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Alaska Oil and Gas Conservation Commission
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HomeMy WebLinkAboutPBU GC 1 - BP Exploration (Alaska), Inc.STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number 2. Facility Name
0290000031 PBU GC 1
Disposition
3. Field
PBU - WOA
Volume MCF
4. Operator 5. Month/Year of Disposition
BP Janua -2019
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name
Pool Code
Percent
7. Reinjected
0
PRUDHOE
640150
94.81%
LISBURNE
640144
0.00%
8. Flared or vented 1 hour or less
470
MIDNIGHT SUN
640158
0.43%
PT MCINTYRE
640180
4.76%
9. Flared or vented more than 1 hour (see instr.)
79,116
10. Pilot and Purge
51,615
11. Assist Gas
12. Fuel gas used in lease operations.
816,793
13. Other (see instructions)
0
Official Use Only
Authorization >1 hr:
1�
Safety
1!6
MCF
14. TOTAL VOLUME (ITEMS 6-12)
947,994
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste:
MCF
17. Transferred from:
nV� /^ ) C
' V Commissioner Date
18. Transferred to: (Express as a negative #) CGF
19. Remarks:
-66,775,419
l
I hereby certify t le foregoing is true and jorrect to the best of my knowledge.
i
Signature Title Head of Control BP Alaska
Printed Name David Knapp Phone (907) 564-5775 Date Z/t
Note: All volumes must be corrected
to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
Form 10-422 Rev. 5/2009 inicToi 1rT1nni0 nr, .--
PI
nplanned events less than or equal
DATE TIME
10/10/2019 0756-0801
10/13/2019 1149-1215
10/14/2019 1700-1707
TOTAL
nplanned events greater than 1 hour
DATE TIME
1/15/2019 1015-1345
TOTAL
anned events less than or equal to 1
DATE TIME
1/25/2019 2011-2017
TOTAL
anned events greater than 1 hour
DATE TIME
TOTAL
Unplanned Events < 1 Hour
Unplanned Events > 1 Hour
Planned Events < 1 hour and not
exceeding 5,000 MCF
Planned Events > 1 hour or
exceeding 5,000 MCF
Pilot Purge
Assist
TOTAL FLARED VOLUME
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - GC-1
GAS FLARING AND VENTING INCIDENT REPORT
January 2019
to 1 hour
VOLUME DESCRIPTION OF INCIDENT & CAUSE
70 Not required for events <= 1 hr
240
80
hour
390
ME DESCRIPTION OF INCIDENT & CAUSE
79,116 See Attachments
79,116
DESCRIPTION OF INCIDENT & CAUSE
80 Not required for events <= 1 hr
0
TOTAL
390
79,116
80
0
51,615
0
131,201
DESCRIPTION OF INCIDENT & CAUSE
See Attachments
ACTION TAKEN TO ELIMINATE CAUSI
Not required for events <= 1 hr
ACTION TAKEN TO ELIMINATE CAUSE
See Attachments
Not required for events <= 1 hr
ACTION TAKEN TO ELIMINATE CAUSE
See Attachments
Page 6
2/13/2019
12:55 PM
Flare StartDate 01/01/2019
Flare End Date 01/31/2019
GC1 Flare Report Total Volume (MSCF) 79586
Report
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
19-16 Flare Relief 01/15/2019 10:15:00 am 1:45:00 pm 210 min No No No BPI\SHELTI 79116
Determination Cause High gas transit line pressure caused by CGF compressor problems due to losing a tandem compressor
Action Taken Flaring stopped once rates were cut and transit pressure was down.
Total Volume (MSCF) 79586
Generated 02/06/2019 9:23:02AM Page 6 of 8
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number 2. Facility Name
0290000031 PBU GC 1
Disposition
3. Field
PBU - WOA
Volume MCF
4. Operator 5. MonthNear of Disposition
BP Februa -2019
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name
Pool Code
Percent
7. Reinjected
0
PRUDHOE
640150
95.12%
LISBURNE
640144
0.00%
8. Flared or vented 1 hour or less
15,600
MIDNIGHT SUN
640158
0.57%
PT MCINTYRE
640180
4.31%
9. Flared or vented more than 1 hour (see instr.)
6,271
10. Pilot and Purge
46,296
11. Assist Gas
12. Fuel gas used in lease operations.
833,612
13. Other (see instructions)
0
Official Use Only
Authorization >1 hr:
'"z�e
Safety
/ 7
l�
MCF
14. TOTAL VOLUME (ITEMS 6-12)
901,779
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste:
MCF
17. Transferred from:
0
Commissioner bate
18. Transferred to: (Express as a negative #) CGF
-58,972,105
19. Remarks:
I hereby certify th a foregoing is true and correct to the best of my knowledge.
` Note: All volumes must be corrected
Signature Title Head of Control BP Alaska to pressure of 14.65 psia and to a
Printed Name David Knapp Phone (907) 564-5775 Date temperature of 60o F. Authority 20AAC25.235.
Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - GC-1
GAS FLARING AND VENTING INCIDENT REPORT
February 2019
(Unplanned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
2/25/2019 1909-1956 15,600 Not required for events <= 1 hr Not required for events <= 1 hr
TOTAL 15,600
Unplanned events greater than 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
2/15/2019 1000-1400 50 See Attachments See Attachments
2/24/2019 0000-2400 6,221
TOTAL 6,271
Planned events less than or equal to 1 hour
E DESCRIPTION OF INCIDENT & CAUSE
Not required for events <= 1 hr
ACTION TAKEN TO ELIMINATE CAUSI
Not required for events <= 1 hr
Page 6
TOTAL
0
Planned events greater than 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
See Attachments See Attachments
TOTAL
0
TOTAL
Unplanned Events < 1 Hour
15,600
Unplanned Events > 1 Hour
6,271
Planned Events < 1 hour and not
0
exceeding 5,000 MCF
Planned Events > 1 hour or
0
exceeding 5,000 MCF
Pilot Purge
46,296
Assist
0
TOTAL FLARED VOLUME
68,167
3/12/2019
3:34 PM
Flare Start Date 02/01/2019
Flare End Date 02/28/2019
Report GC1 Flare Report
Total Volume (MSCF) 21871
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
19-37 Flare Relief 02/15/2019 10:00:00 am 2:00:00 pm 240 min Yes
No No BPIIDELATI 50
Determination Cause Erratic gas supply to LP and IP compressors via the Annex. GC2 wells were being brought online following their plant upset.
Action Taken No response taken as this was deemed to be of short duration.
19-43 Flare Relief 02/24/2019 12:00:00 am 12:00:00 am 1440 min Yes No
No BP1\SPRINGG 6221
Determination Cause In process of determining excess LP gas source.
Action Taken Manually opened gas flare
Generated 03/04/2019 2:52:17PM
Page 4 of 5
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number
0290000031
2. Facility Name
PBU GC 1
3. Field
PBU - WOA
4. Operator
BP
5. Month/Year of Disposition
I March-2019
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume,
6. Sold
0
Pool Name
Pool Code
Percent
7. Reinjected
PRUDHOE
640150
94.86%
LISBURNE
640144
0.00%
8. Flared or vented 1 hour or less
643
MIDNIGHT SUN
640158
0.87%
PT MCINTYRE
640180
4.27%
9. Flared or vented more than 1 hour (see instr.)
939
10. Pilot and Purge
51,025
11. Assist Gas
0
12. Fuel gas used in lease operations.
926,088
13. Other (see instructions)
0
Official Use Only
Authorization >1 hr,
(�
If
Safety
MCF
14. TOTAL VOLUME (ITEMS 6-12)
978,695
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste:
IMCF
17. Transferred from:
0
Y (
Commissioner Date
18. Transferred to: (Express as a negative #) CGF
-66,427,581
19. Remarks:
I hereby certify that t e oing is true andLcorrect o the best of my knowledge.
Note: All volumes must be corrected
Signature Title Head of Control, BP Alaska to pressure of 14.65 psia and to a
Printed Name David Knapp Phone (907) 564-5775 Date temperature of 60o F. Authority 20
AAC25.235.
Form 10-422 Rev. 5/2009 INSTRUCTIONS ON RFVFRSF SInF C.b... ;
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - GC-1
GAS FLARING AND VENTING INCIDENT REPORT
March 2019
jUnplanned events less than or equal to 1 hour
DATE TIME VOLUME
DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
3/13/2019 1914-1941
510 Not required for events <= 1 hr
Not required for events <= 1 hr
3/17/2019 1846-1856
53
3/25/2019 0559-0603
30
3/25/2019 1150-1151
12
3/25/2019 1151-1156
38
TOTAL
643
Unplanned events greater than 1 hour
DATE TIME VOLUME
DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
3/22/2019 2231-2400
506 See Attachments
See Attachments
3/23/2019 0112-0414
220
3/26/2019 1158-2352
149
TOTAL
875
Planned events less than or equal to 1 hour
DATE TIME VOLUME
DESCRIPTION OF INCIDENT &CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
Not required for events <= 1 hr
Not required for events <= 1 hr
TOTAL
0
Planned events greater than 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
3/2/2019 1517-1636
64 See Attachments See Attachments
TOTAL
64
TOTAL
Unplanned Events < 1 Hour
643
Unplanned Events > 1 Hour
875
Planned Events < 1 hour and not
0
exceeding 5,000 MCF
Planned Events > 1 hour or
64
exceeding 5,000 MCF
Pilot Purge
51,025
Assist
0
TOTAL FLARED VOLUME
52,607
Page 7
4/14/2019
3:00 PM
Flare StartDate 03/01/2019
Flare End Date 03/31/2019
GC1 Flare Report
Total Volume (MSCF) 1582
Report
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
19-49 Flare Relief 03/02/2019 3:17:00 pm 4:36:00 pm 79 min No No Yes BP1\SPRINGG 64
Determination Cause Flared off slugcatchers due to PM2 pigging run
Action Taken Flaring was permitted to continue while waiting for arrival of PM2 pig
19-65 Flare Relief 03/22/2019 10:31:00 pm 12:00:00 am 89 min Yes No No BP1\SPRINGG 506
Determination Cause K-108 IP compressor shutdown because of high temp
Action Taken Flaring was permitted to continue while GC operations personnel attempted to restart the equipment.
19-66 Flare Relief 03/23/2019 1:12:00 am 4:14:00 am 182 min Yes No No BP1\SPRINGG 220
Determination Cause K108 IP compressor shutdown because of a problem associated with temperature
K107 IP compressor would not run because of a problem associated with relay trip and unopening discharge valve
Action Taken Flaring was permitted to continue while GC operations personnel attempted repair of equipment.
19-69 Flare Relief 03/26/2019 11:58:00 am 11:52:00 pm 714 min Yes
Determination Cause V-01-0120A pressure exceeding 5 psig.
Action Taken none
No No BP1\JONESCC 135
19-69 Flare Relief 03/26/2019 11:58:00 am 11:47:00 pm 709 min Yes No No BPI\JONESCC 14
Determination Cause LP Flare Assist Gas FV-01-0610 open.
Action Taken none
Total Volume (MSCF) 1582
Generated 04/02/2019 10:10:59AM Page 4 of 5
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PROnl1CFn roS nispnciTilnti
1. Facility Number
0290000031
2. Facility Name
PBU GC 1
3. Field
PBU - WOA
4. Operator
BP
5. Month/Year of Disposition
A ri1-2019
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
Pool Name
Pool Code
Percent
7. Reinjected
0
PRUDHOE
640150
95.63%
LISBURNE
640144
0.07%
8. Flared or vented 1 hour or less
468
MIDNIGHT SUN
640158
0.74%
PT MCINTYRE
640180
3.56%
9. Flared or vented more than 1 hour (see instr.)
61,464
10. Pilot and Purge
49,506
11. Assist Gas
0
12. Fuel gas used in lease operations.
778,366
13. Other (see instructions)
0
Official Use Only
Authorization >1 h/r:
Safety
6 ,) yby
MCF
14. TOTAL VOLUME (ITEMS 6-12)
889,804/�//�
Lease Use
MCF
15. NGL Gas Equivalent
6
Conservation
MCF
16. Purchased gas
Waste:
MCF
17. Transferred from:
y
Commissioner Date
18. Transferred to: (Express as a negative #) CGF
-68 628 222
19. Remarks:
I hereby certify tha a foregoing is true ancorrect to the best of my knowledge.
tsignature Title Head of Control BP Alaska Note: All volumes must be correctedto pressure of 14.65 psia and to a
Printed Name David Knapp Phone (907) 564-4694 Date temperature of 60o F. Authority 20AA 2 .2
35.
Form 10-422 Rev. 5/2009 INSTPI ycTinNc ON DFvP:DCG ciniz:
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT-GC-1
GAS FLARING AND VENTING INCIDENT REPORT
April 2019
jUnplanned events less than or equal to 1 hour
DATE
TIME VOLUME
DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
4/1/2019
0707-0710
10 Not required for events <= 1 hr Not required for events <= 1 hr
4/3/2019
0404-0406
10
4/8/2019
1004-1015
70
4/14/2019
0050-0105
120
4/27/2019
0141-0156
140
TOTAL
350
jUnplanned events greater than 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT& CAUSE ACTION TAKEN TO ELIMINATE CAUSE
4/2/2019 0728-0911 20 See Attachments See Attachments
4/3/2019 0106-1146 272
4/5/2019 0010-1047 10
4/7/2019 0030-1642 30
4/10/2019 1300-1640 55,902
TOTAL 56,234
(Planned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
4/23/2019 2348-2353 8 Not required for events <= 1 hr Not required for events <= 1 hr
4/24/2019 0308-0315 30
4/24/2019 2140-2145 80
TOTAL 118
Planned events greater than 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT&CAUSE ACTION TAKEN TO ELIMINATE CAUSE
4/20/2019 0358-0512 5,230 See Attachments See Attachments
TOTAL
Unplanned Events < 1 Hour
Unplanned Events > 1 Hour
Planned Events < 1 hour and not
exceeding 5,000 MCF
Planned Events > 1 hour or
exceeding 5,000 MCF
Pilot Purge
Assist
TOTAL FLARED VOLUME
TOTAL
350
56,234
118
5,230
49,506
0
111,438
Page 7
5/11 /2019
11:54 AM
Flare StartDate 04/01/2019
Flare End Date 04/30/2019
GC1 Flare Report
Report Total Volume (MSCF) 61932
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
19-72 Flare Relief 04/02/2019 7:28:00 am 9:11:00 am 103 min Yes
No No BPIISPRINGG 20
Determination Cause LP/IP combination inadequate for current process conditions.
Action Taken No response taken as this was deemed to be of short duration.
19_74 Daily Volume (MSCF) 20
Flare Relief 04/03/2019 2:06:00 am 11:46:00 am 580 min Yes
No No BP1\JONESCC 225
Determination Cause LP Flaring: LP/IP combination inadequate for current process conditions.
Action Taken None
19-74 Flare Relief 04/03/2019 2:06:00 am 11:41:00 am 575 min Yes
No No BP1IJONESCC 47
Determination Cause LP Flaring.
Action Taken None
19-76 Flare Relief 04/05/2019 12:10:00 am 10:47:00 am 637 min Yes
No No BP116ROWNK 10
Determination Cause Flared due to fluctuating oil rate / IP compressor losing forward flow.
Action Taken No action taken due to short duration of flaring events each time
19-78 Daily Volume (MSCF) 10
Flare Relief 04/07/2019 12:30:00 am 4:42:00 pm 972 min Yes
No No BPIIBROWNK 30
Determination Cause Shut down and De -pressured K-3200fluctuating oil rates causing IP compressor to flare
Action Taken oil rates stabilized
Daily Volume (MSCF) 30
19-82 Flare Relief 04/10/2019 1:00:00 pm 4:40:00 pm 220 min No
No No BP1\DELATI 45833
Determination Cause High gas transit line pressure caused by CCP compressor problems due to booster shutdown.
Action Taken Gas was routed to CGF and GC1 and FS1 managed transit gas pressure by flaring until rates were reduced and equipment restarted.
19-82 Flare Relief 04/10/2019 1:05:00 pm 3:30:00 pm 145 min No -
No No BPI\DELATI 10069
Determination Cause High gas transit line pressure caused by CCP compressor problems due to booster pump shutdown. The LPS compression system PIOC
limit of 666 PSI was reached due to transit line pressure, tripping K7000.
Action Taken Equipment was restarted
Daily Volume (MSCF) 55902
Generated 05/05/2019 2:12:32PM
Page 9 of 12
Flare Start Date 04/01/2019
Flare End Date 04/30/2019
19-89 Flare Relief 04/20/2019 3:58:00 am 5:12:00 am 74 min Yes
Determination Cause CCP S/D machine for H2O wash
Action Taken WOA reduced Production rates
No Yes BP1\SPRINGG
5230
Daily Volume (MSCF) 5230
Total Volume (MSCF) 61932
Generated 05/05/2019 2:12:32PM
Page 10 of 12
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITIMI
1. Facility Number
0290000031
2. Facility Name
PBU GC 1
3. Field
PBU - WOA
4. Operator .
BP
5. MonthNear of Disposition
Ma -2019
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name
Pool Code
Percent
7. Reinjected
O
PRUDHOE
640150
96.26%
LISBURNE
640144
0.26%
8. Flared or vented 1 hour or less
6
MIDNIGHT SUN
640158
0.55%,263
PT MCINTYRE
640180
2.93%
9. Flared or vented more than 1 hour (see instr.)
408
10. Pilot and Purge
49,969
11. Assist Gas
0
12. Fuel gas used in lease operations.
796,398
13. Other (see instructions)
0
Official Use Only
Authorization >1 hr:
A
Safety
-/
�d v
MCF
14. TOTAL VOLUME (ITEMS 6-12)
853,038
Lease Use15.
MCF
NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste:
MCF
17. Transferred from:
6
Commissioner Date
18. Transferred to: (Express as a negative #) CGF
-68,477,918
19. Remarks:
I hereby certify th foregoing is true Ind correct to the best of my knowledge.
Note: All volumes must be corrected
Signature Title Head of Control. BP Alaska to pressure of 14.65 psia and to a
Printed Name David Knapp Phone (907) 564-4694 Date temperature of 60o F. Authority 20AA 2 .2
35.
Form 10-422 Rev. 5/2009 INSTRI ICTI(lNS nK] RFVFRCF cinG
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - GC-1
GAS FLARING AND VENTING INCIDENT REPORT
May 2019
jUnplanned events less than or equal to 1 hour
DATE
TIME
VOLUME DESCRIPTION OF INCIDENT &CAUSE ACTION TAKEN TO ELIMINATE CAUSE
5/13/2019
0930-0950
50 Not required for events <= 1 hr Not required for events <= 1 hr
5/13/2019
1635-1705
5,208
5/16/2019
1807-1817
550
5/30/2019
2004-2043
335
TOTAL
6,143
Unplanned events greater than 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT& CAUSE ACTION TAKEN TO ELIMINATE CAUSE
5/14/2019 1000-1700 12 See Attachments See Attachments
TOTAL 12
Planned events less than or equal to 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
5/18/2019 0523-0524
10 Not required for events <= 1 hr
Not required for events <= 1 hr
5/20/2019 0227-0229
20
5/20/2019 2025-2036
90
TOTAL
120
Planned events greater than 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT &CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
5/20/2019 0930-1400
396 See Attachments
See Attachments
TOTAL
396
TOTAL
Unplanned Events < 1 Hour
6,143
Unplanned Events > 1 Hour
12
Planned Events < 1 hour and not
120
exceeding 5,000 MCF
Planned Events > 1 hour or
396
exceeding 5,000 MCF
Pilot Purge
49,969
Assist
0
TOTAL FLARED VOLUME
56,640
Page 6
6/10/2019
4:30 PM
Flare Start Date 05/01/2019
Flare End Date 05/31/2019
GC1 Flare Report
Report
Total Volume (MSCF) 6671
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
19-112 Flare Relief 05/14/2019 10:00:00 am 5:00:00 pm 420 min Yes
No No BP1\DELAT1 12
Determination Cause Low Ip and ip gas rates into the plant resulting in periodic compressor starvation . Cause "F pad ESD testing. Volume is an estimate.
Action Taken Rate brought back on following testing, issue resolved.
19-118 Controlled Blowdown 05/20/2019 9 30:00 am 2:00:00 pm 270 min No
No Yes BPIIDELATI 396
Determination Cause Depressured T" LDF for maintenance. 150psi to approximately 1 psi.
Action Taken Shut in when pressure was equal to flare header pressure.
Total Volume (MSCF) 6671
Generated 06/04/2019 9:21:23AM
Page 7 of 7
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number 2. Facility Name
0290000031 PBU GC 1
Disposition
3. Field
PBU - WOA
Volume MCF
4. Operator 5. Month/Year of Disposition
BP June-2019
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name
Pool Code
Percent
7. Reinjected
0
PRUDHOE
640150
97.50%
LISBURNE
640144
0.23%
8. Flared or vented 1 hour or less
1,154
MIDNIGHT SUN
640158
0.34%
PT MCINTYRE
640180
1.93%
9. Flared or vented more than 1 hour (see instr.)
5,321
10. Pilot and Purge
49,118
11. Assist Gas
0
12. Fuel gas used in lease operations.
727,808
13. Other (see instructions)
Official Use Only
Authorization >1 hr:
/
`
Safety
Lease Use
2 , /
MCF
MCF
14. TOTAL VOLUME (ITEMS 6-12)
783,401
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
Waste:
MCF
17. Transferred from:
Commissioner Date
18. Transferred to: (Express as a negative #) CGF
-63,091,533
19. Remarks:
I hereby certify the foregoing is true and correct to the best of my knowledge.
' Note: All volumes must be corrected
Signature Title Head of Control BP Alaska to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
Printed Name David Knapp Phone (907) 564-4694 Date AAC2 .2 35.
Form 10-422 Rev. 5/2009 INCTRI Ir`TfnKIQ /lnI Dc%/rocs --
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - GC-1
GAS FLARING AND VENTING INCIDENT REPORT
June 2019
Unplanned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT& CAUSE
ACTION TAKEN TO ELIMINATE CAUSE CAUSE
6/3/2019 OOSO-0056 50 Not required for events <= 1 hr Not required for events <= 1 hr
6/4/2019 0805-0809 20
6/8/2019 1533-1550 944
TOTAL 1,014
junplanned events greater than 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT& CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
6/1/2019 0105-1946
200 See Attachments
See Attachments
6/13-16/19 0000-2400
4,042
6/16/2019 1215-1340
300
6/23/2019 0930-1543
217
6/25/2019 0000-1655
379
6/29/2019 0100-1850
183
TOTAL
5,321
Planned events less than or equal to 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
6/20/2019 1835-1840
60 Not required for events <= 1 hr
Not required for events <= 1 hr
6/20/2019 2254-2258
80
TOTAL
140
Planned events greater than 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
See Attachments
See Attachments
TOTAL 0
TOTAL
Unplanned Events < 1 Hour
1,014
Unplanned Events> 1 Hour
5,321
Planned Events < 1 hour and not
140
exceeding 5,000 MCF
Planned Events > 1 hour or
0
exceeding 5,000 MCF
Pilot Purge
49,118
Assist
0
TOTAL FLARED VOLUME
55,593
Page 6
7/15/2019
1:49 PM
Flare Start Date 0610112019
Flare End Date 06/30/2019
GC1 Flare Report Total Volume (MSCF) 6475
Report
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
19-131 Flare Relief 06/01/2019 1:05:00 pm 7 46:00 pm 401 min Yes No
No BPIIBROWNK 200
Determination Cause IP compressor problems causing flaring off V-136. took down and De -pressured K-3200 GLT
Action Taken Started K-107 stopping flare off V-136
19-136 Flare Relief 06/13/2019 12:00:00 am 12:00:00 am 1440 min Yes No
No BPIISPRINGG 713
Determination Cause Intermittent flaring from V-136 vessel because IP compressor K-108 is unable to handle current process conditions. V-136 flare valve was
off the seat for 1.71 hours.
Action Taken Waiting for less demanding process conditions.
19-137 Flare Relief 06/14/2019 12:00:00 am 12:00:00 am 1440 min Yes No
No BP1\SPRINGG 879
Determination Cause Intermittent flaring from V-136 vessel because IP compressor K-108 is unable to handle current process conditions. V-136 flare valve was
off the seat for 2.11 hours.
Action Taken Waiting for less demanding process conditions.
19-138 Flare Relief 06/15/2019 12:00:00 am 12:00:00 am 1440 min Yes No
No BP1\SPRINGG 1575
Determination Cause intermittent flaring from V-136 vessel 'because IP compressor K-108 is unable to handle current process conditions. V-136 flare valve was
off the seat for 3.78 hours.
Action Taken Waiting for less demanding process conditions.
19-139 Flare Relief 06/16/2019 12:00:00 am 12:00:00 am 1440 min Yes No No BP1\SPRINGG 875
Determination Cause Intermittent flaring from V-136 vessel because IP compressor K-108 is unable to handle current process conditions. V-136 flare valve was
off the seat for 2.10 hours.
Action Taken Waiting for less demanding process conditions.
19-139 Flare Relief 06/16/2019 12:15:00 pm 1:40:00 pm 85 min No No No BPI\SPRINGG 300
Determination Cause LPS compressors capacity limited by piperack PSV's. Excess gas flares at Slugcatchers.
Action Taken Contact PCC to reduce production.
Generated 07/09/2019 4:06:38PM
Page 6 of 8
Flare Start Date 06/01/2019
Flare End Date 06/30/2019
19-148 Flare Relief 06/23/2019 9:30:00 am 3:43:00 pm 373 min Yes
No No BP1\SPRINGG
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions. V-136 flare valve was off the seat for .52 hours.
Action Taken Waiting for less demanding process conditions.
19-150 Flare Relief 06/25/2019 12:00:00 am 4:55 00 pm 1015 min Yes
No No BPIISPRINGG
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions. V-136 flare valve was off the seat for.91 hours.
Action Taken Waiting for less demanding process conditions.
19-152 Flare Relief 06/29/2019 1:00:00 am 6:50:00 pm 1070 min Yes
No No BP1\BROWNK
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions. V-136 flare valve was off the seat for .44 hours.
Action Taken Waiting for less demanding process conditions.
Total Volume (MSCF)
217
379
183
6475
Generated 07/09/2019 4:06:38PM
Page 7 of 8
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number
0290000031
2. Facility Name
PBU GC 1
3. Field
PBU - WOA
4. Operator
BP
5. Month/Year of Disposition
I Jul -2019
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name
Pool Code
Percent
7. Reinjected
PRUDHOE
640150
97.11%
LISBURNE
640144
0.22%
8. Flared or vented 1 hour or less
4
MIDNIGHT SUN
640158
0.27%,570
PT MCINTYRE
640180
2.40%
9. Flared or vented more than 1 hour (see instr.)
16,905
10. Pilot and Purge
52,019
11. Assist Gas
0
12. Fuel gas used in lease operations.
828,373
13. Other (see instructions)
0
Official Use Only
Authorization>1 hr;
/
Safety
1� pO
[
MCF
14. TOTAL VOLUME (ITEMS 6-12)
901,867
Lease Use
MCF
15. NGL Gas Equivalent
0/
Conservation
MCF
16. Purchased gas
0
Waste:
JMCF
17. Transferred from:
0
e-
Commissioner Date
18. Transferred to: (Express as a negative #) CGF
-63,386,938
19. Remarks:
I hereby certify that the foregoing is true and orrect to the best of my knowledge.
Note: All volumes must be corrected
Signature Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
Printed Name Mark Littlefield Phone (907) 564-5775 Date A C2 .23 .
�
Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - GC-1
GAS FLARING AND VENTING INCIDENT REPORT
July 2019
jUnplanned events less than or equal to 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT& CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
7/16/2019 1305-1321
1,240 Not required for events <= 1 hr
Not required for events <= 1 hr
7/22/2019 1212-1237
2,751
7/22/2019 1216-1220
139
7/27/2019 1149-1219
350
TOTAL
4,480
Unplanned events greater than 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
7/3-5/19 0100-2330
979 See Attachments
See Attachments
7/8/2019 0100-2330
642
7/18/2019 1017-2217
50
7/22/2019 1203-1327
14,146
7/27/2019 1135-1539
63
7/28/2019 0016-2200
58
7/31/2019 1742-2300
967
TOTAL
16,905
Planned events less than or equal to 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
7/12/2019 2052-2057
90 Not required for events <= 1 hr
Not required for events <= 1 hr
TOTAL
90
Planned events greater than 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
See Attachments
See Attachments
TOTAL 0
TOTAL
Unplanned Events < 1 Hour
4,480
Unplanned Events> 1 Hour
16,905
Planned Events < 1 hour and not
90
exceeding 5,000 MCF
Planned Events > 1 hour or
0
exceeding 5,000 MCF
Pilot Purge
52,019
Assist
0
TOTAL FLARED VOLUME
73,494
Page 6
8/13/2019
3:14 PM
Flare Start Date 07/01/2019
Flare End Date 07/31/2019
GC1 Flare Report Total Volume (MSCF)
21475
Report
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By
Volume
19-165 Flare Relief 07/03/2019 01:00:00 am 11:59:00 pm 1380 min No No No BP1\SHELT1
433
Determination Cause Intermittent flaring from V-136 vessel because IP compressor K-108 is unable to handle current process conditions.
Action Taken Waiting for less demanding process conditions
19-166 Flare Relief 07/04/2019 12:00:00 am 11:59:00 pm 1440 min No No No BP1\SHELT1
446
Determination Cause Intermittent flaring from V-136 vessel because IP compressor K-108 is unable to handle current process conditions.
Action Taken Waiting for less demanding conditions
19-167 Flare Relief 07/05/2019 12:00:00 am 11:30:00 pm 1410 min No No No BP1\SHELTI
100
Determination Cause Intermittent flaring from V-136 vessel because IP compressor K-108 is unable to handle current process conditions.
Action Taken Waiting for less demanding process conditions
19-178 Flare Relief 07/08/2019 01:00:00 am 11:30:00 pm 1350 min No No No BP1\SHELTI
642
Determination Cause Intermittent flaring due to tandem compressor shutting down
Action Taken PCC / EOA cut rates to get transit pressure down
19-199 Controlled Blowdown 07/18/2019 10:17:00 am 1017:00 pm 720 min Yes No No BPI\BROWNK
50
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken Waiting for less demanding process conditions.
19-209 Flare Relief 07/22/2019 12:03:00 pm 1:27:00 pm 84 min No No No BP1 \JONESCC
14146
Determination Cause CGF S/D
Action Taken Rates cut to the Annex.
19-217 Flare Relief 07/27/2019 11:35:00 am 3:39:00 pm 244 min Yes No No BP1\BROWNK 63
Generated 08/07/2019 3:47:46PM
Page 7 of 9
Flare Start Date 07/01/2019
Flare End Date 07/31/2019
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions
Action Taken Waiting for less demanding process conditions.
19-218 Flare Relief 07/28/2019 12:16:00 am 10:00:00 pm 1304 min Yes No
No
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken Waiting for less demanding process conditions.
19-221 Flare Relief 07/31/2019 5:42:00 pm 11:00:00 pm 318 min Yes
No No
Determination Cause Intermittent flaring from V-136 vessel and Slug Catchers because of current process conditions
Action Taken EOA and PCC cut rates to get transit pressure under control
BPI\BROWINK 58
BP1 \SHELTI 967
Total Volume (MSCF) 21475
Generated 08/07/2019 3.47:46PM
Page 8 of 9
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number
0290000031
2. Facility Name
PBU GC 1
3. Field
PBU - WOA
4. Operator
BP
5. Month/Year of Disposition
I Au ust-2019
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name
Pool Code
Percent
7. Reinjected
O
PRUDHOE
640150
96.19%
LISBURNE
640144
0 29%
8. Flared or vented 1 hour or less
25
MIDNIGHT SUN
640158
0.35%,266
PT MCINTYRE
640180
3.17%
9. Flared or vented more than 1 hour (see instr.)
14,977
10. Pilot and Purge
54,270
11. Assist Gas
0
12. Fuel gas used in lease operations.
499,445
13. Other (see instructions)
0
Official Use Only
Authorization >1 hr:
7'( y
9 ( '
Safety
( -t
� G 77 y
MCF
14. TOTAL VOLUME (ITEMS 6-12)
593,958
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
Waste:
MCF
17. Transferred from:
0
' A
1
Commissioner Date
18. Transferred to: (Express as a negative #) CGF
-52,729,577
19. Remarks:
I hereby certify that the foregoing is true and orrect to the best of my knowledge.
Note: All volumes must be corrected
Signature Title Manaqer Production Taxes and Royalties Alaska to pressure of 14.65 psia and to a
Printed Name Mark Littlefield Phone (907) 564-5775 Date temperature of 60o F. Authority 20 AAC2 .23 .
Form 10-422 Rev. 5/2009 inicTPI 1rT1nn1c nni DC\/CDec cinc
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT-GC-1
GAS FLARING AND VENTING INCIDENT REPORT
August 2019
Unplanned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
8/6/2019 1524-1535 76 Not required for events <= 1 hr Not required for events <= 1 hr
8/29/2019 1019-1110 21,250
TOTAL 21,326
jUnplanned events greater than 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
8/4/2019 0030-2330 75 See Attachments See Attachments
8/7-8/19 2100-1010 11,250
8/9/2019 0900-1100 667
8/30/2019 0001-2359 125
TOTAL 12,117
Planned events less than or equal to 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
8/7/2019 2100-2125
3,750 Not required for events <= 1 hr
Not required for events <= 1 hr
8/10/2019 1415-1457
60
8/11/2019 1746-1800
90
8/18/2019 0418-0421
40
TOTAL
3,940
Planned events greater than 1 hour
DATE TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
8/24/2019 1500-2350
2,860 See Attachments
See Attachments
TOTAL
2,860
TOTAL
Unplanned Events < 1 Hour
21,326
Unplanned Events > i Hour
12,117
Planned Events < 1 hour and not
3,940
exceeding 5,000 MCF
Planned Events > 1 hour or
2,860
exceeding 5,000 MCF
Pilot Purge
54,270
Assist
0
TOTAL FLARED VOLUME
94,513
Page 7
9/13/2019
10:26 AM
Flare Start Date 08/01/2019
Flare End Date 08/31/2019
GC1 Flare Report
Total Volume (MSCF) 40243
Report
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
19-225 Flare Relief 08/04/2019 12:30:00 am 11:30:00 pm 1380 min No No No BPI\SHELTI 75
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken Waiting for less demanding process conditions.
19-231 Flare Relief 08/07/2019 9:00:00 pm 12:00:00 am 180 min Yes No No BP1\SPRINGG 950
Determination Cause Intermittent flaring from V-136 vessel because of process upset(power loss)conditions at CGF.
Action Taken WOA reduced production rates and EOA reduced production rates
19-239 Flare Relief 08/08/2019 12:01:00 am 10:10:00 am 609 min Yes Yes No BP1 \DELATI 10300
Determination Cause Flaring continued with intermittent black smoke, short 10-15 second intervals 12-15 events due to low LP gas rates, causing LP flaring.
Flared to reduce DP across valve at CGF to allow flow to CCP.
Action Taken Flaring ended following establishment of flow path for 60" gas line to CCP, lowering transit gas pressure.
19-240 Flare Relief 08/09/2019 9:00:00 am 11:00:00 am 120 min No No No
Determination Cause GC1 plant upset causing rate reduction. Flared until rate to be brought back to satisfy IP compressor.
Action Taken Plant was stabilized and then lined up to restart production.
19-259 Controlled Blowdown 08/24/2019 3:00:00 pm 11:50:00 pm 530 min Yes
Determination Cause Took plant down and depressured HP & LP piping.
Action Taken Flared stopped once plant piping was depressured.
Generated 09/06/2019 9:55:18AM
BP1\DELAT1 667
No Yes BP1\SHELTI 2860
Page 9 of 12
Flare Start Date 08/01/2019
Flare End Date 08/31/2019
C--L 1
19-270 Controlled Blowdown 08/30/2019 12:01:00 am 11:59:00 pm 1438 min Yes
No No BP1\SHELTI 125
Determination Cause Intermitten Faring from V-136 vessel because of current process conditions.
Action Taken Waiting for less demanding process conditions.
Total Volume (MSCF) 40243
Generated 09/06/2019 9:55:18AM
Page 10 of 12
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number
0290000031
2. Facility Name
PBU GC 1
3. Field
PBU - WOA
4. Operator
BP
5. Month/Year of Disposition
I Se tember-2019
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name
Pool Code
Percent
7. Reinjected
0
PRUDHOE
640150
96.81 %
LISBURNE
640144
0.29%
8. Flared or vented 1 hour or less
381
MIDNIGHT SUN
640158
0.21%
PT MCINTYRE
640180
2.69%
9. Flared or vented more than 1 hour (see instr.)
55,538
10. Pilot and Purge
56,529
11. Assist Gas
0
12. Fuel gas used in lease operations.
599,350
13. Other (see instructions)
0Official
Use Only
Authorization >1 hr:
�
Safety
✓
MCF
14. TOTAL VOLUME (ITEMS 6-12)
711,798
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste:
MCF
17. Transferred from:
0
Commissioner Date
18. Transferred to: (Express as a negative #) CGF
-61,149,568
19. Remarks:
I hereby certify that the foregoing i rue and correct to the best of my knowledge.
^ Note: All volumes must be corrected
Signature G Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
Printed Name Mark Littlefield Phone (907) 564-5775 Date Z0hS-12-eZ1 AAC25.235.
Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDF
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - GC-1
GAS FLARING AND VENTING INCIDENT REPORT
September 2019
jUnplanned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
9/4/2019 2145-2235 139 Not required for events <= 1 hr Not required for events <= 1 hr
9/8/2019 1611-1646 102
9/26/2019 1010-1045 10
9/27/2019 1530-1610 130
TOTAL 381
jUnplanned events greater than 1 hour
DATE TIME
VOLUME
DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
9/3/2019 1638-2051
46,383
See Attachments
See Attachments
9/8/2019 2155-2302
202
9/9/2019 1323-1602
683
9/18/2019 0050-2358
1,466
9/19/2019 0010-1735
435
9/20/2019 0730-2320
100
9/21/2019 0130-2025
44
9/23/2019 0400-2236
25
9/24/2019 0930-2354
4,910
9/30/2019 0830-1341
1,290
TOTAL
55,538
Planned events less than or equal to 1 hour
DATE TIME
VOLUME
DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
Not required for events <= 1 hr
Not required for events <= 1 hr
TOTAL
0
Planned events greater than 1 hour
DATE TIME
VOLUME
DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
See Attachments
See Attachments
TOTAL
0
TOTAL
Unplanned Events < 1 Hour
381
Unplanned Events > 1 Hour
55,538
Planned Events < 1 hour and not
0
exceeding 5,000 MCF
Planned Events > 1 hour or
0
exceeding 5,000 MCF
Pilot Purge
56,529
Assist
0
TOTAL FLARED VOLUME
112,448
Page 7
10/15/2019
10:03 AM
Flare Start Date 09/01/2019
Flare End Date 09/30/2019
GC1 Flare Report
Report
Total Volume (MSCF) 55919
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
19-278 Controlled Blowdown 09/03/2019 4:38:00 pm 8:51:00 pm 253 min No
No No BP1ISHELTI 46383
Determination Cause SK-18 PCM processor went bad. It shutdown both LP & IP compressors causing V-136 flare valve to come off seat. During the event
K-7000 recycle went to full open causing the slug catchers to pressure up and go to flare.
Action Taken Flaring stopped when process was more stable and processor was repaired.
19-285 Controlled Blowdown 09/08/2019 9:55:00 pm 11:02:00 pm 67 min Yes
No No BP1\HELMIGBJ 202
Determination Cause Intermittent flaring from V-136 due to reduced rates.
Action Taken Off gas rates stabilized.
19-288 Controlled Blowdown 09/09/2019 1:23:00 pm 4:02:00 pm 159 min Yes
No No BP1\HELMIGBJ 683
Determination Cause Intermittent flaring from V-136 due to low gas rate and high transit pressure.
Action Taken Lowered transit pressure enabled K-108 to lower V-136 high pressure.
19-291 Flare Relief 09/18/2019 12:50:00 am 11:58:00 pm 1388 min Yes
NO No BP1ISPRINGG 1466
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions. IP compressor will not handle current transit pressures.
Action Taken Waiting for conditions to stabilize.
19-294 Flare Relief 09/19/2019 12:10:00 am 5:35:00 pm 1045 min Yes
No No BP1\BROWNK 435
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken Waiting for less demanding process conditions.
19-295 Flare Relief 09/20/2019 7:30:00 am 11:20:00 pm 950 min Yes
No No BP116ROWNK 100
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken Waiting for less demanding process conditions.
19-296 Flare Relief 09/21/2019 1:30:00 am 8:25:00 pm 1135 min Yes
No No BPIIBROWNK 44
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken Waiting for less demanding process conditions.
19-303 Flare Relief 09/23/2019 4:00:00 am 10:36:00 pm 1116 min Yes
No No BP116ROWNK 25
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken Waiting for less demanding process conditions.
19-305 Flare Relief 09/24/2019 9:30:00 am 11:54:00 pm 864 min Yes
No No BP116ROWNK 4910
Generated 10/08/2019 3:17:38PM --
Page 6 of 9
Flare StartDate 09/01/2019
Flare End Date 09/3o/2o19'
Determination Cause Blown fuse on the B phase in ups panel causing production banks to shutdown_
Action Taken Fuse replaced
19-316 Flare Relief 09/30/2019 8:30:00 am 1:41:00 pm 311 min Yes
No
Determination Cause K-108 shutdown on high discharge temp and intermittent flaring off of V-136 due to machine being weak BPIIFUELMO
1290
Action Taken Re started K-108. K-107 is un available to run.
Generated 10/08/2019 3:17:38PNI
Page 7 of 9
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number 2. Facility Name 3. Field 4. Operator 5. Month/Year of Disposition
0290000031 PBU GC 1 PBU - WOA BP October-2019
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6.
Sold
0
Pool Name
Pool Code
Percent
7.
Reinjected
0
PRUDHOE
640150
97.14%
LIII SBURNE
640144
0.28%
8.
Flared or vented 1 hour or less
30,624
MIDNIGHT SUN
640158
0,20%
PT MCINTYRE
640180
2.38%
9.
Flared or vented more than 1 hour (see instr.)
23,155
10.
Pilot and Purge
58,344
11.
Assist Gas
0
12. Fuel gas used in lease operations.
759,311
13.
Other (see instructions)
0
Official Use Only
Authorization >1 hr:
fii""
Safety
- 3 7.,7
1/J
MCF
14. TOTAL VOLUME (ITEMS 6-12)
871,434
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16.
Purchased gas
0
Waste:
MCF
17.
Transferred from:
0
�1)--7
Commissioner TDate
18.
19.
Transferred to: (Express as a negative #) CGF
Remarks:
-65,170.179
I hereby certify that the
Printed Name Mark
true and correct to the best of my knowledge.
on
Phone (907) 564-5775 Date 1111P12-e
Note: All volumes must be corrected
to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
Form 10-422 Rev. 5/2009 INSTRUCTIONS ON RFvFRRF cinF
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - GC-1
GAS FLARING AND VENTING INCIDENT REPORT
October 2019
Unplanned events less than or equal to 1 hour
DATE
TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
10/14/2019
2210-2250
470 Not required for events <= 1 hr Not required for events <= 1 hr
10/15/2019
0952-1007
80
10/20/2019
1212-1308
26,288
10/23/2019
1445-1528
3,434
10/28/2019
1542-1634
215
TOTAL
30,487
Unplanned events greater than 1
hour
DATE
TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
10/1/2019
0000-0300
21 See Attachments See Attachments
10/2/2019
0122-2305
530
10/3/2019
0406-2208
3,190
10/4/2019
0015-2220
2,790
10/5/2019
1300-2400
2,293
10/6/2019
1216-2349
456
10/7/2019
0511-2328
796
10/8/2019
0333-2310
1,276
10/9/2019
1327-2205
623
10/13/2019
0138-2014
187
10/14/2019
0447-2330
1,760
10/15/2019
0433-1958
1,066
10/16/2019
0327-1203
95
10/17/2019
1000-1645
262
10/18/2019
0217-1630
466
10/19/2019
0400-1700
272
10/20/2019
1008-2224
350
10/21-22/2019
0734-1640
2,879
10/23/2019
1116-1626
780
10/26/2019
0420-1612
730
10/26/2019
1026-2355
615
10/27/2019
1200-2359
1,585
10/29/2019
0346-2359
133
TOTAL
23.155
Page 7
11 /17/2019
1:15 PM
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - GC-1
GAS FLARING AND VENTING INCIDENT REPORT
October2019
Planned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
10/6/2019 2307-2314 20 Not required for events <= 1 hr Not required for events <= 1 hr
10/23/2019 2225-2231 117
TOTAL 137
anned events greater than 1
DATE TIME
See Attachments
TOTAL 0
TOTAL
Unplanned Events < 1 Hour
30,487
Unplanned Events> 1 Hour
23,155
Planned Events < 1 hour and not
137
exceeding 5,000 MCF
Planned Events > 1 hour or
0
exceeding 5,000 MCF
Pilot Purge
58,344
Assist
0
TOTAL FLARED VOLUME
112,123
See Attachments
NATE
Page 8
11 /17/2019
1:15 PM
Flare Start Date 10/01/2019
Flare End Date 10/31/2019
GC1 Flare Report Total Volume (MSCF) 53779
Report
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
19-317 Flare Relief 10/01/2019 12:00:00 am 3:00:00 am 180 min Yes No No BP1\FUELMO 21
Determination Cause Flaring off of V-136. K-108 shut down on high discharge temp, "J" pad was shutdown for maintenance causing gas flow to the old plant to
swing. K-108 1 know to be a weak machine and have issues with high discharge temps.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-318 Flare Relief 10/02/2019 1:22:00 am 11:05:00 pm 1303 min Yes No No BP1\SPRINGG 530
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken K_108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-319 Flare Relief 10/03/2019 4:06:00 am 10:08:00 pm 1082 min Yes No No BP1 \SPRINGG 3190
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-320 Flare Relief 10/04/2019 12:15:00 am 10:20:00 pm 1325 min Yes No No BP1 \SPRINGG 2790
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken_ K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-323 Flare Relief 10/05/2019 1:00:00 pm 12:00:00 am 660 min Yes No No BP1\SPRINGG 2293
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken _ K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-326 Flare Relief 10/06/2019 12:16:00 pm 11:49:00 pm 693 min Yes No No BP1\SPRINGG 456
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-327 Flare Relief 10/07/2019 5:11:00 am 11:28:00 pm 1097 min Yes No No BP1\SPRINGG 796
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-329 Flare Relief 10/08/2019 3:33:00 am 11:10:00 pm 1177 min Yes No No BP1 \SPRINGG 1276
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-330 Flare Relief 10/09/2019 1:27:00 pm 10:05:00 pm 518 min Yes No No BP1 \SPRINGG 623
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken K_108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-338 Flare Relief 10/13/2019 1:38:00 am 8:14:00 pm 1116 min Yes No No BP1\SPRINGG 187
Generated 11/08/2019 11:44:02AM Page 9 of 12
Flare StartDate 10/01/2019
Flare End Date 10/31/2019
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken Waiting for less demandin G—C
g process conditions.
19-340 Flare Relief 10/14/2019 4:47:00 am 11:30:00 pm 1123 min Yes
No No BPIISPRINGG 1760
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions, plus (LP flare stg. valve #3) LP compression system not
capable of preventing LP flaring at reduced oil rate.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-341 Flare Relief 10/15/2019 4:33:00 am 7:58:00 pm 925 min Yes
No No BP1ISPRINGG 1066
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions, plus (LP flare stg. valve #3) LP compression system not
capable of preventing LP flaring at reduced oil rate.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-342 Flare Relief 10/16/2019 3:27:00 am 12:03:00 pm 516 min Yes
No No BP1\BROWNK 95
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-344 Flare Relief 10/17/2019 10:00:00 am 4:45:00 pm 405 min Yes
No No BP1IBROWNK 262
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
further -evaluate K-4ggP�ssorweak performancE -
19-346 Flare Relief 10/18/2019 2:17:00 am 4:30:00 pm 853 min Yes
No No BP1\BROWNK 466
Determination Cause Intermittent flaring from V-136 vessel because of current process conditions.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
ressarweak perfor
19-347 Flare Relief 10/19/2019 4:00:00 am 5:00:00 pm 780 min Yes
NO No BP1\BROWNK 272
Determination Cause Intermittent flaring from V-136 and LP flare because of current process conditions.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
from V=9-36� ar�fnrther evaluate-IF1-B8 eamPressar weak performance:-------
19-349 Flare Relief 10/20/2019 10:08:00 am 10:24:00 pm 736 min Yes
No No BPIIBROWNK 350
Determination Cause Intermittent flaring from V-136 and LP flare because of current process conditions.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
erfcrmarnce-------
19-358 Flare Relief 10/21/2019 7:34:00 am 11:59:00 pm 985 min Yes
Yes No BPIISHELTI 900
Determination Cause Flaring occurred during plant shutdown due to lose of power. Intermittent Black smoke due no LP gas rates
Generated 11/08/2019 11:44 02AM
Page 10 of 12
Flare Start Date 10/01/2019
Flare End Date 10/31/2019
Action Taken Flaring stopped once plant was back online
19-360 Flare Relief 10/22/2019 12:00:00 am 4:40:00 pm 1000 min Yes
No
Determination Cause Flare due to bringing plant back online from power outage.
Action Taken Plant back on line
No BP1\BROWNK 1979
19-364 Flare Relief 10/23/2019 11:16:00 am 4:26:00 pm 310 min Yes
No No BP1ISHELTI 78C
Determination Cause Intermittent flaring from V-136 and LP flare because of current process conditions.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-371 Flare Relief 10/26/2019 4:20:00 am 4:12:00 pm 712 min Yes
No No BPIISHELT1 730
Determination Cause Flaring off slugcatchers due to high transit gas pressure.
Action Taken Flaring stopped once PCC and EOA made rate cuts.
19-371 Flare Relief 10/26/2019 10:26:00 am 11.55:00 pm 809 min Yes
No No BP1\SHELTI 615
Determination Cause Intermittent flaring from V-136 and LP flare because of current process conditions
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited far K-107 compressor so it can be brought back on
19-372 Flare Relief 10/27/2019 12:00:00 pm 11:59:00 pm 719 min Yes
No No BP1\SHELTI 1585
Determination Cause Intermittent flaring from V-136 and LP flare because of current process conditions.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-375 Flare Relief 10/29/2019 3:46:00 am 11:59:00 pm 1213 min Yes
No No BPIISHELTI 131�
Determination Cause Intermittent flaring from V-136 and LP flare due to current process conditions.
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
' ewatuate K=168-eampressorwealrperfarrrrartee --
Total Volume (MSCF) 53779
Generated 11/08/2019 11:44:02AM
Page 11 of 12
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCFn ro-q niSpnc1T1nK1
-
1. Facility Number 2. Facility Name
0290000031 PBU GC 1
Disposition
--- - - -
3. Field
PBU - WOA
Volume MCF
- -- ---- - -/ -0.....
4. Operator 5. Month/Year of Disposition
BP I November-2019
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name
Pool Code
Percent
7. Reinjected
0
PRUDHOE
640150
96.88%
LISBURNE
640144
0.29%
8. Flared or vented 1 hour or less
856
MIDNIGHT SUN
640158
0.18%
PT MCINTYRE
640180
2.65%
9. Flared or vented more than 1 hour (see instr.)
37,625
10. Pilot and Purge
57,347
11. Assist Gas
12. Fuel gas used in lease operations.
763,283
13. Other (see instructions)
Official Use Only
Authorization >1 hr:
/G " / 019
Safety
3 7
/ r
MCF
14. TOTAL VOLUME (ITEMS 6-12)
859,111
Lease Use
MCF
15. NGL Gas Equivalent
0
Conservation
MCF
16. Purchased gas
0
Waste:
MCF
17. Transferred from:
0
✓ l
Commissioner Date
18. Transferred to: (Express as a negative #) CGF
-65,500,013
19. Remarks:
I hereby certify that the foregoing is true and rrect to the best of my knowledge.
Note: All volumes must be corrected
Signature Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
Printed Name Mark Littlefield Phone (907) 564-5775 Date AAC25.235.
Form 10-422 Rev. 5/2009 INSTRUCTIONS ON RFvFRCF cinF
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - GC-1
GAS FLARING AND VENTING INCIDENT REPORT
November 2019 Page 6
(planned events less than or equal to 1 hour
DAZE TIME VOLUME DESCRIPTION OF INCIDENT&CAUSE
11/28/2019 1742-1825 142 Not required for events <= 1 hr ACTION TAKEN TO ELIMINATE CAUSE
11/29/2019 0409-0414 Not required for events <= 1 hr
347
11/29/2019 0754-0758 277
TOTAL 766
11/14/2019
1038-1737
a ""`''Uery i a� CAUSE
SeeAttach
See Attachments
ACTION TAKEN TO ELIMINATE CAU
11/16/2019
1000-1133
645
645
See Attachments
11/17/2019
1830-2300
173
11/18/2019
1800-1935
137
11/19/2019
1830-2130
278
11/20/2019
0030-2330
216
11/21/2019
0030-2300
566
11/22/2019
0030-2300
727
11/22/2019
0508-0718
34,000
11/23/2019
0030-2330
180
11/24/2019
0030-2330
194
11/25/2019
0030-2330
147
11/26/2019
0030-2330
99
TOTAL
37,625
finned events less than or equal to 1 hour
DATE
11/9/2019
TIME
1512-1520
VOLUME DESCRIPTION OF INCIDENT & CAUSE
ACTION TAKEN TO ELIMINATE CAUS
90 Not required for events <= 1 hr
Not required for events <= 1 hr
TOTAL
90
nned events greater than 1 hour
DATE
TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE
See Attachments
ACTION TAKEN TO ELIMINATE CAUSE
See Attachments
TOTAL
0
TOTAL
Unplanned Events < 1 Hour
766
Unplanned Events > 1 Hour
37,625
Planned Events < 1 hour and not
exceeding 5,000 MCF
90
Planned Events > 1 hour or
exceeding 5,000 MCF
0
Pilot Purge
57,347
Assist
0
TOTAL FLARED VOLUME
95,828 12/14/2019
3:48 PM
Flare Start Date 11/01/2019
Flare End Date 11/30/2019
GC1 Flare Report Total Volume (MSCF) 38481
Report
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
19-393 Controlled Blowdown 11/14/2019 10:38:00 am 5:37:00 pm 419 min Yes No No BP1\BROWNK 263
Determination Cause Intermittent flaring from V-136 vessel
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
— - �tneto-stoP irttermittertt ffar ng frorrrit 43Eanct
k-perfor�-- --
19-394 Controlled Blowdown 11/16/2019 10:00:00 am 11:33:00 am 93 min Yes No No BP1\BROWNK 645
Determination Cause Intermittent flaring from V-136
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
436, -d-
19-395 Controlled Blowdown 11/17/2019 6:30:00 pm 11:00:00 pm 270 min Yes No No BP1\BROWNK 173
Determination Cause Intermittent flaring from V-136 vessel
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
19-396 Controlled Blowdown 11/18/2019 6:00:00 pm 7:35:00 pm 95 min Yes No No BP1\BROWNK 137
Determination Cause Intermittent flaring from V-136 vessel
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back on
---line
19-397 Controlled Blowdown 11/19/2019 6:30:00 pm 9:30:00 pm 180 min Yes No No BP1\BROWNK 278
Determination Cause Intermittent flaring from V-136 / High transit pressure
Action Taken PCC cut rate to lower gas transit pressure, also K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for
--- —---K--t&Tc mpressprgo can-i-broughttiack
performance. -408 compressorweak---
19-399 Controlled Blowdown 11/20/2019 12:30:00 am 11:30:00 pm 1380 min Yes No No BPI\SHELT1 216
Determination Cause Intermittent flaring from V-136, due to high transit gas pressure
Action Taken PCC cut rate to lower gas transit pressure, also K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for
performance. --
19-400 Controlled Blowdown 11/21/2019 12:30:00 am 11:30:00 pm 1380 min Yes No No BP1\SHELTI 566
Determination Cause Intermittent flaring from V-136 and LP flare, due to high transit gas pressure.
Action Taken - PCC cut rate to lower gas transit pressure, also K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for
performance. ftne-to-stop
19-402 Controlled Blowdown 11/22/2019 12:30:00 am 11:30:00 pm 1380 min Yes No No BP1\SHELTI 727
Determination Cause Intermittent flaring off V-136 and LP Flare, due to high transit gas pressure.
Action Taken PCC cut rate to lower gas transit pressure, also K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for
— — -- performance.
so t rteto stapintermittent flaring from�t=936 and furtherevaluateiE=198 compressorweak-
19-402 Controlled Blowdown 11/22/2019 5:08:00 am 7:18:00 am 130 min No No No BP1\DELATI 34000
Determination Cause High gas transit line pressure caused by CGF compressor Compressor shut down, temperature instrument failure
Generated 12/03/2019 2:48:43PM
Page 8 of 9
Flare Start Date 11/01/2019 ��
Flare End Date 11/30/2019
Action Taken _ Controlled flaring from the Annex to reduce Transit gas pressure, reducing field wide flaring while the CGF repair was made. GC1 report is
gasfitarirt9 from
19-405 Controlled Blowdown 11/23/2019 12:30:00 am 11:30:00 pm 1380 min Yes No
No BP1\SHELTI 18C
Determination Cause Intermittent flaring off V-136 and LP flare, due to high transit gas pressure.
Action Taken PCC cut rate to lower gas transit pressure, also K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for
��e-� �ampressarso-rt can to brpugftt-
performance.
19-406 Controlled Blowdown 11/24/2019 12:30:00 am 11:30:00 pm 1380 min Yes
No No BP1\SHELTI 194
Determination Cause Intermittent flaring from V-136 and LP flare due to high transit gas pressure.
Action Taken PCC cut rate to lower gas transit pressure, also K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for
performance.
19-408 Controlled Blowdown 11/25/2019 12:30:00 am 11:30:00 pm 1380 min Yes No
No BP1\SHELTI 147
Determination Cause Intermittent flaring off V-136 and LP flare, due to high transit gas pressure.
Action Taken PCC cut rate to lower gas transit pressure, also K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for
tiraught tack orriine-tO-M in i
performance. 436 artctfiarther
19-409 Controlled Blowdown 11/26/2019 12:30:00 am 11:30:00 pm 1380 min Yes
No No BP1\SHELTI gg
Determination Cause Intermittent flaring of V-136 and LP flare, due to high transit gas pressure.
Action Taken PCC cut rate to lower gas transit pressure, also K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for
performance. +fh- 1 and fr�rthe� evataate -
Total Volume (MSCF) 38481
Generated 12/03/2019 2:48:43PM
Page 9 of 9
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facility Number
0290000031
2. Facility Name
PBU GC 1
3. Field
PBU - WOA
4. Operator
BP
5. Month/Year of Disposition
I December-2019
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
0
Pool Name
Pool Code
Percent
7. Reinjected
PRUDHOE
640150
97,14%
LISBURNE
640144
0.36%
8. Flared or vented 1 hour or less
1
MIDNIGHT SUN
640158
0.21%,433
PT MCINTYRE
640180
2.29%
9. Flared or vented more than 1 hour (see instr.)
25,067
10. Pilot and Purge
55,580
11. Assist Gas
0
12. Fuel gas used in lease operations.
870,501
13. Other (see instructions)
0
Official Use Only
Authorization >1 hr:
��3��
Safety
2Y 067
MCF
14. TOTAL VOLUME (ITEMS 6-12)
952,581
Lease Use
MCF
15. NGL Gas Equivalent
Conservation
MCF
16. Purchased gas
0
Waste:
MCF
17. Transferred from:
6
JI� 'N
Commissioner Date
18. Transferred to: (Express as a negative #) CGF
-62,597,719
19. Remarks:
I hereby certify that the foregoing is tru and correct to the best of my knowledge.
Note: All volumes must be corrected
Signature Title Manager Production Taxes and Royalties Alaska to pressure of 14.65 psis and to a
temperature of 60o F. Authority 20
Printed Name Mark Llttleflel Phone (907) 564-5775 Date / 6 GdZ 0 AAC25.235.
Form 10-422 Rev. 5/2009 INSTRUCTIONS ON REVERSE SIDE c„ti ;+;., n,,
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - GC-1
GAS FLARING AND VENTING INCIDENT REPORT
December 2019
jUnplanned events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
12/1/2019 2139-2228 1,341 Not required for events <= 1 hr Not required for events <= 1 hr
12/6/2019 0129-0135 43
12/6/2019 0428-0435 39
12/16/2019 1530-1540 10
TOTAL 1.433
DATE
TIME
VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
12/2/2019
0335-0820
1,778 See Attachments See Attachments
12/3/2019
1310-1536
132
12/5/2019
0030-1142
167
12/5/2019
1142-1440
69
12/7/2019
0114-2359
294
12/7/2019
2111-2234
184
12/8/2019
0020-2300
1,050
12/9/2019
0029-1919
800
12/10/2019
0619-2359
250
12/11/2019
0348-2359
1
12/12/2019
1452-1953
14,310
12/13-14/19
0001-2359
60
12/15/2019
0001-2359
570
12/18/2019
0030-2330
446
12/19/2019
0030-2330
78
12/20/2019
0030-2330
962
12/21/2019
0030-2330
783
12/22/2019
0030-2330
459
12/23/2019
0030-2330
920
12/24/2019
0030-2330
148
12/25/2019
0035-2400
103
12/26/2019
0038-2400
740
12/27/2019
0036-2400
430
12/28/2019
0041-1650
333
TOTAL
25,067
Planned events less than or equal to 1
hour
E DESCRIPTION OF INCIDENT & CAUSE
Not required for events <= 1 hr
TOTAL 0
ACTION TAKEN TO ELIMINATE CAUSE
Not required for events <= 1 hr
Page 6
1 /15/2020
2:45 PM
BP EXPLORATION (ALASKA) INC.
PRUDHOE BAY UNIT - GC-1
GAS FLARING AND VENTING INCIDENT REPORT Page 7
December 2019
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
See Attachments See Attachments
TOTAL 0
TOTAL
Unplanned Events < 1 Hour
1,433
Unplanned Events > 1 Hour
25,067
Planned Events < 1 hour and not
0
exceeding 5,000 MCF
Planned Events > 1 hour or
0
exceeding 5,000 MCF
Pilot Purge
55,580
Assist
0
TOTAL FLARED VOLUME
82,080
1 /15/2020
2:45 PM
Flare Start Date 1210112019
Flare End Date 12/31/2019
GC1 Flare Report
Report
Total Volume (MSCF) 26500
Numbe System Date Start Time Stop Time Duration Intermittent Black Smoke Planned Reported By Volume
19-414 Flare Relief 12/02/2019 3:35:00 am 8:20:00 am 285 min
Determination Cause T/S K-107 deficient performance
No
No
Yes
BP1IJONESCC 1778
Action Taken Performance diagnosis complete
19-416 Flare Relief 12/03/2019 1:10:00 pm 3:36:00 pm 146 min
Determination Cause LP/IP combination inadequate for current process conditions.
Yes
No
No
BPIIJONESCC 132
Action Taken none
19-419 Flare Relief 12/05/2019 12:30:00 am 11:42:00 am 672 min
Determination Cause LP/IP combination inadequate for current process conditions.
Yes
No
No
BPIIJONESCC 167
Action Taken none
19-419 Flare Relief 12/05/2019 11:42:00 am 2:40:00 pm 178 min
Determination Cause LP/IP combination inadequate for current process conditions.
Yes
No
No
BP1\JONESCC 69
Action Taken none
19-422 Flare Relief 12/07/2019 1:14:00 am 11:59:00 pm 1365 min Yes
Determination Cause LP/IP combination inadequate for current process conditions.
No
No
BP1\JONESCC 294
Action Taken none
19-422 Flare Relief 12/07/2019 9:11:00 pm 10:34:00 pm 83 min Yes
Determination Cause LP/IP combination inadequate for current process conditions.
No
No
BP1IJONESCC 184
Action Taken none
19-424 Flare Relief 12/08/2019 12:20:00 am 11:00:00 pm 1360 min Yes
Determination Cause LP/IP combination inadequate for current process conditions & high transit pressure.
No
No
BPIIJONESCC 1050
Action Taken none
19-425 Flare Relief 12/09/2019 12:29:00 am 7:19:00 pm 1130 min Yes
Determination Cause LP/IP combination inadequate for current process conditions & K-108 TSDH.
No
No
BPIIJONESCC 800
Action Taken none
Generated 01/08/2020 10:56:38AM
Page 6 of 8
Flare StartDate 12/01/2019
Flare End Date 12/31/2019
19-427 Flare Relief 12/10/2019 6:19:00 am 11:59:00 pm 1060 min Yes
Determination Cause LP/IP combination inadequate for current process conditions. No No BPI IJONESCC
Action Taken none
19-428 Flare Relief 12/11/2019 3:48:00 am 11:59:00 pm 1211 min Yes
Determination Cause LP/IP combination inadequate for current process conditions & K-108 S/D. No No BPIIJONESCC
Action Taken none & restarted K-108
250
19-430 Flare Relief 12/12/2019
2:52:00 pm 7:53:00 Pm 301 min Yes
No No BP1\FUELMO
14310
isolated. Flared off of separators.
Determination Cause Leak was found off of HP gas K.O. 9557 drain line. Closed 1st stage 449's and 448's off of 1st and 2nd stages in order to ge
t leak
Action Taken Leak isolated and stopped flaring. ge
19-431 Flare Relief 12/13/2019 12:01:00 am 11:59:00 pm 1438 min Yes
Determination Cause Intermittent flaring off of V-136 K-108 is a weak machine and K-107 is unavailableNo NO BPIIFUELMO 20
Action Taken _ K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought back
19-432 Flare Relief 12/14/2019 12:00:00 am 11:59:00 pm 1439 min Yes
Determination Cause K-108 performance issues NO NO BPIIFUELM0
40
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brou
ght back on
19-433 Flare Relief 12/15/2019 12:01:00 am 11:59:00 pm 1438 min Yes
No No Determination Cause EVEN train TEG is fowled up with oil/condensates causing DP across the packing in the contactor. The Ca Br prevention
570
DP and flares off of slugcatchers when high DP is seen.
Action Taken We are cutting rate to below 550mm in order block in the inlet to the even contactor and clean up the system.over prevention looks at the
--------------
19-435 Flare Relief 12/18/2019 12:30:00 am 11:30:00 pm 1380 min Yes
Determination Cause Intermittent flaring off V-136 and LP flare due to K-108 weak performance. No No BPIISHELT1 446
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be bro
ught back on
19-436 Flare Relief
12/19/2019 12:30:00 am 11:30:00 pm 1380 min Yes
Determination Cause Intermittent flaring from V-136 and LP flare due to K-108 weak performance. No No BPI ISHELTI
78
Action Taken - K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brought rto ught back on
19-437 Flare Relief 12/20/2019 12:30:00 am
11:30:00 pm 1380 min Yes
Determination Cause Intermittent flaring off V-136 and LP flare due to K-108 weak performance No No BPI ISHELT1
962
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can be brou
ght back on
19-438 Flare Relief 12/21/2019 12:30:00 am 11:30:00 pm 1380 min Yes
No No
Generated 01/08/2020 1056:38AM
BPI ISHELTI 783
Page 7 of 8
0
Flare StartDate 12/01/2019 �--
Flare End Date 12/31/2019
Determination Cause Intermittent flaring off V-136 and LP flare due to K-108 weak performance
Action Taken K-108 has a weak compressor bundle/ Poor P P performance.
Repairs are being expedited for K-107 compressor so it can be brought back or
19-440 Flare Relief
12/22/2019 12:30:00 am 11:30:00 pm 1380 min Yes
Determination Cause Intermittent flaring off V-136 and LP Flare due to K-108 weak performance. No
No BPIISHELTI
Action Taken 459
K-108 has a weak compressor bundle/ poor performance. Repairs ar
K �� being expedited for K-107 compressor so it can be
brought back on
19-441 Flare Relief
12/23/2019 12:30:00 am 11:30:00 pm 1380 min Yes
Determination Cause Intermittent flaring from V-136 and LP flare due to K-108 weak performance. No
NO BP1ISHELT1
Action Taken 920
K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107
compressor so it can be brought back on
19-442 Flare Relief
12/24/2019 12:30:00 am 11:30:0o pm 1380 min Yes
Determination Cause Intermittent flaringfrom V-136 and LP flare due to K-108 weak NO No
BPIISHELTI 148
Action Taken Performance
K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-107 compressor so it can b e brought back on
19-445 Flare Relief
12/25/2019 12:35:00 am 12:00:00 am 1405 min No
Determination Cause Intermittent flaring off V-136 and LP flare due to K-108 weak performance No
No BPIISPRINGG
Action Taken103
K-1 OS has a weak compressor bundle/ poor performance. Repairs are being.......
tine to stopmy
19-446 Flare Relief
12/26/2019 12:38:00 am 12:00:00 am
1402 yes Determination Cause Intermittent flaring off V-136 and LP flare due to K-108 we kI No No BP1ISPRINGG 740
Performance
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are being expedited for K-1 _ 07 compressor so it can be brought back on
19-447 Flare Relief
12/27/2019 12:36:00 am 12:00:00 am
1404 min Yes
Determination Cause Intermittent flaring off V-136 and LP flare due to K-108 weak performance
No No
BPIISPRINGG 430
Action Taken K-108 has a weak compressor bundle/ poor performance. Repairs are bein
g expedited for K-107 compressor so it can be brought back on
19-449 Flare Relief
12/28/2019 12:41:00 am 4:50:0o Pm 969 min
Yes Determination Cause intermittent flaring off V-136 and LP flare due to K-108 weak performance No
NO BP1ISPRINGG
Action Taken � 333
K-108 has a weak compressor bundle/ poor performance.
_ Repairs are being expedited for K-107 compressor so it can be wrought back on
Generated 01/08/2020 10:
Total Volume (MSCF) 26500
Page 8 of 8