017 18:25 with a volume of 8333 (MSCF). The event had a volume greater than 5000 (MSCF) and was due to a CGF Tandem Compressor unloading for further adjustments in follow-up to earlier repairs. The event stopped when field rates were cut and the T/C was reloaded. A flaring event occurred at FS1 starting at 04/14/2017 07:30 and stopping at 04/14/2017 10:00 with a volume of 1187 (MSCF). The event lasted for 150 minutes and was due to A flaring event occurred at FS1 starting at 0411712017 13:30 and stopping at 04/17/2017 22:00 with a volume of 2833 (MSCF). The event lasted for 510 minutes and was due to a STV/fP compressor (1825) shutdown due to a problem associated with one control system (IP.21) not communicating with a different control system (Honeywell) due to failure of a communication protocol (Bridgemaster). The event stopped when the STVAP Compressor was reloaded. Thanks, )enni/er 81oke EOC Production Optimization Team Lead Office (907) 564-5926 Cell (907) 830-6204 Jell II f_c-r, b_ak<,a o Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Thursday, May 4, 2017 7:18 AM To: AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; Schinagl, Weiner; Fortenberry, Christopher; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A Subject: Flaring Event at FS1 To: AOGCC Reporting CC: Victoria Loepp, AOGCC From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 04110/2017 17:50 and stopping at 04/10/2017 18:25 with a volume of 8333 (MSCF). The event had a volume greater than 5000 (MSCF) and was due to a CGF Tandem Compressor unloading for further adjustments in follow-up to earlier repairs. The event stopped when field rates were cut and the TIC was reloaded. A flaring event occurred at FS1 starting at 04/14/2017 07:30 and stopping at 04/14/2017 10!00 with a volume of 1187 (MSCF). The event lasted for 150 minutes and was due to a STV/IP compressor (1825) shutdown for planned maintenance. The event stopped when the STV/IP Compressor was reloaded shortly after midnight A flaring event occurred at FS1 starting at 04117/2017 13:30 and stopping at 04/17/2017 22:00 with a volume of 2833 (MSCF). The event lasted for 510 minutes and was due to a STV/IP compressor (1825) shutdown due to a problem associated with one control system (IP.21) not communicating with a different control system (Honeywell) due to failure of a communication protocol (Bridgemaster). The event stopped when the STV/IP Compressor was reloaded. Thanks, jufmwfcr 31uke EOC Production Optirni7atmfl Team Lean! Office (907) 564 5926 C(III iPCM 93G-6 Uu Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Tuesday, April 18, 2017 3:23 PM To: Loepp, Victoria T (DOA); Regg, James B (DOA); 'aogcc.reporting@aiaska.gov' Cc: AK, OPS FS1 Field OTL; AK, OPS FS1 OSM; Loader, Neil; Benson, Gary A; Arthur, Gregory; AK, HSSEE Env Adv East; AK, HSSEE Env TL (North Slope); Schinagl, Werner, Buckbee, Rachel A; Buckendorf, Randal; Burden, Andrew J; Covey, Jasper O Subject: FS1 DS2 Well 3 Uncontrolled Release 5 Day Report Attachments: 5 Day AOGCC Report - FS1 DS2 Well 3.pdf Victoria Leopp & Jim Regg, Please find enclosed the 5-day report for the release which occurred at FS1 Drill Site 2 Well 3, on 4114/2017. This was also faxed to 907-276-7542. Please give me a call if you have further questions. A 30-day report will be provided after completion of the incident investigation. Regards, PCC/EOC Produt ton O ,tinusatkm Tr:)am Lead (u!t Davit; S�xrl!) Office 19071659-i47= Cell (907) 8.30-6204 ,pA/111/2017 TVE 15:39 FAX 907 554a 5587 BFXA 11th Floor 20011002 BP Exploration (Alaska) Inc. P.O. Box 196612, Anchorage, AK 99519-6612 REPORT OF ACCIDENTAL OIL AND/OR GAS RELEASE (36-day report per 20 ACC 25.205 (b)) Dato:71612015 For Ail Releases To: Chairman Alaska Oil and Gas Conservation Commission 333 W. 7tb Ave, Suite 100 Anchorage, AK 99501-3539 Fax. (907)276-7542 DESCRIPTION OF RELEA E 'L_DAta and Tim&• k All df9017. of annmY1matah, n7M am Aadami _Northstar Other 3. Volume of oil andlor natural gas released _ Released: No estimate of the leak volume Is available at and recovered: this time Recovered: There is no recovered volume available yet. Once the well is secured downhols, BPXA will work with their Oil Spill Response Organization, Alaska Clean Seas to begin delineation and response clean-up efforts under the plan that has been approved by the Unified Command BP, EPA, ADEC, NSB) 4. Cause of release: Unknown at this time. 5. Responsive actions taken to prevent SSV closed, drill site shut in, and common lines leaving additional releases: DS2 do -pressure to flare. iMT formed and response action worked under direction of the Unified Command. ADEC as the State agency on the unified command acted as the lisson with the AOGCC. On Monday April 17 the well was killed and on Tuesday April Id' plans to install a mechanical plug were approved by the Unified Command and AOGCC. 6. Plans, actions, equipment or procedural Unknown at this time. rhnnmpq to nrcvnnf nr In(mHo rfc4 n Signature: __ CC: Jim Regg, AOGCC dJ Victoria Leopp, AOGCC Jennifer Hunt, AOGCC 04/18/2017 TUE 15t19 PAX 907 564 5949 anCp182 0002/002 BPX Air Quality Technical Authority MB 11-6 (Fax: 564-5020) BPX Volume Accounting MS 12-4 (Fax: 564-4094) East Area Operations Manager, 11-62B Production Optimization Team Leader, F-1 04/18/2017 TUB 15!24 FAX 907 564 5949 sncp182 Z001/002 SP Exploration (Alaska) Inc P.O. Box 196612, Anchorage, AK 99519-6612 REPORT OF ACCIDENTAL OIL AND/OR GAS RELEASE (30-day report per 20 ACC 25.205 (b)) Date:91612016 For All Releases To; Chairman Alaska Oil and Gas Conservation Commission W1812017 TUE 15!24 Fax 907 564 5949 ancP182 0002/002 BPX Air Quality Technical Authority MB 11-6 (Fax 564-5020) BPX Volume Accounting MB 12-4 (Fax: 564-4094) Cast Area Operations Manager, 11-62B Production Optimization Team Leader, F-1 STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCFn GAS nicpnciTinN 1. Facility Number2. Facility Name 0290000028 PBU FS 1 Disposition 3. Field PBU - EOA Volume MCF 4. Operator . •... • 5. MonthNear of Disposition BP Aril -2017 20. Forproduction from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold Pool Name Pool Code Percent 7. Reinjected p PRUDHOE 640150 100.00°/ 8. Flared or vented 1 hour or less 8,333 9. Flared or vented more than 1 hour (see instr.) 4,020 10. Pilot and Purge 23,025 11. Assist Gas 93,838 12. Fuel gas used in lease operations. 622,928 13. Other (see instructions) G Official Use Only Authorization 4 C 2-C MCF k TOTAL VOLUME (ITEMS 6-12) 752,144 se MCF 15. NGL Gas Equivalent Q ation MCF 16. Purchased gas : MCF 17. Transferred from: CGF 176770 -27 -� Commissioner Date 18. Transferred to: (Express as a negative #) CGF 8 CCP -64,298'842 19, Remarks: I hereby certify that the foregoing is true and correct to the best of my knowledge. ����j �l�, Note: All volumes must be corrected Signature Title Manager Production Taxes and Ro alties Alaska to pressure of 14.65 psis and to a temperature of 60o F. Authority 20 Printed Name Diane Colley Phone (907) 564-5775 Date 4417 AAC25.235. Form 10-422 Rev. 512009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate events less than or equal to 1 TOTAL BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - FS -1 GAS FLARING INCIDENT REPORT April 2017 Not required for unplanned events <= 1 hr 0 ACTION TAKEN TO ELIMINATE CAUSE Not required for unplanned events <= 1 hr TOTAL Unplanned Events < 1 Hour Unplanned Events > 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events > 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME See attachments 0 TOTAL 0 4,020 8,333 0 23,025 93,838 129,216 See attachments Page 4 5/14/2017 2:06 PM vuwmt UL9CKIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 4/14/2017 0730-1000 1,187 See attachments See attachments 4/17/2017 1330-2200 2,833 TOTAL 4,020 Planned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 4/10/2017 1750-1825 8,333 See attachments See attachments TOTAL 8,333 TOTAL Unplanned Events < 1 Hour Unplanned Events > 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events > 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME See attachments 0 TOTAL 0 4,020 8,333 0 23,025 93,838 129,216 See attachments Page 4 5/14/2017 2:06 PM Flare Start Date 04/01/2017 Flare End Date 04/30/2017 FSI Flare Report Total Volume (MSCF) 12353 Report Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume 17-112 Flare Relief 04/10/2017 5:50:00 pm 6:25:00 pm 35 min No No Yes BP1%GRIMDO 8333 Determination Cause Flare for field and CGF T/C maintenance. Action Taken Closed Flare valve after maintenance completed. Daily Volume (MSCF) 8333 17-117 Controlled Blowdown 04/14/2017 7:30:00 am 10:00:00 am 150 min No No No BP1%BELLZO 1187 Determination Cause Blow down of DS2 and associated common lines to FS1 Flare. Action Taken Depressurization of DS2 and associated common lines complete. Daily Volume (MSCF) 1187 17-124 Other 04/17/2017 1:30:00 pm 10:00:00 pm 510 min No No No SP7\GRIMDO 2833 Determination Cause STV -IP 1825 shutdown due to a problem associated with IP21 not communicating with Honeywell. Problem with Bndgemaster. Action Taken Loaded STV/IP 1825. Daily Volume (MSCF) 2833 Total Volume (MSCF) 12353 Generated 05/02/2017 1:16:36PM Page 6 of 10 Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Monday, June 12, 2017 4:56 PM To: AKOpsProdEOCTL; AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; Schinagl, Werner; Fortenberry, Christopher, AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A Subject: CORRECTION: Flaring Event at FS1 CORRECTION: I had a template copy/paste error in my 04/14/2017 flare report (carry over from the 03/20/2017 report submitted on 04/10/2017). Please see the revision in red below. Thank you, Jennifer From: AKOpsProdEOCTL Sent: Thursday, May 04, 2017 7:18 AM To: 'aogcc.reporting@alaska.gov' Cc: 'Loepp, Victoria T (DOA) (victoria.loepp@alaska.gov)'; Benson, Gary A; Arthur, Gregory; Schinagl, Werner; Fortenberry, Christopher; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A Subject: Flaring Event at FS1 To: AOGCC Reporting CC: Victoria Loepp, AOGCC aogcc. reporting(a)alaska.gov From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 04/10/2017 17:50 and stopping at 04/10/2017 18:25 with a volume of 8333 (MSCF). The event had a volume greater than 5000 (MSCF) and was due to a CGF Tandem Compressor unloading for further adjustments in follow-up to earlier repairs. The event stopped when field rates were cut and the T/C was reloaded. A flaring event occurred at FS1 starting at 04/14/2017 07:30 and stopping at 04/14/2017 10:00 with a volume of 1187 (MSCF). The event lasted for 150 minutes and was due to an unplanned event that required blowing down drill site 02 and the associated common lines to flare. The event stopped DS02 and the associated common lines were depressurized. A flaring event occurred at FS1 starting at 04/17/2017 13:30 and stopping at 04/17/2017 22:00 with a volume of 2833 (MSCF). The event lasted for 510 minutes and was due to a STV/IP compressor (1825) shutdown due to a problem associated with one control system (IP.21) not communicating with a different control system (Honeywell) due to failure of a communication protocol (Bridgemaster). The event stopped when the STV/IP Compressor was reloaded. Thanks, Jennifer Blake EOC Production Optimization Team Lead Office (907) 564-5926 Cell (907) 830-6204 Jen nifer.bla kePbp.com Link, Liz M (DOA) From: AKOpsProcIEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Thursday, May 4, 2017 7:18 AM To: AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory, Schinagl, Werner; Fortenberry, Christopher, AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 CSM; Glover, Robin; Buckbee, Rachel A Subject: Flaring Event at FS1 To: AOGCC Reporting CC: Victoria Loepp, AOGCC aoqcc. reporting (dalaska.gov From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 04/10/2017 17:50 and stopping at 04/10/2017 18:25 with a volume of 8333 (MSCF). The event had a volume greater than 5000 (MSCF) and was due to a CGF Tandem Compressor unloading for further adjustments in follow-up to earlier repairs. The event stopped when field rates were cut and the T/C was reloaded. A flaring event occurred at FS1 starting at 04/14/2017 07:30 and stopping at 04/14/2017 10:00 with a volume of 1187 (MSCF). The event lasted for 150 minutes and was due to a STV/IP compressor (1825) shutdown for planned maintenance. The event stopped when the STV/IP Compressor was reloaded shortly after midnight. A flaring event occurred at FS1 starting at 04/17/2017 13:30 and stopping at 04/17/2017 22:00 with a volume of 2833 (MSCF). The event lasted for 510 minutes and was due to a STV/IP compressor (1825) shutdown due to a problem associated with one control system (IP.21) not communicating with a different control system (Honeywell) due to failure of a communication protocol (Bridgemaster). The event stopped when the STV/IP Compressor was reloaded. Thanks, Jennifer Blake EOC Production Optimization Team Lead Office (907) 564-5926 Cell (907) 830-6204 Jennifer.blake@bp.com Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Tuesday, April 18, 2017 3:23 PM To: Loepp, Victoria T (DOA); Regg, James B (DOA); 'aogcc.reporting@alaska.gov' Cc: AK, OPS F51 Field OTL; AK, OPS FS1 OSM; Loader, Neil; Benson, Gary A; Arthur, Gregory; AK, HSSEE Env Adv East; AK, HSSEE Env TL (North Slope); Schinagl, Werner; Buckbee, Rachel A; Buckendorf, Randal; Burden, Andrew 1; Covey, Jasper 0 Subject: FS1 DS2 Well 3 Uncontrolled Release 5 Day Report Attachments: 5 Day AOGCC Report - FS1 DS2 Well 3.pdf Victoria Leopp & Jim Regg, Please find enclosed the 5 -day report for the release which occurred at FS1 Drill Site 2 Well 3, on 4/14/2017. This was also faxed to 907-276-7542. Please give me a call if you have further questions. A 30 -day report will be provided after completion of the incident investigation. Regards, Jennifer Blake PCC/EOC Production Optimization Team Lead (alt David Spall) Office (907) 659-4472 Cell (907) 830-6204 Jennifer.blake@bp.com (lI4/1 T1VE 15:39 FAX 907 564 5587 EPxA lith Floor 0001/002 BP Exploration (Alaska) Inc. P,O. Box 186612, Anchorage, AK 99519-6612 REPORT OF ACCIDENTAL OIL AND/OR GAS RELEASE 0 -day report per 20 ACC 25.205 (b)) 5 - Date:7/8/2016 For For All Releases To: Chairman Alaska Oil and Gas Conservation Commission 333 W. 7t' Ave, Suite 100 Anchorage, AK 99501-3539 Fax: (907) 276-7542 DESCRIPTION OF RELEA E —DAFAI Anrl Tlma, d��Q('�n�]_ nnnmvimnfP1%, n7nn Am _Aadami Northstar Other 3. Volume of oil and/or natural gas released Released: No estimate of the leak volume Is available at and recovered: this time Recovered: There is no recovered volume available yet. Once the well is secured downhole, BPXA will work with their Oil Spill Response Organization, Alaska Clean Seas to begin delineation and response clean-up efforts under the plan that has been approved by the Unified Command 8P, EPA, ADEC, NSB). 4. Cause of release: Unknown at this time. 5. Responsive actions taken to prevent SSV closed, drill site shut in, and common lines leaving additional releases: DS2 de -pressure to flare. IMT formed and response action worked under direction of the Unified Command. ADEC as the State agency on the unified command acted as the liason with the AOGCC. On Monday April 17 the well was killed and on Tuesday April 1 B4i plans to Install a mechanical plug were approved by the Unified Command and AOGCC. S. Plans, actions, equipment or procedural Unknown at this time. nhennn }n nravAn} nr rplmlmlv& ride n Signature: cc: Jim Regg, AOGCC Victoria Leopp, AOGCC Jennifer Hunt, AOGCC 04/18/2017 TUE 15:19 FAX 907 564 5969 anop182 0002/002 BPX Air Quality Technical Authority MB 11-6 (Fax: 564-5020) BPX Volume Accounting MB 12-4 (Fax: 564-4094) East Area Operations Manager, 11-62B Production Optimization Team Leader, F-1 06/18/2017 TUE 15:26 aax 907 566 5969 ancp182 ®001/002 SP Exploration (Alaska) Inc. P.O. Box 196612, Anchorage, AK 99519-6612 REPORT OF ACCIDENTAL OIL AND/OR GAS RELEASE (30 -day report per 20 ACC 25.205 (b)) Date:7/512015 For All Releases To: Chairman Alaska Oil and Gas Conservation Commission 04/18/2017 TUE 15:26 FAX 907 564 5949 ancp182 BPX Air Quality Technical Authority MB 11-6 (Fax 564-5020) SPX Volume Accounting MB 124 (Fax: 564-4094) Beast Area Operations Manager, 11-628 Production Optimization Team Leader, F-1 2002/002 STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCFD [.oS n1Sanc1T1nti 1. Facility Number2. Facility Name 0290000028 PBU FS 1 Disposition 3. Field PBU - EOA Volume MCF 4. Operator 5. MonthNear of Disposition BP May -2017 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold 0 Pool Name Pool Code Percent T Reinjected 0 PRUDHOE 640150 100.00% 8. Flared or vented 1 hour or less 9,167 9. Flared or vented more than 1 hour (see instr.) 530 10. Pilot and Purge 22,987 11, Assist Gas 93,085 12. Fuel gas used in lease operations. 604,242 13. Other (see instructions) 0 Official Use Only Authorization >1 h[ Safety C3� J MCFy.J 14. TOTAL VOLUME (ITEMS 6-12) 730,011 Lease Use M F 15, NGL Gas Equivalent 0 Conservation MCF 16. Purchased gas 0 Waste: MCF 17. Transferred from: CGF 164,318 '/ —7 77 18. Transferred to: (Express as a negative #) CGF & CCP -66,957,875 Commissioner Date 19. Remarks: I hereby certify that the �forego ing is true and correct to me best of my knowledge. �l�I rC L4 Note: All volumes must be corrected Signature_ C'^ Title Manager Production Taxes and Ro allies Alaska to pressure of 14.65 psis and to a — temperature of 60o F. Authority 20 Printed Name Diane Colley Phone (907) 564-5775 Date AAC25.235. 1_ Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT- FS -1 GAS FLARING INCIDENT REPORT May 2017 junplanned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 5/19/2017 1605-1637 6,667 Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr TOTAL 6,667 - I-- IwLwsvll ucua.mr i wry ur nrmum l & wuoe ACTION TAKEN TO ELIMINATE CAUSE 5/19/2017 1605-1714 431 See attachments See attachments TOTAL 431 Planned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 5/9/2017 0745-0805 2,500 See attachments See attachments TOTAL 2,500 UA H, TIME VOLUME DESCRIPTION OF IN 5/13/2017 0530-0700 99 See attachments TOTAL 99 TOTAL Unplanned Events < 1 Hour 6,667 Unplanned Events > 1 Hour 431 Planned Events < 1 hour and not 2,500 exceeding 5,000 MCF Planned Events> 1 hour or 99 exceeding 5,000 MCF Pilot Purge 22,987 Assist 93,085 TOTAL FLARED VOLUME 125,769 See attachments Page 3 6/14/2017 1:58 PM Flare Start Date 05/01/2017 Flare End Date 05/31/2017 FS1 Flare Report Total Volume (MSCF) 9697 Report Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume 17-152 Other 05/09/2017 7:45:00 am 8:05:00 am 20 min No No Yes BP1\GRIMD0 2500 Determination Cause High gas transit line pressure caused by CGF [rooster cool stop. Action Taken CGF booster loaded up and completed the cool stop. 17-166 Other 05/13/2017 5:30:00 am 70000 am 90 min No Determination Cause Oepressurizing 5D and 5B for choke repairs at drill site. Action Taken Depressurization completed. 17-179 Flare Relief 05/19/2017 4:05:00 pm 5:14:00 pm 69 min No Determination Cause STV -IP T\C 1825 unloaded due to low gas rates. Action Taken Loaded STV/IP 1825 T/C, No Yes BPI\GRIMDO 99 No No BPI\BUTLRM 431 Total Volume (MSCF) 9697 Generated 06/09/2017 2:22:08PM Page 3 of 9 Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Thursday, May 18, 2017 12:42 PM To: AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; Schinagl, Werner; Fortenberry, Christopher; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A; Dean, lames A Subject: Flaring Event at FS1 To: AOGCC Reporting CC: Victoria Loepp, AOGCC aogcc. reporting(d.alaska.gov From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 05/13/2017 05:30 and stopping at 05/13/2017 07:00 with a volume of 99 (MSCF). The event lasted for 90 minutes and was due to depressurizing Common Lines 5D and 5B for choke repairs at the drill site. The event stopped when depressurization was completed. Thanks, Jennifer Blake EOC Production Optimization Team Lead Office (907) 564-5926 Cell (907) 830-6204 Jennifer.blake@bp.com Link, Liz M (DOA) From: Blake, Jennifer! <Jennifer.Blake@bp.com> Sent: Wednesday, June 14, 2017 9:27 AM To: AKOpsProdEOCTL; AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; Schinagl, Werner; Fortenberry, Christopher; AK, HSSEE Env Adv East; AK, OPS FSI Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A; Dean, lames A Subject: Flaring Event at FS1 To: AOGCC Reporting CC: Victoria Loepp, AOGCC aogcc.reporting (o)alaska.gov From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 05/19/2017 16:05 and stopping at 05/19/2017 16:37 with a volume of 6667 (MSCF). The event was due to a shutdown of T/Compressor 1804 due to a problem associated with F-61AV. The event stopped when 1804 was restarted. A flaring event occurred at FS1 starting at 05/19/2017 16:05 and stopping at 05/19/2017 17:14 with a volume of 431 (MSCF). The event lasted for 69 minutes and was due to STV -IP Compressor 1825 unloading due to low gas rates. The event stopped when 1825 was reloaded. A flaring event occurred at FS1 starting at 06/12/2017 16:45 and stopping at 06/12/2017 18:00 with a volume of 610 (MSCF). The event lasted for 75 minutes and was due to depressurizing Common Line 18B to flare due to a leaking valve. The event stopped when depressurization was completed. Thanks, Jennifer Blake EOC Production Optimization Team Lead Office (907) 564-5926 Cell (907) 830-6204 Jennifer.blakePbp.com Flare Start Date 05/01/2017 Flare End Date 05/31/2017 FSI Flare Report Total Volume (MSCF) 9697 Report Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume 17-152 Other 05/09/2017 7:45:00 am 8:05.00 am 20 min No No Yes BP7\GRIMD0 2500 Determination Cause High gas transit line pressure mused by CGF booster cool stop. Action Taken CGF booster loaded up and completed the cool stop. 17-166 Other 05/13/2017 5:30:00 am 7:00:00 am 90 min No No Yes BP1\GRIMDO 99 Determination Cause Depressurizing 5D and 58 for choke repairs at drill site. Action Taken Depressurization completed. 17-179 Flare Relief 05/19/2017 4:05:00 pm 5:14:00 pm 69 min No Determination Cause STV -IP TIC 1825 unloaded due to low gas rates. Action Taken Loaded STV/IP 1825 T/C. No No BP1\BUTLRM 431 Total Volume (MSCF) 9697 Generated 06/09/2017 2:22:08PM Page 3 of 9 STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number2. 0290000028 Facility Name PBU FS 1 3. Field PBU - EOA 4. Operator BP 5. Month/Year of Disposition June -2017 Disposition Volume MCF 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold Q Pool Name Pool Code Percent 7. Reinjected 0 PRUDHOE 640150 100.00% B. Flared or vented 1 hour or less 1,953 9. Flared or vented more than 1 hour (see instr.) 14,611 10. Pilot and Purge 21,568 11, Assist Gas 93,874 12. Fuel gas used in lease operations. 542,655 13. Other (see instructions) 0 Official Use Only Authorization 11 hr: Safety / �� / l MCF 14. TOTAL VOLUME (ITEMS 6-12) 674,661 Lease Use MCF 15. NGL Gas Equivalent 0 Conservation MCF 16. Purchased gas 0 Waste: MCF 17. Transferred from: COE 143,301 18. Transferred to: (Express as a negative #) CGF & CCP -51,868,113 Commissioner Date 19, Remarks: I hereby certify that the foregoing is true and correct to the best of my knowledge. ��`�/ �� Note: All volumes must be corrected Signature Title Manager Production Taxes and Ro aloes Alaska to pressure of 14.65 psis and to a 7 temperature of 60o F. Authority 20 Printed Name Diane Colley Phone (907) 564-5775 Date / AAC25.235. Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate DATE TIME BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - FS -1 GAS FLARING INCIDENT REPORT June 2017 Not required for unplanned events <= 1 hr ACTION TAKEN TO ELIMINATE CAUSE Not required for unplanned events <= 1 hr TOTAL 0 Unplanned Events < 1 Hour 0 Unplanned Events > 1 Hour 14,611 Unplanned events greater than 1 hour 1,953 exceeding 5,000 MCF DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 6/12/2017 1645-1800 2,639 See attachments See attachments 6/23/2017 1013-1200 113 93,874 6/23/2017 1013-2359 11,859 TOTAL 14,611 Planned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 6/5/2017 1410-1500 1,224 See attachments See attachments 6/9/2017 0400-0455 683 6/25/2017 0910-0950 46 TOTAL 1,953 DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE See attachments TOTAL 0 See attachments Page 4 7/18/2017 11:37 AM TOTAL Unplanned Events < 1 Hour 0 Unplanned Events > 1 Hour 14,611 Planned Events < 1 hour and not 1,953 exceeding 5,000 MCF Planned Events > 1 hour or 0 exceeding 5,000 MCF Pilot Purge 21,568 Assist 93,874 TOTAL FLARED VOLUME 132,006 See attachments Page 4 7/18/2017 11:37 AM Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Monday, July 3, 2017 11:14 AM To: AKOpsProdEOCTL; AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; Schinagl, Werner; Fortenberry, Christopher; AK, HSSEE Env Adv East; AK, OPS FS1 Facility CTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A; Dean, James A Subject: Flaring Event at FS1 To: AOGCC Reporting CC: Victoria Loepp, AOGCC aogcc. reportingaalaska.gov From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 06/12/2017 16:45 and stopping at 06/12/2017 18:00 with a volume of 2639 (MSCF). The event lasted for 75 minutes and was due to depressurization of the 18B commonline for the Make Piggable project. The event stopped when depressurization was completed. A flaring event occurred at FS1 starting at 06/23/2017 10:13 and stopping at 06/23/2017 23:59 with a volume of 11859 (MSCF). The intermittent event lasted for 826 minutes and was due to a plant shutdown and partial depressurization due to the CPS power failure. The event stopped when production was shut-in (isolated). Thanks, Jennifer Blake EOC Production Optimization Team Lead Office (907) 564-5926 Cell (907) 830-6204 Jennifer.blake@bp.com Flare Start Date 06/01/2017 Flare End Date 06/30/2017 FSI Flare Report Total Volume (MSCF) 16564 Report Numbs System Date StartTime Stop Time Duration Intermittent Black Smoke Planned Reported By Volume 17-196 Flare Relief 06/05/2017 2:10:00 pm 3.0000 pm 50 min No No Yes BP1\LYLEPE 1224 Determination Cause Depressuring DS18B/D CL for make piggable project. Action Taken Completed CL depressunng. Daily Volume (MSCF) 1224 17-201 Flare Relief 06/09/2017 4:00:00 am 4:55:00 am 55 min No No Yes BP1\GRIMDO 683 Determination Cause Depressurization of Annex for reboiler management upgrades, and PSV Pm's. Action Taken Completed depressurization. Daily Volume (MSCF) 683 17-205 Flare Relief 06/12/2017 4:45:00 pm 6:00:00 pm 75 min No No No BP1\MCCADJ 2639 Determination Cause Operational DE pressure of 18B Common Line to Flare. Action Taken Completed depressunng. Daily Volume (MSCF) 2639 17-225 Flare Relief 06/23/2017 10:13:00 am 12:00:00 pm 107 min Yes No No BP1\NOBLC4 113 Determination Cause Plant shutdown and partial depressurization due to CPS power failure Action Taken Shut in production and secured equipment 17-225 Flare Relief 06/23/2017 10:13:00 am 11:59:00 pm 826 min Yes No No BP1WOBLC4 11859 Determination Cause Plant shutdown and partial depressurization due to CPS power failure Action Taken Shut in production and secured equipment Daily Volume (MSCF) 11972 17-226 Flare Relief 06/25/2017 9:10:00 am 9:50:00 am 40 min No No Yes BP1\NOBLC4 46 Determination Cause Depressunzed5BCLfcr PSVPM's Action Taken Finished depressurization Daily Volume (MSCF) 46 Total Volume (MSCF) 16564 Generated 07/062017 2:44:22PM Page 4 of 10 STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSiTinN 1. Facility Number 0290000028 2. Facility Name PBU FS 1 3. Reid PBU - EOA 4. Operator • BP 5. MonthNear of Disposition Jul -2017 Disposition Volume MCF 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold Pool Name Pool Code Percent 7. Reinjected 0 PRUDHOE 640150 100.00% 8. Flared or vented 1 hour or less 13,460 9. Flared or vented more than 1 hour (see matt.) 19,071 10. Pilot and Purge 22,603 11. Assist Gas 67,157 12. Fuel gas used in lease operations. 416,332 13. Other (see instructions) 6 Official Use Only Authorization >1 he Safety g p MCF t�T - /a 14. TOTAL VOLUME (ITEMS 6-12) 538,623 Lease Use MCF 15. NGL Gas Equivalent 0 Conservation MCF 16. Purchased gas 0 Waste: MCF 17. Transferred from: CGF 147,932 Commissioner Dat 18. Transferred to: (Express as a negative #) CGF 8 CCP -49,786,304 19. Remarks: I hereby certify that the foregoing is true and correct to the best of my knowledge. Note: All volumes must be corrected Signature cae Title Manager Production Taxes ano Royalties Alaska to pressure of 14.65 psia and to a Printed Name Diane ColleyPhone (907) 564-5775 Date /� I temperature of 60o F. Authority 20 Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - FS -1 GAS FLARING INCIDENT REPORT July 2017 ---- 7/8/2017 ••.••- 0930-1025 .vcw.�c vcxmruvry yr ur4rucrvl&vuoc ACTION TAKEN TO ELIMINATE CAUSE 0430-0500 113 11,500 Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr 7/14/2017 2205-2216 76 428 7/29/2017 1522-1536 583 7/23/2017 0319-0350 TOTAL 12,159 0125-0142 Unplanned events greater than 1 hour 22,603 TOTAL DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 7/6/2017 1625-1740 18,000 See attachments See attachments TOTAL 18,000 7/1/2017 1352-1415 371 See attachments 7/2/2017 0430-0500 113 7/6/2017 0715-0735 126 7/6/2017 1455-1520 428 7/21/2017 1632-1642 15 7/23/2017 0319-0350 153 7/25/2017 0125-0142 95 22,603 TOTAL 1,301 7/25/2017 1522-1625 253 See attachments 7/29/2017 1925-2245 818 TOTAL 1,071 TOTAL Unplanned Events < 1 Hour 12,159 Unplanned Events> 1 Hour 18,000 Planned Events < 1 hour and not 1,301 exceeding 5,000 MCF Planned Events> 1 hour or 1,071 exceeding 5,000 MCF Pilot Purge 22,603 Assist 67,157 TOTAL FLARED VOLUME 122,291 See attachments ACTION TAKEN TO f See attachments Page 5 8/13/2017 3:49 PM Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Thursday, July 27, 2017 8:50 AM To: AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory, Schinagl, Werner; Fortenberry, Christopher; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A; Dean, James A Subject: Flaring Event at FS1 To: AOGCC Reporting CC: Victoria Loepp, AOGCC aogcc. reoorting(cD.a laska.gov From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 07/06/2017 16:25 and stopping at 07/06/2017 17:40 with a volume of 18000 (MSCF). The event lasted for 75 minutes and was due to high gas transit line pressure caused by CGF compressor problems. The event stopped when rates were reduced with wells shut-in. A flaring event occurred at FS1 starting at 07/08/2017 09:30 and stopping at 07/08/2017 10:25 with a volume of 11500 (MSCF). The event had a volume greater than 5000 (MSCF) and was due to a LPS T/C 1803 shutdown. The event stopped when the LPS T/C 1804 compressor was started up and rates were reduced. A flaring event occurred at FS1 starting at 07/25/2017 15:22 and stopping at 07/25/2017 16:25 with a volume of 253 (MSCF). The event lasted for 63 minutes and was due to depressurization of the 2B, 2D, 2E, and 5E commonlines for un - blinding of the 2C commonlines. The event stopped when the commonlines depressurization was complete. Thanks, Jennifer Blake EOC Production Optimization Team Lead Office (907) 564-5926 Cell(907)830-6204 Jennifer.blakepbp.com Flare StartDate 07/01/2017 Flare End Date 07/31/2017 FSS Flare Report Total Volume (MSCF) 32531 Report Numbs System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume 17-239 Flare Relief 07/01/2017 1:52:00 pm 2:15:00 pm 23 min No No Yes BP1\8ELLZ0 371 Determination Cause Depressurized C -HP separator and C HP gas scrubber to change out L-14 spool. Action Taken Depressurized C -HP separator and C HP gas scrubberto flare header pressure and blocked in going to flare. Daily Volume (MSCF) 371 17-241 Flare Relief 07/02/2017 4:30:00 am 5:00:00 am 30 min No No Yes BP1\GRIMDO 113 Determination Cause Depressurize 5B,5D, 5E for maintenance activities. Action Taken Complete depressurization. Daily Volume (MSCF) 113 17-250 Flare Relief 07/06/2017 7:15:00 am 7:35:00 am 20 min No No Yes BP7\GRIMDO 126 Determination Cause Depressurizing 2D and 2B oommonlines to flare header pressure for make piggable project. Action Taken Completed depressurization 17-250 Flare Relief 07/06/2017 2:55:00 pm 3:20:00 pm 25 min No No Yes BP1\GRIMD0 428 Determination Cause Depressurizing 2C and 2E oommonlines to flare header pressure for make piggable project. Action Taken Completed depressurization 17-250 Flare Relief 07/06/2017 4:25:00 pm 5:40:00 pm 75 min No No No BPI\GRIMDO 18000 Determination Cause High gas transit line pressure caused by CGF compressor problems. Flare for field. Action Taken Shut in wells. Field stabilized at lower rate. Daily Volume (MSCF) 18554 17-284 Other 07/21/2017 4:32:00 pm 4:42:00 pm 10 min No No Yes BP7\NOBLC4 15 Determination Cause -RC 1804 Startup. The starting Copus motor vents to flare. Action Taken Completed Start up of 1804 compressor Daily Volume (MSCF) 15 17-287 Controlled Blowdoom 07/23/2017 3:19:00 am 3:50:00 am 31 min No No Yes BP7\HUNTL2 153 Determination Cause Depressuring 1C CL forwork Action Taken Depressuring of 1C complete Daily Volume (MSCF) 153 17-295 Controlled Blowdo 07/25/2017 1:25:00 am 1:42:00 am 17 min No No Yes BP1\HUNTL2 95 Determination Cause Depressuring 1D CL for upcoming work Action Taken Completed depressuring of 1 D CL 17-295 Controlled Blowdown 07/25/2017 3:22:00 pm 4:25:00 pm 63 min No No Yes BP1\NOBLC4 253 Determination Cause Depressurize 2B / 2D / 2E / 5E for un blinding of 2C C/L Action Taken Completed depressurization of C/L's 2B / 2D / 2E / 5E Generated 08/15/2017 1:28:23PM Page 8 of 15 Flare Start Date 07101/2017 Flare End Date 07/31/2017 17-302 Controlled Biowdown 07/29/2017 7:25:00 pm 10:45:00 pm 200 min No Determination Cause Depressudng 12B and 12C common lines for make piggable project. Action Taken Finished with depressure No Yes BP1\OTTOKL 818 Daily Volume (MSCF) 1401 Total Volume (MSCF) 32531 Generated 08/15/2017 1:28:23PM Page 9 of 15 Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Friday, August 25, 2017 3:31 PM To: AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A; Starck, Jennifer L; Bessler, Mark Subject: Flaring Events at FS1 Follow Up Flag: Follow up Flag Status: Flagged To: AOGCC Reporting CC: Victoria Loepp, AOGCC aogcc. report) ng(c)alaska. qo From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 07/29/2017 19:25 and stopping at 07/29/2017 22:45 with a volume of 818 (MSCF). The event lasted for 200 minutes and was due to depressurizing 12B and 12C commonlines for the Make Piggable project work. The event stopped when depressurization was complete. A flaring event occurred at FS1 starting at 08/09/2017 13:15 and stopping at 08/09/2017 14:00 with a volume of 12500 (MSCF) and was due to high transit gas pressure caused by a CGF compressor shutdown. The event stopped when rate was cut and the CGF compressor was restarted. Thanks, Jennifer Blake EOC Production Optimization Team Lead Office (907) 564-5926 Cell (907) 830-6204 lennifer.blake@bp.com STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PROn11CFn rAS ni-qpnciTinti 1. Facility Number 0290000028 2. Facility Name PBU FS 1 3. Field PBU - EOA 4. Operator ... • BP 5. Monthlyear of Disposition Au ust-2017 Disposition Volume MCF 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold Pool Name PoolCode Percent 7. Reinjected 0 PRUDHOE 640150 100.00% B. Flared or vented 1 hour or less 12,626 9. Flared or vented more than 1 hour (see instr.) 0 10. Pilot and Purge 22,452 11, Assist Gas 61,954 12. Fuel gas used in lease operations. 429,088 13. Other (see instructions) 0 Official Use Only Authorization>1 hr: Safety MCF 14. TOTAL VOLUME (ITEMS 6-12) 526,120 Lease Use MCF 15. NGL Gas Equivalent 0 Conservation MCF 16. Purchased gas Waste: MCF 17. Transferred from: CGF 143,938 Commissioner Date 18. Transferred to: (Express as a negative #) CGF 8 CCP -62,214,571 19. Remarks: I hereby certify that the foregoing is true and correct to the best of my knoviledge. Note: All volumes must be corrected Signature Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psis and to a �/ Printed Name Diane ColleyPhone (907) 564-5775 Dateq//I I temperature of 60o F. Authority 20 A Form 10-422 Rev. 512009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT- FS -1 GAS FLARING INCIDENT REPORT August 2017 junplanneo events less than or equal to 1 hour 0 DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 8/9/2017 1315-1400 12,500 Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr TOTAL 12,500 8/21/2017 1700-1710 Unplanned events greater than 1 hour 8/31/2017 0300-0330 81 DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE Planned events greater than 1 hour See attachments See attachments TOTAL 0 Planned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 8/21/2017 1430-1440 15 See attachments See attachments 8/21/2017 1455-1505 15 8/21/2017 1700-1710 15 8/31/2017 0300-0330 81 TOTAL 126 Planned events greater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE See attachments See attachments TOTAL 0 TOTAL Unplanned Events < 1 Hour 12,500 Unplanned Events> 1 Hour 0 Planned Events < 1 hour and not 126 exceeding 5,000 MCF Planned Events> 1 hour or 0 exceeding 5,000 MCF Pilot Purge 22,452 Assist 61,954 TOTAL FLARED VOLUME 97,032 Page 3 9/14/2017 4:31 PM Flare StartDate 08/01/2017 Flare End Date 08/31/2017 FS1 Flare Report Total Volume (MSCF) 12626 Report Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume 17-339 Other 08/21/2017 2:30:00 pm 2:40:00 pm 10 min No Yes Yes BPI \NOBLC4 15 Determination Cause Attempted to start 1803 LIPS compressor - Starting copus vents to STV flare. Black smoke because of liquids being trapped in the low point on the STV flare candles. Action Taken Attempted start was shut down due to copus starter not disengaging 17-339 Other 08/21/2017 2:55:00 pm 3:05:00 pm 10 min No No Yes BPI\NOBLC4 15 Determination Cause -RC 1803 attempt to start#2- Copus starting motor vents to STV flare Action Taken Compressor did not start 17-339 Other 08/21/2017 5:00:00 pm 5:10:00 pm 10 min No No Yes BP1 W OBLC4 15 Determination Cause T\C 1803 Startup- Copus starting motorvents to STVflare Action Taken Compressor started Daily Volume (MSCF) 17-351 Controlled Blowdown 08/31/2017 3:00:00 am 3:30:00 am 30 min No No Yes BPI\BELLZO Determination Cause Shut down and depressurized 1D common line. We need to remove blind in 12C common line and 1D purge divert leaks. Action Taken Blocked in Flare once 1D common line was depressurized Daily Volume (MSCF) 45 81 81 Total Volume (MSCF) 12626 Generated 09/06/2017 4:06:25PM Page 4 of 11 Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Friday, August 25, 2017 3:31 PM To: AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL, AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A; Starck, Jennifer L; Bessler, Mark Subject: Flaring Events at FS1 Follow Up Flag: Follow up Flag Status: Flagged To: AOGCC Reporting CC aogcc.reporting(a alaska.gov Victoria Loepp, AOGCC From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 07/29/2017 19:25 and stopping at 07/29/2017 22:45 with a volume of 818 (MSCF). The event lasted for 200 minutes and was due to depressurizing 12B and 12C commonlines for the Make Piggable project work. The event stopped when depressurization was complete. A flaring event occurred at FS1 starting at 08/09/2017 13:15 and stopping at 08/09/2017 14:00 with a volume of 12500 (MSCF) and was due to high transit gas pressure caused by a CGF compressor shutdown. The event stopped when rate was cut and the CGF compressor was restarted. Thanks, Jennifer Blake EOC Production Optimization Team Lead Office (907) 564-5926 Cell (907) 830-6204 Jennifer. blake@bp.com STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PROnLICFn c,nS n1cpnc1T1nti 1. Facility Number 2. Facility Name 0290000028 PB FS 1 Disposition 3. Field PBU - EOA Volume MCF 4. Operator 5. Month/year of Disposition BP Se tember-2017 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold 0 Pool Name Pool Code Percent 7, Reinjected 0 PRUDHOE 640150 100.00% 8. Flared or vented 1 hour or less 113 9. Flared or vented more than 1 hour (see instr.) 0 10. Pilot and Purge 21,884 11. Assist Gas 59,359 12. Fuel gas used in lease operations. 572,575 13. Other (see instructions) p Official Use Only Authorization >1 hr: Safety MCF 14. TOTAL VOLUME (ITEMS 6-12) 653,931 Lease Use MCF 15, NGL Gas Equivalent 0 Conservation MCF 16. Purchased gas p Waste: MCF 17. Transferred from: CGF 153,476 Commissioner Date 18. Transferred to: (Express as a negative #) CGF & CCP -62,059,814 19. Remarks. I hereby certify that the foregoing is true and correct to the best of my knowledge. 6 � Note: All volumes must be corrected Signature_ Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psia and to a /�J, temperature of 60o F. Authority 20 Printed Name Diane Colley Phone (907) 564-5775 Date / i AAC25.235. Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT- FS -1 GAS FLARING INCIDENT REPORT September 2017 Unplanned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr TOTAL 0 Unplanned events greater than 1 hour TOTAL 9/24/2017 0110-0205 TOTAL TOTAL Unplanned Events < 1 Hour Unplanned Events > 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME See attachments 0 113 See attachments 113 See attachments 0 TOTAL 0 0 113 0 21,884 59,359 81,356 See attachments See attachments ACTION TAKEN TO E See attachments Page 3 10/12/2017 2:33 PM Flare Start Date 09/01/2017 Flare End Date 09/30/2017 FSI Flare Report Total Volume (MSCF) 113 Report Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume 17-382 Controlled Blowdown 09/24/2017 1:10:00 am 20500 am 55 min No No Yes BP1\LYLEPE 113 Determination Cause Shut down DS5 for Test Header spool and header valve replacement. This event depressured 5D, 5B and 5E Common Lines. Action Taken Completed depressuring. Daily Volume (MSCF) 113 Total Volume (MSCF) 113 Generated 10/02/2017 2:13:02PM Page 2 of 8 STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY RFPnRT nF PPnni irCn fl- n0 n1c1nr%c+iTir..i Farm 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Tuesday, October 31, 2017 8:28 AM To: AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A; Starck, Jennifer L; Bessler, Mark Subject: Flaring Events at FS1 To: AOGCC Reporting CC: Victoria Loepp, AOGCC aoocc. reporting (5)alaska.gov From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 10/27/2017 01:20 and stopping at 10/27/2017 04:37 with a volume of 1368 (MSCF). The event lasted for 197 minutes and was due to spin cooling 1803 turbine compressor for water wash.. The event stopped when spin cooling was completed. A flaring event occurred at FS1 starting at 10/28/2017 21:50 and stopping at 10/28/2017 23:59 with a volume of 896 (MSCF). The event lasted for 129 minutes) and was due to spin cooling 1804 turbine compressor for water wash.. The event stopped when spin cooling was completed. Thanks, Jennifer Blake EOC Production Optimization Team Lead Office (907) 564-5926 Cell (907) 830-6204 Jennifer.bla ke@bp.com Flare Start Date 10/01/2017 10/27/2017 1:20:00 am 4:37:00 am 197 min No Determination Cause Flare End Date 10/31/2017 Action Taken Completed spin cooling. F51 Flare Report Total Volume (MSCF) 7350 Report T\C 1603 spin dry after water wash Action Taken Numbs System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume 17-399 Controlled Blowdown 10/19/2017 11:49:00 pm 11:59:00 pm 10 min No No Yes BP1\NOBLC4 284 Determination Cause Depressurize CHP from 400psi to 3psi in order to replace spool piece DS of L14 Completed attempted start Action Taken CHP depressurized Daily Volume (MSCF) 284 17-414 Other 10/27/2017 1:20:00 am 4:37:00 am 197 min No Determination Cause T\C 1803 spin cooling Action Taken Completed spin cooling. 17-414 Other 10/27/2017 5:00:00 pm 6:00:00 pm 60 min No Determination Cause T\C 1603 spin dry after water wash Action Taken Completed spin dry 17-414 Other 10/27/2017 9:30:00 pm 9:40:00 pm 10 min No Determination Cause TIC 1803 Attempted start Action Taken Completed attempted start No Yes BPI\NOBLC4 1368 No Yes BPIWOBLC4 21 No Yes BP1\NOBLC4 69 17-414 Other 10/27/2017 9:50:00 pm 10:00:00 pm 10 min No No Yes BPI\NOBLC4 69 Determination Cause T\C 1803 Attempted start#2 Action Taken Completed start attempt #2 Daily Volume (MSCF) 1527 17-415 Other 10/28/2017 9:50:00 pm 11:59:00 pm 129 min No No Yes BP1\NOBLC4 896 Determination Cause T\C 1804 spin cooling Action Taken Completed spin cooling. 17-416 Other 10/29/2017 12:00:00 am 12:50:00 am 50 min No Determination Cause T\C 1804 spin cooling Action Taken Completed spin cooling. Daily Volume (MSCF) 896 No Yes BPI\NOBLG4 347 Daily Volume (MSCF) 347 Total Volume (MSCF) 7360 Generated 11/03/2017 1:17:48PM Page 5 of 8 BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT- FS -1 GAS FLARING INCIDENT REPORT October 2017 junplanneo events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 10/22-23/2017 2351-0027 4,306 Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr TOTAL 4,306 Unplanned events greater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE See attachments See attachments TOTAL 0 Planned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 10/19/2017 2349-2359 284 See attachments See attachments 10/27/2017 1700-1800 21 10/27/2017 2130-2140 69 10/27/2017 2150-2200 69 TOTAL 443 DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE 10/27/2017 0120-0437 1,368 See attachments 10/28-29/17 2150-0050 1,243 TOTAL 2,611 TOTAL Unplanned Events < 1 Hour 4,306 Unplanned Events> 1 Hour 0 Planned Events < 1 hour and not 443 exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME 2,611 25,734 64,409 97,503 See attachments Page 4 11/13/2017 9:27 AM STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 0290000028 2. Facility Name PBU FS 1 3. Field PBU - EOA 4. Operator BP 5. Monthfyear of Disposition I November -2017 Disposition Volume MCF 20. Forproduction from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold p Pool Name Pool Code Percent 7. Reinjected U PRUDHOE 640150 100.00% 8. Flared or vented 1 hour or less 0 9. Flared or vented more than 1 hour (see instr.) 34,486 10. Pilot and Purge 22,172 11. Assist Gas 55,023 12. Fuel gas used in lease operations. 580,284 13. Other (see instructions) 0 Official Use Only Authorization >1 hr: �rj 3/16(15 Safety � J y 96 MCF l f 14. TOTAL VOLUME (ITEMS 6-12) 691,965 Lease Use MCF 15. NGL Gas Equivalent Conservation MCF 16. Purchased gas 0 Waste MCF 17. Transferred from: CGF 161,381 3 /C` AQ lie( 18. Transferred to: (Express as a negative #) CGF &CCP -64,237,385 Commissioner Date 19. Remarks: I hereby certify that the foregoing is true and correct to the best of my knowledge. l/�//y�,Q�� Note: All volumes must be corrected Signature `� �"="��l Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 Printed Name Diane ColleyPhone (907) 564-5775 Date ��' Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - FS -1 GAS FLARING INCIDENT REPORT November 2017 DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE Not required for unplanned events <= 1 hr Not required for unplanned events <= 1 hr TOTAL 0 ..,z I Irvin VULUIVIt UESCKIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 11/16/2017 0905-1027 7,972 See attachments See attachments 11/16/2017 1200-1430 26,042 11/30/2017 1450-1610 472 TOTAL 34,486 Planned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE See attachments See attachments TOTAL 0 TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE TOTAL Unplanned Events < 1 Hour Unplanned Events > 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events > 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME See attachments 0 TOTAL 0 34,486 0 0 22,172 55,023 111,681 See attachments Page 3 12/13/2017 9:07 AM Flare StartDate 11/01/2017 Flare End Date 11/30/2017 FS1 Flare Report Total Volume (MSCF) 14486 Report Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volu •e 17-429 Flare Relief 11/16/2017 9:05:00 am 10:27:00 am 82 min No No No BPI\OTTOKL 7972 Determination Cause LPS T\C 1804 shutdown because of a problem associated with Fire and Gas cutovers. Action Taken Shut in wells, DS18-4,3. DSS -23,11,21. DS2-22,8,7,15. 17-429 Flare Relief 11/16/2017 12:00:00 pm 2:30:00 pm 150 min No No No BP1\OTTOKL 26042 Determination Cause LPS T\C 1803 shutdown because of a problem associated with wires crossed on ere and gas s/d trip. Action Taken 1603 T/C restarted. Daily Volume (MSCF) 34014 17-433 Flare Relief 11/30/2017 2:50:00 pm 4:10:00 pm 80 min No No No BP1\OTTOKL 472 Determination Cause STV -IP -RC 1825 down to idle for Fire & Gas cutover in that module. Action Taken Loaded STV/IP T/C. Daily Volume (MSCF) 472 Total Volume (MSCF) 34486 Generated 12/06/2017 9:22:30AM Page 3 of 6 Link, Liz M (DOA) From: AKOpsProdEOCTL <AKOPSPCCEOCTL@bp.com> Sent: Monday, December 18, 2017 2:21 PM To: AOGCC Reporting (DOA sponsored) Cc: Loepp, Victoria T (DOA); Benson, Gary A; Arthur, Gregory; AK, HSSEE Env Adv East; AK, OPS FS1 Facility OTL; AK, OPS FS1 OSM; Glover, Robin; Buckbee, Rachel A; Starck, Jennifer L, Bessler, Mark Subject: Flaring Events at FS1 To: AOGCC Reporting CC: Victoria Loepp, AOGCC aogcc.reporting (a)alaska.gov From: Jennifer Blake, GPB Production Team Leader A flaring event occurred at FS1 starting at 11/16/2017 09:05 and stopping at 11/16/2017 10:27 with a volume of 7972 (MSCF). The event lasted for 82 minutes and was due to a LPS Turbine Compressor 1804 shutdown caused by a problem associated with the Fire and Gas cutovers. The event stopped when spin production rate was cut. A flaring event occurred at FS1 starting at 11/16/2017 12:00 and stopping at 11/16/2017 14:30 with a volume of 26042 (MSCF). The event lasted for 150 minutes and was due to a LPS T\C 1803 shutdown caused by a problem associated with wires crossed on the fire and gas s/d trip. The event stopped when TIC 1803 was restarted. A flaring event occurred at FS1 starting at 11/30/2017 14:50 and stopping at 11/30/2017 16:10 with a volume of 472 (MSCF). The event lasted for 80 minutes and was due to ramping down STV -IP T\C 1825 to idle for Fire & Gas cutover in that module. The event stopped when the T/C was restarted. Thanks, Jennifer Blake EOC Production Optimization Team Lead Office (907) 564-5926 Cell (907) 830-6204 Jennifer.blake@bo.com STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 0290000028 2. Facility Name PBU FS 1 3. Field PBU - EOA 4. Operator BP 5. MonthNear of Disposition I December -2017 Disposition Volume MCF 20. Forproduction from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold 0 Pool Name Pool Code Percent 7. Reinjected 0 PRUDHOE 640150 100.00% 8. Flared or vented 1 hour or less 0 9. Flared or vented more than 1 hour (see instr.) 1,625 10. Pilot and Purge 22,710 11. Assist Gas 56,418 12. Fuel gas used in lease operations. 617,174 13. Other (see instructions) O Official Use Only Authorization >1 hr: b !4 �j(l �a �/ � Safety Ify 6 �) MCF 14. TOTAL VOLUME (ITEMS 6-12) 697,927 Lease Use MCF 15. NGL Gas Equivalent 0 Conservation MCF 16. Purchased gas 0 Waste: MCF 17. Transferred from: CGF 163,755 // 3 _ /� _/ Commissioner 7-�r�--- Date 18. Transferred to: (Express as a negative # CGF & CCP ( p g ) -77,538,151 19. Remarks: I hereby certify that the foregoing is true and correct to the best of my knowledge. �� Note: All volumes must be corrected Signature Title Manager Production Taxes and Royalties Alaska t0 pressure of 14.65 psia and to a Printed Name Diane ColleyPhone (907) 564-5775 Date temperature of 60o F. Authority 20 / / �> _) SAAr9.5 91 Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT- FS -1 GAS FLARING AND VENTING INCIDENT REPORT December 2017 events less than oreaualto Page 4 1/12/2018 9:58 AM Not required for events <= 1 hr Not required for events <= 1 hr TOTAL 0 Unplanned events greater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 12/21/2017 0630-1300 1,625 See attachments See attachments TOTAL 1,625 Planned events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE Not required for events <= 1 hr Not required for events <= 1 hr TOTAL 0 Planned events greater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE See attachments See attachments TOTAL 0 TOTAL Unplanned Events < 1 Hour 0 Unplanned Events> 1 Hour 1,625 Planned Events < 1 hour and not 0 exceeding 5,000 MCF Planned Events > 1 hour or 0 exceeding 5,000 MCF Pilot Purge 22,710 Assist 56,418 TOTAL FLARED VOLUME 80,753 Page 4 1/12/2018 9:58 AM Flare Start Date 12/01/2017 Flare End Date 12/31/2017 FS1 Flare Report Total Volume (MSCF) Report Numbs System Date StartTime Stop Time Duration Intermittent Black Smoke Planned Reported By Volume 17-456 Flare Relief 12/21/2017 6:30:00 am 1:00:00 pm 390 min No No No BP1\MCCADJ 1625 Determination Cause STV-IP TRC 1825 shutdown due to a problem associated with the ASD Drive And Transmitter. Action Taken Loaded STV/IP T/C. Electricians trouble shot ASD and 1825 was re started and loaded. Total Volume (MSCF) Generated 01/08/2018 10:33:46AM Page 4 of 9