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208-142
MEMORANDUM State of Alaska Alaska Oil and Gas Conservation Commission DATE:Wednesday, July 23, 2025 SUBJECT:Mechanical Integrity Tests TO: FROM:Sully Sullivan P.I. Supervisor Petroleum Inspector NON-CONFIDENTIAL Hilcorp North Slope, LLC V-219 PRUDHOE BAY UN ORIN V-219 Jim Regg InspectorSrc: Reviewed By: P.I. Suprv Comm ________ JBR 07/23/2025 V-219 50-029-23397-00-00 208-142-0 G SPT 4491 2081420 1500 827 285 4YRTST F Sully Sullivan 5/24/2025 4 Year MIT-IA - Failed to catch pressure after 10 bbls. 30 MinPretestInitial15 Min Well Name Type Test Notes: Interval P/F Well Permit Number: Type Inj TVD PTD Test psi API Well Number Inspector Name:PRUDHOE BAY UN ORIN V-219 Inspection Date: Tubing OA Packer Depth 326IA 45 Min 60 Min Rel Insp Num: Insp Num:mitSTS250718130935 BBL Pumped:10 BBL Returned: Wednesday, July 23, 2025 Page 1 of 1 MEMORANDUM State of Alaska Alaska Oil and Gas Conservation Commission DATE:Monday, July 21, 2025 SUBJECT:Mechanical Integrity Tests TO: FROM:Sully Sullivan P.I. Supervisor Petroleum Inspector NON-CONFIDENTIAL Hilcorp North Slope, LLC V-219 PRUDHOE BAY UN ORIN V-219 Jim Regg InspectorSrc: Reviewed By: P.I. Suprv Comm ________ JBR 07/21/2025 V-219 50-029-23397-00-00 208-142-0 G SPT 4491 2081420 3100 809 835 897 952 290 299 299 300 OTHER F Sully Sullivan 5/27/2025 4 year MIT-IA, Tested to 3100psi as a MAIP for the purpose of applying for an AA due to losses in the IA fluid level. There was obvious communication to the tubing from the IA. Well is being secured and evaluated. During bleed back breakover to the tubing continued all the way down to 1200psi IA pressure and tubing ended at 976 psi. 30 MinPretestInitial15 Min Well Name Type Test Notes: Interval P/F Well Permit Number: Type Inj TVD PTD Test psi API Well Number Inspector Name:PRUDHOE BAY UN ORIN V-219 Inspection Date: Tubing OA Packer Depth 295 3400 3220 3063IA 45 Min 60 Min Rel Insp Num: Insp Num:mitSTS250527133634 BBL Pumped:4.5 BBL Returned:3.8 Monday, July 21, 2025 Page 1 of 1 CAUTION: This email originated from outside the State of Alaska mail system. Do not click links or open attachments unless you recognize the sender and know the content is safe. From:Wallace, Chris D (OGC) To:AOGCC Records (CED sponsored) Subject:FW: NOT OPERABLE: Injector V-219 (PTD #2081420) MIT-T and MIT-IA failed Date:Wednesday, June 4, 2025 11:42:32 AM Attachments:V-219.pdf From: PB Wells Integrity <PBWellsIntegrity@hilcorp.com> Sent: Wednesday, June 4, 2025 11:31 AM To: Wallace, Chris D (OGC) <chris.wallace@alaska.gov> Cc: Regg, James B (OGC) <jim.regg@alaska.gov>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Torin Roschinger <Torin.Roschinger@hilcorp.com>; PB Wells Integrity <PBWellsIntegrity@hilcorp.com> Subject: NOT OPERABLE: Injector V-219 (PTD #2081420) MIT-T and MIT-IA failed Mr. Wallace, Slickline set a DGLV in sta #6 and a TTP @ 8,746’ MD. A subsequent MIT-T and MIT-IA failed. The well is now classified as NOT OPERABLE until the well barriers are restored. Please respond with any questions. Andy Ogg Hilcorp Alaska LLC Field Well Integrity andrew.ogg@hilcorp.com P: (907) 659-5102 M: (307) 399-3816 From: PB Wells Integrity Sent: Saturday, May 24, 2025 5:24 PM To: 'Wallace, Chris D (CED)' <chris.wallace@alaska.gov> Cc: 'Regg, James B (CED)' <jim.regg@alaska.gov>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Torin Roschinger <Torin.Roschinger@hilcorp.com> Subject: UNDER EVALUATION: Injector V-219 (PTD #208142) MIT-IA failed to reach test pressure Mr. Wallace, Injector V-219 (PTD #208142) MIT-IA failed to reach test pressure after pumping 10 bbls on 05/24/25. The tubing / casing pressure does not appear to be treading which would indicate a potential casing leak. The well is now classified as UNDER EVALUATION and on a 28 day clock to be resolved. Plan forward: 1. Downhole Diagnostics: Attempt to bleed IAP to 0 psi 2. Fullbore: Load and MIT-IA a. AOGCC MIT-IA if passes, b. Liquid leak rate if fails 3. Well Integrity: Further action as required. Please call with any questions or concerns. Ryan Holt Hilcorp Alaska LLC Field Well Integrity / Compliance Ryan.Holt@Hilcorp.com P: (907) 659-5102 M: (907) 232-1005 From: Alaska NS - PB - Field Well Integrity Sent: Wednesday, May 26, 2021 1:15 PM To: Wallace, Chris D (CED) <chris.wallace@alaska.gov> Cc: Regg, James B (CED) <jim.regg@alaska.gov>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Aras Worthington <Aras.Worthington@hilcorp.com>; John Condio - (C) <John.Condio@hilcorp.com> Subject: OPERABLE: Injector V-219 (PTD #208142) AOGCC MIT-IA Passed Mr. Wallace, Injector V-219 (PTD #208142) passed an AOGCC MIT-IA on 03/25/21 and has shown no signs of pressure communication during the online period. The well is now classified as OPERABLE. Please call with any questions or concerns. Ryan Holt Hilcorp Alaska LLC Field Well Integrity / Compliance Ryan.Holt@Hilcorp.com P: (907) 659-5102 M: (907) 232-1005 From: Wallace, Chris D (CED) <chris.wallace@alaska.gov> Sent: Thursday, April 15, 2021 3:03 PM To: Alaska NS - PB - Field Well Integrity <PBFieldWellIntegrity@hilcorp.com> Cc: Regg, James B (CED) <jim.regg@alaska.gov>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Aras Worthington <Aras.Worthington@hilcorp.com>; John Condio - (C) <John.Condio@hilcorp.com> Subject: [EXTERNAL] RE: Request: Injector V-219 (PTD #208142) Continued Diagnostic Work Andy, Your request for up to 28 days injection for additional monitoring and diagnostics is approved. Thanks and Regards, Chris Wallace, Sr. Petroleum Engineer, Alaska Oil and Gas Conservation Commission, 333 West 7th Avenue, Anchorage, AK 99501, (907) 793- 1250 (phone), (907) 276-7542 (fax), chris.wallace@alaska.gov CONFIDENTIALITY NOTICE: This e-mail message, including any attachments, contains information from the Alaska Oil and Gas Conservation Commission (AOGCC), State of Alaska and is for the sole use of the intended recipient(s). It may contain confidential and/or privileged information. The unauthorized review, use or disclosure of such information may violate state or federal law. If you are an unintended recipient of this e-mail, please delete it, without first saving or forwarding it, and, so that the AOGCC is aware of the mistake in sending it to you, contact Chris Wallace at 907-793- 1250 or chris.wallace@alaska.gov. From: Alaska NS - PB - Field Well Integrity <PBFieldWellIntegrity@hilcorp.com> Sent: Thursday, April 15, 2021 1:28 PM To: Wallace, Chris D (CED) <chris.wallace@alaska.gov> Cc: Regg, James B (CED) <jim.regg@alaska.gov>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Aras Worthington <Aras.Worthington@hilcorp.com>; John Condio - (C) <John.Condio@hilcorp.com> Subject: Request: Injector V-219 (PTD #208142) Continued Diagnostic Work Mr. Wallace, Injector V-219 (PTD #208142) was recently made Not Operable on 04/11/21 for failing an AOGCC witnessed MIT-IA and follow up diagnostic work indicated a leak at the uppermost packer. The well was shut in on 04/09/21 and Eline performed a leak detect log on 04/11/21. During the log, a leak rate of 1.0 gpm @ 2500 psi was established and the log indicated a packer leak @ 8365’ MD. The objective was to complete the log to surface to identify any other leaks. However, approximately 3.5 hours after starting the log, the leak stopped and a passing MIT-IA was performed to 2739 psi. On 04/13/21 DHD performed another passing MIT-IA to 2429 psi. Hilcorp is requesting permission to put the well back on injection Under Evaluation for up to 28 days to perform additional pressure testing and more diagnostic work if necessary. Plan Forward: 1. Operations: Put on injection 2. DHD: Perform MIT-IA 3. DHD/Fullbore (pending). If MIT-IA passes, perform AOGCC witnessed MIT-IA 4. Well Integrity: Additional diagnostics as needed Please respond with any questions. Andy Ogg Hilcorp Alaska LLC Field Well Integrity / Compliance andrew.ogg@hilcorp.com P: (907) 659-5102 M: (307)399-3816 From: Alaska NS - PB - Field Well Integrity Sent: Sunday, April 11, 2021 7:55 AM To: Wallace, Chris D (CED) <chris.wallace@alaska.gov> Cc: Regg, James B (CED) <jim.regg@alaska.gov>; Aras Worthington <Aras.Worthington@hilcorp.com>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com> Subject: NOT OPERABLE: Injector V-219 (PTD #208142) failed AOGCC MIT-IA Mr. Wallace, WAG Injector V-219 (PTD #208142) was made Under Evaluation for failing an AOGCC witnessed MIT-IA. On 03/19/21 DHD established a LLR of 1.0 gpm @ 2500 psi while pumping into the Inner Annulus. A passing PPPOT-T was performed ensuring the leak was not through the wellhead seals. Reviewing the downhole gauge data; there is evidence to suggest the leak is at the upper most packer. The slickline step to re-set the DGLV will be cancelled and E-line will perform an LDL. The well has been shut, freeze protected and will now be classified as NOT OPERABLE until the barriers are restored. Please respond with any questions. Andy Ogg Hilcorp Alaska LLC Field Well Integrity / Compliance andrew.ogg@hilcorp.com P: (907) 659-5102 M: (307)399-3816 From: Alaska NS - PB - Field Well Integrity <PBFieldWellIntegrity@hilcorp.com> Sent: Sunday, March 14, 2021 3:44 PM To: Wallace, Chris D (CED) <chris.wallace@alaska.gov> Cc: Regg, James B (CED) <jim.regg@alaska.gov>; Aras Worthington <Aras.Worthington@hilcorp.com>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Alaska NS - PB - Field Well Integrity <PBFieldWellIntegrity@hilcorp.com> Subject: UNDER EVALUATION: Injector V-219 (PTD #208142) failed AOGCC MIT-IA Mr. Wallace, WAG Injector V-219 (PTD #208142) failed its 4-year AOGCC MIT-IA on 03/14/21. The failed MIT-IA indicates a failure in one or more well barriers. The well is now classified as UNDER EVALUATION and is on the 28-day clock for diagnostics. Plan Forward: 1. Slickline: Re-Set DGLV in GLM #8. Perform MIT-IA 2. Fullbore/DHD: If MIT-IA passes after DGLV is re-set, perform online AOGCC witnessed MIT-IA 3. Slickline (Pending): Perform LDL with OE approval 4. Well Integrity: Additional diagnostics as needed Please respond with any questions. Andy Ogg Hilcorp Alaska LLC Field Well Integrity / Compliance andrew.ogg@hilcorp.com P: (907) 659-5102 M: (307)399-3816 The information contained in this email message is confidential and may be legally privileged and is intended only for the use of the individual or entity named above. Ifyou are not an intended recipient or if you have received this message in error, you are hereby notified that any dissemination, distribution, or copy of this email is strictlyprohibited. If you have received this email in error, please immediately notify us by return email or telephone if the sender's phone number is listed above, then promptlyand permanently delete this message. While all reasonable care has been taken to avoid the transmission of viruses, it is the responsibility of the recipient to ensure that the onward transmission, opening, oruse of this message and any attachments will not adversely affect its systems or data. No responsibility is accepted by the company in this regard and the recipientshould carry out such virus and other checks as it considers appropriate. The information contained in this email message is confidential and may be legally privileged and is intended only for the use of the individual or entity named above. Ifyou are not an intended recipient or if you have received this message in error, you are hereby notified that any dissemination, distribution, or copy of this email is strictlyprohibited. If you have received this email in error, please immediately notify us by return email or telephone if the sender's phone number is listed above, then promptlyand permanently delete this message. While all reasonable care has been taken to avoid the transmission of viruses, it is the responsibility of the recipient to ensure that the onward transmission, opening, oruse of this message and any attachments will not adversely affect its systems or data. No responsibility is accepted by the company in this regard and the recipientshould carry out such virus and other checks as it considers appropriate. 4-1/16" CM FMc SUPPORTS V-207 WELLHEAD = ACTUATOR= LEO INITIAL KB. ELE 87 BF. ELEV = 562' KOP= 250' Max Angle = 71" @ 6748' Datum MD= 83 45' DatumTVD= 4400'SS L-80, D = 8.835' I9-5/8" TAM PORT COLLAR 9-5/8" CSG, 47#, L-80 BTC, D = 8.681" 4481' " CSG. 26#. L-80 TCII XO TO L-80 BTC-M 6983- V-219 SAFETY NOTES: H2S READINGS AVERAGE 125 ppm WHEN ON MI. WELL REQUIRES A SSSV WHEN ON Mi. """HES PKR @ 8365' IS "PULL TO RELEASE' BUT CAN ALSO BE RBLEAS® BY PRESSURE DO NOT EXCEED 2000 PSI ON THE IA w/OUT PERFORMING TBG MOVEMENT CALC'S & DISCUSSING w/APE' WELL ANGLE> 70" 0 6748'. 362T 3-12" HE.S X NP, ID = 2.813" GAS LIFT MANDRELS ISTI MD TVDIDEVI TYPE I VLV LATCHIPORTI DATE 8 18283 ji 44511 61 1 MMG I DMY I RK 1 0 108119115 WATER INJECTION MANDRELS Minimum ID =2.75" @ 9276' 3-1/2" HES XN NIPPLE 6 5 4 3 2 1 8722 8793 8837 8892 9011 9226 4669 4704 4726 4753 4812 4919 60 60 60 60 60 61 MMG-W MMG-W MW W MW W MMG-W MMG-W AL-WFR DMY AL-WFR DMY AL-WFR MF-WFR RK RK RK RK RK RK 11 0 11 0 11 MAX 01/0825 1122108 09/10/23 1122108 09/10/23 09/10/23 7" MARKER JOINT w / RA TAG 8325' 7" X 3-1/2" HES DUEL F®THRU 8365' PK R, D = 2.965" 8312' 3-1 /2" HES X NIP, ID = 2.813" 8379' 3-1/2" NDPG MULTI -SUB, ID = 2.992" Nb 8746' 3-12" HES X NIP, ID = 2.813" Ej-- ml 3-1/2"MARKER JOINTw/RA TAG 8461' � 7 PERFORATION SUMMARY REF LOG: USTT LOG ON 1121108 ANGLEATTOPPERF: WA Note: Refer to Production DB for historical pert data SIZE SPF ZONE INTERVAL Opn/Sgz SHOT SQZ 4-12" 5 Nb 8415 - 8447 O 1120/08 4-12" 5 Oba 8801 - 8857 O 1120108 4-12" 5 OBb 8883 - 8909 O 1120108 4-12" 5 OBd 9088 - 9171 O 11120/08 4-12" 5 OBe 9235 - 9285 O 1120/08 TBG, 9.2#, L-80 TCI, .0087 bpf, ID = 2.992" 929W PBTD 949W 7" CSG, 26#, L-80 BTC-M .0383 bpf, D = 6276" 9673' PKR, D=2.965" 8776' 3-1/2" NDPG MULTI -SUB, D=2.992" OBa 8866' 7" X 3-1/2" HES DUELFEED TI-RU RIR, D = 2.965" 9041' �1 7" X 3-1/2" HES DUEL FEED THRU RICK D = 2.965" 9064' 3-1/2'NDPG SNGLESUB,D=2.992" OBd 13-112" HES X NIP, ID = 2.813" 1 9298' 3-1/2" WLEG, D=2.992" DATE REV BY COMMENTS DATE REV BY COMMENTS 11/22/08 N9ES ORIGINAL COMPLETION 0911123 CK/JMD WFR C/O (09/1023) 12/03/08 ?1 PJC DRI_GDRAFT CORRECTION 01/1325 CK/JMD WFRC/0(01/0825) 05/13/16 JMuVJMD PULLED PXN & SET RMX RUG (5/12/16) 01/04/17 JUJMD ADDED CSG XO 0125/18 FZ/JMD ADDED SPRING WEIGHT TO WFR 06/27/18 ZV/JraD WFR GfO(06126118) ORION UNIT WELL: V-219 PERMIT No: r`1081420 API No: 50-029-23397-00 SEC 11. T71 N 1171 E. 554' FNL It 4892' FEL Hilcorp North Slope, LLC CAUTION: This email originated from outside the State of Alaska mail system. Do not click links or open attachments unless you recognize the sender and know the content is safe. From:Wallace, Chris D (OGC) To:AOGCC Records (CED sponsored) Subject:FW: UNDER EVALUATION: Injector V-219 (PTD #208142) MIT-IA failed to reach test pressure Date:Tuesday, May 27, 2025 8:27:28 AM From: PB Wells Integrity <PBWellsIntegrity@hilcorp.com> Sent: Saturday, May 24, 2025 5:24 PM To: Wallace, Chris D (OGC) <chris.wallace@alaska.gov> Cc: Regg, James B (OGC) <jim.regg@alaska.gov>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Torin Roschinger <Torin.Roschinger@hilcorp.com> Subject: UNDER EVALUATION: Injector V-219 (PTD #208142) MIT-IA failed to reach test pressure Mr. Wallace, Injector V-219 (PTD #208142) MIT-IA failed to reach test pressure after pumping 10 bbls on 05/24/25. The tubing / casing pressure does not appear to be treading which would indicate a potential casing leak. The well is now classified as UNDER EVALUATION and on a 28 day clock to be resolved. Plan forward: 1. Downhole Diagnostics: Attempt to bleed IAP to 0 psi 2. Fullbore: Load and MIT-IA a. AOGCC MIT-IA if passes, b. Liquid leak rate if fails 3. Well Integrity: Further action as required. Please call with any questions or concerns. Ryan Holt Hilcorp Alaska LLC Field Well Integrity / Compliance Ryan.Holt@Hilcorp.com P: (907) 659-5102 M: (907) 232-1005 From: Alaska NS - PB - Field Well Integrity Sent: Wednesday, May 26, 2021 1:15 PM To: Wallace, Chris D (CED) <chris.wallace@alaska.gov> Cc: Regg, James B (CED) <jim.regg@alaska.gov>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Aras Worthington <Aras.Worthington@hilcorp.com>; John Condio - (C) <John.Condio@hilcorp.com> Subject: OPERABLE: Injector V-219 (PTD #208142) AOGCC MIT-IA Passed Mr. Wallace, Injector V-219 (PTD #208142) passed an AOGCC MIT-IA on 03/25/21 and has shown no signs of pressure communication during the online period. The well is now classified as OPERABLE. Please call with any questions or concerns. Ryan Holt Hilcorp Alaska LLC Field Well Integrity / Compliance Ryan.Holt@Hilcorp.com P: (907) 659-5102 M: (907) 232-1005 From: Wallace, Chris D (CED) <chris.wallace@alaska.gov> Sent: Thursday, April 15, 2021 3:03 PM To: Alaska NS - PB - Field Well Integrity <PBFieldWellIntegrity@hilcorp.com> Cc: Regg, James B (CED) <jim.regg@alaska.gov>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Aras Worthington <Aras.Worthington@hilcorp.com>; John Condio - (C) <John.Condio@hilcorp.com> Subject: [EXTERNAL] RE: Request: Injector V-219 (PTD #208142) Continued Diagnostic Work Andy, Your request for up to 28 days injection for additional monitoring and diagnostics is approved. Thanks and Regards, Chris Wallace, Sr. Petroleum Engineer, Alaska Oil and Gas Conservation Commission, 333 West 7th Avenue, Anchorage, AK 99501, (907) 793- 1250 (phone), (907) 276-7542 (fax), chris.wallace@alaska.gov CONFIDENTIALITY NOTICE: This e-mail message, including any attachments, contains information from the Alaska Oil and Gas Conservation Commission (AOGCC), State of Alaska and is for the sole use of the intended recipient(s). It may contain confidential and/or privileged information. The unauthorized review, use or disclosure of such information may violate state or federal law. If you are an unintended recipient of this e-mail, please delete it, without first saving or forwarding it, and, so that the AOGCC is aware of the mistake in sending it to you, contact Chris Wallace at 907-793- 1250 or chris.wallace@alaska.gov. From: Alaska NS - PB - Field Well Integrity <PBFieldWellIntegrity@hilcorp.com> Sent: Thursday, April 15, 2021 1:28 PM To: Wallace, Chris D (CED) <chris.wallace@alaska.gov> Cc: Regg, James B (CED) <jim.regg@alaska.gov>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Aras Worthington <Aras.Worthington@hilcorp.com>; John Condio - (C) <John.Condio@hilcorp.com> Subject: Request: Injector V-219 (PTD #208142) Continued Diagnostic Work Mr. Wallace, Injector V-219 (PTD #208142) was recently made Not Operable on 04/11/21 for failing an AOGCC witnessed MIT-IA and follow up diagnostic work indicated a leak at the uppermost packer. The well was shut in on 04/09/21 and Eline performed a leak detect log on 04/11/21. During the log, a leak rate of 1.0 gpm @ 2500 psi was established and the log indicated a packer leak @ 8365’ MD. The objective was to complete the log to surface to identify any other leaks. However, approximately 3.5 hours after starting the log, the leak stopped and a passing MIT-IA was performed to 2739 psi. On 04/13/21 DHD performed another passing MIT-IA to 2429 psi. Hilcorp is requesting permission to put the well back on injection Under Evaluation for up to 28 days to perform additional pressure testing and more diagnostic work if necessary. Plan Forward: 1. Operations: Put on injection 2. DHD: Perform MIT-IA 3. DHD/Fullbore (pending). If MIT-IA passes, perform AOGCC witnessed MIT-IA 4. Well Integrity: Additional diagnostics as needed Please respond with any questions. Andy Ogg Hilcorp Alaska LLC Field Well Integrity / Compliance andrew.ogg@hilcorp.com P: (907) 659-5102 M: (307)399-3816 From: Alaska NS - PB - Field Well Integrity Sent: Sunday, April 11, 2021 7:55 AM To: Wallace, Chris D (CED) <chris.wallace@alaska.gov> Cc: Regg, James B (CED) <jim.regg@alaska.gov>; Aras Worthington <Aras.Worthington@hilcorp.com>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com> Subject: NOT OPERABLE: Injector V-219 (PTD #208142) failed AOGCC MIT-IA Mr. Wallace, WAG Injector V-219 (PTD #208142) was made Under Evaluation for failing an AOGCC witnessed MIT-IA. On 03/19/21 DHD established a LLR of 1.0 gpm @ 2500 psi while pumping into the Inner Annulus. A passing PPPOT-T was performed ensuring the leak was not through the wellhead seals. Reviewing the downhole gauge data; there is evidence to suggest the leak is at the upper most packer. The slickline step to re-set the DGLV will be cancelled and E-line will perform an LDL. The well has been shut, freeze protected and will now be classified as NOT OPERABLE until the barriers are restored. Please respond with any questions. Andy Ogg Hilcorp Alaska LLC Field Well Integrity / Compliance andrew.ogg@hilcorp.com P: (907) 659-5102 M: (307)399-3816 From: Alaska NS - PB - Field Well Integrity <PBFieldWellIntegrity@hilcorp.com> Sent: Sunday, March 14, 2021 3:44 PM To: Wallace, Chris D (CED) <chris.wallace@alaska.gov> Cc: Regg, James B (CED) <jim.regg@alaska.gov>; Aras Worthington <Aras.Worthington@hilcorp.com>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Alaska NS - PB - Field Well Integrity <PBFieldWellIntegrity@hilcorp.com> Subject: UNDER EVALUATION: Injector V-219 (PTD #208142) failed AOGCC MIT-IA Mr. Wallace, WAG Injector V-219 (PTD #208142) failed its 4-year AOGCC MIT-IA on 03/14/21. The failed MIT-IA indicates a failure in one or more well barriers. The well is now classified as UNDER EVALUATION and is on the 28-day clock for diagnostics. Plan Forward: 1. Slickline: Re-Set DGLV in GLM #8. Perform MIT-IA 2. Fullbore/DHD: If MIT-IA passes after DGLV is re-set, perform online AOGCC witnessed MIT-IA 3. Slickline (Pending): Perform LDL with OE approval 4. Well Integrity: Additional diagnostics as needed Please respond with any questions. Andy Ogg Hilcorp Alaska LLC Field Well Integrity / Compliance andrew.ogg@hilcorp.com P: (907) 659-5102 M: (307)399-3816 The information contained in this email message is confidential and may be legally privileged and is intended only for the use of the individual or entity named above. Ifyou are not an intended recipient or if you have received this message in error, you are hereby notified that any dissemination, distribution, or copy of this email is strictlyprohibited. If you have received this email in error, please immediately notify us by return email or telephone if the sender's phone number is listed above, then promptlyand permanently delete this message. While all reasonable care has been taken to avoid the transmission of viruses, it is the responsibility of the recipient to ensure that the onward transmission, opening, oruse of this message and any attachments will not adversely affect its systems or data. No responsibility is accepted by the company in this regard and the recipientshould carry out such virus and other checks as it considers appropriate. The information contained in this email message is confidential and may be legally privileged and is intended only for the use of the individual or entity named above. Ifyou are not an intended recipient or if you have received this message in error, you are hereby notified that any dissemination, distribution, or copy of this email is strictlyprohibited. If you have received this email in error, please immediately notify us by return email or telephone if the sender's phone number is listed above, then promptly and permanently delete this message. While all reasonable care has been taken to avoid the transmission of viruses, it is the responsibility of the recipient to ensure that the onward transmission, opening, oruse of this message and any attachments will not adversely affect its systems or data. No responsibility is accepted by the company in this regard and the recipientshould carry out such virus and other checks as it considers appropriate. MEMORANDUM State of Alaska Alaska Oil and Gas Conservation Commission TO: Jim Regg j� r DATE: Wednesday, May 26, 2021 P.I. Supervisor `�� 1 SUBJECT: Mechanical Integrity Tests Hilcorp Noah Slope, LLC V-219 FROM: Lou Laubenstein PRUDHOE BAY UN ORIN V-219 Petroleum Inspector Sre: Inspector Reviewed By: -13 P.I. Supry i NON -CONFIDENTIAL Comm Well Name PRUDHOE BAY UN ORIN V-219 API Well Number 50-029-23397-00-00 Inspector Name: Lou Laubenstein Permit Number: 208-142-0 Inspection Date: 5/25/2021 - Insp Num: mitLOL210526080656 Rel Insp Num: Packer Depth Pretest Initial 15 Min 30 Min 45 Min 60 Min Well V-219 -Type Inj w -;TVD 4491 Tubing sol sol - 798 - soo - PTD 2081420 Type Test SPT ,iTest psi 1500 IA 724 1743 - 1681 - 1674 - BBL Pumped: 1 1.8 BBL Returned: 1.8- - - OA 288 292 - 292 - 291 Intervale 4YRTST p/F P ----- Notes: MIT -IA standard 4 year --,,I ; Gel lel �?ti2i �n l L S� Wednesday, May 26, 2021 PaL'e I of I Wallace, Chris D (CED) From: Wallace, Chris D (CED) Sent: Thursday, April 15, 2021 3:03 PM To: Alaska NS - PB - Field Well Integrity Cc: Regg, James B (CED); Oliver Sternicki; Aras Worthington; John Condio - (C) Subject: RE: Request: Injector V-219 (PTD #208142) Continued Diagnostic Work Andy, Your request for up to 28 days injection for additional monitoring and diagnostics is approved. Thanks and Regards, Chris Wallace, Sr. Petroleum Engineer, Alaska Oil and Gas Conservation Commission, 333 West 7th Avenue, Anchorage, AK 99501, (907) 793-1250 (phone), (907) 276-7542 (fax), chris.wallace@alaska.gov CONFIDENTIALITY NOTICE: This e-mail message, including any attachments, contains information from the Alaska Oil and Gas Conservation Commission (AOGCC), State of Alaska and is for the sole use of the intended recipient(s). It may contain confidential and/or privileged information. The unauthorized review, use or disclosure of such information may violate state or federal law. If you are an unintended recipient of this e-mail, please delete it, without first saving or forwarding it, and, so that the AOGCC is aware of the mistake in sending it to you, contact Chris Wallace at 907-793-1250 or chris.wallace@alaska.gov. From: Alaska NS - PB - Field Well Integrity <PBFieldWelllntegrity@hilcorp.com> Sent: Thursday, April 15, 20211:28 PM To: Wallace, Chris D (CED) <chris.waIlace @alaska.gov> Cc: Regg, James B (CED) <jim.regg@alaska.gov>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Aras Worthington <Aras.Worthington@hilcorp.com>; John Condio - (C) <John.Condio@hilcorp.com> Subject: Request: Injector V-219 (PTD #208142) Continued Diagnostic Work Mr. Wallace, Injector V-219 (PTD #208142) was recently made Not Operable on 04/11/21 for failing an AOGCC witnessed MIT -IA and follow up diagnostic work indicated a leak at the uppermost packer. The well was shut in on 04/09/21 and Eline performed a leak detect log on 04/11/21. During the log, a leak rate of 1.0 gpm @ 2500 psi was established and the log indicated a packer leak @ 8365' MD. The objective was to complete the log to surface to identify any other leaks. However, approximately 3.5 hours after starting the log, the leak stopped and a passing MIT -IA was performed to 2739 psi. On 04/13/21 DHD performed another passing MIT -IA to 2429 psi. Hilcorp is requesting permission to put the well back on injection Under Evaluation for up to 28 days to perform additional pressure testing and more diagnostic work if necessary. Plan Forward: 1. Operations: Put on injection 2. DHD: Perform MIT -IA 3. DHD/Fullbore (pending). If MIT -IA passes, perform AOGCC witnessed MIT -IA 4. Well Integrity: Additional diagnostics as needed Please respond with any questions. Andy Ogg Hilcorp Alaska LLC Field Well integrity/ Compliance MEMORANDUM State of Alaska Alaska Oil and Gas Conservation Commission TO: Jim Regg,\ 5I?�?2� -1 DATE: Wednesday, April 14, 2021 SUBJECT: Mechanical Integrity Tests P.I. Supervisor ( `�q Hilcorp North Slope, LLC V-219 FROM: Jeff Jones PRUDHOE BAY UN ORIN V-219 Petroleum Inspector Sre: Inspector Reviewed By: i6c— P.I. Supry NON-CONFIDENTIAL Comm Well Name PRUDHOE BAY UN ORIN V-219 API Well Number 50-029-23397-00-00 Inspector Name: Jeff Jones Permit Number: 208-142-0 Inspection Date: 3/14/2021 Insp Num: mitJJ210319094006 Rel Insp Num: Packer Depth WeII ;242 19 y e Inj �WJTVD a491 BBL Pum: T e BesBt SP JTest psi Lsoo o ? yp L Returned: z.3 Interval 4YRTST Notes: Repressured for a 2nd attempt; pressure loss >I0% Pretest Initial 15 Min 30 Min 45 Min 60 Min Cubing 1511 "1 1510- 1511 . IA 1851 2256 1873 OA 355 356 355, Wednesday, April 14, 2021 Page I of I MEMORANDUM TO: Jim Regg �J oejol P.I. Supervisor FROM: Jeff Jones Petroleum Inspector NON -CONFIDENTIAL State of Alaska Alaska Oil and Gas Conservation Commission DATE: Wednesday, April 14, 2021 SUBJECT: Mechanical Integrity Tests Hilcorp North Slope, LLC V-219 PRUDHOE BAY UN ORIN V-219 Sre: Inspector Reviewed By- P.I. Supry i Comm Well Name PRUDHOE BAY UN ORIN V-219 API Well Number 50-029-23397-00-00 Inspector Name: Jeff Jones Permit Number: 208-142-0 Inspection Date: 3/14/2021 Insp Num: mitJJ210315115000 Rel Insp Num: Packer Depth Well V-219 Type In,j w TVD 4491 PTD 2081420 - Type Test SPT Test psi 1500 BBL Pumped: 49 , BBL Returned: Interval 4YRTST ,. P Notes: Initial attempt; pressure loss >10% Pretest Initial 15 Min 30 Min 45 Min 60 Min Tubing 1511 1524 - 1511 IA 204 1 2238 - 1851' QA 350 356 - 355 i Wednesday, April 14, 2021 Page I of 1 Wallace, Chris D (CED) From: Alaska NS - PB - Field Well Integrity <PBFieldWelllntegrity@hilcorp.com> Sent: Sunday, April 11, 2021 7:55 AM To: Wallace, Chris D (CED) Cc: Regg, lames B (CED); Aras Worthington; Oliver Sternicki Subject: NOT OPERABLE: Injector V-219 (PTD #208142) failed AOGCC MIT -IA Mr. Wallace, WAG Injector V-219 (PTD #208142) was made Under Evaluation for failing an AOGCC witnessed MIT -IA. On 03/19/21 DHD established a LLR of 1.0 gpm @ 2500 psi while pumping into the Inner Annulus. A passing PPPOT-T was performed ensuring the leak was not through the wellhead seals. Reviewing the downhole gauge data; there is evidence to suggest the leak is at the upper most packer. The slickline step to re -set the DGLV will be cancelled and E -line will perform an LDL. The well has been shut, freeze protected and will now be classified as NOT OPERABLE until the barriers are restored. Please respond with any questions. Andy Ogg Hilcorp Alaska LLC Field Well Integrity/ Compliance a ndrew.oaePhilcoro.com P:(907)659-5102 M:(307)399-3816 From: Alaska NS - PB - Field Well Integrity <PBFieldWelllntegrity@hilcorp.com> Sent: Sunday, March 14, 20213:44 PM To: Wallace, Chris D (CED) <chris.waIlace @alaska.gov> Cc: Regg, James B (CED) <jim.regg@alaska.gov>; Aras Worthington <Aras.Worthington@hilcorp.com>; Oliver Sternicki <Oliver.Sternicki@hilcorp.com>; Alaska NS - PB - Field Well Integrity <PBFieldWelllntegrity@hilcorp.com> Subject: UNDER EVALUATION: Injector V-219 (PTD #208142) failed AOGCC MIT -IA Mr. Wallace, WAG Injector V-219 (PTD #208142) failed its 4 -year AOGCC MIT -IA on 03/14/21. The failed MIT -IA indicates a failure in one or more well barriers. The well is now classified as UNDER EVALUATION and is on the 28 -day clock for diagnostics. Plan Forward: 1. Slickline: Re -Set DGLV in GLM #8. Perform MIT -IA 2. Fullbore/DHD: If MIT -IA passes after DGLV is re -set, perform online AOGCC witnessed MIT -IA 3. Slickline (Pending): Perform LDL with OE approval 4. Well Integrity: Additional diagnostics as needed Please respond with any questions. Andy Ogg Hilcorp Alaska LLC Field Well Integrity/ Compliance andrew.ogg@hilcorp.com MEMORANDUM State of Alaska Permit Number: 208-142-0 Alaska Oil and Gas Conservation Commission To: Jim Regg DATE: Friday, March 19, 2021 Rel Insp Num: ``� y^7, r P.I. Supervisor �r/cq I �1 �6L1 SUBJECT: Mechanical Integrity Tests LL �� Hilcorp North Slope, LLC V-219 FROM: Jeff Jones PRUDHOE BAY UN ORIN V-219 Petroleum Inspector 1524 - 1511. Sre: Inspector Reviewed By: 2081420 'i P.I. Sup" JBV— NON-CONFIDENTIAL Comm Well Name PRUDHOE BAY UN ORIN V-219 API Well Number 50-029-23397-00-00 Inspector Name: Jeff Jones Permit Number: 208-142-0 Inspection Date: 3/15/2021 Insp Num: miUJ210315115000 Rel Insp Num: Packer Depth Pretest Initial 15 Min 30 Min 45 Min 60 Min Well V-219 - - Tubing 1511 1524 - 1511. PTD 2081420 'i WTVD4491 1500 - IA 204 2238 - 1851 BBL Pumped: OA 350 - 356 355Interval 0F Notes: mitijLLt1lanZ Pressure loss >10% 2�0— L M?4Oo- Friday, March 19, 2021 Pagc I of I MEMORANDUM State of Alaska Alaska Oil and Gas Conservation Commission TO: Jim RCgg DATE: Friday, March 19, 2021 I��j / / P.1. Supervisor `e/ ei, R(. Z SUBJECT: Mechanical Integrity Tests Hilcorp North Slope, LLC V-219 FROM: Jeff Jones PRUDHOE BAY UN ORIN V-219 Petroleum Inspector Src: Inspector Reviewed By: P.I. Sup" .T9P— NON-CONFIDENTIAL Comm Well Name PRUDHOE BAY UN ORIN V-219 API Well Number 50-029.23397-00-00 Inspector Name: Jeff Jones Permit Number: 208-142-0 Inspection Date: 3/1512021 ✓ Insp Num: mitJJ210319094006 Rel Insp Num: Packer Depth Pretest Initial 15 Min 30 Min 45 Min 60 Min pe Injt 491 ' Tubing 1511 1510- 1511 K1nterva10j1NrFAL 'Type Testi 1500 IA 1851 2256 - 1873 . BB 2.3 OA ass - 386 - 355 F Notes: Repressured for a 2nd attempt; pressure loss>10% v P—Cer an A0GCC--7rsP ept - µ it �cT?i1031 S115buo Friday, March 19, 2021 Page 1 of 1 Wallace, Chris D (CED) From: Alaska NS - PB - Field Well Integrity<PBFieldWelllntegrity@hilcorp.com> Sent: Sunday, March 14, 2021 3:44 PM To: Wallace, Chris D (CED) Cc: Regg, James B (CED); Aras Worthington; Oliver Sternicki; Alaska NS - PB - Field Well Integrity Subject: UNDER EVALUATION: Injector V-219 (PTD #208142) failed AOGCC MIT -IA Attachments: V-219.pdf Mr. Wallace, WAG Injector V-219 (PTD #208142) failed its 4 -year AOGCC MIT -IA on 03/14/21. The failed MIT -IA indicates a failure in one or more well barriers. The well is now classified as UNDER EVALUATION and is on the 28 -day clock for diagnostics. Plan Forward: 1. Slickline: Re -Set DGLV in GLM #8. Perform MIT -IA 2. Fullbore/DHD: If MIT -IA passes after DGLV is re -set, perform online AOGCC witnessed MIT -IA 3. Slickline (Pending): Perform LDL with OE approval 4. Well Integrity: Additional diagnostics as needed Please respond with any questions. Andy Ogg Hilcorp Alaska LLC Field Well Integrity / Compliance andrew.oRi=_C@hilcorD.com P: (907) 659-5102 M: (307)399-3816 4.000 3.800 3.6170 3,4W 3.200 3.00{} 1,800 2.600 2,400 2.200 2 X 1,800 1.60D 1.4'00 1,200 1.000 800 600 4DO 2 C Well -V-219 12,1420 12'21,20 122&24 CV0421 GIM -21 _"1821 012521 -2 &21 0215.21 022121 0301:21 03,0}21 220 200 180 160 140 0 120 0 1 0 60 60 40 20 TIO Plot —!— Tbg On ■ Bleed * Operabl -i- Not Ope ♦ Under E • MAN_IA —�— MAN 01 MAN 01 ♦ MAN_O( 0 Tempen The information contained in this email message is confidential and may be legally privileged and is intended only for the use of the individual or entity named above. If you are not an intended recipient or if you have received this message in error, you are hereby notified that any dissemination, distribution, or copy of this email is strictly prohibited. If you have received this email in error, please immediately notify us by return email or telephone if the sender's phone number is listed above, then promptly and permanently delete this message. 1 • • MEMORANDUM State of Alaska Alaska Oil and Gas Conservation Commission DATE: Tuesday,March 14,2017 TO: Jim Regg � P.I.Supervisor r` e -3(1511 7 SUBJECT: Mechanical Integrity Tests BP EXPLORATION(ALASKA)INC. V-219 FROM: Jeff Jones PRUDHOE BAY UN ORIN V-219 Petroleum Inspector Src: Inspector Reviewed By: P.I.Suprv�.`:7r-- NON-CONFIDENTIAL Comm Well Name PRUDHOE BAY UN ORIN V-219 API Well Number 50-029-23397-00-00 Inspector Name: Jeff Jones Permit Number: 208-142-0 Inspection Date: 3/7/2017 Insp Num: mitJJ170307161105 Rel Insp Num: Packer Depth Pretest Initial 15 Min 30 Min 45 Min 60 Min Well V-219 - Type Inj W- TVD 4491 - Tubing 1000 1007 - 1022 1020 PTD 2081420 ,Type Test SPT Test psi 1500 - IA 81 1690 • 1637 1628 BBL Pumped: 3 BBL Returned: 2 OA 480 489 489 492 Interval 4YRTST �P/F P 1-7 Notes: 1 well inspected,no exceptions noted. SCANNED AUG 2 4 2017. Tuesday,March 14,2017 Page 1 of 1 0 . PRS. V- z t? Pia zee3(4io ' Regg, James B (DOA) From: AK, D&C Well Integrity Coordinator <AKDCWellIntegrityCoordinator@bp.com> Sent: Sunday, October 04, 2015 8:14 PM To: Regg, James B (DOA);Wallace, Chris D (DOA); Brooks, Phoebe L (DOA); DOA AOGCC Prudhoe Bay ail- (O( (/5-- Cc: AK, D&C Well Integrity Coordinator Subject: September 2015 AOGCC MIT forms Attachments: September 2015 MIT Forms.zip All, SCANNED ,. ' ,, Please find the attached MIT forms for September 2015: Well: PTD#: Notes: GNI-02A 2061190 EPA form included GNI-03 1971890 EPA form included GNI-04 2071170 EPA form included OWDW-C 1002420 witness waived/EPA form included OWDW-NW 1002400 witness waived/EPA form included OWDW-SE 1002390 witness waived/EPA form included 09-11 1760840 09-22 1831730 B-17 1790280 NGI-13A 2071140 P-13 1901110 P5I-01 2021450 V-219 2081420 non-witnessed X-33 1961440 Thank you, Whitney Pettus (AIternute: /<cvin Pat ks) BP Alaska-Well Integrity Coordinator 0, ,,r4 ci WIC Office: 907.659.5102 WIC Email: AKDCWellIntegrityCoordinator@JBP.com 1 V • • STATE OF ALASKA ' ALASKA OIL AND GAS CONSERVATION COMMISSION Mechanical Integrity Test Submit to: jim.reoc aialaska.gov; AOGCC.Inspectors(5alaska.00v phoebe.brooks@alaska.00v chris.wallaceraalaska.00v OPERATOR: BP Exploration(Alaska),Inc. FIELD/UNIT/PAD: Prudhoe/GPB/V �Q l i d bi.r� DATE: 09/04/15 OPERATOR REP: Whitney Pettus AOGCC REP: Packer Depth Pretest Initial 15 Min. 30 Min. 45 Min. 60 Min. Well V-219 " Type Inj. N " TVD -4,491' Tubing • 27 "57 -44 '43 Interval p P.T.D. 2081420 ' Type test P - Test psi - 1500 Casing ' 3,009 - 2,849 2,814 P/F P V Notes: Non witnessed SI MIT-IA post GLV c/o OA 310 317 317 318 Well Type Inj. TVD Tubing Interval P.T.D. Type test Test psi Casing P/F Notes: OA Well Type Inj. TVD Tubing Interval P.T.D. Type test Test psi Casing P/F Notes: OA Well Type Inj. TVD Tubing Interval P.T.D. Type test Test psi Casing P/F Notes: OA Well Type Inj. TVD Tubing Interval P.T.D. Type test Test psi Casing P/F Notes: OA TYPE INJ Codes TYPE TEST Codes INTERVAL Codes D=Drilling Waste M=Annulus Monitoring I=Initial Test G=Gas P=Standard Pressure Test 4=Four Year Cycle I=Industrial Wastewater R=Internal Radioactive Tracer Survey V=Required by Variance N=Not Injecting A=Temperature Anomaly Survey 0=Other(describe in notes) W=Water D=Differential Temperature Test Form 10-426(Revised 11/2012) MIT PBU V-219 NON WITNESSED 09-04-15.xls Wallace, Chris D (DOA) From: Wallace, Chris D (DOA) Sent: Wednesday, September 09, 2015 9:53 AM To: 'AK, D&C Well Integrity Coordinator' Cc: Regg, James B (DOA) Subject: RE:Injector V-219 (PTD2081420) Permission to Return to Injection Whitney, As discussed, I agree with the plan below and your request for continued injection is approved. Thanks and Regards, Chris Wallace Sr. Petroleum Engineer Alaska Oil and Gas Conservation Commission 333 West 7`"Avenue Anchorage,AK 99501 �.��cn � P O ��� (907)793-1250(phone) �� Gf+ (907) 276-7542(fax) chris.wallace@alaska.gov CONFIDENTIALITY NOTICE:This e-mail message, including any attachments, contains information from the Alaska Oil and Gas Conservation Commission (AOGCC), State of Alaska and is for the sole use of the intended recipient(s). It may contain confidential and/or privileged information.The unauthorized review, use or disclosure of such information may violate state or federal law. If you are an unintended recipient of this e-mail, please delete it, without first saving or forwarding it, and, so that the AOGCC is aware of the mistake in sending it to you, contact Chris Wallace at 907-793-1250 or chris.wallace@alaska.gov. From: AK, D&C Well Integrity Coordinator [mailto:AKDCWeIIIntegrityCoordinator@bp.com] Sent: Wednesday, September 09, 2015 9:12 AM To: Wallace, Chris D (DOA) Cc: Regg, James B (DOA); AK, D&C Well Integrity Coordinator Subject: Injector V-219 (PTD2081420) Permission to Return to Injection Chris, Injector V-219 (PTD2081420) is a WAG well that had a dummy gas lift valve (station #8) removed during well work performed on August 16, 2015. The removal of the valve caused the well to lack two competent downhole barriers. The valve was reset on August 19, 2015 and a subsequent MIT-IA passed to 3000 psi on September 4, 2015. This injector is on a four year test cycle. The last state witnessed AOGCC MIT-IA was performed on February 26, 2013. BP requests permission to continue injection in this well utilizing the non-state witnessed MIT-IA performed on September 04, 2015 to demonstrate that the mechanical integrity of this well has been restored following wellwork. Another AOGCC state witnessed test will be requested in or before February 2017 in accordance with the four year cycle MIT testing requirements. A copy of the wellbore schematic, TIO and injection plot, and MIT form have been included for reference. Please call with any questions or concerns. Thank you, 1 Whitney Pettus (Alternate:Kevin Parks) BP Alaska-Well Integrity Coordinator GW WIC Office: 907.659.5102 WIC Email: AKDCWellIntegrityCoordinator@BP.com 2 • • Injector V-219(PTD#2081420) TIO Plot September 09,2015 MO 1.3111 V''.-•-•-•-• :..,... 1-.N. t• --.0;_01 -4 000. 1 0. ,................ ' \-.....- V \......-•-•-•-• ,r,...••••••••=*,..=...,,,,:I....V...S.:..Z...11.r.=ft•=.(7.-S...••••••••••••••••••.=_ 0699,5 36 16 IS 66.22.13 66 2.0 15 070113 e-w 15 ro:15 9129 13 OM 13 43 1115 oe pole 082545 019113 0406 15 Injection Plot %,•11'V-7111 2 460 -----.Nr 2 400 2 100 1 KO 2 000 1900 IOW 1 60D 1 500 1 400 ... IL& 1 1 400 -II L"--Oftel 1 200 "CO IMO SOD 260 700 600 , SLO 400 . X0 . 200 - ICC . 0,0413 r 1615 0,:.2.1, 071015 on,o.pos co.07S 017015 .. , 0;0' STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION Mechanical Integrity Test Submit to: jim.regq@a alaska.gov AOGCC.Inspectors@alaska.gov phoebe.brooks@alaska.gov chris.wallace(S alaska.gov OPERATOR: BP Exploration(Alaska),Inc. FIELD/UNIT 1 PAD: Prudhoe/GPB/V DATE: 09/04/15 OPERATOR REP: Whitney Pettus AOGCC REP: Non Witnessed Packer Depth Pretest Initial 15 Min. 30 Min. 45 Min. 60 Min. Well V-219 Type In). N TVD 4,491'_ Tubing 27 57 44 43 Interval 0 P.T.D. 2081420 Type test P Test psi 1500 Casing 3,009 2,849 2,814 P/F P Notes: Non witnessed SI MIT-IA post GLV c/o OA 310 317 317 318 Well Type lnj. TVD Tubing Interval P.T.D. Type test Test psi CasingP/F Notes: OA Well Type Inj. TVD Tubing Interval P.T.D. Type test Test psi Casing P/F - - Notes: OA Well Type Inj._ TVD Tubing Interval P.T.D. Type test Test psi Casing P/F Notes: OA Well Type Inj. TVD Tubing Interval - - P.T.D. Type test Test psi Casing P/F - - Notes: OA TYPE INJ Codes TYPE TEST Codes INTERVAL Codes D=Drilling Waste M=Annulus Monitoring I=Initial Test G=Gas P=Standard Pressure Test 4=Four Year Cycle I=Industrial Wastewater R=Internal Radioactive Tracer Survey V=Required by Variance N=Not Injecting A=Temperature Anomaly Survey 0=Other(describe in notes) W=Water D=Differential Temperature Test Form 10-426(Revised 11/2012) MIT PBU V-219 NON WITNESSED 09-04-15(2).xls Wallace, Chris D (DOA) From: AK, D&C Well Integrity Coordinator <AKDCWellIntegrityCoordinator@bp.com> Sent: Monday, August 17, 2015 10:27 AM To: AK, OPS GC2 OSM; AK, OPS GC2 Field O&M TL; AK, OPS GC2 Wellpad Lead; AK, OPS Prod Controllers; Cismoski, Doug A; Daniel, Ryan; AK, D&C Wireline Operations Superintendent; AK, D&C Well Services Operations Superintendent; AK, RES GPB West Wells Opt Engr; AK, RES GPB East Wells Opt Engr; AK, OPS Well Pad LV; Swensen, Brenden; 'chris.wallace@alaska.gov' Cc: AK, D&C Well Integrity Coordinator;AK, D&C DHD Well Integrity Engineer; AK, D&C Projects Well Integrity Engineer; AK, OPS FF Well Ops Comp Rep; Sternicki, Oliver R; Pettus, Whitney; Regg, James B (DOA) Subject: NOT OPERABLE: Injector V-219 PTD (#2081420) TxIA communication due to Valve Left out of Pocket All, Injector V-219 PTD (#2081420) had a gas lift valve removed during well work performed on August 16, 2015 that caused the well to lack two competent barriers downhole. The well is reclassified as Not Operable until tubing integrity can be restored.This well has been added to the Quarterly Not Operable Injector Report. Please call with any questions or concerns. Thank you, Whitney Pettus (Alternate: Kevin Parks) BP Alaska-Well Integrity Coordinator GVV WIC Office: 907.659.5102 WIC Email: AKDCWeIlIntegrityCoordinator@BP.com 1 Ima a Pro~ct Well History File Cov~age g XHVZE This page identifies those items that were not scanned during the initial production scanning phase. They are available in the original file, may be scanned during a special rescan activity or are viewable by direct inspection of the file. gj - ~ ~- ~, Well History File Identifier Or anizin (done) wo-sided II I II'I II II II I II III ^ Rescan Needed II I II') II II I I II I III 9 9 RES AN DIG TAL DATA OVERSIZED (Scannable) Color Items: Diskettes, No. , ^ Maps: ^ Greyscale Items: ^ Other, No/Type: ^ Other Items Scannable by a Large Scanner ^ Poor Quality Originals: OVERSIZED (Non-Scannable) ^ Other: ^ Logs of various kinds: NOTES: ^ Other:: BY: Maria Date: , ~ /s~ Pro "ect Proo~n II I II ~I II I I III V III 5 Maria Date ~ ~s~ 1 BY: x 30 = D + ! D =TOTAL PAGES ~~ Scanning Preparation _~ (Count does not include cover sheet) BY: _ Maria Date: 3 ~`7 ~ /s/ Prnt~luctinn Scanning Stage 1 Page Count from Scanned File: ~' (Count does include cov sheet) Number in Scan in Pre aration: YES NO Page Count Matches g P BY: Maria Date: ~ ~ ~~ ~s~ Stage 1 If NO in stage 1, page(s) discrepancies were found: YES NO BY: Maria Date: ~s~ Scannin is com lets at this point unless rescanning is required. II I II II II I II II I I I 9 P Rescanned III IIIIIIIIIII VIII BY: Maria Date: ~s~ Comments about this file: Quality Checked III IIIIII III III III 10/6/2005 Well History File Cover Page.doc 11/30/10 SISMOIMPP ,.... NO. 5852 Alaska Data & Consulting Services Company: State of Alaska 2525 GambsH Street, Suite 400 Alaska Oil & Gas Cons Comm Anchorage, AK 99503 Attn: Christine Shartzer ATTN: Beth 333 West 7th Ave, Suite 100 Anchorage, AK 99501 Well Job* Log Description Date BL Color CD Z-01B BD88-00070 MEM PROD PROFILE 00 /f - it/ if' 10131110 1 ' , c9 1 04.25 BJOH-00005 INJECTION PROFILE (2") u-r.... /tea C.049 11108/10 1 1 '.4i I 04-25 BJOH-00005 INJECTION PROFILE 5 _ -. .._ 11109110 1 4 0. V.* 1 V-07 BAUJ-00052 MEM PROD PROFILE _ / it 11/12/10 1 gi Al 1 1 08-24A BCRD-00088 PRODUCTION PROFILE a k - ' 11/11110 1 F-19A AWJI-00121 MEM PROD PFIORLE _ . 11/09/10 1 ,,,.ko • 1 X-25 131388-00088 MEMORY OLS 10/30/10 1 F. .-, 1 P-08A BCUE-00090 MEMORY OLS - /11 • , 10122/10 1 . 14 1 04-30 8088-00083 MEM PROD PROFILE -=- - - • ,), 10128110 1 Fir,-ett. I 01-08A BCRD-00083 PRODUCTION PROFILE E, • 10/23/10 1 p.m., _ 1 D-33 BD88-00081 Ell==1111111na411 10420110 1 .1 LATA4lio al Z-26A 131388-00087 MEM PROD PROFILE WM.1171• -ir 10/28/10 1 "..A. 1 Z-13A 8088-00062 MEM PROD PRORLE i .e .L 1 012 21 10 1 PI 01-02 SCRD-00088 ll ' I ; ;IC 0 1 / A 0 MIIIMWOri iffnilliTaal:P i V 19 -, -00069 12z 10131110 1 WSW I PLEASE ACKNOWLEDGE RECEIPT BY SIGNING AND RETURNING ONE COPY EACH TO: _ BP Exploration (Alaska) Inc Alaska Data & Consulting Services Petrotechnical Data Center LR2-1 2525 Gembell Street, Suite 400 900 E. Benson Blvd. Anchorage, AK 99503-2838 %AWNED MAR 14 201'i 0 § 1 Pit• r ‘, , . II il 00 0 0 k• eanp, fr,-,. .-. e nt r alti . AratotfIVA DATA SUBMITTAL COMPLIANCE REPORT 3/15/2010 Permit to Drill 2081420 Well Name/No. PRUDHOE BAY UN GRIN V-219 Operator 8P EXPLORATION (ALASKAt INC API No. 50-0(29~-23397-00-00 MD 9583 TVD 5090 Completion Date 11/23/2008 Completion Status WAGIN Current Status WAGIN ~IW"- REQUIRED INFORMATION Mud Log No Samples No Directional Survey Ye -- -- -- ~ - DATA INFORMATION Types Electric or Other Logs Run: MWD, GR, RES, NEU, AZI DEN, PWD, CBL /USIT (data taken from Logs Portion of Master Well Data Maint Well Log Information: Log/ Electr Data Digital Dataset Log Log Run Interval OH / r yp meamrmi rvumaer Name acme meara No start stop cti Kecerved comments g Sonic C eau ~K#-E..,.~ 5 Col 200 8297 Case 12/31/2008 USIT Cement, GR, CCL 21- / Nov-2008 ED C Pds 17385 ~'Se~ie C.~.~: R`F"~ ~ 200 8297 Case 12/31/2008 USIT Cement, GR, CCL 21- Nov-2008 ~ D C Lis 17430 duction/Resistivity 106 9585 Open 1/14/2009 LIS Veri, GR, Rop, FET, RPX, RPS, RPM, RPD, DRHO, NPHI Log Induction/Resistivity 25 Blu 108 9540 Open 1/14/2009 MD Vision Service Lo , Indyction/Resistivity .25 ~ Blu 108 9540 Open 1/14/2009 TVD Vision Service D C Lis 17536~Gam~a-Ray ~, ~~^~ ~u ~~ 111 9296 Case 1/28/2009 LIS Veri, GR, CCL, Tens ED C Pds 17747'~Seaie C e~n.•.~ ~•~; - C~ ~~'~ 200 9297 Case 3/20/2009 USIT-D, CEL, GR, CCL, ~~ ~ GPIT 21-Nov-2008 og 17747 Sonic C''""''1~ 5 Col 200 9297 Case 3/20/2009 USIT-D, CEL, GR, CCL, GPIT 21-Nov-2008 D,-' b Asc Directional Survey 0 9583 Open 11/25/2008 Rpt Directional Survey 0 9583 Open 11/25/2008 Well Cores/Samples Information: • Sample Interval Set Name Start Stop Sent Received Number Comments DATA SUBMITTAL COMPLIANCE REPORT 3/15/2010 Permit to Drill 2081420 Well Name/No. PRUDHOE BAY UN ORIN V-219 Operator BP EXPLORATION (ALASICI~ INC API No. 50-029-23397-00-00 MD 9583 TVD 5090 Completion Date 11!23/2008 Completion Status WAGIN Current Status WAGIN UIC Y ADDITIONAL INFORM ION j~, Well Cored? Y / Daily History Received? (U]'~~N Chips Received? ~% N Formation Tops y"" N .,.~-- Analysis Y / N Received? - . Comments: Compliance Reviewed By: ~~ Date: ~> ~^'~- ~~ BP Exploration (Alaska) Inc. Attn: Well Integrity Coordinator, PRB-20 Post Office Box 196612 Anchorage, Alaska 99519-6612 August 14, 2009 by ~CEI~/~ ocT o ~ zoo9 Mr. Tom Maunder Alaska Oil and Gas Conservation Commission 333 West 7th Avenue Anchorage, Alaska 99501 Subject: Corroslon Inhlbltor Treatments of GPB V-Pad Dear Mr. Maunder, eta Oil & Gas Cons. CatnmiR+~ion Anchorage v- ~-.-~ Enclosed please find multiple copies of a spreadsheet with a list of wells from GPB V- Pad that were treated with corrosion inhibitor in the surface casing by conductor annulus. The corrosion inhibitor is engineered to prevent water from entering the annular space and causing external corrosion that could result in a surface casing leak to atmosphere. The attached spreadsheet represents the well name, API and PTD numbers, top of cement depth prior to filling and volumes of corrosion inhibitor used in each conductor. As per previous agreement with the AOGCC, this letter and spreadsheet serve as notification that the treatments took place and meet the requirements of form 10-404, Report of Sundry Operations. If you require any additional information, please contact me or my alternate, Anna Dube, at 659-5102. Sincerely, Torin Roschinger BPXA, Well Integrity Coordinator BP Exploration (Alaska) Inc. Surface Casing by Conductor Annulus Cement, Corrosion inhibitor, Sealant Top-off Report of Sundry Operations (10-404) 1 ..-~ Date V-pad 8/13/2009 Well Name PTD # API # Initial top of cement Vol. of cement um ed Final top of cement Cement top off date Corrosion inhibitor Corrosion inhibitor/ sealant date ft bbls ft na al V-Ot 2040900 50029232100000 NA 2 NA 17 6/30!2009 V-02 2040770 50029232090000 NA 3 NA 43.4 7!11/2009 V-03 2022150 50029231240000 surface NA NA NA NA V-04 2061340 50029233220000 NA 1.5 NA 20.4 6/29/2009 V-05 2080930 50029233910000 NA 1.75 NA 20.4 5/10/2009 V-07 2071410 50029233720000 NA 0.25 NA 1.7 6/29/2009 V-100 2010590 50029230080000 NA 1.5 NA 20.4 5/9/2009 V-101 2020560 50029230740000 NA 3.75 NA 32.3 7/10/2009 V-102 2020330 50029230700000 NA 7.75 NA 98.2 8/7!2009 V-103 2021860 50029231170000 NA 0.5 NA 9.4 7/12/2009 V-104 2021420 50029231030000 NA 1.5 NA 21.3 7/11/2009 V-105 2021310 50029230970000 NA 2.25 NA 23.8 6/29/2009 V-106A 2041850 50029230830100 NA 1.75 NA 17 6/29/2009 V-107 2021550 50029231080000 NA 1.75 NA 13.6 7/11!2009 V-108 2021660 50029231120000 NA 1.5 NA 14.5 7/10/2009 V-109 2022020 50029231200000 NA 1.2 NA 10.2 6/30/2009 V-111 2031030 50029231610000 NA 1.5 NA 11.9 7/12/2009 V-112 2060200 50029233000000 NA 1.5 NA 15.3 5/10/2009 V-113 2022160 50029231250000 NA 2.5 NA 37.4 5/10/2009 V-114A 2031850 50029231780100 NA 2.5 NA 34 6/30/2009 V-115 2040270 50029231950000 NA 1.5 NA 13.1 5/9/2009 V-117 2030900 50029231560000 NA 1.25 NA 22.1 5/10/2009 V-119 2040410 50029232010000 NA 2 NA 18.7 6/30/2009 V-120 2041790 50029232250000 NA 1.5 NA 8.5 7/12/2009 V-121 2070360 50029233480000 NA 1.9 NA 17 6/30/2009 V-122 2061470 50029233280000 NA 1.5 NA 6.8 5/10/2009 V-201 2012220 50029230540000 SC leak NA 4 NA 90.6 8/7/2009 V-202 2030770 50029231530000 NA 1.75 NA 12.8 7/11/2009 V-203 2051680 50029232850000 NA 2 NA 12.8 7/10/2009 V-204 2041310 50029232170000 NA 2 NA 22.1 6/30/2009 V-205 2061800 50029233380000 NA 1.8 NA 13.6 6/30/2009 V-207 2080660 50029233900000 NA 1.75 NA 18.28 1/9/2009 V-210 2042100 50029232310000 NA 2 NA 18.7 7/11/2009 V-211 2042200 50029232320000 NA 1.5 NA 13.6 7/10/2009 V-212 2051500 50029232790000 NA 1.2 NA 11.9 6/29/2009 V-213 2041160 50029232130000 NA 1.75 NA 6.3 5/9/2009 V-214 2051340 50029232750000 NA 0.5 NA 9.4 7/11/2009 V-215 2070410 50029233510000 NA 2.8 NA 30.6 6/30/2009 V-216 2041300 50029232160000 NA 1.5 NA 13.6 6/29/2009 V-217 2061620 50029233340000 NA 2.3 NA 25.5 6/30/2009 V-218 2070400 50029233500000 NA 2 NA 17.9 7/12/2009 V-219 2081420 50029233970000 NA 1 NA 16.2 7/12/2009 u-228 2080200 50029233830000 NA 1.75 NA ~ 3/9/2008 V-221 2050130 50029232460000 NA 0.8 NA 8.5 6/29/2009 V-222 2070590 50029233570000 NA 2.5 NA 21.3 7/11/2009 V-223 2080220 50029233840000 NA 2 NA 20.5 9/7/2008 PTD 208-142, V-219 • • Page 1 of 1 Fleckenstein, Robert J (DOA) From: Stewman, Sondra D [Sondra.Stewman@bp.com] Sent: Tuesday, September 15, 2009 10:34 AM To: Fleckenstein, Robert J (DOA) Subject: PTD 208-142, V-219 Attachments: V-219, 10-407:pdf; PTD 208-142, V-219, Ops Summary 11-2008.pdf; V-219.pdf; V-219 ASP Final Survey.xls Bob, As requested attached are the following electronic data files as it pertains to Well V-219, 11- 2008 Completion Summaries /data: 10-407 Well Completion Report Summary of Daily Drilling Reports Well Schematic Diagram Surveys «V-219, 10-407.pdf» «PTD 208-142, V-219, Ops Summary 11-2008.pdf» «V-219.pdf» «V-219 ASP Final Survey.xls» Please advise if you require further information. Thank you, Sondra Stewman ADW Drilling Technologist ~(? real, 13e~re~er~t ctncl n~~aSt r>fall lie POSITIVE! 9/15/2009 STATE OF AEASKA AtASftA ~ANQ GAS CONSERVATION COMMION VtiELL CQNIPLETfON C~Ft RECC?MPL.ETlOfV Rt~PORT ANf~ L.QG 'Eck, Wet) Status: ^ Oil [~ Gas Q Plugged. ~ Abandoned ^ Suspended zepac 25.~4s 2orwG zs „o ^ GINJ [~ WINJ ^ WDSPL ~ WAG ^ t7thet No. of Completions Otte 1b. Well Class: ^ Development ^ Expforafory ®Service ^ Stratigraphic 2. Operator Name: BP Explarafion (Alaska) Inc. 5. Date Oomp., Susp., or Abend. 11-23-2008 / 12. Permit to Drill Number 208-142 3. Address: P.O. Box 196612, Anchorage, Alaska 99519-6612 f. Date Spudded '11-3-2008 v 13. API Number 50-029-23397-00-00 /~ 4a. Location of Well (Governmental Section): Surface: 7. Date T,D. Reached 11/'1712008 ~ 14, Weil Name and Number: PDU V-219 j 472E f=SL, 1488' FEI_, SBC. 11, T11N, Ft11E, UM Tap of Productive Horizon: 4184' FSL, 543' FCL, SEG. 12, T11P+1, R11E, UM ~ 8. KB (~ above MSL): 82 Ground (ft MSL): 53.5 i 15, Field /Pool(s): Prudhoe Bay Field l Arian Total Depth: 4759' FSL, 4608' FEL, SEC. U7, T11N, f~12E, Clf~~f 9. Plug f3acR Depth (MD+TVD} 9490` 5045 Schrader Bluff ~ 4b. Location of Well (State Base Plane Coordinates, NAD 27): Surface: x- 590813 y- 5969976 Zane- ASP4 1f1. Total Depth (MD+TVD} 9583 ' 5090 ~ 1fa. Property Designation: ,,~ ADL 028240,'~DL 047450 TPI: x- 597045 y_ 5969512 Zane- ASP4 _. _ -- -- ---_ _ . v _ ASP4 5970099 ~ Z 597880 ~ 11. SSSV t?epth (MD+TVD) None 17. Land Use Permit: one- y- Total Depth: x- f TVD 18. Directional Survey ~ Yes ^ No Suomi electronic an rin ed inf rm tion er 2 19. Water depth, if offshore N/A ft MSt. rost ( ): 20. Thickness of Perma 1900' (Approx.} 21. Logs Obtained (List all logs here and submit electronic and'. printed Information per 20 AAG 25.071): MWD , GR, RES, NEU, AZI DEN, PWD, CBL / USIT 22. CASING. LINER AHa G>snaENTING RECORD CASING SETTING DEPTH MD SETTING [}EpTtt TVD I'{OLE AMOUNT. Wf. PER FT, GRADE TOP BOTTOM TOP BOTTOM SI"T_E CEMENTING RECORD PULLED 20" 91.fi#t A-53 Surface 108' Surface 108' 42" 2 0 sx Arc is Set A ~rox. g-r/~" _ 4 #~ -30 2 44 ~ ~ 1 .-114" 776 x Dee ,roe 415 ~x ass 'G' __ 7, ; ~,?k t_-30 6' 857 ' 6' .5036' 8-314" lOE1 sx LiteCrrae 403 sx Cf:~s. 'G' 23. ppen to production or inject ion? ®Yes ^ t~lo 24. TUyING RECORD tf YeS, IISt eaoh Interval Open d N i b P rf S SIZE DEPTH SET RhD PACKER SET MD er}: um ize an e orat (MD+TVD of Top & Bottom; on 5 Si~F Diameter 4 1/2" G 3-1 /2" 9.2#, L-80 9298' 8365', 876T, 8856' & J041` , - un MD TVD MD TVD 841 `J'' - X447° 4516' - 4532 ' ' ' 25. ACID, FRACTURE, CEMENT SQUEEZE, ETC. - 4736 - 885T 4708 8801 H883~ - £3909' 4740' - 4762' DEPTFt INTERVAL MD AMOUNT & KWD OP MATERIAL USED 9088' - 917~t' A851`-4x92' ' ' ` ' Freeze Protected with 122 Bbis Diesel 4024 - 4948 - 9285 9235 2fs. PRQDUCTION TEST ... Gate First Production: Not on injection tc. Method of Operation (Flowing, Gas Lift, A~as~a Oil & Gas Cons, Commission .. Date of Test: t'IOUrS Tested: t7RODUCTIQN ~aR TEST pERIQD ()~l•BBf.: GAS-McF: WATER-BE3t,: Ceti .GAS-Qtt_ E~ATrO: FIOW Tubinr~ Press. Casing P(eSS: CALCULATED 2a-HOl)R RATE QIL-~EiL: GAS-MCE: WATER-BE3L: Orr_ GRAVITY-API (CORK}: 27. CORE DATA Conventianai Cores} Acquired? ^ Yes ~ No SideWal i Gores Ac uired? ^ Yes ®No If Yes to either question, list formations end intervals cored (MD+TVD of top and 4attpm 4f each), and summarize lithology and presence of oil, gas or water (submit separate sheets with this form, if needed}. Submit. detailed descripti©ns, care Chips, photographs and laboratory analyticat results per 20 AAC 250.071.. cor~Pl~-~-aPa None l~ D ., 1a Form 10-407 F~evised 02/2007 GDNTtNUED CAN F~EUERSE s~Qe ~~~~~ ~., . ~ ~ _ 200 ~ ~'~~~ t~ l~ ZS, GEdLOGIC MARKERS LIST ACt. FORF.tATIONS AND S ENCOUNTERED): ~~. FQRMATtdN TESTS NAMt; MD TVD Weli Tested? ~ Yes ~ No if yes, list intervals and formations tested, briefly summarizing test perrnafra5t Taf} results. Attach separate sheets to this form, if needed, and su6mik Permafrost Base detailed test information per 20 AAC 25.Q71. Tap of Ugnu 4550' 294Q' None Shrader E3h:ff NA 8350' 444' at~rader Chuff NB 8408' 451' Shrader Bluff NC 84"ll' 4547` Shrader Bluff NB $494` 455x' Shrader Bluff NF 8597' <i60c6' Shrader F31uff OA 8675` 4640' Shrader Bluff OBa 3796` 4705' Shrader Bluff ~E3b £3£377' 4746° ihrader Bluff OBc 8979' 4797 5hr-ader Bluff Of3cl 9034` 4849' Shrader Bluff OBe 9230' ,921' Shrader Bluff OBf 9325` 4967 Base of Shrader Bluff OBf t Top of Colville Mudstane 9441" 5022` Formation atTofa! Depth (Name): Co{ville Mudstor7a 9441' 5C122F 30. List of Attachments: Summaryof Daily Drilling Reports, Well Scherrtatic Diagram, Surveys, artd a Leak-Off Test Summary. 31. I hereby certify That the foregoing is true and correct to the best of my knowledge.. ~,,,.. - ~ t D ~ " ~ ~ ate ~.~' . ,.,z.,~-.--_~_Titte Drilling Technologis Signed Sor~ara St~wman , f ~ ~~ pBU V-219 208-142 Prepared ByName/Number. Sandra Sfewman, 564-475Q Well Number DrriltrrgEngrnaer Arpanda F?ebol, 664-5543 O. ~ r v l INSTRUCttONs GEKERAI: This#qnn is designed far submitting a complete and correct w8ll completion report and log on all types of lands and leases in Alaska. Subrrtita well schematic diagranrwith each 10-A07 well completion report and 1Q-4t74 wall sundry report when the downhole welt design is changed. STEM 1a: Glassificatian of Service Walls: Gas Injection, Water Injection, Water-Alternating-Gas Injection, Salt Water Disposal, WaterSupply for Injection., Observation, or E7ther. Multiple completion is dettnad as a well prgducing from more than one pool with production #ram each pool completely segregated. Each segregated pool is a completion, ITEM 4t}i Tpt (Top of Producing Interval). treat 8: The Keliy Bushiny and Ground Level elevation In feet abgva mean sea level. Use lama as reference for depth measurements given in other spaces on this form and in any attachments. IT~ha 13: The API number reported to AOGCC must be 1A digits (ex: 50-029-20123-00-00), .ITEM 2f}: Report true vertical thickness of permafrost in Box 2d. provide MD and TVC7 fqr the top and base of permafrost in Box 28, ITEM 22: Attached supplemental recgrds for this weft should show the details of any multiple stage cementing and the Igcation of the cementing tool. ITEM 23r If this well is completed for separate production tram mare titan qne interval (multiple cgrnpietion), so state in item 1, and in'item 23 show the producing intervals for only the interval reported in item 2t3. (Submit a separate form far each additional interval to be separately produced, showing the data pertinent to such Interval). ITEM 26: Method of Operation: Flowing, Gas Lift, Rod pump, FlydrauliC pump, Submersible, Water (njecfion, Gas (njection, Shut-In, or Other (explainj: ITEM 27: Provide a listing of intervals cared and the correspgnding formations, and a brief descriptign in this box. Submit detailed description and analytical. laboratory information required by 20 AAC 25.071. ITEM Z9: provide a listing of intervals tasted and the correspgnding fgrmatian, and a brief sumrrtary in this box, Submit datailecl fast and analytical laboratory information required by 20 AAC 25.471. Form 10-407 Revised 02/2007 Submit Origirrat Only BP EXPLORATION Page 1 of 13 Operations Summary Report Legal Well Name: V-219 Common Well Name: V-219 Spud Date: 11/8/2008 Event Name: DRILL+COMPLETE Start: 11/6!2008 End: 11/23/2008 Contractor Name: NABOBS ALASKA DRILLING I Rig Release: 11/23/2008 Rig Name: NABOBS 9ES Rig Number: 9ES !! I Date 'From - To Haurs 1 Task Code NPT Phase Description of Operations 11!6/2008 100:00 - 01:00 ~ 1,00 ~ MOB ~ P ~ ~ PRE I Rig released from Annual Maintenance at 00:00 hrs 01:00 - 02:00 ( 1.00 ~ MOB [ P 02:00 - 03:30 f 1.50 MOB I P 03:30 - 14;00 ( 10.501 CONS I P 14:00 - 17:00 1 3.001 MOB 1 P f 17:00 - 22:00 { 5.00 ~ MOB ~ P I -00:00 I 2.003 R1GU {P 1.11!7!2008 100:00 - 12:00 1 1.2.00 (RIGU 'Begin rig move. Stage pits at V-2191 PRE Move sub and stage in front of V-219i. PRE Set rig mats. Spread pit liner. remove hand rail from V-213 well house. '..'Call out crane to move V-213 well house back -1 foot to make room for beaver slide. PRE CONTINUE WITH RIG MAINTENANCE: -re-route man rider cables. -Connect service loop to top drive. -Bring sub rack, subs, and pipe handling tools from pipe shed back to rig floor. -Bring iron roughneck spinners and tong jaws to rig floor. -Clean and clear the rig maintenance site. -Install EZ Torque. -Check and fill oil in top drive. PRE PJSM. Spot rig over V-2191. Lay rig mats. PJSM. Spot pits next to rig. Hook up innerconnect. Close cellar. Prep pipe shed for drill pipe. 'SIMOPS: CONTINUE WITH RIG MAINTENANCE Connect top drive power lines. PRE Load 3400' of 4" drill pipe into pipe shed and begin to strap. Remave A-leg brace. Bridle Down. Hook up electric inner connect. SIMOPS: CONTINUE WITH RIG MAINTENANCE. -Hook hydraulic service loop to top drive. -Install link tilt cylinders. -Test top drive: Not working. Trouble shoot top drive. PRE Prepare cellar for nipple up. SIMOPS: CONTINUE W{TH RIG MAINTENANCE -Trouble shoot top drive. PRE CONTINUE ANNUAL RIG MAINTENANCE: j -Gontinue to trouble shoot top drive electrical problem. -install blower duct on top drive. -Install jaws and spinners on tron Roughneck. -Hang tongs and cut excess line. -Function test Iron Roughneck. SiMOPS for V-219i. -Tie back bridle lines. -Nipple up riser and dresser sleeve. Printed: 9t15120099:58i53AM C __ BP EXPLORATION Page 2 of 13 Operations Summary Report Legal Well Name: V-219 Common Well Name: V-2i9 Spud Date: 11/8/2008 Event Name: DRILL+COMPLETE Start: 11/6/2008 End: 11/23/2008 Contractor Name: NABOBS ALASKA DRILLING I Rig Release: 11/23!2008 'Rig Name: NABOBS 9ES Rig Number: 9ES I Date I From - To Hours Task (Code NPT Phase Description of Operations 11(7/2008 00:00 12:00 12.00 'RIGU {P PRE -Finish strap on 4" drill pipe and HWDP. 12:00 - 18:00 6.00 CONS P PRE CONTINUE ANNUAL RIG MAINTENANCE: ~-Continue to trouble shoot top drive. -Remove lower tap drive mud saver valve and adjust actuator. !-Install Bails and 4" elevators. -Torque wash pipe to 4500 ft-Ibs. -Install lower mud saver valve and lower !BOP. ', -Torque lower !BOP to 28K ft-Ibs. i -Install clamp and torque to 198 it-Ibs. -Torque top drive quill tc 58K ft-Ibs. -Slip drilling line to 19 wraps. 18:00 - 00:00 6.00 RIGU P PRE ACCEPT RIG AT 18:00 hours. -Finish slipping drill line. -Install Kelly hose. 11/8/2008 00:00 - 02:00 2.00 RIGU P PRE Finish hooking up kelly hose to top drive. Install safety cables. Tie service loop hoses together. ,Rig up MWD pressure sensor 02:00 -04:00' 2.00 'RIGU P PRE PJSM io pick up 4" drill pipe and stand back In derrick. Problems with Iron Roughneck while making up firstjoint. Bring 12-1/4" drilling BHA to rig floor while Iron Roughneck repaired. 04:00 - 08:30 4,50 RIGU P PRE Pick up 111 joints of 4" drill pipe singles from the pipe shed and stand back in the derrick. . 08:30 - 10:30 2.00 RIGU P PRE Pick up 21 joints of 4" HWDP and stand back in the derrick. 10:30 - 11:30 1:00 RIGU P PRE Function test the diverter bag and knife valve. Test witness waived by AOGCC rep Bob Noble. 'Test witnessed by Nabors Tool Pusher Bill Bixby and BP WSL Blair Neufeld. 11:30 - 15:30 4.00 ' RIGU P PRE :Make up 12.25" drilling BHA with bit, 1.5 degree bent motor, 2 I NMLC, Stabililizer, MWD, and UBHO (rack remaining BHA back in derrick). -Orient MWD/UBHO. 15:30 - 17:30 2.00 RIGU ' P PRE PJSM with SLB and rig crew. Rig up Schlumberger's E-line sheaves. Make up Gyro tools. 17:30 - 21:30 4.00 DRILL P SURF Fill lines and well with 8.8 ppg spud mud. -Test lines to 3000 psi. Spud well at 18:00 hrs. Drill from 108' to 35T MD. ~. t ' •550 gpm, 1045 psi on. 9G5 psi o`?. a0 RPM, 2K Tq on, t K Tq eft, ', 0K W OB: -Circulate 5 mi~lutea prier ?n gYa~o. -i=irsl Uyro at 173'. 21:30 -.23:00 1.50 DRILL P SURF 1 POhI to 8t' tAG. Pick up rnmainir~g BHA j2 s'~~b~;izers, and jar si~ind). F31H ar~~d tag tG' of fill a13~.7' h1G. 23:00 - 0,00 DRILL P SURF ~ Grill t2.25" rurfa~;e i~~c;le tron~ 347' to 372' fJ1G.. -550 gpiti, 1406 psi on, 1002 psi oif. l 4J RPtv1, 3K 7q on, 1{f Fq c~Ft -Girailata 5 minutes (?rior to t~,rc~s and wi~+e 10`. !!!-Acti:al Slide Time - O.hB hr, (hx toifr). - Printari OIt F/9(10G 9.5A53 AM n ~~ BP EXPLORATION Page 3 of 13 Operations Summary Report .Legal Well Name: V-219 Common Well Name: V-219 Spud Date: 11/8!2008 Event Name: DRILL+COMPLETE Start: 11/6/2008 End: 11/23/2008 Contractor Name: NABOBS ALASKA DRILLING I Rig Release: 11/23/2008 Rig Name: NABOBS 9ES Rig Number: 9ES Date ~ From - To I Nours Task ~ Code NPT Phase I Description of Operations ~.. w ~..~~- __ 1118/2008 23:00 - 0.00 DRILL P SURF -Actual Rotate Time = 0.90 hrs (for tour). 11/9(2008 00:00 - 19:00 19.001 DRILL P SURF Drill 12.25" surface hole from 372'to 1871` MD. 19:00 - 20:00 1.00 DRILL ~ P 20:00- 22:30 ~ 2.50 DRILL I P ~ I SURF - 00:00 ~ 1.501 DRILL I P ~ (SURF (11110/2008 00:00 - 01:00 j 1.00 ~ DRILL ~ P ~ SURF 1:00.03:00 1 2.001 DRILL 1',P ~ ~ SURF -03:30 1 1.00 DRILL IP 1 ISURF 03:3004:30 1 AO, DRILL ~P ~ SURF 04:30-19:00 ~ 14.50~DRILL ~P ~SURF -550 GPM, 1965 psi on, 1850 psl off. -40 RPM, 30K WOB, 5K Tq on, 3K Tq off. -Circulate 5 minutes prior to gyros. -Last gyro at 931' MD. -Actual Slide Time = 11.24 hrs. -Actual Rotate Time = 3.34 hrs. -Survey every 90'. Circulate bottoms up 3 times while slowly pulling a stand of drill pipe. -550 gpm, 1800 psi. -50 RPM, 3-4K Tq. Monitor well: Static. Mud weight in/out 9.2 ppg. POH with 12.25" drilling BHA from 1780' MD. -15 - 25K over pulls at 1295', 1148', and 1122' able to pull through. -Work pipe from 1100' tc 1089' with 25K over pull. -Pump out of hole from 1089' to 1015'. -500 gpm, 1333 psi. -Continue to POH with no pumps from 1015' to 829' MD. -10 - 25K intermittent over pulls wiped through from 829' to 27 7'. Ruck back jar stand- Rtsmove stabilizer frcm eoilar stand and slancf h,uP: collars. lay doom UE3HQ Nf~1X0, and r:f~t stabiliz!~r- Lay dotianl 12.25" mill tooth Lit. -E3it grade: 3.3-~n,'T-~1-E-!•~:c-6HA_ `Pick up a new 12.25" r7~iq tooth I:dt. Run bacx in ho?e ~.vith 12.25" bil tr, 84'- Clear ibis rig boar. PJSi'e1 S'ih slid cut 108' of t~iriiEir,cd line. Sarvice the tcp drive, dram~.vorks, 7r~d crewn. RIH bvith Nf~1 drill Collars. hAake up stabitizer. ~': RIH witi7 jar stand and 7 s:ar~ds of Hr.rDP tc 979` r~'iD. RIH vffh 12.25' drilling t31~1A to 1172' rrfD. Shailo'.. hole test the tviWD at 1013' ~'~~ b50 GPhA, 7~~50 psi; '~, W orht:U throi3gt~ tighf spoiy tivl?i!e runnin3 in the t~oie from 1 Y r~J' to 15$0'. V4'ash Iasi stand datit~n tram i 172` to 1871' tAD. ~,0 GF'h1, 7950 psi, &t) RPrvi. 3.SK Ty. •„~ ©rili 12.25" surt<nro hole from 787 1' to 3987' t~tb PU 107K, SO ISK, HOT 83K. -550 - 638 GPt`A, 3`.~ 0 t?si a+7, 3330 psi off (GPh1 limit:d Ly pressure). ~-100 RPhi. 30K ~t~/QB, 6K Tq on, £7K Tu Cof'. -Actual SHdis Time ; 3,9 hrs. -Actual R(J1a1F Time = 5.24 hrs. 9/151209 9:58:53 AM BP EXPLORATION Operations Summary Report Page 4 of 13 ~' Legal Well Name: V-219 Common Well Name: V-219 Spud Date: 11/8/2008 Event Name: DRILL+COMPLETE Start: 11/6/2008 End: 11/23/2008 Contractor Name: NABOBS ALASKA DRILLING I Rig Release: 11/23/2008 Rig Name: NABOBS 9ES Rig Number: 9ES Date ~ From - To Hours Task , Code I NPT Phase Description of Operations 1 i110l2008 04:30 - 19:00 14.50 DRILL P SURF -Survey every 90' -Back ream 30' prior to connections. -Noted minor hydrates breaking out at 2650'. 19:00 - 20:30 1.50 DRILL N WAIT SURF Wait on Super Suckers and Vac trucks due to mechanical . problems, CH2MHILL safety meeting, and Phase 1 weather conditions. ` Circulate and condition mud while waiting. -400 GPM, 1575 psi, 50 RPM, 5K Tq. 20:30 - 00:00 3.50 DRILL P SURF Estimated -3 additional hours for required trucks to continue drilling. Make wiper trip rather than wait on trucks. I Monitor well: Static Mud weight in/out = 9.5 ppg. I POH from 3987' to 2719' MD. -PU 112K, SO 75K -Work pipe with 30K over pulls and hole swabbing. Pump out of hole from 2719' MD to 2387' MD. -500 GPM, 1943 psi. 11/11/2008 00:00 - 00:30 0.50 DRILL P 'SURF Continue to pump out of the hole to 1772' MD, -500 GPM, 1943 psi. -100K Wt. Pulled last stand with no pumps to 1678' MD. -No over pull or swabbing. 00:30 - 03:00 2.50 DRILL P SURF RIH from 1678' MD to 3872' MD. -No problems running in hole to 2740' MD. -Work pipe down from 2740' MD to 3872' MD. Make up to Cup driv; nrid c:~ Si7 dawn irUn-~ 3872.' 10 3t~II7` t~.1L7. _03:00 - 07:00 4,00 DRILL P SURF Continue to drill '12.25" sur(ac~: t~~7IY to T(} at 4-192' b:1J -u30 r~PEti1, 3350 psi or., 3400 psi oif. •100 RPPA, 30K INOB. 9.8K Ty cn, ii.6K Tq cfi, -PU 110K, SO 70K, E~OT BdK. -Aciua! Slide lime = 0.70 Ixs. -Act;iG I WGtaiQ Time = 1.87 l~srs. {-Encountered h~r<+rates at 4068' a~~d 4240' to 4=192' F.d[~. STD called by ;et~iogis~ ~t ;492' Md at 07:00. .07:00 - 09:00 2.00 DRILL P SURF ~Circlllzte 3 bottc~ii~s up at mrix r~~tc (limited ley I>:~mps}. -630 GPt~d, 3k80 psi, 100 RI'Pdt, 6.:~1< Tq. -09:00 - 12:30 3.50 DRILL P SURF ~~ Monitor well: Static Mud w~?igl~! inla~~t -'?.5 t~~~0, '~ Pump ou; of hale frorn 4492' tv10 to 3400' DAIS. -500 GPM, 2015 psi, -Hydrates i~reaking cut peri~dic<:Ily. 42:30. 21:30 9.00 'DRILL P SURF '; Baekteartt from 34CC1` to 3U0 DflD, i -5C6 GPDA. 2Q05 psi, 00 f~Ptvl, UK Tr1. -Redt,re Rr D~1 to X40 at 2700'. Printari• 9tt 5!?_(169 9'58'53 • BP EXPLORATION Page 5 of 13 Operations Summary Report Legal Well Name: V-219 Common Well Name: V-219 Spud Date: 11/8/2008 I~Event Name: DRILL+COMPLETE Start: 11/6/2008 End: 1 i/23/2008 Contractor Name: NABOBS ALASKA DRILLING I Rig Release: 11/23/2008 Rig Name: NABOBS 9ES Rig Number: 9ES Date From - To I Hours Task (Code NPT Phase Description of Operations ~. ~.~._ _---- - _ _.. ___ - m..._ 11/11/2008 12:30 21:30 0 DRILL P SURF -Experienced wellbore breathing. -Recorded gains/losses and time with pump onloff. -Hydrates slowly diminished. -Attempted to pull on elevators at 1772' MD. •Hofe still swabbing and 30K overpull, returned to backreaming. -Attempt two more times up to 800' without success. 21:30 - 00:00 2.50 DRILL P ' SURF ~ Rack back stands of HWDP, jar stand, and collar stand. Begin laying down remaining 12.25" drilling BHA. 11/12/2008 00:00 - 02:00 2.00 DRILL P SURF Continue to lay down 12.25" surface BHA including: MWD, Stabilizer, and NMLCs. 02:00 - 02:30 0.50 DRILL P SURF Service Top drive. Clean and clear the rig floor. 02:30 •03:00 0.50 DRILL N RREP SURF Repair Top drive. '-The handler's hydraulic latching pin sheared which did not :allow the handler on the top drive to rotate. 03:04 - 03:30'. 0.50 DRILL P 'SURF Continue to lay down bent housing motor and mill tooth bit. Bit in good condition, Grade: 1-0-WT-A-E-I-NO-TD ' 03:30 - 07:00 3.50 CASE P SURF PJSM. Rig up to run 9-5/8", 47#/ft, L-80, BTC-M surface casing. Make a dummy run with the hanger. 07:00 - 00:00 17.00 CASE ' P .SURF PJSM with nabors rig crew, casing hand and WSL. ' Run 9-518", 47#/ft, L-80, BTC-M surface casing. -Use Best-O-Life 2000 pipe dope. -Torque connections to 10,800 ft-Ibs. -Run bow spring centralizer on first 25 joints. Set down at 980' attempt to work past obstruction with out pump no -go. Break circulation 200 gpm, 220 psi full returns gat past obstruction after several hrs, large amounts of sand .and a considerable amount of small wood chunks coming over shakers. Bow spring centralizers hanging upon obstruction e3vory d0' -Takiity w@ight and I?aCkirtg oft. -Work pipe down with and vdithout pimii>iny. -Adjus' rur'irtir,<~ spcle<}s as neeti~~U to itl~intain full returns. -Attampt to ;itinimizB delta P. ~bVork pile down to 2:i~a7 r,9D at end pf To~u. 11/13/2008 00:00 - 08:30 8.50 CASE P SURF Coi'ttinue to F~i11 vrrth 9.519', 47»'fi, L-80, BTG-tvt easing !a 3100' tv10. Taking wei~dht and a;tjustiny rurinincd si)~ed~'wgrkiny pipe id avoid p€tckir7g oit. -11Q GPfJI, 338gsi, Continue in mole wi,h no p~.trnps Cron1 3100' tvtD to ad49' fv1D .;With n9 f;rOt~IBrnS. t 70K PU. £35K SQ. ~- i Use Bost-O-Lif~3 2000 thread dope. IAver2grn aTtake up torct,e: t0,a00 ii~it~s. ', 25 bow sF~rin+g cni~tralizeas ran an first i_'5 jomts. '~ 2 f~W spring centralizers arau,td 7a:n Port Uoliar. 08:30 - 09:30 ' 1.00 CASE P SURF ~Aake ut? landing join? and land casing at x481' ivtU. ~ Rig down the Franks total. ;Blow do~.vn tho toe drive. Printad: 9!1512009 9:58.53 AM e • __ BP EXPLORATION Page 6 of i3 Operations Summary Report Legal Well Name: V-219 Common Well Name: V-219 Spud pate: 11/8/2008 Event Name: DRILL+COMPLETE Start: 11/6/2008 End: 11123/2008 Contractor Name: NABOBS ALASKA DRILLING I Rig Release: 11/23/2008 Rig Name: NABOBS 9ES Rig Number: 9ES Date From - To Nours I Task I Code NPT Phase I Description of Operations __. _e~ ~ ! ~.a-_.,. 11!13(2008 08:30 - 09:30 1.00 CASE P SURF 'Make up the cement head and circulating lines. 09:30 - 14:30 5.00 CEMT P SURF Break circulation and stage up pumps to 7 bblslmin -~ 10:00 - 7 bpm, 640 psi. -Circulate and condition mud at 7 bpm -Mud weight 9.4 ppg, funnel vis 68 sec/qt. -~? 14:00 - hrs 7 bpm, 426 psi. 14:30 - 15:30 1.00. CEMT ' P SURF Swap over to SLB pumps. -Pump 5 bbls of H2O, test lines to 4000 psi. -Pump 96 bbls of 10 ppg Mud push II. -5.5 bpm, 269 psi. -Drop the bottom plug. -Pump 547 bbls of 10.7 ppg DeepCRETE cement. -6.6 bpm average, 300 psi. -Reciprocate pipe up to this point, stop prior to pumping tail. -Pump 86 bbls of 15.8 ppg class G cement. -5 bpm average, 380 psi. -Drop the bottom plug and kick out with 10 bbls of water. 15:30 - 18:30 .3.00 CEMT ' P SURF .Swap over to rig pumps. -Displace well with 312 bbls. -7 bpm, 500 psi for 2000 strokes. -Mud Push to surface after 1550 strokes. -Reduce rate to 4.5 bpm to handle clabbered up mud in pits. -4.5 bpm, 480 psi for additional 1000 strokes. -Reduce rata to 3.5 bpm to handle clabbered up mud in pits. -3.5 bpm, 700 psi. -Bump plug and held 1400 psi i -Plug bumped on calculated stroke count (4410 sks, 312 bbls). -Bled pressure and checked floats: floats held. -100 bbls of cement returned to surface. 18:30 - 19:00 0.50 CEMT P . SURF Bring pressure back up to 3500 psi and chart for 30 minutes. -Pressure bled 0 psi in first 15 min, 0 psi in second 15 min. -Good test. Flush diverter stack and remove diverter lines and 4" valves while testing. 19:00 - 20:30 1.50 DIVRTR P ~ SURF .Rig down the cement head. Flush the Hydrill and diverter spool. ...Lay down the landing joint. 20:30 - 00:00 3.50 DIVRTR ' P SURF 'Remove the riser and diverter spool. Rig down casing running equipment, 11/14!2008 00:00 - 01:00 1.00 DIVRTR P ~ SURF :Continue to nli;ple dawn diverter systcai Chango ot~t 2Q" flange to 1 ~~° <sir tx~o{. -Remove surface: Hydril from co0ar. Finish riyyiny down using running tools. 01:00 - 03:00 2.00 ' WHSUR P SURF PSiphle u~ tlla FDAC casing, and tithing s}~oals~ 1-Tzst metal to metal seal to tOG~ f~si for t0 minutes. 03:00 - 06:30 3.50 BOPSU P SURF ~ Nipple up tht~ BC3P's. , ~-Position BOP shark ~avcr weI[ head. '-Torque ti7nrfe bola. Make up tum b~tCklas. ~ -Install the riser and +varkiny ~:alves. .06:30 - 07:30 1.00 BOPSU °P SURF ~~Icar~ c:f~t rotary drain par•, irosl~t surface job. r i D.fn~nri~ 6/t 5t9f1tiq ~~GR~F'a AM BP EXPLORATION Operations Summary Report 'Legal Well Name: V-219 .Common Well Name: V-219 Event Name: DRILL+COMPLETE Start: 11/6/2008 Contractor Name: NABOBS ALASKA DRILLING I Rig Release: 11!23/2008 Rig Name: NABOBS 9ES Rig Number: 9ES Date From - To ( Hours Task Code NPT Phase 11!14!2008 07:30 - 10:30 ~ 3.00 BOPSU N RREP SURF 10:30 - 13:00 ` 2.50 BOPSU P SURF : 13:00 - 17:30 4.50 BOPSU P SURF 17;30 - 18:00 0.50 BOPSU P ' SURF 18:00 - 21:00 3.00 DRILL P PROD1 21:00 - 22:00 1.00 DRILL P PROD1 22:00=00.,00 2.00 DRILL P PROD1 11/15/2008 00:00- Oi:30 ' 1,50: . DRILL P PROD1 01:30 -02:00 0.50 DRILL P PROD1 -02:00 -06:00 4.00 DRILL P PRODt '06:00.08:00 ~ 2.00 i DRILL P PROD1 08:00 - 08:30 0.50 DRILL P PRODi .08:30 - 09:00 0.50 DRILL P PRODi Page 7 of 13, Spud Date: 11/8/2008 End: 11 /23/2008 Description of Operations Change out the top drive torque tube slides. Rig up to test BOP's -Pick up test tools. -Make up floor valves and test joint. -Install test plug. -Fill lines with H2O. Test BOP's to 250 psi low, 4000 psi high. -Test with 4" and 3.5" test joints. -Test witnessed by AOGCC Rep Jeff Jones. -Test witnessed by Nabors Tool Pusher Bill Bixby and BP WSL Brian Buzby. -Brass API ring on kill line hose required replacement. -Replaced kill line and uni-bolt on kill line. Lay down test joint. Rig down testing equipment. Install wear ring. Blow down the choke body and surface lines. Pick up 69 joints of 4" drill pipe from the pipe shed and stand back in the derrick. Safety stand down with Nabors Tool pusher Roy Hunt, BP WSL Kris Hones, the rig crew and SLB DD and MWD hands. -Discussed injuries on Nabors 4ES and 3S as well as recent HSE incidents on 9ES. Concluded safety stand down with PJSM for making up 8.5" drilling BHA. ',Make up 8.5" dr1111ng BHA including: '8.5" PDC bit, 1.15 degree bent motor, NM collar, EcoScope ,and Telescope (DIR, GR, RES, DEN, NEU, PWD). i-Load Nukes from side into EcoScope. ',-Check bit, stabilizers and ghost reamers for proper gauge. Conitinue to make 8.5" drilling BHA including: -NMDC's, stabilizers, saver subs, HWDP's, hydraulic jars, XO, 8.5" Ghost Reamer. -No problems noted when RIH past TAM collar. Pressure test TAM collar to 1500 PSI. -Test Good. Continue to RIH w( 4" DP singles to 4218' MD. -115K PU, 65K SO. MU to top drive. Break Circulation, 300 GPM, 1650 psi. Wash down to top of float collar ~ 4398' MD and tag cement: ~prill cetl7e!ii out of shoe track -a50 GPNI, 19GLt psi otf, 19_°,0 i~si cn. -40 RPM, 0-5K ,NCB, 6k Tq on, SK Tq off. •a2t{ R+JT w.csight. Swappvti rnuci ovor to 8.f3 ppy LSND drillir~3 mud while ttrilliny cut shoe tack. ' Drill vut rat hale + 2G foot of rtev>< hrla to 4572` h~9D. i •Circulate i~ole claarz at SOd GPPrI, 13`>0 psi, t; 3K Tq. Perform L07 and chart. Printed: 9!15!2009 9:5$:53 AM ~ ~ BP EXPLORATION Operations Summary Report Page 8 of 13 ;Legal Well Name: V-219 ;Common Well Name: V-219 Spud Date: 11/8/2008 Event Name: DRILL+COMPLETE Start: 11/6/2008 End: 11/23/2008 Contractor Name: NABOBS ALASKA DRILLING I Rig Release: 11/23/2008 Rig Name: NABOBS 9ES Rig €Number: 9ES Date 'From - To I Hours ~ Task ~ Code NP7 I Phase ( Description of Operations 11/15/2008 08:30 - 09:00 ( 0.50 DRILL P I PROD1 ~-Mud weight 8.8 ppg, 2911' TVD, 950 psi surface pressure. 09:00 - 00:00 15.00] DRILL I P ~ ~PROD1 11/16/2008 ~ 00:00 -12:00 ' 12,00 ~ DRILL ~ P 12:00 - 00:00' 12.001 DRILL [ P .11117/2008 00:00 - Oi:00 ~ 1.00 DRILL ~' 01:00-02:00 ~' 1.00~DR1LL ~P - 16:30 14.50 DRILL ~P LOT = 15.0 ppg EMW. gill 8.5" production hole from 4512' MD to 6638' MD. 143K PU, 75K SO, 100K ROT. 580 GPM, 2500 psi off, 2580 psi on. 100 RPM, 10K WOB, 9.1 K Tq on, 8.6K Tq off: Back ream 90 ft on connections. Survey every 90 ft. Actual Rotate Time = 5.14 hrs. -Actual Slide Time = 3.3 hrs. -Calculated ECD = 10.2 ppg EMW. •Actual EGD = 10.4 ppg EMW. -Pump 25 bbls high vis sweep at 5200' MD with 10% increase In cuttings Drill 8.5" production hole from 6638' MD to 7780' MD. -148K PU, 75K SO, 105K ROT. •580 GPM, 2925 psf off, 3127 psi on. -100 RPM, 5-10K WOe, 10.3K Tq on, 8.5K Tq off. -Survey every 90 ft (30' in turn). -Actual Rotate Time = 1.92 hrs. -Actual Slide Time = 4.55 hrs. -Calculated ECD = 9.86 ppg EMW. -Actual ECD = 10.34 ppg EMW. -Mud Weight = 9.0 ppg Drill 8.5" production hole from 7780' MD to 9401' MD. -175K PU, 95K SO, 115K ROT. -580 GPM, 3357 psi off, 3494 psi on. -100 RPM, 5-15K WOB, 12.3K Tq on, 11.4K Tq off. -Survey every 90 ft. -Actual Rotate Time = 5.62 hrs. -Actual Slide Time = 1.53 hrs. -Calculated ECD = 10.02 ppg EMW. -Actual ECD = 11.01 ppg EMW. -Mud Weight = 9.2 ppg in / 9.3 ppg out. -Add 50 bbls/hr water to reduce mud weight and screen up. PROD1 PROD1 I Note: -150 psi drop in pressure and 3% increase in flow at ' 9243' MD. Shut down pumps and monitored Well for 10 minutes. Gas breaking out at surface but Well was not flowing. Drill down remaining 15' of drill pipe stand and monitor well i again. V~edl static avith nu gas k~r~~aking out. PROD1 :Drill II.5" prnUurtic:n izola frasn 0401' fJ7D to 95&5' 6~G. ~~-550 GPM, 340Q psi bn, 3215 psi off_ -lni~if RU, 9C~K SO, 118K ROT. -100 RPM, 5-15K tnJp6, 12.AK Tq cn, 11.4k Tc{ off. -Survey every 90 ft. '4TD called by Geologist ~ g5fl3` MD (351?' heio~N 03~- tel)j. PRODi ' Gircuiate one apes bola annular volumc_ -550 GPM, 321Ei psi. •167K PU, 901 50, 120K ROT. PROD1 ~ hA~nitor we(t Static. ~~ BP EXPLORATION Page 9 of 13', Operations Summary Report Legal Well Name: V-219 Common Well Name: V-219 Spud Date: 11/8/2008 Event Name: DRILL+COMPLETE Start: 11/6/2008 End: 11/23/2008 Contractor Name: NABOBS ALASKA DRILLING I Rig Release: 11/23/2008 Rig Name: NABOBS 9ES Rig Number: 9ES Date I From - To ~ Hours I Task I Code I NPT { Phases Description of Operations .~ _..._ ~. _.._.. III ~ .~.~ _ __._____.._. 11/17/2008 102:00 - 16:30 i4.50~ DRILL P PROD1 Mud weight in/out = 9.2 PPg• 16:30 - 17:30 I 1,001 DRILL LP 17:30.22;00 J' 4.501 DRILL 1 P 22:00 - 00:00 2.00 DRILL P 11118/2008 ~ 00:00 - 02:00 1.00: BOPSU P 02:00 ~-03:00 ~ 1.00 ~ CASE P 03:00 ~ 05:00 2.00 CASE P 05:00 - 11:30 ~ 6.501 CASE ~ P 11:30 - 12:00 0.50 ~ CASE ~ P 12:00 - 00:00 12.00 CASE P Back ream out of hole from 9583' MD to 4520' MD. -580 GPM, 2464 psi. -600 - 800 ftlhr. -7.9K Tq Tight pulling through window at 4520'. Well packing off. Work pipe down -20'. Pick back up slowly at 580 GPM and pull into 9-5/8" shoe. PRODi Circulate 1.5 bottoms up. -550 GPM, 1940 psi. -95 RPM, 5K Tq, -115K PU, 70K SO, 85K ROT. PROD1 Pull out of hole from 4480' to BHA. Lay down 8.5" drilling BHA. -Lay down source. Bit graded: 1-2-WT-S-X-1-ER-TD PRODi Remove wear ring bushing. Flush the stack. Install lower test plug. Blow down top drive. Clear floor of BHA. PROD1 Change upper rams from 3-1/2" x 6" VBR to 7" Rams. PROD1 Rig up and test 7" Rams to 250 psi low / 4000 psi high with 7° test joint. -Rig down testing equipment. RUNPRD Service top drive and repair the back up wrench. RUNPRD Rig up to run 7", 26 Ib/ft, L-80, BTC-MIrC-II casing. -Rig up Franks tool, casing tongs, and spider elevators. -Rig up scaffolding, safety valve, and make dummy run -good. RUNPRD 'Run 7" 26# L-80 BTC-M casing as per running detail to 3589'. -Dope with Best of Life 2000. -Torque connections to 7400 ft-Ibs. -Run 2 centralizers per joint free floating, seperated by stop ring. -Obtain PUlSO weights every i0 joints. -120k Up Wt, 78k Dn Wt. RUNPRD Rig up Torque Tum equipment for 7" TCII Threads. RUNPRD Run 7" 26# L-80 TCII Casing as per running detail from 3589' to 7950'. -Torque turn connections to 10,100 ft-Ibs. -Dope with Jet Lube Sea{ Guard. '~ •Obtair~ PUJSO weights every 10 jtS -Bret~k circulrstion every 15 jts for 1.5 mi;atjotnt isi a5g an~~ 2 'mi~Y~jaint in open hgle_ CBU 1 5x at 9 5'S' i~o~ Gn; dd80' at 6 f?hri~, G6~ psi. •Start to pri~h mud iN 3y v?i d~ ~ 1~ . -Circulate down ,a~ 3 5 Lprri IrJRI ;6d2 to <1~3T. Hole starting 1 to pack oft, but cleaned up ri, z93''. -Continue to R1Ff ai3d t;reak ciroula!i6t~ e!~ery 1 ~; ioin(s ~~~ 3-:~ ,bp~tt, tidy psi. Prinlyd 9/75/2009 9:58:53 AM C] i BP EXPLORATION Page 10 of 13 Operations Summary Report :Legal Well Name: V-219 ;Common Well Name: V-219 Event Name: DRILL+COMPLETE Contractor Name: NABOBS ALASKA DRILLING Rig Name: NABOBS 9ES Date From - To I Hours I Task I Code I NPT 11/18/2008 12:00 - 00:00 12.00 ~ CASE ~ _. P ,_~. 11119!2008 . 00:00 - 02:00 2.00 CASE P , 02:00 - 02:30 j 0.501 CEMT I P 02:30 - 05:00 2.50 CEMT P 05;00.- 08:30' 3.50 ~ CEMT P - 100:30 ~ 10.50 CEMT ~P 0:30 - 11:30 ~ 1.00 WHSUR 11:30 - 12:30 1.00 ~ BOP 12:30 - 13:30 t 1.00 BOP Spud Date: 11 /8!2008 Start: 11/6/2008 End: 1112312008 I Rig Release: 11/23/2008 Rig Number: 9ES Phase Description of Operations RUNPRD 100 bbis of mud lost to formation for day. RUNPRD ~ Continue to run 7" 26# L-80 TCII Casing from 7950' to 9544'. -Make up landing joint and hanger. !-Land Casing ~ 9573' -250k Up Wt, 85k Dn Wt "Lost 14 bbis mud to formation. 'Total of i 14 bbis mud lost to formation while running casing. RUNPRD Rig down Frank's Tooi and rig up Cement Head. -Clean and clear rig floor. RUNPRD Circulate and condition mud by staging pumps up to 5 bpm, .780 psi. `-Hold PJSM with cementers while circulating. -Begin batch mixing tail slurry. "19 bbls lost to formation while circulating. RUNPRD .PJSM w/SIB cementers. Switch over to Schlumberger. -Pump 5 bbis of water. Pressure test lines to 4,000 psi - OK. -Pump 25 bbis of 10.0 ppg of MudPush II ~ 5.0 bpm, 500 psi. -Shut down and release bottom plug, positive indication plug left head. -Pump 50 bbis of 11 ppg LiteCrete lead cement ~ 5 bpm, 650 psi. -Pump 74 bbis of 15.8 ppg Class "G" tail cement ~ 5 bpm, 5500 psi. -Drop top plug, positive indication plug left head, -Wash up cement lines to pits. Switch over to rig pumps and displace cement with total of 367 bbls 9.0 ppg Brine ~ 6 bpm, 520 psi ICP, 700 psi FCP. -Slow pump to 1.5 bpm prior to bumping plug. -Bumped plug G~ 6242 strokes with 900 psi and pressured up to 1550 psi. -Held 1550 psi on plug for 2 minutes. Bled off and checked .floats -good. i "Saw losses at 280 bbis into displacement. Slowed pump rate Ito 3 bpm and continued to see g~~od lift pressurE and partisf iraturns. 'Recipreeated pipe in 10' strokes rrntii 375 bLls rota ' dispta Cement. Lur~ded easrrg dur~ [a Ir~w stack oit %.^eir,i~t. '~CIP ~ QII:04 hrs. l.o°t a51?E~is during cerrrnf joy. RUNPRD iTost casing to 4000 psi for 34 minutCS • zraod. RUNPRD (?ig dc~~~~n cen~cnt haa~J and Ianciin0 joint, -Ctianea out Lals anU alevators. ' -E3(ow dog^ar all Tines. RUNPRD ~ Insttr3l 9•S/8" x 7'^ packoff. -Torq>>o LDS to 350 ft-ibs_ -TESL seals to 5000 psi for 15 mir~ut~s - gocxi. RUNPRD Ghar~ge out upper rams Iran 7° Barns to 3-1I2" x G" VCiR. RUNPRD !Test Uppor 3•U2" x G" VBR and Lower P-7I8" x 5" VER to 250 psi low / 4040 psi i~icdh with 3.5° and ~+" :+->st joints - geed. ~ -Pertnm7 inactivity test down ~-518" x 7" annulus. lnjuct 4 f?t>fs 1 bprn, 50G psi. 13:30 - 14:00 0.50 BOPSU ` P RUNPRD i Flig cloven and bio:v do;vn ail tostir;{~ cqu.pnrnnt. -insti3i~ year ring. 9tt 5!2009 9:58:53 AM BP EXPLORATION Operations Summary Report '.Legal Well Name: V-219 Common Well Name: V-219 Event Name: DRILL+COMPLETE Start: 11/6/2008 Contractor Name: NABOBS ALASKA DRILLING I Rig Release: 11/23/2008 Rig Name: NABOBS 9ES Rig Number: 9ES Page 11 of 13 Spud Date: 1118/2008 End: 11 /23/2008 Date ( From - To Hours Task I Code ( NPT Phase ~ Description of Operations i 1/19/2008 14:00 - 17:30 3.50 PERFO .m.~._ P ___~_ ~.. OTHCMP PJSM with SLB Perforating Hands. Pick up 4-112" perforating guns and firing heads as per running detail. 17:30 - 00:00 6.50 PERFO P ' OTHCMP ' RIH with pert guns on 4" DP @ 90 fpm and tag float collar on depth at 9489'. ' -Use minimal pipe dope on pin ends only. -Shallow hole test MWD C~ 1200' with 250 gpm, 410 psi -good. *Freeze Protect 9-518" x 7" annulus with 115 bbls of 9.1 ppg 'LSND mud followed by 90 bbls dead crude ~ 2 bpm, 1100 psi. 11/20/2008 00:00 - 02:30 2.50 ' PERFO P OTHCMP iog up and correlate to MW D log ~ 250 gpm. Confirm depth . and log up to depth on confirmation pass. Place guns on depth. ' 02:30 = 03:00 0,50 PERFO P OTHCMP ' PJSM with SLB on firing guns. Initiate firing sequence and fire guns. -Perforate Nb sand from 8410' to 8442'. -Perforate OBa sand from 8796' to 8852'. -Perforate OBb sand from 8878' to 8904'. -Perforate OBd sand from 9083' to 9166'. -Perforate OBe sand from 9230' to 9280'. -Good indication both firing heads fired. -Fluid level dropped 20' after first shot, then 10' after second set of guns fired. Loss of 11 bbls total. *Confirm that tail cement has reached 1000 psi compressive strength prior to firing guns. 03:00 - 03:30 0.50 PERFO P OTHCMP POH from 9300' to 8394'. 03:30 - 04:30, 1.00 PERFO P OTHCMP CBU x1 ~ 402 gpm, 1612 psi. 04:30 - 08:30` ' 4.00. PERFO P OTHCMP POH from 8394' to top of pert guns. 08:30 - 13:00 4.50 PERFO P OTHCMP PJSM with SLB. Lay down MWD, Bumper Sub, Firing Heads, and Perf Guns. -All charges fired. 13:00 - 14:00 1.00 i PERFO P OTHCMP Clean and clear rig floor of all SLB handling tools and firing heads. 14:00 - 16:00 . 2.00 CLEAN P ~ CLEAN PJSM. Make up 6-1/8" Gleanout Assembly consisting of flat bottom mill, string mill, junk baskets (x2), string magnet, and jars. 16:00 - 17:00 1.00 CLEAN P ' CLEAN Cut and slip 89' of drilling line. 17;00 - 17:30 0.50 CLEAN P CLEAN Service Top Drive and Crown. 17:30 - 20:30 3.00 CLEAN P CLEAN RIH on 4" DP and tag float collar (~ 9489'. -Less than 1' of fill on top of float collar and plugs. 20:30 - 22:00 1.50 CLEAN P CLEAN Pull up to 9430' and work mills and junk baskets. -Reciprocate pipe 80' strokes. -70 rpm ~ f 2k TO. -500 gpm ~ 3000 psi. •Pur.~p 25 trt3l nE-vis ~~~eel3. Sar fens than 1 gailon of sand anU lirretai sha:~s~rys I:ar~i~ ~ ~itii s~.~eep 22:00 - 23:30 t.50 CLEAN P CLEAN ' pump out of hold from 043(3' to 8318' (at:ova tc~p p~arls~, -513 gpm +.~. 2~t34 psi. 23:30 -00:00 O.bO CLEAN P CLEAN ;CBU x1 and work mills Arid iunk baskets. -60 rpna ~ 9.3k 'CQ. ''Lost 18th hbls of rrinr; tc perfc7ratiort; for ihC; Clay, Loss rate i Priniad: 9t1 EJ2909 9'Sfl:53 AM, BP EXPLORATION Page 12 of 13 Operations Summary Report Legal Weli Name: V-219 Common Well Name: V-219 Spud Date: 11!8/2008 .Event Name: DRILL+COMPLETE Start: 11/6/2008 End: 11/23/2008 Contractor Name: NABOBS ALASKA DRILLING I Rig Release: 11/23/2008 Rig Name: NABOBS 9ES Rig Number: 9ES Date 'From - To Hours Task Code NPT Phase ~ Description of Operations 11/20!2008 i 23:30 - 00:00 11/21/2008 i 00:00 - 01:30 0.50 1.50 CLEAN ' CLEAN ' P P CLEAN CLEAN diminishing throughout day. Losing ~1 bph at end of day. Pump down from 8318' to 9430' (below perforations}. -500 gpm ~ 2800 psi. 01:30 - 02:00 0.50 CLEAN P CLEAN Work mills and junk baskets and pump 25 bbls hi-vis sweep. -60 rpm ~ 10.5k TO. -515 gpm ~ 3000 psi. -Saw -1-2 quarts of sand and metal flakes back with sweep. -Shut down and monitor well -static. 02:00 - 10:30 8.50' CLEAN P . CLEAN 'POH from 9430' to top of cleanout BHA, laying down drill pipe. 10:30 - 11:00 0.50 CLEAN ' P } CLEAN Lay dawn cleanout BHA. 1 -Recover -4 cups metal debris from junk baskets and magnet. 11:00 - 12:00 1.00 GLEAN P CLEAN Clean and clear rig floor. 12:00 - 16:30 4.50 EVAL ~ P OTHCMP Rig up SLB Wireline and RIH with 6.125" Gauge Ring /Junk Basket to 9330' and POH. -Recover <1 cup of debris from junk basket. 16:30 -22:30 6,00 EVAL P OTHCMP Make up and run USIT from 9320' to surface. •TOC found ~ 6960' 22:30 - 23:30 1.00. EVAL P OTHCMP Rig down SWS and lay down USIT logging tools. 23:30 •00:00 0:50 BUNCO RUNCMP Pull wear ring and make dummy run with hanger -good. '33 bbls brine lost to perforations for the day. 11/22/2008 00:00 - 01:00 : 1.00 BUNCO WAIT RUNCMP Wait on SLB Wireline Unit to move from beaver slide area white processing logs. 01:00 - 02:30 1.50 BUNCO RUNCMP Rig up torque turn equipment to run 3.5" 9.2# L-80 TCII '.Completion. -Rig up sheaves and I-wire spool. 02:30 - 00:00 21.50 ' BUNCO. p RUNCMP Run 3.5" 9.2# L-80 TCII completion with I-wire as per running i detail to 8034'. -Baker Loc all connections below 1st packer, -Terminate I-wire to 4 NDPG sensor subs. -Test I-wire connections on each packer (4 total) to 5000 psi for 5 min -good. -Dope connections with Jet Lube Seal Guard -TO connections to 2300 ft-Ibs. -Install full clamps every other joint. -Test I-wire integrity every 1000' -good. 11123/200800:00 - 02:30 2.50 BUNCO RUNCMP Continue to run 3,5" 9.2# L-80 TCII completion with I-wire as per running detail from 8034' to 9296'. -Dope connections with Jet Luba Seal Guard -TQ connections to 2300 ft-Ibs. -Install full clamps every other joint. -Test I-wire integrity every 1000' -good. -Space out and place completion on depth ~ 9296'. -105k Up Wt, 60k Dn Wt. -Ran 151 Full Cannon Clamps and 21 Half Cannon Clamps. 02:30 - 03:30 1.00 BUNCO. RUNCMP PJSM with SWS. Rig up SLB Wireline •RirJ up siz~aves, pu~~~p•in sub. ~ncf 4^.~relirte :aacko#. -Riy up Gara,~,~a Flay and CCL t~7ais. 03:30 - 04:30 1.00' BUNCO RUNCMP ~ RIH wriij GR+'CCt. un aiit;Iii~;~ to 9200'. 04:30 - 05:30 1.00' BUNCO P RUNCMP ~ Loq from B2fJ0` to 8~~}0 ovtti~ C~R,~CCL to correlate ~.<ynlrletion. -Tip ctxroiation 4~ass in u+riih >~eal-[imE Lt~Via lava. -Found canpletiorr j©welry 2' shaR~sw;. 05:30 - 06:00 0.50 BUNCO RUNCMP ~!, POH ~,vith GF3tCCL from £320u`. Prin#ed: 9115/2009 9:58:53 AM • i BP EXPLORATION Page 13 of 13 Operations Summary Report Legal Well Name: V-219 Common Well Name: V-219 Spud Date: 11/8/2008 Event Name: DRILL+COMPLETE Start: 11/6/2008 End: 1 i/23/2008 Contractor Name: NABOBS ALASKA DRILLING I Rig Release: 11/23/2008 Rig Name: NABOBS 9ES Rig Number: 9ES Date {From - To I Hours Task ~ Code NPT 'Phase ' Description of Operations ........~. ~__ _._. _____ _ ~~_ : ...... : 11/23/2008 .~ 06:00 - 0630 0.50 RUNCOM L° __ _m_ RUNCMP _ Rig down SLB Wireline 06:30 - 08:,30 2.00 ' RUNCOfv t° RUNCMP Space out and. land 3 i/2" 9.2# L-80 TCII completion. j -Terminate I-wire in hanger and land hanger in tbg spool. -Drop 1-5/16" ball and rod. •RILDS as per FMC hand. r -Lay down landing joint. 08:30 - 10:30 2.00 BUNCO RUNCMP Close blind rams and pressure up to set packers and test tubing to 4000 psi for 30 minutes -good. -Bleed tbg pressure to 2500 psi. -Pressure up annulus to 4000 psi for 30 minutes -good. -Bleed annulus, then tubing to 0 psi. ~ -Pressure up on annulus and shear DCR-1 Shear Valve C~ i 2600 psi. ' -Confirm circulation both ways ~ 3 bpm -good. -Install BPV and test from below to 1000 psi for 10 minutes - 10:30 - 14:00 3.50' BOPSU P 14:00 - 16:00 2.00 WHSUR P 16:00 - 17:00 1.00 WHSUR P 17:00 - 18:30. 1.50 WHSUR P 18:30 - 21;00 2.50 WHSUR.. P 21:00.22:'30' 1.50 WHSUR' P 22:30•-00:00 1,50 WHSUR P -Blow down all surface lines. RUNCMP `PJSM. Drain stack and nipple down BOPE. -Remove mouse hole, turnbuckles, and riser. -Set stack on pedestal and secure. RUNCMP Nipple up Adapter Flange and Double Master Valves. -Install I-wire through adapter flange and terminate. -Test adapter flange and tree with DSM to 5000 psi -good. RUNCMP 'Rig up DSM and pull TWC. '-Tested Lubricator to 1000 psi -good. RUNCMP Rig up and reverse circulate 126 bbls of corrosion inhibited 'brine @ 137 gpm, 450 psi.3 RUNCMP Rig up Hot Oil Unit for freeze protection. -Pump 122 bbls Diesel down the backside ~ 2.5 bpm, 280 psi -Allow diesel to U-tube through tree. RUNCMP .'Rig up DSM and install BPV. -~ -Test to 1000 psi from below -good. -Rig down Hot Oii. RUNCMP .Secure weAhead, tree, and cellar. -Remove double annulus valves and install VR plugs. -Prep rig floor for move. *Release rig from operations on V-219 ~ 23:59 hrs on 11 /23/08 TREE= 4-1/16" CM/ WELLHEAD= FMC ACTU_A_TOR = KB. ELEV = BF. ELEV = KOP -~ LEO 82' 56.2' ~~.~~ 250;. Max Angle = 71'° @6748' Datum MD = 8345' Datum TVD = 4400' SS (CONDUCTOR I9-5/8" TAM PORT COLLAR ~-L 717' r 9-518" CSG, 47#, L-80 BTC, ID = 8.681" 44$1' 7" CSG, 26#, L-80 TCII XO TO L-80 BTGM 5983' Minimum ID = 2.754" @ 9276' 3-1 /2" HES XN NIPPLE 7" MARKER JOINT w / RA TAG 8325° 7" X 3-1/2" HES DUEL FEED THRU 83$5' PKR, ID - 2.965" 3-1 /2"MA RKER JOINT w / RA TAG (--) 8451' -2 ~ ~ 3-112" NDPG MULTFSUB, ID = 2.992" ~ $746' -j 3-1 /2" HES X NIP, ID = 2.813" 8767' 7" X 3-1/2" HES DUEL FEED THRU PKR, ID = 2.965 8775' 3-112" NDPG MULTI-SUB, ID = 2.992" ' " " 8$66 HES DUEL FEED THRU X 3-112 7 PERFORATION SUMMARY PKR, ID - 2.965" REF LOG: USIT LOG ON 11/21/08 ANGLE AT TOP PERF: N/A 8879' 3-1 /2" NDPG MULTI-SUB, ID = 2.992" Note: Refer to Production DB for historical perf data SIZE SPF ZONE INTERVAL Opn/Sqz DATE 9034' 3-1/2" HES X NIP, ID = 2.813" 4-112" 5 Nb 8415 - 8447 O 11/20/08 4-1/2" 5 Oba 8801 - 8857 O 11/20/08 4-1/2" 5 OBb 8883 - 8909 O 11/20!08 9041' 7" X 3-1/2" HES DUEL FEED THRU 4-112" 5 OBd 9088 - 9171 O 11 /20!08 PKR, ID = 2.965" 4-1/2" 5 OBe 9235 - 9285 O 11/20!08 9054' 3-112" NDPG SINGLE-SUB, ID = 2.992" 9205' 3-1/2" HES X NIP, ID = 2.813" 3-112" TBG, 9.2#, L-80 TCII, .0087 bpf, ID = 2.992" ~ 9298° PBTD 9490' 7" CSG, 26#, L-80 BTGM .0383 bpf, ID = 6.276" 9573° I,~j 3527' ~-) 3-112" HES X NIP, ID = 2.813" GAS LIFT MANDRELS ST MD TVD DEV TYPE VLV LATCH PORT DATE 8 8283 4451 61 MMG DMY RK 0 01/23!09 WATFR IN.IFC;TIf)N MANDRELS ST MD TVD DEV TYPE VLV LATCH PORT DATE 7 8399 4508 60 MMG-W DMY RK 0 11!22/08 6 8722 4669 60 MMG-W P-15 RK 8 01/23/09 5 8793 4704 60 MMG-W DMY RK 0 11/22/08 4 8837 4726 60 MMG-W P-15 RK 12 01/23/09 3 8892 4753 60 MMG-W DMY RK 0 11!22/08 2 9011 4812 60 MMG-W P-15 RK 11 01/23/09 1 9226 4919 61 MMG-W P-15 RK 19 01/23/09 8312' ~-13-1/2" HES X NIP, ID = 2.813" 9255' -(3-1/2" HES X NIP, ID = 2.813" 9276' 3-1/2" HES X NIP, ID = 2.750" 9298' 3-1/2" WLEG, ID = 2.992" DATE REV BY COMMENTS DATE REV BY COMMENTS 11/22108 N9E5 ORIGINAL COMPLETION 12/03/08 ?! PJC DRLG DRAFT CORRECTIONS 12!15/08 TW/PJC FINAL DRAFT CORRECT1ONS 02/05(09 GJF/SV GLV CIO (01123109) ORION UNIT WELL: V-219 PERMIT Na: ~Z081420 API No: 50-029-23397-00 SEC 11, T11N, R11E, 554' FNL & 4892' FEL BP Exploration (Alaska} by .r f~= .~~ V-219 Survev Resort Schlumherger r Client: BP Exploration Alaska Field: Prudhoe Bay Unit- WOA Structure 1 Slot: V-Pad I V-219 (SY) well: V-219 Borehole: V-219 UWIIAPI#: 500292339700 Survey Name 1 Date: V-219 I November 17, 2008 Tort 1 AHD 1 DDI 1 ERD ratio: 172.822° 17501.66 ft 16.388 / 1.474 Grid Coordinate System: NAD27 Alaska State Planes, Zone 04, US Feet Location LatlLong: N 70.32770172, W 149.26350162 Location Grid NIE YIX: N 5969976.030 ftUS, E 590813.860 ftUS Grid Convergence Angle: 10.69351583° Survey 1 DLS Computation Method: Minimum Curvature I Lubinski Vertical Section Azimuth: 89.760° Vertical Section Origin: N 0.000 ft, E 0.000 ft ND Reference Datum: Rotary Table ND Reference Elevation: 82.00 ft relative to MSL Sea Bed 1 Ground Level Elevation: 53.50 ft relative to MSL Magnetic Declination: 22.710° Total Field SVength: 57670.307 nT Magnetic Dip: 80.870° Declination Date: November 08, 2008 Magnetic Declination Model: BGGM 2008 North Reference: TNe North • Total Corr Mag North -> True North: +22.710° Comments Measured Inclination Azimuth Sub-Sea ND ND Vertical Along Hole Closure NS EW DLS Northing Easting Latitude Longitude Depth Section Departure ft de (de ) ft ft) ft (ft ft (ft) ft de 700 ft) ftUS (ftUS KIt U. UU U.VU V. VV -tSL. UU U .UU U. VU U. UU U. UV U. UU U. VV V.VV J~7V.7 ~7r v. VJ J'VO IJ .OV IV /V .JL/lV 1lL VV IYJ .LVJJV IVL GYD GC SS 74. 00 0.10 180. 37 -8. 00 74 .00 0. 00 0. 06 0. 06 -0. 06 0. 00 0.14 5969975. 97 590813 .86 N 70 .32770154 W 149 .26350162 166. 00 0.05 242. 81 84. 00 166 .00 -0. 04 0. 17 0. 17 -0. 16 -0. 04 0.10 5969975. 87 590813 .83 N 70 .32770127 W 149 .26350192 258. 00 1.00 126. 04 176. 00 258 .00 0. 57 0. 97 0. 87 -0. 65 0. 58 1.11 5969975. 38 590814 .44 N 70 .32769993 W 149 .26349694 274. 00 1.37 118. 63 191. 99 273 .99 0. 85 1. 30 1. 19 -0. 83 0. 86 2.50 5969975. 21 590814 .73 N 70 .32769946 W 149 .26349466 365. 00 2.95 113. 96 282. 92 364 .92 3. 94 4. 72 4 .57 -2. 30 3. 95 1.75 5969973. 78 590817 .84 N 70 .32769543 W 149 .26346957 456. 00 4.23 115. 30 373. 74 455 .74 9. 11 10. 42 10 .26 -4. 69 9. 13 1.41 5969971. 46 590823 .04 N 70 .32768892 W 149 .26342761 547. 00 5.67 112. 16 464. 40 546 .40 16. 29 18. 27 18 .10 -7. 82 16. 32 1.61 5969968. 41 590830 .28 N 70 .32768037 W 149 .26336924 640. 00 7.26 115. 45 556. 81 638 .81 25. 84 28. 74 28 .56 -12. 07 25. 89 1.75 5969964. 27 590839 .89 N 70 .32766873 W 149 .26329171 730. 00 9.86 114. 04 645 .80 727 .80 37. 99 42. 13 41 .96 -17. 66 38. 06 2.90 5969958. 84 590852 .13 N 70 .32765348 W 149 .26319299 MWD+IFR+MS 760. 76 10.67 115. 69 676 .07 758 .07 42. 95 47. 62 47 .44 -19. 96 43. 03 2.80 5969956. 59 590857 .13 N 70 .32764717 W 149 .263 851. 47 12.43 117. 87 764 .94 846 .94 59. 11 65. 77 65 .59 -28. 17 59. 23 2.00 5969948. 58 590873 .42 N 70 .32762476 W 149 1 .2630 946. 33 15.54 118. 31 856 .97 938 .97 79. 28 88. 70 88 .49 -38. 97 79. 45 3.28 5969938. 03 590893 .77 N 70 .32759525 W 149 .2628 1040. 80 20.23 115. 18 946 .85 1028 .85 105. 17 117. 69 117 .49 -51. 93 105. 39 5.07 5969925. 38 590919 .86 N 70 .32755985 W 149 .26264705 1135. 43 24.04 114. 83 1034 .49 1116 .49 137. 42 153 .34 153 .13 -66. 99 137. 70 4.03 5969910. 72 590952 .35 N 70 .32751870 W 149 .26238504 1231. 75 29.15 114. 79 1120 .59 1202 .59 176. 47 196 .45 196 .23 -85. 08 176. 83 5.31 5969893. 11 590991 .69 N 70 :32746929 W 149 .26206776 1325. 27 33.29 114. 69 1200 .55 1282 .55 220. 40 244 .91 244 .69 -105. 36 220. 84 4.43 5969873. 36 591035 .94 N 70 .32741388 W 149 .26171084 1419. 89 36.59 115. 57 1278 .11 1360 .11 269. 35 299 .10 298 .87 -128. 38 269. 89 3.53 5969850. 94 591085 .26 N 70 .32735098 W 149 .26131314 1515. 59 39.76 115. 93 1353 .33 1435 .33 322. 51 358 .24 358 .01 -154. 08 323. 15 3.32 5969825. 89 591138 .82 N 70 .32728076 W 149 .26088123 1611. 39 42.95 115 .85 1425 .23 1507 .23 379. 33 421 .53 421 .29 -181. 71 380. 09 3.33 5969798. 95 591196 .09 N 70 .32720526 W 149 .26041954 1705. 94 45.32 115 .47 1493 .09 1575 .09 438. 55 487 .36 487 .13 -210. 22 439. 44 2.52 5969771. 16 591255 .77 N 70 .32712738 W 149 .25993835 1802. 39 46.02 115 .48 1560 .48 1642 .48 500. 71 556 .35 556 .12 -239. 89 501. 72 0.73 5969742. 25 591318 .40 N 70 .32704630 W 149 .25943331 1895. 47 46.42 116 .74 1624 .89 1706 .89 560. 93 623 .56 623 .32 -269. 47 562. 06 1.07 5969713. 41 591379 .09 N 70 .32696549 W 149 .25894403 SurveyEditor Ver SP 2.1 Bld(doc40x_100) V-219 (SY)\V-219\V-219\V-219 Generated 9/15/2009 10:50 AM Page 1 of 4 Comments Measured Inclination Azimuth Sub-Sea ND ND Vertical Along Hole Closure NS EW DLS Northing Easting Latitude Longitude Depth Section Departure ft) de (de ) (ft) ft (ft ft (ft) ft (ft de 100ft) (ftUS (ftUS) lyy"I.lti 2086.50 2180.63 2275.77 2371.65 2466.91 2562.79 2657.95 2752.90 2846.30 2942.04 3037.69 4b.U4 47.81 50.56 54.13 57.86 61.14 63.87 "I l /.U/ Iby I.U25 I / /3.Ui5 bLL.4L byL.bb 116.86 1756.19 1838.19 684.35 762.30 113.72 1817.72 1899.72 748.63 110.50 1875.84 1957.84 818.29 106.93 1929.47 2011.47 893.45 104.19 1977.81 2059.81 972.41 100.48 2022.09 2104.09 1055.40 64.82 96.13 2063.30 2145.30 64.47 96.31 2103.96 2185.96 65.77 95.82 2143.26 2225.26 64.99 96.42 2183.14 2265.14 64.13 95.98 2224.23 2306.23 3132. 32 65. 58 96. 16 3227. 97 65. 51 96. 42 3323. 22 65. 30 96. 47 3418. 77 64. 79 96. 42 3515. 02 65. 57 95. 94 3610. 20 65. 11 96. 32 3706. 12 64. 39 96. 13 3801. 06 65. 08 98. 31 3897. 00 63. 53 98. 12 3993. 68 65 .20 97. 34 4088. 63 64 .99 97. 81 4184. 32 65 .30 98. 33 4279. 60 65 .04 98. 92 4375. 10 66 .83 98. 97 4423. 36 66 .58 98. 97 4470 .66 66 .36 98. 60 4566 .41 65 .71 98. 30 4661 .01 65 .83 98. 25 4755 .88 65 .83 99. 02 4849 .82 63 .34 100. 47 4945 .39 63 .28 101. 41 5041 .67 65 .90 101. 58 5134 .71 65 .99 102. 21 5228 .43 65 .49 102. 86 5322 .96 67 .85 101. 45 5416 .27 68 .28 100. 67 5512 .31 67 .24 99. 61 5607 .69 68 .10 100. 13 5701 .99 67 .52 99. 66 2264.44 2304.04 2343.68 2383.99 2424.39 2464.11 2505.02 2545.55 2587.14 2628.97 2668.96 2709.18 2749.19 2788.13 2807.21 2346.44 2386.04 2425.68 2465.99 2506.39 2546.11 2587.02 2627.55 2669.14 2710.97 1140.20 1225.46 1309.68 1396.18 1482.01 1567.15 1653.65 1739.67 1825.71 1912.52 833.52 908.82 988.29 1070.35 1155.38 1241.15 1326.96 1411.69 1498.72 1585.10 1670.76 1757.83 1844.44 1931.06 2018.42 OyL.4U 762.03 833.24 908.39 987.32 1068.36 1151.68 1234.69 1317.34 1399.27 1483.78 1567.95 1651.61 1736.91 1821.96 1907.18 1993.17 -JUU. / 4 -332.31 -362.70 -390.99 -416.43 -438.41 -456.54 -468.92 -478.21 -487.16 -496.44 -505.77 -514.83 -524.37 -534.09 -543.81 -553.22 1998 .49 2104. 92 2078. 41 -562. 45 2084 .69 2191. 68 2164. 03 -571. 86 2169 .81 2277. 53 2249. 06 -582. 66 2255 .32 2363. 98 2334. 92 -595. 01 2341 .64 2451. 14 2421. 45 -606. 73 2750.96 2426.96 2537.26 2506.96 2791.18 2512.88 2624.09 2593.29 2831.19 2598.32 2710.56 2679.39 2870.13 2684.39 2797.76 2766.27 2889.21 2728.15 2842.08 2810.45 2826.10 2908.10 2770.98 2885.45 2853.66 2864.99 2946.99 2857.47 2972.95 2940.81 2903.81 2985.81 2942.78 3059.21 3026.74 2942.66 3024.66 3028.30 3145.77 3113.01 2982.97 3064.97 3111.86 3230.61 3197.71 3025.90 3107.90 3195.62 3067.21 3149.21 3280.76 3105.13 3187.13 3363.82 3143.64 3225.64 3447.15 3181.08 3263.08 3531.92 3215.93 3297.93 3616.80 3252.28 3334.28 3704.23 3288.52 3370.52 3791.09 3324.14 3406.14 3877.04 3315.99 3402.95 3487.91 3573.35 3660.15 3746.70 3835.60 3923.82 4011.14 3283.03 3369.96 3454.91 3540.35 3627.13 3713.64 3802.44 3890.55 3977.76 -618.08 -630.27 -643.24 -656.80 -663.71 -670.33 -683.19 -695.60 -708.60 -722.95 -739.15 -756.48 -773.99 -792.54 -810.80 -827.41 -843.06 -858.18 -873.19 OLJ. bO V.Y( J~7V.'IVVL. O-J J~IYY I.VV IV /V. JLVUUV VJ VV IYJ. LJVYYYJJ 685. 75 1.86 5969652. 07 591503. 52 N 70. 32679378 W 149. 25794112 750. 16 3.86 5969622. 47 591568. 29 N 70. 32671074 W 149. 25741888 819. 94 4.61 5969595. 02 591638. 39 N 70. 32663343 W 149. 25685313 895. 20 4.97 5969570. 50 591713. 95 N 70. 32656391 W 149. 25624286 974. 26 4.24 5969549 .48 591793. 26 N 70. 32650384 W 149. 25560184 1057. 32 4.46 5969532 .36 591876. 53 N 70. 32645428 W 149. 25492832 1142 .18 4.24 5969521 .02 591961. 52 N 70. 32642044 W 149. 25424032 1227. 47 0.41 5969512 .75 592046. 92 N 70. 32639501 W 149. 25354869 1311 .73 1.47 5969504 .82 592131. 27 N 70. 32637052 W 149. 25286552 1398 .27 0.99 5969496 .59 592217. 91 N 70. 32634513 W 149. 25216384 1484 .14 0.99 5969488 .31 592303. 87 N 70. 32631960 W 149. 2514 1569 .32 1.54 5969480 .28 592389. 15 N 70. 32629480 W 149. 250776 3 1655 .86 0.26 5969471 .79 592475. 79 N 70. 32626869 W 149. 25007521 1741 .92 0.23 5969463 .11 592561. 96 N 70. 32624208 W 149. 24937741 1828 .00 0.54 5969454 .43 592648. 14 N 70. 32621546 W 149. 24867944 1914 .86 0.93 5969446 .08 592735. 09 N 70. 32618971 W 149. 24797524 2000 .86 0.60 5969437 .89 592821. 20 N 70. 32616441 W 149. 24727791 2087 .10 0.77 5969429 .52 592907. 54 N 70. 32613865 W 149. 24657864 2172 .27 2.20 5969419 .76 592992. 82 N 70. 32610909 W 149. 24588808 2257 .84 1.63 5969408 .45 593078. 52 N 70. 32607528 W 149. 24519433 2344 .20 1.87 5969397 .77 593165. 02 N 70. 32604319 W 149. 24449406 2429 .57 0.50 5969387 .46 593250. 51 N 70. 32601210 W 149. 24380190 2515 .54 0.59 5969376 .31 593336 .61 N 70. 32597872 W 149 .24310489 2601 .03 0.62 5969364 .38 593422 .25 N 70 .32594322 W 149 .24241172 2687 .17 1.87 5969351 .87 593508 .53 N 70 .32590609 W 149 .24171335 2730 .95 0.52 5969345 .49 593552 .39 N 70 .32588717 W 149 .24135836 2773 .81 0.85 5969339 .38 593595 .32 N 70 .32586903 W 149 .24101087 2860 .36 0.74 5969327 .57 593682 .01 N 70 .32583382 W 149 .240 2945 .72 0.14 5969316 .19 593767 .51 N 70 .32579981 W 149 3 .2396 3031 .29 0.74 5969304 .24 593853 .23 N 70 .32576422 W 149 .23892 3114 .91 2.99 5969290 .90 593937 .00 N 70 .32572492 W 149 .23824531 3198 .75 0.88 5969275 .71 594021 .02 N 70 .32568056 W 149 .23756563 3283 .96 2.73 5969259 .42 594106 .43 N 70 .32563311 W 149 .23687476 3367 .09 0.63 5969242 .92 594189 .76 N 70 .32558517 W 149 .23620076 3450 .50 0.83 5969225 .38 594273 .38 N 70 .32553441 W 149 :23552456 3535 .35 2.85 5969208 .15 594358 .44 N 70 .32548440 W 149 .23483666 3620 .30 0.90 5969192 .58 594443 .57 N 70 .32543893 W 149 .23414797 3707 .80 1.49 5969177 .99 594531 .25 N 70 .32539605 W 149 .23343855 3794 .72 1.03 5969163 .92 594618 .34 N 70 .32535461 W 149 .23273386 3880 .74 0.77 5969149 .95 594704 .52 N 70 .32531350 W 149 .23203650 SurveyEditor Ver SP 2.1 Bld(doc40x_100) V-219 (SY)\V-219\V-2191V-219 Generated 9/15/2009 10:50 AM Page 2 of 4 Comments Measured Inclination Azimuth Sub-Sea ND 7Vp Vertical Along Hole Closure NS EW DLS Northing Easting Latitude Longitude Depth Section Departure ft (de (de ft (ft) (ft) ft ft ft 00o cn ft) ~nc~ on (de I100ft ~ 42 (ftUS Goao~~G RR ftUS FOd 7O1 7r, AI 7n Z7~.771 dR 1A/ 1dO 7'31 '3Zr1R~. .7/.N/. `J25 bU. OL IUU. JL JJO 1..74 J44J. a4 J.7V4. V4 4V ~~. JY YVVV. VI -VVU.JC .'ovi. VV .. ..i v.iv.i ..iv. vv ....T... .. . .. ~. .... ..~ ..... ... .. .... .... ........... 5891. 55 66. 56 99. 80 3398. 71 3480. 71 4048. 53 4185. 41 4151. 85 -903.52 4052. 35 0.51 5969121. 70 594876. 47 N 70. 32523038 W 149. 23064521 5987. 44 66. 12 99. 71 3437. 19 3519. 19 4135. 02 4273. 24 4239. 58 -918.40 4138. 91 0.47 5969107. 87 594963. 19 N 70. 32518960 W 149. 22994345 6083. 02 66. 49 99. 97 3475. 60 3557. 60 4221. 19 4360. 76 4327. 00 -933.36 4225. 14 0.46 5969093. 96 595049. 60 N 70. 32514861 W 149. 22924433 6176. 42 67. 14 100. 27 3512. 37 3594. 37 4305. 65 4446. 62 4412. 79 -948.45 4309. 66 0.76 5969079. 90 595134. 28 N 70. 32510726 W 149. 22855911 6273. 77 67. 02 99. 94 3550. 29 3632. 29 4393. 86 4536. 28 4502. 38 -964.18 4397. 93 0.34 5969065. 24 595222. 73 N 70. 32506414 W 149. 22784348 6369. 23 66. 65 100. 26 3587. 84 3669. 84 4480. 19 4624. 05 4590. 08 -979.57 4484. 34 0.50 5969050. 90 595309. 31 N 70. 32502196 W 149. 22714300 6463. 01 65. 37 100. 65 3625. 97 3707. 97 4564. 38 4709. 72 4675. 71 -995.12 4568. 59 1.42 5969036. 37 595393. 74 N 70. 32497935 W 149. 22645995 6557. 57 66. 47 98. 88 3664. 55 3746. 55 4649. 40 4796. 05 4761. 95 -1009.75 4653. 67 2.07 5969022. 77 595478. 98 N 70. 32493922 W 149. 22577024 6652. 95 68. 32 97. 37 3701. 21 3783. 21 4736. 51 4884. 10 4849. 78 -1022.19 4740. 83 2.43 5969011. 39 595566. 27 N 70. 32490510 W 149 .22506360 6748. 02 70. 51 93. 87 3734. 65 3816. 65 4825. 02 4973. 09 4938. 18 -1030.88 4829. 38 4.15 5969003. 77 595654. 92 N 70. 32488119 W 149 .22434568 6843. 75 69 .94 90. 18 3767. 04 3849. 04 4915. 02 5063. 17 5026. 90 -1034.07 4919. 39 3.68 5969001. 67 595744. 95 N 70. 32487232 W 149 .2236. 6937. 29 68 .32 86. 41 3800. 38 3882. 38 5002. 37 5150. 57 5111. 88 -1031.49 5006. 73 4.14 5969005. 31 595832. 25 N 70. 32487923 W 149 .22290775 7033. 44 66 .21 84. 07 3837. 54 3919. 54 5090. 76 5239. 24 5197. 00 -1024.14 5095. 09 3.14 5969013. 72 595920. 50 N 70 .32489913 W 149 .22219128 7128. 51 65 .46 80. 77 3876. 47 3958. 47 5176. 77 5325. 98 5279. 11 -1012.71 5181. 06 3.26 5969026. 19 596006. 32 N 70 .32493020 W 149 .22149422 7222. 97 65 .24 77. 75 3915. 87 3997 .87 5261. 17 5411. 82 5358. 90 -996.71 5265. 39 2.92 5969043. 21 596090. 44 N 70 .32497373 W 149 .22081035 7319. 29 64 .45 74. 05 3956. 82 4038 .82 5345. 80 5499. 00 5438. 14 -975.49 5349. 93 3.57 5969065. 45 596174 .71 N 70 .32503156 W 149 .22012479 7414 .75 65 .56 71. 64 3997. 16 4079 .16 5428. 57 5585. 52 5515. 02 -949.96 5432. 59 2.57 5969091. 97 596257 .05 N 70 .32510112 W 149 .21945445 7510 .56 66 .18 68. 68 4036. 34 4118 .34 5510. 92 5672. 95 5591. 09 -920.29 5514. 83 2.89 5969122. 64 596338 .91 N 70 .32518204 W 149 .21878753 7606 .48 66 .33 66. 09 4074. 97 4156 .97 5592. 10 5760. 75 5665. 66 -886.53 5595. 87 2.48 5969157. 37 596419 .53 N 70 .32527410 W 149 .21813026 7700 .06 65 .70 64. 52 4113. 01 4195 .01 5669. 93 5846. 25 5736 .98 -850.81 5673. 54 1.67 5969194. 02 596496 .76 N 70 .32537151 W 149 .21750023 7795 .70 65 .81 61. 23 4152. 29 4234 .29 5747. 69 5933. 45 5808 .05 -811.06 5751. 14 3.14 5969234. 71 596573 .86 N 70 .32547995 W 149 .21687081 7890 .47 65 .93 59. 85 4191 .04 4273 .04 5823. 18 6019. 94 5876 .91 -768.52 5826. 45 1.33 5969278. 15 596648 .64 N 70 .32559600 W 149 .21625998 7986 .02 65 .86 60. 60 4230 .06 4312 .06 5899. 06 6107. 16 5946 .54 -725.21 5902. 15 0.72 5969322. 37 596723 .81 N 70 .32571416 W 149 .21564589 8081 .29 61 .95 60. 71 4271 .96 4353 .96 5973. 80 6192. 70 6015 .65 -683.29 5976. 71 4.11 5969365. 19 596797 .85 N 70 .32582853 W 149 .21504104 8176 .50 61 .08 61. 70 4317 .37 4399 .37 6047. 30 6276. 38 6084 .12 -642.98 6050. 05 1.29 5969406. 38 596870 .68 N 70 .32593849 W 149 .21444617 8271 .61 60 .75 59. 91 4363 .60 4445 .60 6120. 02 6359. 50 6152 .17 -602.44 6122. 60 1.68 5969447. 79 596942 .74 N 70 .32604908 W 149 .21385761 8366 .43 60 .55 59. 55 4410 .08 4492 .08 6191. 58 6442 .14 6219 .31 -560.78 6193. 98 0.39 5969490. 31 597013 .60 N 70 .32616273 W 149 .21327856 8461 .58 60 .06 57. 66 4457 .22 4539 .22 6262. 31 6524 .80 6285 .89 -517.73 6264. 53 1.80 5969534. 21 597083 .62 N 70 .32628019 W 149 .2127 8557 .10 60 .55 56. 35 4504 .54 4586 .54 6332. 09 6607 .77 6351 .72 -472.54 6334. 12 1.30 5969580. 23 597152 .65 N 70 .32640347 W 149 .2121 8650 .94 59 .80 55. 64 4551 .21 4633 .21 6399. 76 6689 .18 6415 .84 -427.01 6401. 61 1.03 5969626. 56 597219 .58 N 70 .32652769 W 149 .21159 8747 .22 60 .36 55. 60 4599 .23 4681 .23 6468. 83 6772 .63 6481 .62 -379.89 6470. 48 0.58 5969674. 51 597287 .86 N 70 .32665626 W 149 .21103535 8842 .10 60 .09 55. 63 4646 .35 4728 .35 6536. 99 6854 .98 6546 .94 -333.38 6538. 44 0.29 5969721. 84 597355 .25 N 70 .32678316 W 149 .21048393 8937 .59 60.15 55 .12 4693 .92 4775 .92 6605. 32 6937 .78 6612 .78 -286.34 6606. 58 0.47 5969769. 70 597422 .80 N 70 .32691152 W 149 .20993114 9033 .72 59 .95 55 .80 4741 .91 4823 .91 6674 .13 7021 .07 6679 .47 -239.11 6675 .19 0.65 5969817. 75 597490 .83 N 70 .32704037 W 149 .20937446 9129 .16 60.19 55 .20 4789 .53 4871 .53 6742 .49 7103 .78 6746 .09 -192.26 6743 .35 0.60 5969865 .41 597558 .42 N 70 .32716819 W 149 .20882140 9224 .73 60 .85 54 .60 4836 .57 4918 .57 6810 .75 7186 .98 6812 .95 -144.42 6811 .41 0.88 5969914 .07 597625 .89 N 70 .32729872 W 149 .20826912 9320 .28 61 .27 55 .17 4882 .80 4964.80 6879 .35 7270 .60 6880 .49 -96.33 6879 .81 0.68 5969962 .98 597693 .70 N 70 .32742994 W 149 .20771413 9416 .56 61 .96 54 .16 4928 .57 5010 .57 6948 .65 7355 .30 6949 .07 -47.34 6948 .91 1.17 5970012 .80 597762 .19 N 70 .32756361 W 149 .20715346 Last Survey 9502 .63 61 .43 54 .70 4969 .39 5051 .39 7010 .48 7431 .08 7010 .55 -3.26 7010 .55 0.83 5970057 .62 597823 .29 N 70 .32768388 W 149 .20665331 TD (Projected) 9583 .00 d 61 .43 54 .70 5007 .82 5089 .82- 7068 .25 7501 .66 7068 .26 37.53 7068 .16 0.00 5970099 .10 597880 .39 N 70 .32779515 W 149 .20618587 SurveyEditor Ver SP 2.1 Bld( doc4Ox_1OO) V-219 (SY)\V-219\V-219\V-219 Generated 9/15/2009 10:50 AM Page 3 of 4 Comments Measured Inclination Azimuth Sub-Sea ND ND Vertical Along Hole Closure NS EW DLS Northing Easting Latitude Longitude Depth Section Departure ft (de ) de ) ft (ft) ft (ft) ft) ft (ft) de 1100ft) ftUS (ftUS) Survey Type: Definitive Survey NOTES: GYD GC SS - (Gyrodata -gyro single shots -- Gyrodata gyro orientation surveys. Not to be run above 70 degrees inclination. ) MWD + IFR + MS - (In-field referenced MWD with mutt-station analysis and correction applied in post-processing. Assumes a BHA sag correction is applied to enhance inclination accuracy. ) Leval Description: Northing (Y) fftUSl Easting (X) fftUSl Surface : 4725 FSL 1488 FEL S11 T11N R11E UM 5969976.03 590813.86 BHL : 4760 FSL 4608 FEL S7 T11 N R12E UM 5970099.10 597880.39 SurveyEditor Ver SP 2.1 Bld( doc40x_100) V-219 (SY)\V-219\V-219\V-219 Generated 9/15/2009 10:50 AM Page 4 of 4 N SCHLUMBERGER Survey report Client .................... Field ..................... Well ...................... API number ...............: Engineer .................. RIG :...................... STATE :.................... ----- Survey calculation m Method for positions.....: Method for DLS...........: BP Exploration (Alaska) Inc. Orion V-219 50-029-23397-00 Thor Kallestad Nabors 9ES Alaska ethods------------- Minimum curvature Mason & Taylor ----- Depth reference ----------------------- Permanent datum..........: Mean Sea Level Depth reference..........: Driller's Pipe Tally GL above permanent.......: 53.50 ft KB above permanent.......: 53.50 ft DF above permanent.......: 82.00 ft ----- Vertical section origin---------------- Latitude (+N/S-).........: 0.00 ft Departure (+E/W-)........: 0.00 ft ----- Platform reference point--------------- Latitude (+N/S-).........: 0.00 ft Departure (+E/W-)........: 0.00 ft Azimuth from Vsect Origin to target: 89.76 degrees 17-Nov-2008 09:23:33 Page 1 of 5 Spud date ................: 08-Nov-2008 Last survey date.........: 17-Nov-08 Total accepted surveys...: 105 MD of first survey.......: 0.00 ft MD of last survey........: 9583.00 ft ----- Geomagnetic data ---------------------- Magnetic model...........: BGGM version 2008 Magnetic date ............: 08-Nov-2008 Magnetic field strength..: 57671.77 GAMA Magnetic dec (+E/W-).....: 22.71 degrees Magnetic dip .............: 80.87 degrees ----- MWD survey Reference Reference G ..............: Reference H ............... Reference Dip ............: Tolerance of G...........: Tolerance of H............ Tolerance of Dip.........: Criteria --------- 1002.68 meal 57672.00 GAMA 80.87 degrees (+/-) 2.50 meal (+/-)300.00 GAMA (+/-) 0.45 degrees ----- Corrections --------------------------- Magnetic dec (+E/W-).....: 22.71 degrees Grid convergence (+E/W-).: 0.00 degrees Total az corr (+E/W-)....: 22.71 degrees (Total az corr = magnetic dec - grid cony) Survey Correction Type .... I=Sag Corrected Inclination M=Schlumberger Magnetic Correction S=Shell Magnetic Correction F=Failed Axis Correction R=Magnetic Resonance Tool Correction D=Dmag Magnetic Correction • • ~[(c)2008 IDEAL ID13_OC_13] SCHLLTMBERGER Survey Report 17-Nov-2008 09:23:33 Page 2 of 5 Seq Measured Incl Azimuth Course TVD Vertical Displ Displ Total At DLS Srvy # depth angle angle length depth section +N/S- +E/W- displ Azim (deg/ tool - (ft) (deg) (deg) (ft) (ft) (ft) (ft) (ft) (ft) (deg) 100f) type 1 0.00 0.00 0.00 0.00 0.00 0.00 0.00 0.00 0.00 0.00 0.00 TI P 2 74.00 0.11 180.37 74.00 74.00 -0.00 -0.07 -0.00 0.07 180.37 0.15 BP _GYD SS 3 166.00 0.05 242.81 92.00 166.00 -0.04 -0.18 -0.04 0.18 191.68 0.11 BP _GYD SS 4 258.00 1.00 126.04 92.00 258.00 0.57 -0.67 0.58 0.88 139.21 1.11 BP _GYD SS 5 274.00 1.37 118.63 16.00 273.99 0.85 -0.84 0.86 1.20 134.48 2.50 BP _GYD SS 6 365.00 2.95 113.96 91.00 364.92 3.94 -2.31 3.95 4.58 120.35 1.75 BP GYD SS 7 456.00 4.23 115.30 91.00 455.74 9.11 -4.70 9.13 10.27 117.25 1.41 BP _ _GYD SS • 8 547.00 5.67 112.16 91.00 546.40 16.29 -7.83 16.32 18.11 115.62 1.61 BP _GYD SS 9 640.00 7.26 115.45 93.00 638.81 25.84 -12.09 25.89 28.57 115.03 1.75 BP _GYD SS 10 730.00 9.86 114.04 90.00 727.80 37.99 -17.67 38.06 41.96 114.91 2.90 BP _GYD 55 11 760.76 10.67 115.69 30.76 758.07 42.95 -19.98 43.03 47.44 114.91 2.80 BP _MWD+IFR+MS 12 851.47 12.43 117.87 90.71 846.94 59.11 -28.18 59.23 65.59 115.45 2.00 BP _MWD+IFR+MS 13 946.33 15.54 118.31 94.86 938.97 79.28 -38.99 79.45 88.50 116.14 3.28 BP _MWD+IFR+MS 14 1040.80 20.23 115.18 94.47 1028.85 105.17 -51.94 105.39 117.49 116.24 5.07 BP _MWD+IFR+MS 15 1135.43 24.04 114.83 94.63 1116.49 137.42 -67.00 137.70 153.13 115.95 4.03 BP _MWD+IFR+MS 16 1231.75 29.15 114.79 96.32 1202.59 176.47 -85.09 176.83 196.23 115.70 5.31 BP _MWD+IFR+MS 17 1325.27 33.29 114.69 93.52 1282.55 220.40 -105.37 220.84 244.69 115.51 4.43 BP _MWD+IFR+MS 18 1419.89 36.59 115.57 94.62 1360.11 269.35 -128.40 269.89 298.87 115.44 3.53 BP _MWD+IFR+MS 19 1515.59 39.76 115.93 95.70 1435.33 322.50 -154.10 323.15 358.01 115.49 3.32 BP _MWD+IFR+MS 20 1611.39 42.95 115.85 95.80 1507.23 379.33 -181.73 380.09 421.30 115.55 3.33 BP _MWD+IFR+MS 21 1705.94 45.32 115.47 94.55 1575.09 438.55 -210.23 439.44 487.14 115.57 2.52 BP _MWD+IFR+MS • 22 1802.39 46.02 115.48 96.45 1642.48 500.71 -239.91 501.72 556.13 115.56 0.73 BP _MWD+IFR+MS 23 1895.47 46.42 116.74 93.08 1706.89 560.93 -269.49 562.06 623.33 115.62 1.07 BP _MWD+IFR+MS 24 1991.16 46.04 117.07 95.69 1773.08 622.42 -300.75 623.68 692.41 115.74 0.47 BP _MWD+IFR+MS 25 2086.50 47.81 116.86 95.34 1838.19 684.35 -332.33 685.75 762.04 115.86 1.86 BP _MWD+IFR+MS 26 2180.63 50.56 113.72 94.13 1899.72 748.63 -362.72 750.16 833.25 115.80 3.86 BP _MWD+IFR+MS 27 2275.77 54.13 110.50 95.14 1957.84 818.29 -391.01 819.94 908.40 115.50 4.61 BP _MWD+IFR+MS 28 2371.65 57.86 106.93 95.88 2011.47 893.45 -416.45 895.20 987.33 114.95 4.97 BP _MWD+IFR+MS 29 2466.91 61.14 104.19 95.26 2059.81 972.41 -438.43 974.26 1068.36 114.23 4.24 BP _MWD+IFR+MS 30 2562.79 63.87 100.48 95.88 2104.09 1055.40 -456.56 1057.32 1151.69 113.35 4.46 BP MWD+IFR+MS [(c)2008 IDEAL ID13_OC_13] 5CHLUMBERGER Survey Report 17-Nov-2008 09:23:33 Page 3 of 5 Seq Measured Incl Azimuth Course TVD Vertical Displ Displ Total At DLS Srvy # depth angle angle length depth section +N/S- +E/W- displ Azim (deg/ tool - (ft) (deg) (deg) (ft) (ft) (ft) (ft) (f t) (f t) (deg) 100f) type 31 2657.95 64.82 96.13 95.16 2145.30 1140.20 -468.93 1142.18 1234.69 112.32 4.24 BP_ M[n]D+IFR+MS 32 2752.90 64.47 96.31 94.95 2185.96 1225.46 -478.23 1227.47 1317.34 111.29 0.41 BP_ MWD+IFR+MS 33 2846.30 65.77 95.82 93.40 2225.26 1309.68 -487.18 1311.73 1399.28 110.38 1.47 BP_ MWD+IFR+MS 34 2942.04 64.99 96.42 95.74 2265.14 1396.18 -496.45 1398.27 1483.79 109.55 0.99 BP_ MVJD+IFR+MS 35 3037.69 64.13 95.98 95.65 2306.23 1482.01 -505.78 1484.14 1567.96 108.82 0.99 BP_ MWD+IFR+MS 36 3132.32 65.58 96.16 94.63 2346.44 1567.15 -514.84 1569.32 1651.61 108.16 1.54 BP_ MWD+IFR+MS 37 3227.97 65.51 96.42 95.65 2386.04 1653.65 -524.38 1655.86 1736.91 107.57 0.26 BP_ MWD+IFR+MS 38 3323.22 65.30 96.47 95.25 2425.68 1739.67 -534.10 1741.92 1821.97 107.05 0.23 BP_ MWD+IFR+MS 39 3418.77 64.79 96.42 95.55 2465.99 1825.71 -543.83 1828.00 1907.18 106.57 0.54 BP_ MWD+IFR+MS 40 3515.02 65.57 95.94 96.25 2506.39 1912.52 -553.23 1914.86 1993.17 106.11 0.93 BP_ MWD+IFR+MS 41 3610.20 65.11 96.32 95.18 2546.11 1998.49 -562.47 2000.86 2078.42 105.70 0.60 BP_ MWD+IFR+MS 42 3706.12 64.39 96.13 95.92 2587.02 2084.69 -571.88 2087.10 2164.03 105.32 0.77 BP_ MWD+IFR+MS 43 3801.06 65.08 98.31 94.94 2627.55 2169.81 -582.67 2172.27 2249.06 105.02 2.20 BP_ MWD+IFR+MS 44 3897.00 63.53 98.12 95.94 2669.14 2255.32 -595.02 2257.84 2334.93 104.76 1.63 BP_ MWD+IFR+MS 45 3993.68 65.20 97.34 96.68 2710.97 2341.64 -606.74 2344.20 2421.45 104.51 1.87 BP MWD+IFR+MS 46 4088.63 64.99 97.81 94.95 2750.96 2426.96 -618.09 2429.57 2506.96 104.27 0.50 BP_ MWD+IFR+MS 47 4184.32 65.30 98.33 95.69 2791.18 2512.88 -630.28 2515.54 2593.30 104.07 0.59 BP_ MWD+IFR+MS 48 4279.60 65.04 98.92 95.28 2831.19 2598.32 -643.25 2601.03 2679.39 103.89 0.62 BP_ MWD+IFR+MS 49 4375.10 66.83 98.97 95.50 2870.13 2684.39 -656.81 2687.17 2766.27 103.74 1.87 BP_ MWD+IFR+MS 50 4423.36 66.58 98.97 48.26 2889.21 2728.15 -663.72 2730.95 2810.45 103.66 0.52 BP MWD+IFR+MS 51 4470.66 66.36 98.60 47.30 2908.10 2770.98 -670.34 2773.81 2853.66 103.59 0.85 BP_ INC+TREND 52 4566.41 65.71 98.30 95.75 2946.99 2857.47 -683.20 2860.35 2940.82 103.43 0.74 BP_ INC+TREND 53 4661.01 65.83 98.25 94.60 2985.81 2942.78 -695.62 2945.72 3026.74 103.29 0.14 BP_ MWD+IFR+MS 54 4755.88 65.83 99.02 94.87 3024.66 3028.30 -708.61 3031.29 3113.02 103.16 0.74 BP_ MWD+IFR+MS 55 4849.82 63.34 100.47 93.94 3064.97 3111.85 -722.96 3114.91 3197.71 103.07 2.99 BP MWD+IFR+MS 56 4945.39 63.28 101.41 95.57 3107.90 3195.62 -739.17 3198.74 3283.04 103.01 0.88 BP _MWD+IFR+MS 57 5041.67 65.90 101.58 96.28 3149.21 3280.76 -756.50 3283.96 3369.97 102.97 2.73 BP _MWD+IFR+MS 58 5134.71 65.99 102.21 93.04 3187.13 3363.82 -774.01 3367.09 3454.91 102.95 0.63 BP_ MWD+IFR+MS 59 5228.43 65.49 102.86 93.72 3225.64 3447.15 -792.55 3450.50 3540.35 102.94 0.83 BP _MWD+IFR+MS 60 5322.96 67.85 101.45 94.53 3263.08 3531.92 -810.82 3535.35 3627.14 102.92 2.85 BP MWD+IFR+MS • r1 L.J [(0)2008 IDEAL ID13_OC_13] SCHLiJN~ERGER Survey Report 17-Nov-2008 09:23:33 Page 4 of 5 Seq Measured Incl Azimuth Course TVD Vertical Displ Displ Total At DLS Srvy # depth angle angle length depth section +N/S- +E/W- displ Azim (deg/ tool - (ft) (deg) (deg) (ft) (ft) (ft) (ft) (ft) (ft) (deg) 100f) type 61 5416.27 68.28 100.67 93.31 3297.93 3616.80 -827.42 3620.29 3713.65 102.87 0.90 BP _MWD+IFR+MS 62 5512.31 67.24 99.61 96.04 3334.28 3704.23 -843.07 3707.80 3802.44 102.81 1.49 BP _MWD+IFR+MS 63 5607.69 68.10 100.13 95.38 3370.52 3791.09 -858.20 3794.72 3890.55 102.74 1.03 BP _MWD+IFR+MS 64 5701.99 67.52 99.66 94.30 3406.14 3877.04 -873.20 3880.73 3977.76 102.68 0.77 BP _MWD+IFR+MS 65 5797.98 66.62 100.32 95.99 3443.54 3964.04 -888.54 3967.80 4066.07 102.62 1.13 BP _MWD+IFR+MS 66 5891.55 66.56 99.80 93.57 3480.71 4048.52 -903.54 4052.35 4151.85 102.57 0.51 BP _MWD+IFR+MS • 67 5987.44 66.12 99.71 95.89 3519.19 4135.02 -918.42 4138.90 4239.58 102.51 0.47 BP _MWD+IFR+MS 68 6083.02 66.49 99.97 95.58 3557.60 4221.19 -933.38 4225.14 4327.01 102.46 0.46 BP _MWD+IFR+MS 69 6176.42 67.14 100.27 93.40 3594.38 4305.65 -948.46 4309.66 4412.79 102.41 0.76 BP _MWD+IFR+MS 70 6273.77 67.02 99.94 97.35 3632.29 4393.85 -964.19 4397.93 4502.39 102.37 0.34 BP _MWD+IFR+MS 71 6369.23 66.65 100.26 95.46 3669.84 4480.19 -979.58 4484.34 4590.08 102.32 0.50 BP _MWD+IFR+MS 72 6463.01 65.37 100.65 93.78 3707.97 4564.38 -995.13 4568.59 4675.71 102.29 1.42 BP _MWD+IFR+MS 73 6557.57 66.47 98.88 94.56 3746.55 4649.40 -1009.77 4653.67 4761.96 102.24 2.07 BP _MWD+IFR+MS 74 6652.95 68.32 97.37 95.38 3783.21 4736.51 -1022.20 4740.83 4849.78 102.17 2.43 BP _MWD+IFR+MS 75 6748.02 70.51 93.87 95.07 3816.65 4825.02 -1030.90 4829.38 4938.18 102.05 4.15 BP MWD+IFR+MS 76 6843.75 69.94 90.18 95.73 3849.04 4915.01 -1034.08 4919.39 5026.90 101.87 3.68 BP _MWD+IFR+MS 77 6937.29 68.32 86.41 93.54 3882.38 5002.37 -1031.50 5006.73 5111.88 101.64 4.14 BP _MWD+IFR+MS 78 7033.44 66.21 84.07 96.15 3919.54 5090.76 -1024.16 5095.09 5197.01 101.37 3.14 BP _MWD+IFR+MS 79 7128.51 65.46 80.77 95.07 3958.47 5176.77 -1012.72 5181.06 5279.11 101.06 3.26 BP _MWD+IFR+MS 80 7222.97 65.24 77.75 94.46 3997.87 5261.17 -996.73 5265.39 5358.90 100.72 2.92 BP _MWD+IFR+MS • 81 7319.29 64.45 74.05 96.32 4038.82 5345.80 -975.50 5349.93 5438.14 100.33 3.57 BP _MWD+IFR+MS 82 7414.75 65.56 71.64 95.46 4079.16 5428.57 -949.98 5432.59 5515.03 99.92 2.57 BP _MWD+IFR+MS 83 7510.56 66.18 68.68 95.81 4118.34 5510.92 -920.30 5514.83 5591.09 99.47 2.89 BP _MWD+IFR+MS 84 7606.48 66.33 66.09 95.92 4156.97 5592.10 -886.54 5595.87 5665.66 99.00 2.48 BP _MWD+IFR+MS 85 7700.06 65.70 64.52 93.58 4195.01 5669.93 -850.83 5673.54 5736.99 98.53 1.67 BP MWD+IFR+MS 86 7795.70 65.81 61.23 95.64 4234.29 5747.69 -811.07 5751.14 5808.05 98.03 3.14 BP _MWD+IFR+MS 87 7890.47 65.93 59.85 94.77 4273.04 5823.18 -768.54 5826.45 5876.91 97.51 1.33 BP _MWD+IFR+MS 88 7986.02 65.86 60.60 95.55 4312.06 5899.06 -725.23 5902.15 5946.54 97.01 0.72 BP _MWD+IFR+MS 89 8081.29 61.95 60.71 95.27 4353.96 5973.80 -683.30 5976.71 6015.65 96.52 4.11 BP _MWD+IFR+MS 90 8176.50 61.08 61.70 95.21 4399.37 6047.30 -642.99 6050.05 6084.12 96.07 1.29 BP MWD+IFR+MS ~ - i [(c)2008 IDEAL ID13_OC_13] SCHLUI~ERGER Survey Report 17-Nov-2008 09:23:33 Page 5 of 5 Seq Measured Incl Azimuth Course TVD Vertical Displ Displ Total At DLS Srvy # depth angle angle length depth section +N/S- +E/W- displ Azim (deg/ tool - (ft) (deg) (deg) (ft) (ft) (ft) (ft) (ft) (ft) (deg) 100f) type 91 8271.61 60.75 59.91 95.11 4445.60 6120.02 -602.45 6122.60 6152.17 95.62 1.68 BP _MWD+IFR+MS 92 8366.43 60.55 59.55 94.82 4492.08 6191.58 -560.79 6193.98 6219.32 95.17 0.39 BP _MWD+IFR+MS 93 8461.58 60.06 57.66 95.15 4539.22 6262.31 -517.74 6264.53 6285.89 94.72 1.80 BP _MWD+IFR+MS 94 8557.10 60.55 56.35 95.52 4586.54 6332.09 -472.56 6334.12 6351.72 94.27 1.30 BP _MWD+IFR+MS 95 8650.94 59.80 55.64 93.84 4633.21 6399.77 -427.03 6401.61 6415.84 93.82 1.03 BP _MWD+IFR+MS 96 8747.22 60.36 55.60 96.28 4681.23 6468.83 -379.91 6470.48 6481.62 93.36 0.58 BP _MWD+IFR+MS 97 8842.10 60.09 55.63 94.88 4728.35 6536.99 -333.40 6538.44 6546.94 92.92 0.29 BP _MWD+IFR+MS 98 8937.59 60.15 55.12 95.49 4775.92 6605.32 -286.35 6606.58 6612.78 92.48 0.47 BP _MWD+IFR+MS 99 9033.72 59.95 55.80 96.13 4823.92 6674.13 -239.13 6675.19 6679.47 92.05 0.65 BP _MWD+IFR+MS 100 9129.16 60.19 55.20 95.44 4871.53 6742.48 -192.28 6743.35 6746.09 91.63 0.60 BP _MWD+IFR+MS 101 9224.73 60.85 54.60 95.57 4918.57 6810.75 -144.44 6811.42 6812.95 91.21 0.88 BP _MWD+IFR+MS 102 9320.28 61.27 55.17 95.55 4964.80 6879.35 -96.34 6879.81 6880.49 90.80 0.68 BP _MWD+IFR+MS 103 9416.56 61.96 54.16 96.28 5010.57 6948.65 -47.35 6948.91 6949.07 90.39 1.17 BP _MWD+IFR+MS 104 9502.63 61.43 54.70 86.07 5051.39 7010.47 -3.27 7010.55 7010.55 90.03 0.83 BP _MWD+IFR+MS 105 9583.00 61.43 54.70 80.37 5089.82 7068.25 37.52 7068.16 7068.26 89.70 0.00 Projection to TD [(c)2008 IDEAL ID13_OC_13] r U 03/18/09 ~l~i`~Fllgl l~~a~~~r~ Alaska Data & Consulting Services 2525 Gambell Street, Suite 400 Anchorage, AK 99503-2838 ATTN: Beth Wall _InF° fk /~~~ ~, R 1-~~,,I~ 4~}.;. ~j~ ~~,~ ,1~0°i"""; ut~'~~ N ,~~ ~~ ,r~ ~i~ ~~~p ~ n.. NO.5133 Company: State of Alaska Alaska Oil & Gas Cons Comm Attn: Christine Mahnken 333 West 7th Ave, Suite 100 Anchorage, AK 99501 J-27A AY3J-00010 CBL - ~ --j ~---- 02/21/09 _ 1~. t S-107 AWJB-26 MEM L L (~ I' ~- 02/25/09 1 1 09-34A AZ4D-00005 USIT (REVISED) 02/07/09 1 1 V-210 AWJB-00025 INJECTION PROFILE ' 02/23/09 1 1 MPB-22A AXBD-00005 MEM SCMT & TEMP PROFILE "' - 12/23/08 1 1 V-219 12103700 USIT (REVISION #2) b. C I 11/21/08 1 1 11-18 BOCV-00006 PRODUCTION LOG / C/ 03/02/09 1 1 B-25 AVYS-00023 USIT - / r /~ 03/06/09 1 1 N-18A AYKP-00013 PRODUCTION LOG p`~- '~S f" - 03/11/09 1 1 F-18 AVY5-00022 USIT / "%':~' ~- - 03/04/09 1 1 3-19/R-28 AZ4D-00009 LDL ( - - 03/06/09 1 1 V-117 BOOR-00003 MEM PRODUCTION PROFILE ~p - ( ~ 03/1?J09 1 1 V-211 AY3J-00014 IPROF/RST WFL - ~ 03/16/09 1 1 V-214 AY3J-00013 (PROF/RST WFL - ~- 03/15/09 1 1 K-06B AWJI-00017 MCNL ~ - 01/28/09 1 1 L5-15 12113027 RST - /D ''~ / • 12/09/08 1 1 07-18 12071915 RST ~j 12/01/08 1 1 15-15C AWJI-00015 MCNL . ~ 01/02/09 1 1 W-218 40018337 OH MWD/LWD EDIT 12/07/08 2 1 R-41 40018496 OH MWD/LWD EDIT _/s• / 01/04/09 2 1 H-18 11999064 RST / - t ~" .12/03/08 1 1 r~GM.~G f~a~n,~V YYLGYVG nCV GIrI OT JI171Y11VV MIVV 1'1C1 UI'tIVINU VNC VVY1 tAt;r7 1V: BP Exploration (Alaska) Inc. Petrotechnical Data Center LR2-1 900 E. Benson Blvd. Anchorage, Alaska 99508 Date Delivered: ~,c ~ _a l~ °I s a c.-o ~ ~ - w a- coo ~- a w~ ~ ~~a/~~ y,~ - ~ ~ r~Gf pu C~ 3 dal U ~ 3 15 ~ C.o~~ ~ Alaska Data & Consulting Services 2525 Gambell Street,jt ADO - _. Anchorage, AK 99E (~dZ w ~ ^ tl ATTN: Beth Received by: ~a ~~ .~ `? ~/- .x ~ •I fl MEMORANDUM To: Jim Regg l~~ 3~ 31b~ P.I. Supervisor FROM: John Cusp Petroleum Inspector State of Alaska Alaska Oil and Gas Conservation Commission DATE: Monday, March 02, 2009 SUBJECT: Mechanical Integrity Tests BP EXPLORATION (ALASKA) INC V-219 PRUDHOE BAY UN ORIN V-219 Src: Inspector NON-CONFIDENTIAL Reviewed By: P.I. Suprv~(' Comm Well Name• PRUDHOE BAY UN ORIN V-2t9 Insp Num: mitJCr090302075853 Rel Insp Num: API Well Number: 50-029-23397-00-00 Permit Number 208-142-0 Inspector Name: John Crisp Inspection Date: 2/25/2009 Packer Depth Pretest Initial 15 Min. 30 Min. 45 Min. 60 Min. Well ~ V-219 • Type Inj. w TVD 4491 ~ IA 820 4000 3940 3920 ^~' P.T. 2081420 TypeTest SPT Test pSl 1500 QA ~ 300 650 550 ) 540 --- -- P ~ Interval____~TAL p/F Tubing i l loo l loo lloo lloo ~ _ _ _ NOtes' 3 bbl's pumped for test no problems witnessed. _ Monday, March 02, 2009 Page 1 of I 01 /23/09 ~chlumberger Alaska Data & Consulting Services a(`' 2525 Gambell Street, Suite 400 `a U Anchorage, AK 99503-2838 Q/ ATTN: Beth Pr~J G ~~~~~ ~Q W/ all \ O -Inh 1k 1 .... n......-:.s:._ NO.5047 Company: State of Alaska Alaska Oil & Gas Cons Comm Attn: Christine Mahnken 333 West 7th Ave, Suite 100 Anchorage, AK 99501 H-35 11970840 PRODUCTION PROFILE 08/12/08 1 1 -11 12111927 IBP & CROSS-FLOW STP .._ 1 11/24/08 1 1 MPS-41 11966291 SCMT ~ - ~ 11/24/08 1 1 K-05C AWJB-00016 MEM PROD PROFILE U _ ~ ~ 12/29/08 1 1 14-17A AXOY-00010 MEM INJECTION PROFILE 0 -Q(} 01/15/09 1 1 F-33 ALYF-00010 CEMENT IMAGE LOG (p- ~'"~" 12/30/08 1 1 K-i6AL2 AXIA-00009 MEM PROD PROFILE 0 - b 01/10/09 1 1 01-29 AP30-00011 USIT 'tj - j 01/04/09 1 1 09-30 AY1M-00007 STATIC SPINNER &IBP .-~ L{ 01/15/09 1 1 N-18A AZCM-00005 JEWELRY LOG/PRESS/TEMP - ~ 01/06/09 1 1 R-24 AY3J-00004 USIT 01/16/09 1 1 N-18A AWLB-00002 USIT 12/26/08 1 1 V-212 AXBD-00010 MEM INJECTION PROFILE ~ 01/16/09 1 1 V-222 ALYF-00011 INJ PROFILE/WFL .r l~~ 01/08/09 1 1 07-OVA AYOO-00009 USIT L 01/22/09 1 1 N-12 12014053 RST - 09/30/08 1 1 E-32B AXOY-00005 MCNL 11/18/08 1 1 P2-15A 11594511 SCMT (PDC) (REVISION 2) t ]~.~ 06/15/07 1 B-27A 11999059 RST ~ ~ ~~ ~ !.35' + 11/07/08 1 1 12-37 40018138 OHM - D/LWD EDIT _~C ~~- 11/07/08 2 1 N-18A 08AKA0037 OH MWD/LWD EDIT ~O~j -- '~ 12/24/08 2 1 H-38 OSAKA0031 OH MWD/LWD EDIT ~ 12/07/08 2 1 -~G s- c '~--o .~~..~...... .........r ..rv v.• • r • v. V.~•.~V e~•~v ••GI VI•I~II~V VI`IG l.Vf ~ GMVII 1 V. BP Exploration (Alaska) Inc. Petrotechnical Data Center LR2-1 900 E. Benson Blvd. J Anchorage, Alaska 99508 n Date Delivered Alaska Data & Consulting Services 2525 Gambell Street. Suite 400 ~ Anchorage, AK 9J50,~ ~~ '' ;~ is ~ f' ATTN: Beth ra -, Received by: t ~,- t~ ..~ _ t, ._ .. ,. . 9....6 ,.v ~RI~ h7if. ~w~F~'r R:T ~~ F 'tl'p l~~~e~'.!6`.~%~I i~7v.;. nrs ' LJ 01 /08/09 Schlumberg~r Alaska Data & Consulting Services 2525 Gambell Street, Suite 400 Anchorage, AK 99503-2838 ATTN: Beth wpu ~..ti NO. 5029 Company: State of Alaska Alaska Oil & Gas Cons Comm Attn: Christine Mahnken 333 West 7th Ave, Suite 100 Anchorage, AK 99501 K-OSC AWJB-00016 ,. MEM PROD PROFILE ~;c. ._ -~ .y ~ - ~aie 12/29/08 o~ 1 e;oror co 1 2-54/0-12 11968974 SBHP SURVEY ~ ; S_: o~ i~,; - '_ '~ '-%=} C. °'-_% 11/23/08 1 1 V-223 AXBD-0001 MEM INJECTION PROFILE rJ~_, o -. „--. _ ~/~ ~ 12/29/08 1 1 18-24B 12066555 MCNL <`~~<'-, 1` . ~`~ '~ ~ j "7 "~ ~ 10/18/08 1 1 J-18 12103680 RST y' ~ ~~ 'i~`'S '~~~' ` '~ ~~i ' 09/25/08 1 1 1-45/0-26 12086686 .-/ ')~~' ~ -"l. -'( ~~'~ RST ) ;r"-j 09/22/08 1 1 V-219 40018249 OH MWD/LWD EDIT '~~,;- -- %~ ;~ ,°,~ L;~;-~ ~~y 11/17/08 2 1 PLEASE ACKNOWI Fr)[:F RF CPIDT RV CI!]W I~I!_ AAlrl oeTnor.ur.~n_ nw~r n~.nv .-..+.. ~.._ - - ------ ---._...-...~ _.._.-... r..,.... .... BP Exploration (Alaska) Inc. Petrotechnical Data Center LR2-1 ~)"" ~i _` d 900 E. Benson Blvd. „ ', ,_ Anchorage, Alaska 99508 Date Delivered: ~ i ~ ', ~ d(~~~,1 ~ __ - . ,,~: Alaska Data & Consulting Services 2525 Gambell Street, Suite 400 '~i Anchorage, AK 995Q3-2838 ATTN: Beth ~ ' J~~ ~ i / ~' Received by: ~ ^ ~~,__.---`'`~ 12/18/08 d~r~'~~~ir~~i~ N0.5011 Alaska Data & Consulting Services 2525 Gambell Street, Suite 400 Anchorage, AK 99503-2838 ATTN: Beth Wnll 1..1. u 11-34 12071901 USIT ~~ - 10117!08 vvtvl 1 li L/ 1 V-219 12103700 USIT ~ 11/21/08 1 1 D-12 12113022 INJECTION PROFILE 12/05/08 1 1 R-11A 12096929 USIT (; 12/07/08 1 1 01-34 12116292 CORRELATION/GR LOG (p - / ' =,l- ~ a 12/06/08 1 1 F-19 AWJI-00011 MEM LDL ~ _ 12/08/08 1 1 18-296 AWJI-00010 MEM LDL _ I;p ~, b 12/05/08 1 1 09-41 12017504 PRODUCTION PROFILE JOl -(S 12/04!08 1 1 18-14B 12005233 MCNL ~ -- 09/21/08 1 1 18-06B 12083417 MCNL - 10/28/08 1 1 18-14C 12066551 MCNL ~ 10/06/08 1 1 OS-10C 11649990 MCNL 10/04/08 1 1 V-219 12103700 CH EDIT (USIT) 11/21/08 1 L o ~ 'a 3 i DI CACC A!`VG~A~IIn enn_c ~c ncmr nv c.~i.w uu~. w BP Exploration (Alaska) Inc. _ w ^•-_ ..-. v. „_„_... v,•~ vvr ~ ~^v„ ~ v. Petrotechnical Data Center LR2-1 900 E. Benson Blvd. Anchorage, Alaska 99508 Date Delivered: Company: State of Alaska Alaska Oil & Gas Cons Comm Attn: Christine Mahnken 333 West 7th Ave, Suite 100 Anchorage, AK 99501 Alaska Data & Consulting Services 2525 Gambell Street, Suite 400 Anchorage, AK 99503-2 8 ATTN: Beth Received by: Schlumberger Drilling & Measurements MWD/LWD Log Product Delivery Customer BP Exploration (Alaska) Inc Dispatched To: Christine Mahnken (AOGCC) Well No V-219 Installation/Rig Nabors-9ES Date Dispatched: 21-Nov-08 Dispatched By: Paul Wyman Data No Of Prints No of Floppies Surveys 2 1 Please sign and return to: James H. Johnson RecelVed By: - BP Exploration (Alaska) Inc. Petrotechnical Data Center (LR2-1) 900 E. Benson Blvd. Anchorage, Alaska 99508 Fax:907-564-4005 e-mail address: johnsojh@bp.com LWD Log Delivery V2.1, 03-06-06 V-219 Surface Casing ~ ~ Page 1 of 1 Maunder, Thomas E (DOA) From: Maunder, Thomas E (DOA) Sent: Wednesday, October 29, 2008 8:09 AM To: 'Rebol, Amanda' Subject: RE: V-219 Surface Casing ~ ~~" `~~ `~~. Hi Amanda, Change the casing weight is not an issue. Either has the performance properties for an adequate design. I will place a copy of this message in the file. Tom Maunder, PE AOGCC From: Rebol, Amanda [mailto:reboa2@BP.com] Sent: Tuesday, October 28, 2008 4:07 PM To: Maunder, Thomas E (DOA) Subject: V-219 Surface Casing Tom- Due to availability issues, we are planning on running 47# 9-5/8" surface casing instead of the originally planned 40# on the upcoming V-219i. The heavier casing requires that we drill a smaller (8-1/2" instead of 8-3/4") production hole. We have all the required materials available and ready to make this change. The 7" casing and 3-1/2" tubing design will not be affected, and the directional plan is not changing. Please let me know if you have any questions or concerns around this change. Thank you! -Amanda Amanda E Rebol Drilling Engineer, GPB Rotary BP Alaska 907.564.5543 907.632.2095 720.933.0172 10/29!2008 4 _1 ! d~'~ ~ ``\\ S ~ ~J ~1 ~~ ALASS-A OIL AI~TD GrAS CO1~T5ER~ATIOI~T COMl-II551O1~T Robert Tirpack Engineering Team Leader BP Exploration Alaska Inc PO Box 196612 Anchorage AK 99519-6612 SARAH PAL/N, GOVERNOR 333 W. 7th AVENUE, SUITE 100 ANCHORAGE, ALASKA 99501-3539 PHONE (907) 279-1433 FAX (907) 276-7542 Re: Prudhoe Bay Field, Orion/Schrader Bluff Oil Pool, PBU V-219 BP Exploration Alaska Inc Permit No: 208-142 Surface Location: 4726' FSL, 1488' FEL, SEC. 11, T 11 N, R 11 E, UM Bottomhole Location: 4751' FSL, 4567' FEL, SEC. 07, T11N, R12E, UM Dear Mr. Tirpack: Enclosed is the approved application for permit to drill the above referenced service well. This permit to drill does not exempt you from obtaining additional permits or an approval required by law from other governmental agencies and does not authorize conducting drilling operations until all other required permits and approvals have been issued. In addition, the Commission reserves the right to withdraw the permit in the event it was erroneously issued. Operations must be conducted in accordance with AS 31.05 and Title 20, Chapter 25 of the Alaska Administrative Code unless the Commission speci$cally authorizes a variance. Failure to comply with an applicable provision of AS 31.05, Title 20, Chapter 25 of the Alaska Administrative Code, or a Commission order, or the terms and conditions of this permit may result in the revocation or suspension of the permit. `Vhen providing notice for a representative of the Commission to witness any required test, contact the Commission's petroleum field inspector at (907) 659-3607 (pager). Sincerely, Daniel T. Seamount, Jr. '~'~ Chair DATED this C day of October, 2008 cc: Department of Fish & Game, Habitat Section w/o encl. Department of Environmental Conservation w/o encl. ' ql ~/os STATE OF ALASKA ~D~ ALAS~IL AND GAS CONSERVATION COMMI~N PERMIT TO DRILL ~~~ 20 AAC 25.005 ~,:_. ~~~~ ~~~ ~ s Zoos t'~ii ~ I ~~3~ t~C?I1S. ~OCTiZiiiSS101ti 1 a. Type of work ® Drill ^Redrill ^ Re-Entry 1 b. Current Well Class ^ Exploratory ^ Development Gas ®Service ^ Multiple Zone ^ Stratigraphic Test ^ Development Oil ^ Single Zone 1 c. Specify if well is pro : ~' ~C ^ Coalbed Methane ~as~Hdrates ^ Shale Gas 2. Operator Name: BP Exploration (Alaska) Inc. 5. Bond: ®Blanket ^ Single Well Bond No. 6194193 11. Well Name and Number: PBU V-219 3. Address: P.O. Box 196612, Anchorage, Alaska 99519-6612 6. Proposed Depth: MD 9671 TVD 5165 12. Field /Pool(s): Prudhoe Bay Field / Orion 4a. Location of Well (Governmental Section): Surface: ' ' 7. Property Designation: ADL 028240, ADL 047450 Schrader Bluff FEL, SEC. 11, T11 N, R11 E, UM FSL, 1488 4726 Top of Productive Horizon: UM 12 T11 N R11 E 585' FEL SEC 4227' FSL 8. Land Use Permit: 13. Approximate Spud Date: October 25, 2008 , , , . , , Total Depth: 4751' FSL, 4567' FEL, SEC. 07, T11 N, R12E, UM 9. Acres in Property: 2560 14. Distance to Nearest Property: 10650' 4b. Location of Well (State Base Plane Coordinates): Surface: x-590813 y-5969976 Zone-ASP4 10. KB Elevation Planned (Height above GL): feet 15. Distance to Nearest Well Within Pool: 2261' 16. Deviated Wells: Kickoff Depth: 250 feet Maximum Hole An le: 66.7 de rees 17. Maximum Anticipated Pressures in psig (see 20 AAC 25.035) Downhole: 2334 Surface: 1817 1 in Pr r cifi i T in h- m uan ' f m n c.f r cks Hole Casin Wei ht Grade Cou lin Len th MD TVD MD TVD includin sta a data 42" 2" 1. A- W I 8' rf urf 10 ' 1 2 Ar i e A r x. 12-1/4" I " 40# -80 BTC 42 Surf urfa 4264' 2817' sos sx Dee Crete, ss sx Durastone, 73 sx'G' -/" T-I rf 7 1 ' 8-3/4" 7" BT -M T 34 71' 51 e v ` , ~ g, PRESENT WELL CONDITION SUMMARY (To be completed for Redrill and Re-entry Operations) Total Depth MD (ft): Total Depth TVD (ft): Plugs (measured): Effective Depth MD (ft): Effective Depth TVD (ft): Junk (measured): Casing Length Size Cement Volume MD TVD Conductor /Structural Surface Intermediate Liner Perforation Depth MD (ft): Perforation Depth TVD (ft): 20. Attachments ^ Filing Fee, $100 ^ BOP Sketch ^ Property Plat ^ Diverter Sketch ®Drilling Program ^ Time vs Depth Plot ^ Shallow Hazard Analysis ^ Seabed Report ®Drilling Fluid Program ®20 AAC 25.050 Requirements 21. Verbal Approval: Commission Representative: Date: 22. I hereby certify that the foregoing is true and correct. Printed Name Robert Tirpack Si nature ~'~ ~ ~ Contact Amanda Rebo1, 564-55x3 Title Engineering Team Leader. Prepared By Name/Number: ~' Sondra Stewman, 564-4750 Phone 564-4166 Date Commission Use rtl Permit To Drill tuber: o?O~ ~~ API Number: SO- Oo?9~339~0000 Permit Approval t See cover letter for th r r it n Conditions of Approval: If box i\s checked`, well may not be used to explore for, test, or produce coalbed methane, gas hydrates,~or gas contained shales: ,,{ ~~ ~ L~_~'['CVVC~-`~~-~ ~,p S Samples Req'd: Yes ~No Mud Log Req'd: ^'Yes ~(.1 No ~ HZS Measures: Yes ^ No Directional Survey Req'd: ~( Yes ^ No ~o oc~ Psi ~o ~ ~~~ Other: V ~ ~-i ~i~ O ~cCt'G~ ~ O ~S ~ v\ G.CCi~ ~ w ~ ~l ~ a C4 ~ , L ~ (v Date APPROVED BY T COMMM SIONER 5ubm~t In uupucate Form 10-401 Revised 12/2005 : ~ ~ ~ /t Well Name: V-2191 Drill and Complete Plan Summary T e of Well service / roducer / injector : Injector Surface Location: 4725' FSL, 1488' FEL, Sec. 11, T11 N, R11 E, Umiat Slot SY As Built X = 590,813 Y = 5,969,976 Target 1 (Top Nb): 4227' FSL, 555' FEL, Sec. 12, T11 N, R11 E, Umiat X = 597,003 Y = 5,969,555 Z = 4450' TVDss Target 2 (Top OBd): 4553' FSL, 4908' FEL, Sec. 7, T11 N, R12E, Umiat X = 597,584 Y = 5,969,888 Z = 4825' TVDss BHL: 4752' FSL, 4567' FEL, Sec. 7, T11 N, R12E, Umiat X = 597,921 Y = 5,970,091 Z = 5083' TVDss API NUMBER: TBD Ri Nabors 9ES Estimated Start Date: October 25, 2008 MD: 9671' TVD: 5165' O eratin Da s to com lete: 18 RT/GL: 28.5' RTE: 82.0' Well Design: USH Grassroots Schrader Bluff Injector 3'/z" TC-II completion, 4 packers for zonal isolation. Ob'ective: Multi-zonal injector into Schrader Bluff Nb, OBa, OBb and OBd/OBe sands Directional Plan Version: Schlumber er P9 KOP: 250' MD Maximum Hole An le: 66.7° Close A roach Wells: All wells pass Ma~or Risk criteria. Reference anti-collision report. Distance to Nearest Property Line: 10,650' to PBU boundary at top Sb_Na (top of pool) Nearest well within Pool: V-218 is 2261' away from Top Sb_Na (top of pool) V-219i Drilling Permit Application '/a Mile Wellbore Mechanical Integrity Summary -There are no wells within aquarter-mile of this injector at completion depth. Well Name Dist. ft Annulus Inte rit Comments N/A - - Leaaina Prearam Surface Interval Drilling, MWD: GR Open Hole: None Cased Hole: None Production Interval Drilling, MWD: GR/RES/NEU/Azimuthal Density/PWD Open Hole: None Cased Hole: CBVUSIT Primar De th Control mode Mud Program 17 1/~" Ci irfar_p Hnl~+• Frpch Watpr Snud Mud Interval Density Funnel Vis Yield Point_ API FL pH seconds Ib/100ft2 mU30 min Surface to BPRF 8.8 - 9.2 Initial= +400, 55 -70 NC - 8.0 9.0 - 9.5 down to 300 BPRFtoTD 9.2-9.5 225-250 45-60 8.0 9.0-9.5 A 3/~" Drnrl~~rtinn Hnlp• I SNIT Interval Density (ppg) PV (cP) YP (Ib/100ft2) API FL (mU30 min) HTHP FL (mU30 min) pH MBT Cs Shoe to TD 9.0-9.5 12-18 18-24 <6.0 N/C 9-10 <18 ('_acina/T~~hina Prearam Hole Size Csg/ Tb O.D. Wt/Ft Grade Connection Length Top MD/TVD RTE Btm MD/TVD RTE 42" Insulated 20" 91.5 A-53 Weld 80' Surface 109'/ 109' 12'/a" 9 /a" 40 L-80 BTC 4264' Surface 4264'/2817' 8 3/a" 7" 26 L-80 TC-II 5764' Surface 5764' / 3409' 8 3/a" 7" 26 L-80 BTC-M 3907' 5764' / 3409' 9671' / 5165' Tubin 3'/i" 9.2 L-80 TC-II 9441' Surface 9441' / 5037' Comments: Tubing crossover to 4'/z"just below tree. ~ Inte rit Testin Test Point Depth Test Type 9 5/ "Surface Casin 20' - 50' from surface shoe LOT V-2191 Drilling Permit Application 2 Cement Calculations Surface Casin Casing Size 9 /$" Basis: ~ Lead: Based on 4264' 12-'/4" open hole with 250% excess above BPRF (1963') and 30% excess below BPRF. TAM port collar used if necessary. Lead TOC: Surface Tail: Based on 80' shoe track volume and 1000' of 12'/a" open hole with 30% excess. DuraSTONE for last 15 bbl. Tail TOC: 1000' MD above the Casin shoe Total Cement Volume: Lead 336.8 bbl / 1889 ft / 507 sks of DeepCrete at 10.7 ppg and 3.72 ft3/sk Tail 72 bbl / 405 ft / 88 sks of Class `G' at 15.8 ppg and 4.56 ft /sk DuraSTONE: 15 bbl / 84.2 ft3 / 73 sks at 16.3 ppg and 1.16 ft3/sk Production Casin Casin Size 7" Basis: Lead: Based on 2427' of 8-3/4" open hole with 30% excess. TOC: 1000' from surface shoe Tail: Based on 80' shoe track volume and 2502' of 83/a" open hole with 30% excess. TOC at 7169' MD, 500' MD above Ma. ,t ~ Total Cement Volume: Lead 84.6 bbl / 474 ft / sks of LiteCRETE at 11.0 ppg and 3.37 ft3/sk Tail 93.8 bbl / 526 ft / 4 sks of Class `G' at 15.8 ppg and 1.17 ft3/sk. ~-I z~ ~~r ~~~~~ V-2191 Drilling Permit Application 3 Estimated Formation Tops (TVDss) and Pore Pressures Formation Top (TVDss) Uncertainty (ft) Commercial Hydrocarbon- Bearin ? Est. Pore pressure (psi) Est. Pore Pressure EMW G1 -250 +/-50' No 113 8.7 SV6 -900 +/-50' No 405 8.7 SV5 -1565 +/-50' No 704 8.7 SV4 -1700 +/-50' Gas hydrates 765 8.7 Base Permafrost -1720 +/-50' No 774 8.7 Fault 1 (V-Pad Fault -2050 +/- 100' M.D. n/a SV3 (faulted top) -2050 +/-50' Gas hydrates 923 8.7 SV2 -2180 +/-50' Gas hydrates 981 8.7 SV1 -2515 +/-50' Gas hydrates 1132 8.7 Surf Casing Pt -2735 1231 8.7 UG4 -2815 +/-50' Thin Coal 1267 8.7 UG4A -2860 +/-50' Heavy Oil 2860'- 2900' SS 1287 8.7 UG3 -3220 +/-50' Thin Coals 1449 8.7 UG1 -3790 +/-50' No (wet) 1706 8.7 UG Ma -4110 +/- 30' No (wet) 1850 8.7 UG Mb1 -4160 +/- 30' No (wet) 1872 8.7 UG_Mb2 -4230 +/- 30' No (wet) 1904 8.7 Fault #2 (Repeat Section -4272 +/- 150' M.D. UG_Mb2 - 2nd Occurrence -4295 +/- 30' No (wet) 1933 8.7 UG Mc -4370 +/- 30' No (wet) 1967 8.7 SB_Na -4425 +/- 30' No 1991 8.7 SB_Nb -4450 +/- 30' Yes 2003 8.7 SB_Nc -4480 +/- 30' Yes 2016 8.7 SB_Ne -4490 +/- 30' Yes 2021 8.7 SB_OA -4595 +/- 30' No (wet) 2045 8.6 SB_OBa -4660 +/- 30' Yes 2074 8.6 SB_OBb -4705 +/- 30' Yes 2094 8.6 SB_OBc -4770 +/- 30' Yes 2123 8.6 SB_OBd -4825 +/- 30' Yes 2147 8.6 SB_OBe -4890 +/- 30' Yes 2176 8.6 SB_OBf -4935 +/- 30' Yes 2196 8.6 Base _SB_OBf -4985 +/- 30' No 2218 8.6 T.D. in Colville Shale -5078 No 2260 8.6 Comments: SV through UG and SB N-sand interval pressures are assumed based on a .45 ppg hydrostatic gradient, and V-100 MDT data. SB Nb, OBa, OBb, OBd, and OBe pressure ranges are estimated and assumed to be at original conditions due to lack of offtake in the V-219 target area. V-2191 Drilling Permit Application 4 Well Control 12'/a" hole will be drilled with diverter. The 8 3/a" intermediate hole will use well control equipment consisting of 5000 psi working pressure pipe rams (2), blind/shear rams, and annular preventer. Annular preventer will be tested to 2500 psi. Rams will be tested to 4000 psi. The BOP test frequency will be conducted on a 14 day frequency, with a function test every 7 days. Except for significant operational issues that may affect well integrity or pose safety concerns, an extension to the 14 day BOP test period should not be requested. Diverter, BOPE and drilling fluid system schematics are on file with the AOGCC. Production Interval: • Maximum anticipated BHP: • Maximum surface pressure: • Planned BOP test pressure: • Annular Preventer • Rams • Planned completion fluid: 2334 psi Cc3 5165' TVD, 8.7 ppg EMW (at TD in Colville Shale, 9671' MD) 1817 psi C~1 surface (based on BHP and a full column of gas from TD C~1 0.10 psi/ft) 250 / 2500 psi 250 / 4000 psi 9.0 ppg brine / 6.8 ppg diesel Kick Tolerance/Integrity Testing Summary Table Casing and Casing Test Maximum Mud Weight Exp Pore LOT / Interval Pressure Influx Press FIT Volume 95/$" Surface 3500 psi 52.5 bbl" 9.5 8.7 LOT Casin 7" Production 4000 psi NA NA NA NA Casin assuming ppg Disposal • No annular disposal in this well. • Cuttings Handling: Cuttings generated from drilling operations will be hauled to grind inject at DS-04. • Fluid Handling: Haul all drilling and completion fluids and other Class II wastes to DS-04 disposal. Haul all Class I wastes to Pad 3 for disposal. and for Variance Request • To avoid the risk of plugging the flow line with large rocks and wood encountered while drilling ~ surface hole, it is requested to drill without a flow paddle for the first portion of the surface hole. After drilling past the larger rocks and wood sections, the flow paddle will be put back in the flow line. V-2191 Drilling Permit Application 5 DRILL AND COMPLETE PROCEDURE SUMMARY Pre-Rig Work: 1. Weld an FMC landing ring for the FMC Gen 5 wellhead on the conductor. 2. If necessary, level the pad and prepare location for rig move. Rig Operations: 1. MIRU Nabors 9ES. 2. Nipple up and function test diverter. 3. MU 12'/4" drilling assembly with MWD/GR and directionally drill surface hole to TD with one BHA. The surface hole TD will be approximately 560' below the top of the SV1. 4. Run and cement 9 5/$" surface casing. A TAM port collar may be run at 1000' as a contingency. Use Durastone in the last 15 bbls of tail cement. Pressure test casing to 3500 psi for 30 minutes at plug bump. 5. ND diverter and NU casing /tubing head. NU BOPE and test. 6. Make up 8 3/a" drilling BHA with MWD/GR/RES/Azi-Den/NEU/PWD and RIH to float collar. Drill out shoe track and displace well to LSND drilling fluid. Drill 20' - 50' of new formation and perform LOT. 7. Drill ahead to production hole target TD (approx. 9671' MD, 350' below OBe). Circulate one BU, back-ream out of hole until the ghost reamer is inside the surface shoe, then POOH to run casing. 8. Run and cement the 7" production casing. Displace with 8.6 ppg seawater. Pressure test casing to 4000 psi for 30 minutes at plug bump. Confirm 500 psi cement compressive strength prior to freeze protecting. Freeze protect the 7" x 9 5/" annulus. 9. PU DPC guns and RIH w/ --230' of 4.5" Power Jet 4505 5 spf, pert guns with Anadrill LWD GR for gun correlation. 10. Space out pert guns by tagging PBTD and tying into GR. Once correlated correctly, circulate over to 9.0 ppg brine. Confirm cement compressive strength is at least 1000 psi before firing. Perforate Nb, OBa, OBb, OBd, and OBe. POOH LD DP and guns. 11. RU Schlumberger E-line. RIH with gauge ring and junk basket to recover any pert debris. Repeat until clean to at least 50' below the bottom perforation. 12. Run USIT log following Primary Depth Control procedures as USIT log will be primary depth control for future well work. 13. Run the 3-'h", 9.2# completion with a 7" x 3-'/z" straddle packer assembly, I-wire, gauges, and injection mandrels. Torque turn TC-II threaded tubing. Top packer must be within 200' of Nb perfs. 14. Confirm that packers are on depth using E-line. 15. Run in lockdown screws and set the packers. Give AOGCC 24 hours notice, then test the production casing/tubing annulus and tubing to 4000 psi each. Shear the DCR valve and pump both ways to confirm ability to circulate. 16. Install and test TWC. Nipple down the BOPE. Nipple up and test the double master to 5000 psi. 17. Freeze protect the well to 2500' TVD by first pumping corrosion inhibited brine down the IA with rig pumps followed by diesel down IA w/ Hot Oil truck, taking clean brine returns to surface. Allow diesel to u-tube into tubing. 18. Install BPV in tubing hanger. Install a VR plug in the 7"x 3-'/z" annulus valve and secure the well. Ensure that IA/OA are protected with two barriers. 19. RDMO. Post-Rig Work: 1. Install tree with electric SSV actuator. 2. MIRU slickline. Pull the ball and rod / RHC plug. 3. Pull shear valve from top mandrel and replace with a dummy GLV. 4. Pull dummy valves from injection mandrels and replace with injection valves. 5. Pull VR plug. 6. Install wellhouse and flowlines. V-2191 Drilling Permit Application 6 Drilling Critical Issues POST THIS NOTICE IN THE DOGHOUSE Well Control The Schrader in the Polygon 2A fault block is expected to be normal to sub-normally pressured at 8.6-8.7 ppg EMW. Hydrates and Shallow Gas Gas hydrates and/or free gas may be present in the SV5 through SV1 below base Permafrost. Setting casing through the SV1 should keep hydrate exposure from extending past the surface hole. Occasionally hydrates are encountered below the SVi . III. Faults/Lost Circulation/Breathing A. Fault #1: "V-pad Fault". V-219 will penetrate this fault in the SV4 interval. The fault will be penetrated at high angle, and the wellbore trajectory is planned to move quickly away from the fault. Fault #2: Separates Orion Polygon 2 from Polygon 2A. V-219 will pass from the upthrown side of the fault to the downthrown side. A repeat of 30'60' of Ugnu Mb sand is expected. No faults are expected in the reservoir interval. However Fault #5 is beyond the TD of V-219. It's position has been included to remind of the necessity to remain within the target circles in the reservoir. B. Lost circulation is not anticipated while drilling V-219 (several previously-drilled V-pad wells have intersected both faults without experiencing losses). If LC does occur, follow LCM decision tree. C. Breathing is not expected on this well. IV. Kick Tolerance/Integrity Testing A. The 9 5/8" casing will be cemented to surface. B. C. The Kick Tolerance for the surface casing is 52.5 bbl with 9.5 ppg mud, 10.8 ppg LOT, and an 8.7 ppg pore pressure. A LOT of 12.5 ppg or higher is anticipated Integrity Testing Test Point Test De th Test t e EMW 9 5/8° shoe 20-50' from shoe LOT >12.5 ex ected V. Hydrogen Sulfide V Pad is not designated as an H2S site, but Standard Operating Procedures for H2S precautions should be followed at all times. No measurable H2S is being produced from the formation at this time; however, all V Pad gas lift wells will likely have H2S levels in the 10-180 ppm range as a result of using PBU lift gas. Well Name H S Level Date of Readin #1 Closest SHL Well H2S Level V-122 30 m 3/31/2007 #2 Closest SHL Well H2S Level V-117 120 m 9/3/2007 #1 Closest BHL Well H2S Level V-122 30 m 3/31/2007 #2 Closest BHL Well H2S Level V-117 120 m 9/3/2007 VI. Anti-Collision Issues All wells pass Major Risk criteria. The following wells are less than 100' center-to-center from V-219 P9: Well Name Ctr-Ctr Distance (ft) Reference MD (ft) Allowable Deviation (ft) V-100 45.94 327.69 40.26 V-115 14.84 567.78 5.48 V-117 66.19 984.33 48.32 V-122 58.21 421.67 50.68 V-213 29.12 308.61 23.37 Use traveling cylinder to reference and track nearby well trajectories during drilling. CONSULT THE V-PAD DATA SHEET AND THE WELL PLAN FOR ADDITIONAL INFORMATION. V-2191 Drilling Permit Application ~ by Client: Field: Structure 1 Slot: Well: Borehole: UWIIAPI#: Survey Name I Date: Tort 1 AND 1 DDI 1 ERD ratio: Grid Coordinate System: Location LaULong: Location Grid NIE YIX: Grid Convergence Angle: V-219 (P9) Pro September 3, 2008 BP Exploration Alaska Prudhoe Bay Unit - WOA V-Pad I V-219 (SY) rOV~ Plan V-219 (SY) Plan V-219 pp 50029 V-219 (P9) /September 3, 2008 116.658° 17501.41 ft 16.214 / 1.452 NAD27 Alaska State Planes, Zone 04, US Feet N 70.32770172, W 149.26350162 N 5969976.030 ftUS, E 590813.860 ftUS +0.69351583° Schlumberger Vertical SecOon Azimuth: 89.760° ~ Vertical Section Origin: N 0.000 ft, E 0.000 ft ' TVD Reference Datum: Rotary Table TVD Reference Elevation: 82.00 ft relative to MSL Sea Bed 1 Ground Level Elevation: 53.50 ft relative to MSL Magnetic Declination: 22.721 ° Total Field Strength: 57669.456 nT Magnetic Dip: 80.870° Declination Date: October 31, 2008 Magnetic Declination Model: BGGM 2008 North Reference: True North Total Corr Mag North •> True North: +22.721 ° Comments Measured Inclination Azimuth Sub-Sea TVD TVD Vertical NS EW Mag 1 Grev DLS Directional Northing Easting Latitude Longitude Depth Section Tool Face Difficulty ft de de ft ft ft ft ft de de 100 ft Index ftUS ftUS RTE 0. 00 0.00 115. 00 -82. 00 0 .00 0. 00 0. 00 0. 00 --- 0.00 0.00 5969976.03 59Ut313. t36 N 7U.3Z//U7 /z w 749.Z635U16Z 100. 00 0.00 115. 00 18. 00 100 .00 0. 00 0. 00 0. 00 --- 0.00 0.00 5969976. 03 590813. 86 N 70. 32770172 W 149. 26350162 200. 00 0.00 115. 00 118. 00 200 .00 0. 00 0. 00 0. 00 --- 0.00 0.00 5969976 .03 590813. 86 N 70. 32770172 W 149. 26350162 Bld 1.5/100 250. 00 0.00 115. 00 168. 00 250 .00 0. 00 0. 00 0. 00 115. OOM 0.00 0.00 5969976 .03 590813. 86 N 70. 32770172 W 149. 26350162 300. 00 0.75 115. 00 218. 00 300 .00 0. 30 -0. 14 0. 30 115. OOM 1.50 0.00 5969975 .90 590814. 16 N 70. 32770134 W 149. 26349921 G1 332. 01 1.23 115. 00 250. 00 332. 00 0. 80 -0. 37 0. 80 115. OOM 1.50 0.03 5969975. 67 590814. 66 N 70. 32770070 W 149. 26349515 Bld 2/100 350. 00 1.50 115. 00 267. 99 349 .99 1. 18 -0. 55 1. 19 115. OOM 1.50 0.29 5969975 .49 590815. 05 N 70. 32770021 W 149. 26349200 400. 00 2.50 115. 00 317. 96 399 .96 2. 76 -1 .29 2. 77 115. OOM 2.00 0.88 5969974 .77 590816. 64 N 70. 32769819 VV 149. 26347917 500. 00 4.50 115. 00 417. 77 499 .77 8. 29 -3 .87 8. 31 115. OOM 2.00 1.62 5969972 .26 590822. 21 N 70. 32769114 W 149. 26343427 600. 00 6.51 115. 00 517 .30 599 .30 16. 97 -7 .93 17. 00 HS 2.00 2.09 5969968 .31 590830. 96 N 70. 32768006 W 149 .26336375 700. 00 8.51 115. 00 616 .44 698 .44 28. 79 -13 .45 28. 85 HS 2.00 2.43 5969962 .93 590842. 86 N 70. 32766497 W 149 .26326771 800. 00 10.51 115. 00 715 .06 797 .06 43. 74 -20 .43 43. 82 HS 2.00 2.71 5969956 .13 590857. 92 N 70. 32764589 W 149 .26314626 900 .00 12.52 115. 00 813 .04 895 .04 61. 79 -28 .87 61. 92 HS 2.00 2.93 5969947 .91 590876. 11 N 70 .32762284 W 149 .262 5 Bld 3.5/100 989 .00 14.30 115. 00 899 .61 981 .61 80. 46 -37 .59 80. 62 HS 2.00 3.11 5969939 .42 590894. 92 N 70 .32759901 W 149 .262 SV6 989. 40 14.31 115. 00. 900. 00 982. 00 80. 55 -37. 64 80. 71 HS 3.50 3.11 5969939. 38 590895. 01 N 70. 32759890 W 149. 26284 15 1000 .00 14.69 115. 00 910 .26 992 .26 82. 95 -38 .76 83. 11 HS 3.50 3.13 5969938 .29 590897. 43 N 70 .32759584 W 149 .26282765 1100 .00 18.19 115. 00 1006 .16 1088 .16 108. 54 -50 .71 108. 75 HS 3.50 3.34 5969926 .64 590923. 21 N 70 .32756317 W 149 .26261976 1200 .00 21.69 115. 00 1100 .15 1182 .15 139. 37 -65 .12 139. 65 HS 3.50 3.53 5969912 .61 590954. 27 N 70 .32752381 W 149 .26236922 1300 .00 25.19 115: 00 1191 .89 1273 .89 175. 34 -81 .92 175. 69 HS 3.50 3.70 5969896 .25 590990. 51 N 70 .32747790 W 149 .26207699 1400 .00 28.69 115. 00 1281 .03 1363 .03 216. 31 -101 .07 216. 73 HS 3.50 3.85 5969877 .60 591031. 78 N 70 .32742561 W 149 .26174415 1500 .00 32.19 115. 00 1367 .23 1449 .23 262. 12 -122 .47 262. 64 HS 3.50 3.98 5969856 .76 591077 .94 N 70 .32736713 W 149 .26137193 1600 .00 35.69 115. 00 1450 .19 1532 .19 312. 61 -146 .06 313. 22 HS 3.50 4.11 5969833 .79 591128 .80 N 70 .32730268 W 149 .26096174 1700 .00 39.19 115. 00 1529 .58 1611 .58 367 .58 -171 .74 368. 31 HS 3.50 4.23 5969808 .77 591184 .18 N 70 .32723250 W 149 .26051510 SV5 1746. 24 40.80 115. 00 1565. 00 1647. 00 394. 46 -184. 30 395. 24 HS 3.50 4.28 5969796. 54 591211. 26 N 70. 32719819 W 149. 26029672 1800 .00 42.69 115. 00 1605 .11 1687 .11 426 .84 -199 .43 427. 68 HS 3.50 4.33 5969781 .81 591243 .88 N 70 .32715686 W 149 .26003367 1900 .00 46.19 115. 00 1676 .51 1758 .51 490 .16 -229 .01 491. 12 HS 3.50 4.43 5969753 .00 591307 .67 N 70 .32707603 W 149 .25951926 SV4 1934. 31 47.39 115. 00 1700. 00 1782. 00 512. 77 -239. 58 513. 78 HS 3.50 4.46 5969742. 71 591330. 46 N 70. 32704716 W 149. 25933550 WeIlDesign Ver SP 2.1 Bld( doc40x_100) V-219 (SY)\Plan V-219 (SY)\Plan V-219\V-219 (P9) Generated 9/5/2008 8:47 AM Page 1 of 4 End Bld 1934. 33 47 .39 115. 00 1700 .01 1782 .01 512. 78 -239 .59 513.79 --- 3.50 4.46 5969742. 70 591330. 47 N 70. 32704714 W 149. 25933542 Base Perm 1963. 85 47. 39 115. 00 1720. 00 1802. 00 532. 44 -248. 77 533.48 - 0.00 4.48 5969733. 76 591350. 27 N 70. 32702205 W 149. 25917575 Crv 3.5/100 1986. 01 47 .39 115. 00 1735 .00 1817 .00 547. 19 -255 .66 548.26 39.88E 0.00 4.50 5969727. 05 591365. 12 N 70. 32700322 W 149. 25905593 2000. 00 47 .76 114. 58 1744 .44 1826 .44 556. 55 -259 .99 557.64 39.60E 3.50 4.51 5969722. 83 591374. 55 N 70. 32699139 W 149. 25897988 2100. 00 50 .50 111. 69 1809 .88 1891 .88 625. 96 -289 .65 627.18 37.71 L 3.50 4.60 5969694. 02 591444. 44 N 70. 32691035 W 149. 25841606 2200. 00 53 .30 109. 02 1871 .59 1953 .59 699. 61 -316 .98 700.95 36.06E 3.50 4.68 5969667. 59 591518. 53 N 70. 32683568 W 149. 25781789 2300. 00 56 .15 106. 54 1929 .34 2011 .34 777. 24 -341 .86 778.68 34.63E 3.50 4.75 5969643. 65 591596. 55 N 70. 32676766 W 149. 25718760 2400. 00 59 .05 104. 22 1982 .91 2064 .91 858. 55 -364 .22 860.08 33.38E 3.50 4.83 5969622. 28 591678. 21 N 70. 32670656 W 149. 25652755 2500. 00 62 .00 102. 04 2032 .12 2114 .12 943. 24 -383 .97 944.85 32.31 L 3.50 4.90 5969603. 56 591763. 20 N 70. 32665259 W 149. 25584021 Fault 1 Crossing 2538. 82 63. 15 101. 22 2050. 00 2132. 00 976. 96 -390. 91 978.61 HS 3.50 4.92 5969597. 02 591797. 03 N 70. 32663360 W 149. 25556654 SV3 2538. 85 63. 15 101. 22 2050. 01 2132. 01 976. 98 -390. 92 978.63 31.93E 3.50 4.92 5969597. 02 591797. 05 N 70. 32663359 W 149. 25556638 2600. 00 64 .97 99. 97 2076 .76 2158 .76 1030. 99 -401 .03 1032.68 31.39E 3.50 4.96 5969587. 57 591851. 22 N 70. 32660595 W 149. 25512812 End Crv 2658. 99 66 .74 98. 80 2100 .90 2182 .90 1084. 06 -409 .80 1085.78 --- 3.50 5.00 5969579. 43 591904. 42 N 70. 32658195 W 149. 25469750 2700. 00 66 .74 98. 80 2117 .09 2199 .09 1121. 26 -415 .57 1123.01 --- 0.00 5.02 5969574. 12 591941. 72 N 70. 32656619 W 149. 25439564 2800. 00 66 .74 98. 80 2156 .59 2238 .59 1211. 99 -429 .63 1213.80 --- 0.00 5.06 5969561. 16 592032. 66 N 70. 32652774 W 149. 25365951 SV2 2859. 28 66. 74 98. 80 2180. 00 2262. 00 1265. 77 -437. 96 1267.61 --- 0.00 5.08 5969553. 48 592086. 56 N 70. 32650494 W 149. 253 2900. 00 66 .74 98. 80 2196 .08 2278 .08 1302. 72 -443 .69 1304.59 --- 0.00 5.10 5969548 .20 592123. 60 N 70. 32648928 W 149. 2 252 3000. 00 66 .74 98. 80 2235 .58 2317 .58 1393. 44 -457 .75 1395.37 --- 0.00 5.13 5969535. 24 592214. 54 N 70. 32645083 W 149. 252 5 3100. 00 66 .74 98. 80 2275 .08 2357 .08 1484. 17 -471 .81 1486.16 --- 0.00 5.17 5969522 .28 592305. 48 N 70. 32641237 W 149: 25145113 3200. 00 66 .74 98. 80 2314 .57 2396 .57 1574. 90 -485 .87 1576.95 --- 0.00 5.20 5969509 .33 592396. 43 N 70. 32637391 W 149. 25071501 3300. 00 66 .74 98. 80 2354 .07 2436 .07 1665. 63 -499 .93 1667.74 --- 0:00 5.23 5969496 .37 592487. 37 N 70. 32633544 W 149. 24997889 3400. 00 66 .74 98. 80 2393 .57 2475 .57 1756. 35 -513 .99 1758.52 --- 0.00 5.26 5969483 .41 592578. 31 N 70. 32629697 W 149. 24924278 3500. 00 66 .74 98. 80 2433 .07 2515 .07 1847. 08 -528 .05 1849.31 --- 0.00 5.28 5969470 .45 592669. 25 N 70. 32625850 W 149. 24850666 3600. 00 66 .74 98. 80 2472 .56 2554 .56 1937. 81 -542 .11 1940.10 --- 0.00 5.31 5969457 .49 592760. 20 N 70. 32622003 W 149. 24777055 3700. 00 66 .74 98. 80 2512 .06 2594 .06 2028. 54 -556 .17 2030.88 --- 0.00 5.33 5969444 .53 592851. 14 N 70. 32618155 W 149. 24703445 SV1 3707. 45 66. 74 98. 80 2515. 00 2597. 00 2035. 29 -557. 22 2037.65 -- 0.00 5.33 5969443. 56 592857. 91 N 70. 32617869 W 149. 24697962 3800. 00 66 .74 98. 80 2551 .56 2633 .56 2119. 26 -570 .23 2121.67 --- 0.00 5.36 5969431 .57 592942. 08 N 70. 32614307 W 149. 24629834 3900 .00 66 .74 98. 80 2591 .05 2673 .05 2209. 99 -584 .29 2212.46 --- 0.00 5.38 5969418 .61 593033. 02 N 70. 32610459 W 149. 24556224 4000 .00 66 .74 98. 80 2630 .55 2712 .55 2300. 72 -598 .35 2303.25 --- 0.00 5.40 5969405 .65 593123. 97 N 70. 32606610 W 149. 24482614 4100 .00 66 .74 98. 80 2670 .05 2752 .05 2391. 45 -612 .41 2394.03 --- 0.00 5.42 5969392 .69 593214. 91 N 70. 32602762 W 149. 24409004 4200 .00 66 .74 98. 80 2709 .54 2791 .54 2482. 17 -626 .47 2484.82 --- 0.00 5.44 5969379 .73 593305. 85 N 70. 32598912 W 149. 24335395 9-5/8" Csg Pt 4264. 46 66. 74 98. 80 2735. 00 2817. 00 2540. 65 -635. 54 2543.34 -- 0.00 5.45 5969371. 38 593364. 47 N 70. 32596431 W 149. 24287949 4300 .00 66 .74 98. 80 2749 .04 2831 .04 2572. 90 -640 .53 2575.61 --- 0.00 5.46 5969366 .78 593396. 79 N 70. 32595063 W 149. 24261786 4400 .00 66 .74 98. 80 2788 .54 2870 .54 2663. 63 -654 .59 2666.40 --- 0.00 5.48 5969353 .82 593487. 74 N 70. 32591213 W 149. 24188177 UG4 4467. 00 66. 74 98. 80 2815. 00 2897. 00 2724. 42 -664. 01 2727.23 --- 0.00 5.49 5969345. 13 593548. 67 N 70. 32588633 W 149. 24138856 4500 .00 66 .74 98. 80 2828 .03 2910 .03 2754. 36 -668 .65 2757.18 --- 0.00 5.50 5969340 .86 593578. 68 N 70 .32587363 W 149. 24114569 UG4A 4580. 94 66. 74 98. 80 2860. 00 2942. 00 2827. 79 -680. 03 2830.66 -- 0.00 5.51 5969330. 37 593652. 29 N 70. 32584247 W 149. 24054991 4600 .00 66 .74 98. 80 2867 .53 2949 .53 2845. 08 -682 .71 2847.97 --- 0.00 5:51 5969327 .90 593669. 62 N 70 .32583513 W 149. 240 4700 .00 66 .74 98. 80 2907 .03 2989 .03 2935. 81 -696 .77 2938.76 --- 0.00 5.53 5969314 .94 593760. 56 N 70 .32579662 W 149. 239 4800 .00 66 .74 98. 80 2946 .52 3028 .52 3026. 54 -710 .83 3029.54 --- 0.00 5.55 5969301 .98 593851. 50 N 70 .32575811 W 149. 23893745 4900 .00 66 .74 98. 80 2986 .02 3068 .02 3117. 27 -724 .89 3120.33 --- 0.00 5.56 5969289 :02 593942. 45 N 70 .32571960 W 149. 23820137 5000 .00 66 .74 98. 80 3025 .52 3107 .52 3208. 00 -738 .95 3211.12 --- 0.00 5.58 5969276 .06 594033. 39 N 70 .32568108 W 149 .23746530 5100 .00 66 .74 98. 80 3065 .01 3147 .01 3298. 72 -753 .01 3301.91 --- 0.00 5.59 5969263 .10 594124. 33 N 70 .32564256 W 149 .23672923 5200 .00 66 .74 98. 80 3104 .51 3186 .51 3389. 45 -767 .07 3392.69 --- 0.00 5.61 5969250 .14 594215 .27 N 70 .32560404 W 149 .23599317 5300 .00 66 .74 98. 80 3144 .01 3226 .01 3480 .18 -781 .13 3483.48 --- 0.00 5.62 5969237 .18 594306 .22 N 70 .32556552 W 149 .23525711 5400 .00 66 .74 98 .80 3183 .50 3265 .50 3570 .91 -795 .19 3574.27 --- 0.00 5.64 5969224 .23 594397 .16 N 70 .32552699 W 149 .23452105 UG3 5492. 41 66 :74 98. 80 3220. 00 3302. 00 3654. 74 -808. 19 3658:16 -- 0.00 5.65 5969212. 25 594481. 20 N 70. 32549138 W 149. 23384087 5500 .00 66 .74 98 .80 3223 .00 3305 .00 3661 .63 -809 .26 3665.05 --- 0.00 5.65 5969211 .27 594488 .10 N 70 .32548846 W 149 .23378499 5600 .00 66 .74 98 .80 3262 .50 3344 .50 3752 .36 -823 .32 3755.84 --- 0.00 5.66 5969198 .31 594579 .04 N 70 .32544992 W 149 .23304893 5700 .00 66 .74 98 .80 3301 .99 3383 .99 3843 .09 -837 .38 3846.63 --- 0.00 5.68 5969185 .35 594669 .99 N 70 .32541139 W 149 .23231288 5800 .00 66 .74 98 :80 3341 .49 3423 .49 3933 .82 -851 .44 3937.42 --- 0.00 5.69 5969172 .39 594760 .93 N 70 .32537285 W 149 .23157683 5900 .00 66 .74 98 .80 3380 .99 3462 .99 4024 .54 -865 .50 4028.20 --- 0.00 5.70 5969159 .43 594851 .87 N 70 .32533430 W 149 .23084079 WeIlDesign Ver SP 2.1 Bld( doc40x_100) V-219 (SY)\Plan V-219 (SY)\Plan V-219\V-219 (P9) Generated 9/5/2008 8:47 AM Page 2 of 4 6000. 00 66. 74 98 .80 3420. 48 3502. 48 4115 .27 -879. 56 4118. 99 --- 0.00 5.71 5969146. 47 594942 .81 N 70. 32529576 W 149. 23010474 6100. 00 66. 74 98 .80 3459. 98 3541. 98 4206 .00 -893. 62 4209. 78 --- 0.00 5.72 5969133. 51 595033 .76 N 70. 32525721 W 149. 22936870 6200. 00 66. 74 98 .80 3499. 48 3581. 48 4296 .73 -907. 68 4300. 57 --- 0.00 5.73 5969120. 55 595124 .70 N 70. 32521866 W 149. 22863267 6300. 00 66. 74 98 .80 3538. 97 3620. 97 4387 .45 -921. 74 4391. 35 --- 0.00 5.75 5969107. 59 595215 .64 N 70. 32518010 W 149. 22789663 6400. 00 66. 74 98 .80 3578. 47 3660. 47 4478 .18 -935. 80 4482. 14 --- 0.00 5.76 5969094. 63 595306 .58 N 70. 32514154 W 149. 22716060 6500. 00 66. 74 98 .80 3617. 97 3699. 97 4568 .91 -949. 86 4572. 93 --- 0.00 5.77 5969081. 68 595397 .52 N 70. 32510298 W 149. 22642457 6600. 00 66. 74 98 .80 3657. 46 3739. 46 4659 .64 -963. 92 4663. 71 --- 0.00 5.78 5969068. 72 595488 .47 N 70. 32506442 W 149. 22568854 6700. 00 66. 74 98 .80 3696. 96 3778. 96 4750 .36 -977. 98 4754. 50 --- 0.00 5.79 5969055. 76 595579 .41 N 70. 32502585 W 149. 22495252 Crv 4/100 6796. 16 66. 74 98 .80 3734. 94 3816. 94 4837 .60 -991. 50 4841. 80 100 .18E 0.00 5.80 5969043. 30 595666 .86 N 70. 32498877 W 149. 22424479 6800. 00 66. 71 98 .64 3736. 46 3818. 46 4841 .09 -992. 03 4845. 29 100 .12E 4.00 5.80 5969042. 80 595670 .35 N 70. 32498730 W 149. 22421649 6900. 00 66. 07 94 .33 3776. 53 3858. 53 4932 .06 -1002. 39 4936. 30 98 .39E 4.00 5.83 5969033. 55 595761 .47 N 70. 32495885 W 149. 22347864 UG1 6933. 09. 65. 88 92. 90 3790. 00 3872. 00 4962. 21 -1004. 29 4966. 46 97. 81E 4.00 5.84 5969032. 01 595791. 65 N 70. 32495360 W 149. 22323414 7000. 00 65. 54 89 .98 3817. 53 3899. 53 5023 .16 -1005. 82 5027. 42 96 .61 L 4.00 5.86 5969031. 22 595852 .62 N 70. 32494930 W 149. 22273986 7100. 00 65. 15 85 .60 3859. 26 3941. 26 5113 .96 -1002. 33 5118. 21 94 .78E 4.00 5.89 5969035. 81 595943 .35 N 70. 32495868 W 149. 22200376 7200. 00 64. 88 81 .20 3901. 52 3983. 52 5204 .02 -991. 92 5208. 22 92 .92E 4.00 5.92 5969047. 31 596033 .22 N 70. 32498695 W 149. 22127392 7300. 00 64. 74 76 .78 3944. 11 4026. 11 5292 .88 -974. 64 5297. 01 91 .04E 4.00 5.95 5969065. 66 596121 .79 N 70. 32503397 W 149. 22 7400. 00 64. 73 72 .36 3986. 80 4068. 80 5380 .13 -950. 59 5384. 15 89 .15E 4.00 5.98 5969090. 76 596208 .63 N 70. 32509951 W 149. 0 219 7500. 00 64. 86 67 .94 4029. 41 4111. 41 5465 .33 -919. 87 5469. 23 87 .27E 4.00 6.01 5969122. 50 596293 .31 N 70. 32518326 W 149. 219 4 7600. 00 65. 11 63 .53 4071. 71 4153. 71 5548 .07 -882. 64 5551 .81 85 .40E 4.00 6.03 5969160. 72 596375 .43 N 70. 32528480 W 149. 21848742 Drp 0.5/100 7691. 56 65. 46 59 .52 4110. 00 4192. 00 5621 .32 -843. 00 5624. 90 HS 4.00 6.05 5969201. 25 596448 .03 N 70. 32539296 W 149. 21789459 Ma 7691. 58 65. 46 59. 52 4110. 01 4192. 01 5621. 34 -842. 99 5624. 92 178. 82E 0.50 6.05 5969201. 26 596448. 05 N 70. 32539299 W 149. 21789443 7700. 00 65. 42 59 .52 4113. 51 4195. 51 5627 .95 -839. 10 5631 .52 178 .82E 0.50 6.05 5969205. 22 596454 .60 N 70. 32540359 W 149. 21784090 7723. 64 65. 30 59 .52 4123. 37 4205. 37 5646 .52 -828. 20 5650 .04 --- 0.50 6.06 5969216. 34 596472 .98 N 70. 32543332 W 149. 21769069 7725. 21 65. 30 59 .52 4124. 02 4206. 02 5647 .75 -827. 48 5651 .26 179 .59R 0.00 6.06 5969217. 08 596474 .20 N 70. 32543530 W 149. 21768073 7800. 00 64. 93 59 .52 4155. 50 4237. 50 5706 .36 -793. 07 5709 .73 179 .59R 0.50 6.06 5969252. 20 596532 .24 N 70. 32552920 W 149. 21720645 Mb1 7810. 62 64. 87 59. 52 4160. 00 4242. 00 5714. 67 -788. 19 5718. 02 179. 59R 0.50 6.07 5969257. 18 596540. 47 N 70. 32554250 W 149. 21713925 7900. 00 64. 43 59 .52 4198. 27 4280. 27 5784 .45 -747. 22 5787 .63 179 .59R 0.50 6.07 5969298. 98 596609 .58 N 70. 32565429 W 149. 21657454 Mb2 7973. 02 64. 06 59. 53 4230. 00 4312. 00 5841. 27 -713. 87 5844. 31 179. 59R 0.50 6.08 5969333. 01 596665. 84 N 70. 32574528 W 149. 21611479 8000. 00 63. 93 59 .53 4241. 83 4323. 83 5862 .22 -701. 57 5865 .21 179 .59R 0.50 6.08 5969345. 56 596686 .59 N 70. 32577884 W 149. 21594524 Fault 2 Crossing 8068. 22 63. 58 59. 53 4272. 00 4354. 00 5915. 09 -670. 54 5917. 95 179. 58R 0.50 6.09 5969377. 23 596738. 94 N 70. 32586349 W 149. 21551743 8100. 00 63. 43 59 .53 4286. 18 4368 .18 5939 .66 -656. 12 5942 .46 179 .58R 0.50 6.09 5969391. 94 596763 .28 N 70. 32590284 W 149. 21531858 Mb2 8119. 69 63. 33 59. 53 4295. 00 4377. 00 5954. 87 -647. 19 5957. 63 179. 58R 0.50 6.10 5969401. 05. 596778. 34 N 70. 32592719 W 149. 21519552 8200. 00 62 .93 59 .54 4331. 30 4413 .30 6016 .77 -610. 87 6019 .38 179 .58R 0.50 6.10 5969438. 11 596839 .63 N 70. 32602628 W 149. 21469462 MC 8284. 41 62. 50 59. 54 4370. 00 4452. 00 6081. 59 -572. 83 6084. 05 179. 58R 0.50 6.11 5969476. 92 596903. 83 N 70. 32613005 W 149. 21417004 8300. 00 62 .43 59 .54 4377. 20 4459 .20 6093 .53 -565. 83 6095 .96 179 .58R 0.50 6.11 5969484. 07 596915 .65 N 70. 32614916 W 149. 21407340 8400. 00 61 .93 59 .54 4423. 88 4505 .88 6169 .95 -521. 00 6172 .19 179 .58R 0.50 6.12 5969529. 82 596991 .33 N 70. 32627146 W 149. 21345498 Na 8402. 38 61. 91 59. 54 4425. 00 4507. 00 6171. 77 -519. 93 6174. 00 179. 58R 0.50 6.12 5969530. 90 596993. 13 N 70. 32627436 W 149. 21344031 8455. 15 61 .65 59 .55 4449. 95 4531 .95 6211 .95 -496. 36 6214 .08 --- 0.50 6.12 5969554. 95 597032 .92 N 70. 32633866 W 149. 213 V-219 Tgt 1 Nb 8455. 25. 61 .65 59 .55 4450. 00 4532 .00 6212 .03 -496. 32 6214 .16 HS 0.00 6.12 5969555. 00 597033 .00 N 70. 32633879 W 149. 213 Nb 8455. 27 61. 65 59. 55 4450. 01 4532. 01 6212. 04 -496. 31 6214. 18 LS 0.50 6.12 5969555. 01 597033. 01 N 70. 32633881 W 149. 21311438 8500. 00 61 .43 59 .55 4471. 33 4553 .33 6246 .02 -476. 38 6248 .07 LS 0.50 6.13 5969575. 35 597066 .66 N 70: 32639318 W 149. 21283939 Nc 8518. 11 61. 34 .59. 55 4480. 00 4562. 00 6259. 76 -468. 32 6261. 78 LS 0.50 6.13 5969583. 57 597080. 26 N 70. 32641516 W 149. 21272823 Ne 8538. 92 61. 23 59. 55 4490. 00 4572. 00 6275. 53 -459. 07 6277. 51 LS 0.50 6.13 5969593. 01 597095. 88 N 70. 32644040 W 149. 21260059 8600. 00 60 .92 59 .55 4519 .54 4601 .54 6321 .73 -431 .98 6323 .60 LS 0.50 6.14 5969620. 66 597141 .64 N 70. 32651432 W 149. 21222672 8700. 00 60 .42 59 .55 4568 .52 4650 .52 6397 .07 -387 .79 6398 .75 LS 0.50 6.15 5969665. 75 597216 .24 N 70. 32663486 W 149. 21161700 OA 8753. 44 60. 16 59. 55 4595. 00 4677. 00 6437. 18 -364. 26 6438. 76 LS 0.50 6.15 5969689. 75 597255. 96 N 70. 32669903 W 149. 21129243 8800 .00 59 .92 59 .55 4618 .25 4700 .25 6472 .04 -343 .82 6473 .54 LS 0.50 6.15 5969710. 62 597290 .48 N 70. 32675481 W 149. 21101030 OBa 8882. 78 59. 51 59. 55 4660. 00 4742. 00 6533. 81 -307. 59 6535. 16 LS 0.50 6.16 5969747. 59 597351. 66 N 70. 32685364 W 149. 21051038 8900 .00 59 .42 59 .55 4668 .75 4750 .75 6546 .63 -300 .07 6547 .94 LS 0.50 6.16 5969755. 26 597364 .35 N 70. 32687415 W 149. 21040665 OBb 8970. 89 59. 07 59. 55 4705. 00 4787. 00 6599. 27 -269. 19 6600. 46 LS 0.50 6.17 5969786. 76 597416. 48 N 70. 32695837 W 149. 20998061 9000 .00 58 .92 59 .55 4720 .00 4802 .00 6620 .84 -256 .55 6621 .97 LS 0.50 6.17 5969799. 67 597437 .83 N 70. 32699287 W 149. 20980611 OBc 9096. 19 58. 44 59. 55 4770. 00 4852. 00 6691. 85 -214. 90 6692. 81 LS 0.50 6.18 5969842. 17 597508. 16 N 70. 32710648 W 149. 20923139 WeIlDesign Ver SP 2.1 Bld( doc40x_100) V-219 (SY)\Plan V-219 (SY)\Plan V-219\V-219 (P9) Generated 9/5/2008 8:47 AM Page 3 of 4 9100. 00 58 .42 59 .55 4771. 99 4853 .99 6694 .65 -213. 26 6695 .60 LS 0.50 6.18 5969843. 84 597510 .93 N 70. 32711096 W 149. 20920872 9200. 00 57 .92 59 .55 4824. 73 4906 .73 6768 .07 -170. 20 6768 .84 LS 0.50 6.18 5969887. 78 597583 .64 N 70. 32722842 W 149. 20861452 V-219 Tgt 2 OBd 9200. 50 57 .92 59 .55 4825. 00 4907 .00 6768 .44 -169. 98 6769 .21 LS 0.50 6.18 5969888. 00 597584 .00 N 70. 32722901 W 149. 20861154 Oed 9200. 52 57. 92 59. 55 4825. 01 4907. 01 6768. 45 -169. 97 6769. 22 LS 0.50 6.18 5969888. 01 597584. 02 N 70. 32722903 W 149. 20861143 9300. 00 57 .42 59 .55 4878. 21 4960 .21 6841 .09 -127. 37 6841 .68 LS 0.50 6.19 5969931. 48 597655 .95 N 70. 32734523 W 149. 20802355 9321. 85 57 .31 59 .55 4890. 00 4972 .00 6856 .99. -118. 04 6857 .55 LS 0.50 6.19 5969941. 00 597671 .70 N 70. 32737067 W 149. 20789484 OBe 9321. 87 57. 31 59. 55 4890. 01 4972. 01 6857. 01 -118. 04 6857. 56 LS 0.50 6.19 5969941. 01 597671. 71 N 70. 32737069 W 149. 20789474 9400. 00 56 .92 59 .55 4932. 43 5014 .43 6913 .70 -84. 78 6914 .12 LS 0.50 6.20 5969974. 94 597727 .86 N 70. 32746139 W 149. 20743587 OBf 9404. 70 56. 90 59. 55 4935. 00 5017. 00 6917. 11 -82. 79 6917. 52 LS 0,50 6.20 5969976. 98 597731. 23 N 70. 32746684 W 149. 20740830 OBf Base 9495. 70 56. 44 59. 55 4985. 00 5067. 00 6982. 81 -44. 26 6983. 05 LS 0.50 6.20 5970016. 30 597796. 29 N 70. 32757194 W 149. 20687658 9500. 00 56 .42 59 .55 4987. 38 5069 .38 6985 .90 -42. 44 6986 .14 LS 0.50 6.20 5970018. 15 597799 .36 N 70. 32757689 W 149. 20685151 9600. 00 55 .92 59 .55 5043. 05 5125 .05 7057 .69 -0. 34 7057 .75 LS 0.50 6.21 5970061. 11 597870 .45 N 70. 32769173 W 149. 20627052 Colville 9662. 11 55. 61 59. 55 5078. 00 5160. 00 7102. 06 25. 69 7102. 02 LS 0.50 6.21 5970087. 67 597914. 39 N 70. 32776271 W 149. 20591136 9670. 96 55. 56 59. 55 5083. 00 5165. 00 7108. 37 29. 39 7108. 31 LS 0.50 6.21 5970091. 44 597920. 64 N 70. 32777280 W 149. 20586031 TD / 7" Csg 9671. 85 55 .56 59 .55 5083. 50 5165 .50 7109 .01 29. 76 7108 .95 --- 0.50 6.21 5970091. 82 597921 .27 N 70. 32777382 W 149. 20585517 Survey Tvae: Definitive Proposal WeIlDesign Ver SP 2.1 Bld( doc40x_100) V-219 (SY)\Plan V-219 (SY)\Plan V-219\V-219 (P9) Generated 9/5/2008 8:47 AM Page 4 of 4 by Schlumberger WELL FIELD STRUCTURE V-219 (P9) Prudhoe Bay Unit - WOA V-Pad Magnetic Parameters Surtaca Location NAD2] Alaska State Planes. 20~ 04. US Feet Mluellaneous Motlet. BGGM 2008 Oip: 808]0° Dale: October 31. 2008 Lal: N]01939 ]2fi N°rtlurg: 59699]603 ftU5 Gntl COnv: •0.69351583" Slol: V-21915Y) TVD ReI: Rdary Tade i8T.00M1above MSLI May Dec. •22.]21° FS'. 5)689.5 nT Lan: W149 15 48 606 Easling: 590813.B611U5 Srale Fah'. 0.999909388fi Plao. V2191P9) Brvy Date: SeD~em6er 03, 2008 0 1000 2000 3000 4000 5000 6000 7000 0 1000 2000 O O O C 0) O7 ~ 3000 4000 5000 ............... RTE............... ............................. .............................. ............................. ............................. ............................. ............................. ...................... Bld 1.51100 _.. _.._.._. .._. .._.._.._..-..-..-..- .i. _.._.._..-..-..-..-.. .-..-..-..-..-..-..-.. .i-..-..-..-..-..-..-.._.. ..-..-..-..-.._.._.. _. ..-..-..-.._..-..-..-..s. -..-..-.. _.._..-. Bld 21100 _ - - - - - - Bld 3.51100 T...T...T...T.. V'~.':.T:..T.. n...T...T...T. !JAlnT.f.T:1.Tll.T..Alt.T:l.~'fJANAxtTxAft.TN.T1l.TXAllITNAxr YAN.T!lAltA!!A:/A:I.TNAr.•AIIAfIAJlA!lAltANA.C All.TIJAltAItANANAxANASlAIlAlfAllAffAJtAIfANA:l.7::n::.T:: n:..T...~. End 814 stt ^ttttt •tt• jt^ tt ^ t: s:: ~:. :: a:: s:: rt:: s:: s:::::::: a:: a:: ~:: s:: is s st ttt tt nstt •tt^ t tatt^ 11)111 ^t t^ ttstt ^tt~t tsttt 1 tt tlsttat ttt tt tts tt ^t t^ 1 t^ tt• P stt •t 1111• ttt tt~t 1 tt tttt~jt• ttst 1 tttt ttatt tt ttf t^ n;tett tsitt tt •t t s:. e Perm Fault 1 Crossing .............. f......................... 5..................................i..................................y..................................j..................................j..................................i.......................... ....EriA Civ ................... .. 9-518" Cog Pt .-..-..-. -3.-..-..-..-..-..-..-.. _.. i. ..-..-..-..-..-..-..- .. -.. _.. .-.. .-..-..-..-..-..-..-.. .i-.-..-..-..-..-..-..-.. ..-..-..-..-..-..-.. -. -5. ..-..-..-..-.. -..-..-.. i. _.._.._. _.. _.. _. Crv 41100 .,_.._.._.._3._..-..-..-..-..-..-..-..i..-..-..-..-..-..-..-..-..i..-..-..-..-..-..-..-..-..L.._..-..-..-..-..-..-..-.i-.. _.._..-..-..-.._.._.. _.. _.._.._..-. _ _ - - -.. _..-..-..-.. _.._. _.._.. _.. _.. _.. _. Drp 0.51100 .... - - - - - - - - - - - - - - - - - - - - - - ~ - -..-..- ~._..~..~..~..~.. ~..~..- -.~..-.. ~..~..~..~.._.. .. _.. _.. _.. _.. - _ _1Fault2 Crossings _ _ - _.. _.._.._.. _.._. 19 (P9) 0 1000 2000 3000 4000 5000 0 1000 2000 3000 4000 5000 6000 7000 Vertical Section (ft) Azim = 89.76°, Scale = 1(in):1000(ft) Origin = 0 N!-S, 0 E!-V by Schlumberger WELL V-219 (P9) FIELD Prudhoe Bay Unit - WOA STRULTDRE V-Pad Magcelic Parameters Surface Lwavon NAD1)Naska Slate PNnes. Zone O4, U5 feet MiscelWneoua Motlel: BGGM 2008 DiD. 808]0' Dale: October 3l, ]008 Lal: N]0 t9 ]9 ]1fi NorlBing 59fi99]fi 03 ttUS Grid GOnV'. •0 fi9351583° Slol: V1191SY) NU Rer. RoUry Table (81.OOM1above MSLI May Deo. •12]11' F5: 5]fifi9.8 nT Lon: Wt49 1548 H1fi Eas4ny. 590813.Bfi ttUS Scale Fac1:0999909368fi Plan: V1191P9) Srvy Dale: September 03. 11HI8 0 1000 2000 3000 4000 5000 6000 7000 2000 1000 n n Z 0 0 0 O C 0) N U Cn ~ -1000 V V V -2000 -219 FIl 2 448055 N Bld 1.SN 00 - - V-219;P9) Bld 21100 TD / 7" Cs Bie ssno° 19 Flt t 2tooss -2197 t20Bd ' .. ... .....rC ....... .. RTE ' V-219 Tgt 1:Nb End Bld 9-5/9" Csg P! Crv 3.51100 Fault 1 Crossing Drp 0.51100 End Crv: ~ CnFM100 ...............)..................................:.......................... ......:....................................................................3.......................... ~ .: ............. ; ; ~~~~Kaull 3~Crossing ;~~ 0 1000 2000 3000 4000 5000 6000 7000 «< W Scale = 1(in):1000(ft) E »> 2000 1000 0 -1000 -2000 Field: Prudhoe Bay Site: PB V Pad Well: Plan V-219 (S-Y) Wellpath: Plan V-219 „~ ,E.,,~•,~ ~.,„ i Flan -219 (S-Y /Plan V-21 -- i~ L ~ ', ~ I i ~I __ - II I~~ li CRID ~ 1 `J ~~~ D~ PLAN~Z - V-220i ^ v-zm ^ v-1zo ^ V-03 ^ V-2181 ^ v-,,, ^ V-2161 ^ V-103 ^ v-212 ^ v-1os ^ v-oa ^ v-lasi ^ V-221i ^ V-07 ^ V-2221 ^ V-102 ^ v-za1 ^ V-107 ^ v-oz ^ v-loci ^ v-zloi ^ V-202 ^ V-2141 ^ V-101 ^ V-211 i ^ V-108 ^ V-203 ^ V-2241 v-21si v-11s ^ V-2131 ^ V-100 ^ V-122 ^ v-117 ^ v-1z1 ^ V-2171 ^ v-2os ^ v-o1 ^ V-2231 ^ V-SPARE (sLOr S-L) ^ SLOT S-J ^ V-215i ^ v-zoa ^ V-114 ^ V-119 ^ V-109 ^ V-113 ^ V-OS ^ v-112 II r , ,, y ~,~ ~ k L-PAD ~~ . ~ ~ wpepsqq~~~ ' i ; o ~ KSTAT~Ue. ~ ~ , ~_ ~ 36 r i v p ~ <,~ ~ ° ~ ~~ er=-S~ _ ., i L~ 5~ ~ ---;~'~ - .. F+~ ~ ~ V-PAD ~~~ ~~~ x_10°Sa..:°~°~,~`.#t d~.: - j' a° .~ 'a o; ~~'~ VICINITY MAP N.T.S. TO SPINE ROAD I _~- P p0 ~ / OP ~, j0 W V-PAD ~(~ ° A ~ q~ ~P° 0 ° °o°°°°°°o°°o°°o°oa°oo°°o°°°°°°o °o°°oo°°o°°a°°ooo°°oo°°°°oo°°°° °°° Richard F. Allison ~°~ ' ~s 10608 ~~ o ~~ ° ~`ESSIONA~ 10 0 F, {<~ ~ . I~z ~_ ~P SURVEYOR'S CERTIFICATE I HEREBY CERTIFY THAT I AM PROPERLY REGISTERED AND LICENSED TO PRACTICE LAND SURVEYING IN THE STATE OF ALASKA AND THAT THIS AS-BUILT REPRESENTS A SURVEY MADE BY ME OR UNDER MY DIRECT SUPERVISION AND THAT ALL DIMENSIONS AND OTHER DETAILS ARE CORRECT AS OF JUNE 3, 2008. NOTES 1. ALASKA STATE PLANE COORDINATES ARE ZONE 4, NAD 27. GEODETIC POSI110NS ARE NAD-27. 2. BASIS OF HORIZONTAL CONTROL IS V-PAD OPERATOR MONUMENTATION. LEGEND 3. BASIS OF ELEVATION IS V-PAD OPERATOR MONUMENTATION. AS-BUILT CONDUCTOR ELEVATIONS ARE BP MEAN SEA LEVEL DATUM. 4. THE MEAN SCALE FACTOR FOR V-PAD IS 0.999909334. ^ EXISTING CONDUCTOR 5. REFERENCE FIELD BOOK: W008-01 PGS. 53-57. 6. DATE OF SURVEY: JUNE 3, 2008. LOCATED WITHIN PROTRACTED SEC. 11, T. 11 N., R. 11 E., UMIAT MERIDIAN, ALASKA WELL A.S.P. PLANT GEODETIC GEODETIC CELLAR BOX SECTION N0. COORDINATES COORDINATES POSITION(DMS) POSITION(D.DD) ELEV. OFFSETS Y=5,969,976.03 N 9,999.91 70'19'39.726" 70.3277025° 53 5' 4,726'FSL V-219i X= 590,813.86 E 5029.87 149'15'48.606" 149.2635017' . 1,488' FEL Y= 5,969,980.10 N 10,000.04 70'19'39.764" 70.3277122° 53 3' 4,730' FSL V-224i X= 590,828.54 E 5,045.11 149°15'48.176" 149.2633822' . 1,474'FEL C. ISODei'1, ~"~~~~~~~ BARNHART CHECKED. ~„ (~ ~FURRER N O ~,~ DATE: II IUJ1 6/5/08 DRAWING' y~ FRaoa wov oa-oo GREATER PRUDHOE BAY V-PAD SHEET: ~°a ~~~OO ~0 0B Na, AS-BUILT CONDUCTOR SCALE: 1 of 1 0 6 5 08 ISSUED FOR INFORMATON 7FB MSF WELLS V-2191 & V-2241 NO. DATE REVISION BY CHK 1°=150 Oilfield Services, Alaska Schlumberger Drilling & Measurements 2525 Gambell, Suite 400 Anchorage, AK 99503 Tel (907) 273-1766 Fax (907) 561-8367 Wednesday, September 03, 2008 Amanda Rebol BP Exploration (Alaska) Inc. Schlumberg~ Prudhoe Bay V-219 (P9) Nabors 9ES Close Approach Analysis We have examined the potential intersections of subject well with all other potentially conflicting wells, according to the BPA Directional Survey handbook (BPA-D-004) dated 09/99. Method of analysis: 1. A list of wells to be analyzed is created in Compass by performing a global scan with an initial search radius of two hundred feet with an increment of one hundred feet for every one thousand feet of measured depth in the subject well. 2. Wells are analyzed using the Compass Anti-collision module (BP Company setup) with major risk safety factors applied. For problem wells that are plugged and abandoned or that can be shut in, risk-based safety factor may be used, with client notification. 3. All depths are relative to the planned well profile. Survey Program: Instrument Type Start Depth End Depth GYD GC SS 28.50' and 700.00' and MWD 700.00' and 2100.00' and MWD + IFR + MS 700.00' and 9671.85' and Close Approach Analysis results: Under method (2), note. All drilled wells pass major risk. All data documenting these procedures is available for inspection at the Drilling & Measurements Directional Planning Center. Close Approach Drilling Aids to be provided: A drilling map and traveling cylinder will be provided. ~~ c a -. ;~ w:, Checked by: Scott DeLapp 09/03/2008 -~ - _ _-BIs as a - Company: BP Amoco Date: 9{3/2008 Time: 13:56:10 Page: 1 Field: Prudhoe Bay PB V P d di t C 1~[l: R f re nce: WeIC Plap True North V-219 (S-Y) - ---- , Reference Site: a n-or na e ,) ( e e , Reference Well: Plan V-219 (S-Y) Vertical (1'VD) Referen ce: V-219 Pla n SY 82.0 Reference Wellpath: Plan V-219 Db: Oracle GLOBALSCAN AP - - - PLIED: All wellpaths within 200'+ 100/1000 of reference -There are [l!QI[i~Hseells in thisRHtldipal Plan & PLANNED PROGRAM Interpolation Method: MD Interval: 5.00 ft Error Model: ISCWSA Ellipse _-_ ep sage: - ~ 967Y:85-~ - - -_ _ . can Method: Trav Cylinder Nor th _"_ Maximum Radius: 1164.34 ft Error Surtace: Ellipse + Casing ~ -- Survey Program for DeSnifive Wellpath Date: 10/10/2007 Validated: No Version: 4 -- . .Punned-lirou~-To- _ _ ~urv~3~_ _ -_ _- T-~-~--a,...aa - Tool N~~ ft ft __ 28.50 __ ___700.00 Planned;_Plan --- #9 V-219 V1____ - GYD-GC-SS _ _ Gyrodata g~tro single shots -r -__.__- 700.00 2100.00 Planned: Plan #9 V-219 V1 MWD MWD -Standard ' ' 2100.00 4200.00 Planned: Plan ' #9 V-219 V1 MWD+IFR " +MS "" MWD + WB + IFR + Mul 4FR +{~ ti Station ti St ti ~ --~- - - 9671~ ' L ^^^ned: Blatt 5~ -#9-1F-248 Vi o WD+IFR + - _ ~A - a or - ~ -- _ - -- - --- _ - _ - Casing Points - --_ MD 1'VD Diameter Hole Size Name ft ft in in - , 4264.46 2817.00 9.625 - 12.250 9 5/8" .. ! 9671.85 5165.50 7.000 8.750 7" , Summary - - - _ _ - _ <_-_-_-~__.._.._,___ - ~'f~t Wellpath --- -- - - -~---a--> - -Reference Offset - Gtr-Ctr No-Co Allowable - ---- Site Wcll Wellpath t1~ID MD Distance Area Deviation Warning ft _ ft ft ft ft _ -- _ PB V Pad _ Plan V-123 (NP) Plan V-123 V3 Plan: PI -, - - 311.01 315.00 225.41 5.90 219.51 _ Pass: Major Risk PB V Pad Plan V-206 (S-K) Plan V-206 V3 Plan: PI 330.42 335.00 250.58 6.53 244.05 Pass: Major Risk PB ~Pa~ -Plan V X24-FS-~~ -Plarr~24-V16~4art:-P _._..408.-59 X05.00 'I~~7_- ~6~ - 8a~ Pass:-I~tajerRisk-- - PB V Pad Plan V-226 (S-L) Plan V-226 V3 Plan: PI 340.20 345.00 235.70 6.56 229.14 Pass: Major Risk PB V Pad Plan V-227 (N-Y) Plan V-227 V3 Plan: PI 356.23 360.00 181.16 6.74 174.41 Pass: Major Risk PB V Pad Plan V-228 (S-S) Plan V-228 V2 Plan: PI 352.60 355.00 90.75 6.67 84.08 Pass: Major Risk PB V Pad V-01 V-01 V15 336.60 340.00 165.51 6.10 159.41 Pass: Major Risk -__ _~ PB V Pad --__ V-03 _ -V03 V7 - _- ___ -_ 324.34 245.00 182.72 5.29._._._ 177.42 __ Pass: Major Risk i PB V Pad V-04 V-04 V7 297.71 300.00 235.65 5.58 230.07 Pass: Major Risk ~ PB V Pad V-100 V-100 V7 327.69 330.00 45.94 5.68 40.26 Pass: Major Risk , __ ad--~ : 1 ^3 - ~"v3-V6 _ '?3:36- "~.^^ ~8~74-- 4~'~ ~97-93 Pass: Wtajer Risk- _ -~ PB V Pad V-105 V-105 V13 394.59 405.00 244.45 6.77 237.68 Pass: Major Risk PB V Pad V-106 V-106 V10 325.15 330.00 214.53 5.44 209.09 Pass: Major Risk - ' ~B V Pam ~Tfi06__ -V=fi06A~7~ fi43'I9 150~0~ 2TT.Dfi 3~fi7 _~13:8~ _ asps: Ma)`o~ Risk ___- PB V Pad V-106 V-106AP61 V7 149.19 150.00 217.01 3.17 213.84 Pass: Major Risk PB V Pad V-106 V-106AP62 V2 149.19 150.00 217.01 3.17 213.84 Pass: Major Risk PB V Pad V-106 V-106APB3 V2 149.19 150.00 217.01 3.17 213.84 Pass: Major Risk PB V Pad V-111 V-111 V25 374.67 380.00 189.21 7.09 182.12 Pass: Major Risk - -~';-RBA-Bad - ~F-1-'L7- -- ~F-1-'~1PB1-V9 - 38&88 - 395.OE}- --4893- - X68- 180:83~ assc llAajer Ris#- PB VPad V-111 V-111 P62 V2 388.88 395.00 189.51 8.68 180.83 Pass: Major Risk PB V Pad V-111 V-111 P63 V6 374.67 380.00 189.21 7.09 182.12 Pass: Major Risk -_ - ~B-V Pad_ _ - -1 CT-fi45--._. -_~1=1 i 5V5-_ -- 56T.78 - 570:Off_ _T4.S~ 9~6 -5.fi8 amass: a)or isk_ _ _ 1 PB V Pad V-115 V-115L1 V1 567.78 570.00 14.84 9.35 5.48 Pass: Major Risk I PB V Pad V-1 15 V-115L2 V2 --_ _- --567.78 - 570.00 14.84 9.35_ _ 5.48.. Pass: Major Risk _- _ _ __ _ PB V Pad . _ V-115 _ V-115L2PB1 V3 567.78 570.00 14.84 9.66 5.18 ~ Pass: Major Risk PB V Pad V-115 V-115PB1 V4 567.78 570.00 14.84 9.66 5.18 Pass: Major Risk - PB~Pad-- - -V 117 -V-11 ~V9 --- _ -_ ~-Q".33-- _ 4000.90-- 66:19 -47.86 ~$.3~ Rass: MajoFRisl~ _.-- ~ - - PB V Pad V-117 V-117P61 V6 984.33 1000.00 66.19 17.86 48.32 Pass: Major Risk PB V Pad V-117 V-117P62 V6 984.33 1000.00 66.19 17.86 48.32 Pass: Major Risk PB V Pad V-120 V-120 V6 259.57 260.00 182.44 5.53 176.90 Pass: Major Risk ', PB V Pad V-121 V-121 V5 321.74 325.00 106.95 6.89 100.06 Pass: Major Risk PB V Pad V-122 V-122 V10 -___- 421.67_.. _ 425.00__ 58.21 __ ._7.53 - __50.68 Pass: Maior Risk _. ___ _ _ PB V Pad V-122 V-122PB1 V10 421.67 425.00 58.21 7.53 50.68 Pass: Major Risk PB V Pad V-122 V-122PB2 V7 421.67 425.00 58.21 7.53 50.68 Pass: Major Risk __ PB~F Pad- - - _ V-295 ~--245/44- _ -- ~~736 _- 32&00_ _~3~59 _ X88 12~7'~ -Pass-Major Risl~ -- - - PB V Pad V-205 V-205L1 V9 317.26 320.00 135.59 5.88 129.71 Pass: Major Risk PB V Pad V-205 V-205L2 V8 317.26 320.00 135.59 5.88 129.71 Pass: Major Risk - _ ~ ~6 V Pad -- --1T-207-dril it n`g - _- - awl n V=207L4 N6 V4~~O:DS 58000 T8fifi5 _ _-9:95-- _471:ZO- a Major iR`s cam- ', PB V Pad V-207 drilling V-207 V5 570.05 580.00 181.15 9.80 171.35 Pass: Major Risk i PB V Pad V-207 drilling V-207L1 V2 570.05 580_00 181.15 9.84 171.31 Pass. M?~or Risk_ _ - - __- _ PB VPad V-207 drilling V-207L2 V3 __. 570.05 580.00 181.15 9.84 171.31 Pass: Major Risk j -. - -- - -- _ - BP A~ ~a - -- - - _ --- - - - _, storr_ Cnmpan~: Field Reference Site: BP Amoco Prudhoe Bay PB V Pad Date: 9/3/2008 "Cime: 13:56:10 Pale: 2 Cu-ordinate(P[F) Reference: Well: Plan V-219 (S-Y), True North - ---- Reference Well: Plan V-219 (S-Y) '~ Reference Wellpath: Plan V-219 Vertical ('CVD) Reference: V-219 Plan SY 82.0 Db: Oracle Summary < ---- - Ofl'set Wellpath -- ----> Reierence .Offset Ctr-Ctr _ Nu-Co Allowable __ __ Site PB V Pad PB V Pad ~B~P--acL - Well - V-207 drilling V-207 drilling ~.2-12- __--- Wellpath V-207L3 V2 V-207P61 V5 ~~_~12-V7-_ _ _ MD ft 570.05 570.05 299,46- MD ft 580.00 580.00 300A0.-. Distance Area ft ft -- - 181.15 9.80 181.15 9.84 -2-09.n~ 5.2F _. Deviation ft 171.35 171.31 __.203,R? Warning Pass: Major Risk Pass: Major Risk Pass:-Major Rick PB V Pad PB V Pad V-213 V-213 V-213 V5 V-213P61 V5 308.61 308.61 310.00 310.00 29.12 29.12 5.75 5.75 23.37 23.37 Pass: Major Risk Pass: Major Risk Pad - - PB VPad PB V Pad V=2t~ V-217 V-218 - V=2t6~i8- - V-217 V5 V-218 V7 -- 25:36- 307.62 302.94 250.OfY 310.00 305.00 ~Y96:42 120.85 185.34 - 4:G7 6.65 6.14 19'r7~_ 114.20 179.20 ~ass`Major Ristr Pass: Major Risk Pass Major Risk - _ _ PB V Pad PB V Pad V-220 V-223 _ V-220 V10 V-223 V8 225.89 370.95 225.00 375.00 184.38 180.84 4.94 8.07 179.44 172.77 Pass: Major Risk i Pass: Major Risk FieldPrudhoe Bay SitePB V Pad We11:Plan V-219 (S-Y) WellpathPlan V-219 From Surface to TD Scan interval 100 ft - -- Scale 1:100 313 Plan V-2$V.B~t~~~(~~tV B)2) 2P11)an V-224 (S-Z) (Plan V-224) 3 0 0 V_ 31~6~~d ~~ ~ N b ), V• 2 1 6 ~2 '1 i 3 ~' ~ g' S 1 5 0 VV - 1 3 - -I ,1 1, 08 8 ~ ~t7 ,1 4 7 1 5 P I anV~~-~1bi61( '~1~" ~~p,Pd 1 - ;2 ~~1:Z., 6 20o v~~~ ~ h ` 6a 6' ~1 3111 5 2ooj'1 a V - 0 4 8 - 0 4~1 T g~~ 5 g.b6 ~ ~ ~ /r V-2233 6226 °S26 ~ '~.~ .3~1 2 l 6 r~ O V- 1 0 5 (gY5- 5. 5q~ ~.. g~ I! 1 2 V- 1 0 2 (v- ~~ 1'118 1 2 1 v-2o1 ~~~o~ >.- ~ ~ '11 1aoloo ~w¢1oo> ~ .f'~o 11a ~w~ ~~P~ r' ~ 1 . ~~ ~ ~~~~1 3 ~~ ~ ~ 1 ~ ' 9 -'~~1 2 9 5 8 ~ ~,1 2 g - g 5.4 ~ 7 1 3' 6 V- 2 1 7 V1-~ 1 7) 1 1~0 7, 5112'F 1.5 6... .1 'V V ~H B 52 _ ~, 8 _, ~ . 9 0 V 3«t~(4 ~ X15) _ ~ .65 7 5 1 4 658 1 8 8~ S~~y~ 8 . 9 1 0 46 3'~"tgp '1 0 11 i1 2 1 '13 14 i1O 100 8 g,/ ~q3 ~ 16500 Ilan V IM ~S.A) (Plan V-'~N,~ ~1 O / s / y~ , s ~,~~ ~ ~ 21 Ian VV~~~2 ~,=bJ~1,j(2PIan V-22s) 22 20 ti2p33 ~ 2 3 200 \~24 24 200 25 25 Plan V-228 S-S) (Plan 5228) 2 0 26 50 3 0 0 V V1-1111 7( 11 PTB)2) 3 0 0 313 Travelling Cylinder Azimuth (TFO+AZI) [deg] vs Centre t F - _ - - _ ~t` - ~t _- _ _ _ Site: P~VPac~ __ _ l Plan V-219 (S-Y) _ ` Dn meet ~orif.~3~~ a~ sed on: Plarine rogram esenphon: ertica ept a ow can ea eve ap o mg: 97955.-60 ~ - oca + - : - 36:32 --- _ . ahtu e: ongitu e: - - _- - - -- ape: trc a ~: 166 i _-0--- _ _~ _ ~ _ _ ~ _ O --- - ~ -- D 0 O O O O O ~ O O O O - , O b _ -- , ~ ~ _ ~~-- __ , - , ~_ ----_ , -~ ~arget~rg~~l._-G_ t/ I7 ~- ite: a ~~ ~ an - 9~S-Y~ ' DriIiing a get Conf.: SSA Wised ori: P anne rogram esenphon: ertica ept a ow can ea eve ---~~rt~g: 59b988$~06 ~ - - _ -Local+NT--S: -169:99 tF -- - ___ - _ --__---- ap- -- - oca atitu e: ongitu e: ape: arc e - - - - --- - -- _ __ a ms: 1~ft -~ i It II WELLHEAD= FMC ACTUAT6R = Electric KB. ELEV = BF. ELEV = KOP = 250' Max Angle = 66.4 deg Datum MD = Daatum ND = V-21~i Proposed ~4-1/2" TBG, 12.6#, L-80, TC-II, .0152 bpf, ID=3.958" H 2S 9-5/8" CSG, 40p, L-80, TGN, ID = 8.835" 4264' 7" CSG, 26#, L-80, TC-II, .0383 bpf, ID = 6.276" 5 Minimum ID = 2.75" ~ xxxx' 3-1/2"HES XN NIPPLE MARKER JOINTw/ RA TAG Na 8395 CENTRAL¢ERw/ RA TAG $460' GAS LIFT MANDRELS ST MD ND DEV TYPE VLV LATCH PORT OIATE 8 8363 MMG DCR RK WATER INJECTION MANDRELS ST MD ND DEV TYPE VLV LATCH PORT DATE 7 8439 MMG-W DMY RK 6 8498 MMG-W DMY RK S 8878 MMG-W DMY RK 4 8937 MMG-W DMY RK 3 8975 MMG-W DMY RK 2 9124 A~IG-W DMY RK 1 9195 N~IAG-W DMY RK PERFORATION SUMMARY REF LOG: SLB Rea~ime LWD A NGLE AT TOP PERF: Note: Refer to Production DB for historical pert data SQE SPF INTERVAL Opn/Sqz DATE 4-1/2" 5 Nb xxxx'-xxxx' O 4-1/2" 5 OA xxxx'-xxxx' O 4-1/2" 5 OBa xxxx'-xxxx' O 4-1/2" 5 OBb xxxx'-xxxx' O 4-1/2" 5 OBc xxxx'-xxxx' O 4-1/2" 5 OBd xxxx'-xxxx' /2" TBG, 9.2#, L-80, TGII, .0087 bpf, ID = 2.992" 9266' PBTD 9579' 7" CSG, 26#, L-80, BTC-M, .0383 bpf, ID = 6.276 9671' SAFETY NOTES: "'HES PKR ~ 6675 IS 'PULL TO RELEASE" BUT CAN ALSO BE RELEASED BY PRESSURE DO CE® 4300 PSI. TEST PRESSURE PKR RAT5415 PSI (4332 PSI IS 80X OF PKR RATING)'"' 29' H4-112" XO 3-112". ~ = 2.992" ( 3453' ~~3-1/2" HES X NIP, ID = 2.813" ssyl• I--~ s-~/z~~ nr~ x Ivir, iu = z.~s~ s° ~ 8413' 7" HES AHR PKR w / 1/4" FEED THRU, ~ = 2.920" 8427' MULTI DROP SGM FOR NDPG GAUGE 8827' 3-1/2" HES X NIP, ~= 2.813" 8847' 7" HES A HR PKR w / 1 /4° FEED THRU, ~ = 2.920" 8861' MULTI DROP SGM FOR NDPG GAUGE 8951' 7" HES A HR PKR w / 114" FEED THRU, ~ = 2.920" 8965' MULTI DROP SGM FOR NDPG GAUGE 8972' ~-~3-1/2" HES X NIP, ~_ 9143' 7" HES A HR PKR w / 1 /4" FEED THRU, ~ = 2.920" 9157' SINGLE SGM FOR NDPG GAUGE 9174' 3-1/2" HES X NIP. ID= 2.813" 9223' I~ 3-1 /2" HES X NIP, ID = 2.813" 9244' 3-112" HES XN Nom, ID = 2.75" 9266' ~-{3-1/2" WLEG, ~=2.992" ~1TE REV BY COMMENTS DATE REV BY COMMENTS 02/21!08 ALM Proposed WBD 03/05/05 ALM Update to PS 09/05108 AER Updated to P9 ORION UNIT WELL: V-2201 PERMIT No: xxxxx API No: 50-029-xxxxx Sec, Tw p, Rge BP Expbration (Alaska) Page 1 of 2 Maunder, Thomas E (D4A) From: Maunder, Thomas E (DOA) Sent: Thursday, September 25, 2008 5:45 AM To: 'Rebol, Amanda' Cc: Tirpack, Robert B Subject: RE: V-219 Is it possible to sen in - mation and - e section operations reports for V-207. Thanks in advance. Tom Maunder, PE ~, AOGCC Prom: Rebol, Amanda [mailto:reboa2@BP.com] Sent: Tuesday, September 23, 2008 6:53 AM To: Maunder, Thomas E (DOA) Cc: Tirpack, Robert B Subject: RE: V-219 Tom- In regard to your email. 1. I re-ran my cement calculations, and the calculations do bring the cement level higher than stated in the permit. In order to bring the lead to 1000' below the surface shoe, and the tail to 500' above the Ma sand, the volume required is Lead: 67 bbl, Tail: 89 bbl. 2. According to the off-set geology information, the only other well that V-219 is near at completion depth is V-207 (154' away from V-219 at 5968' MD). V-207 was completed last weekend, and will not be pop'd by the time V-219 is drilled. It is completed with 5 lateral slotted liners; V-219 is intended to provide injection support to V-207 once both wells are put on production/injection. My apologies- this well should have been included in the permit. Please feel free to call or email me with questions. Thank you! -Amanda Amanda E Rebol Drilling Engineer, GPB Rotary BP Alaska 907.564.5543 907.632.2095 720.933.0172 9/25/2008 Page 2 of 2 from: Maunder, Thomas E (DOA) [mailto:tom.maunder@alaska.gov~ Sent: Friday, September 19, 2008 10:52 AM To: Rebol, Amanda Cc: Tirpack, Robert B Subject: V-219 Amanda, I am reviewing the permit application for this well and have a couple of questions 1. Would you check your 7" casing cement calculations? You state the intent is to raise cement to 1000' below the casing shoe. However if the slurry column lengths given are added and subtracted from the total depth, the TOC is 4764'. I think more cement is better, but the ultimate volume doesn't agree with the stated basis. 2. With regard to proximate wells it is stated that there are no wells within'/4 mile at the completion depth and it is also stated that the nearest well is V-218 some 2261' distant at the top of the pool. Are there other wells that penetrate the Orion Pool within %: mile of V-219s trajectory through the Orion Pool enroute to the deeper Kuparuk and Ivishak pools? If so, these wells should be identified and a statement regarding the external integrity of the wells made. If a map based on the top of the Orion is available, that greatly helps visualize the proximities. I look forward to your reply. Call or message with any questions. Tom Maunder, PE AOGCC 9/25/2008 ~~ 'S4 ~~ 'Su ~475~7 -~. -45(}(7 -~~ ~4~5~ -375 +a~ :~ ~~ ` -r ~:,~ ~ '-i n ~' ~ y~ ~•, .c r ~~ ,'v t- ~ ,, i i~'_z _~. ~. ~ -11 ~a a' G' W - ~Q 22B ~~2 8 i ~5a B S ~~5~~ P\~-~~,,~W~.~~ `~~3~ o~- ~~~ 6050000 6000000 5950000 5900000 5850000 400000 EPA Aquifer Exemption - 40 CFR 147.102 (b)(3) 500000 600000 700000 800000 Alaska Department of Natural Resources Land Administration System Page 1 of/~ See Township, Range, Section and Acreage? ~,, New Search Yes ~~ No I.A~ n;'?~r~e~ I Case Abstract I Case Detail I Land Abstract ,~~ File: ADL ~4?-4~0 ~'"~ Se<~trch for Sta"us P,at U~c~<t,~s ;~~ nI U9'1 S ~Ufl$ Customer: 000107377 BP EXPLORATION (ALASKA)1NC PO BOX 196612/900 E. BENSON BL ATTN_ LAND MANAGER- ALASKA ANCHORAGE AK 995 1 966 1 2 Case Type: ?~ OIL & GAS LEASE COMP DNR Unit: 780 O1L AND GAS Tile Location: DOG D1V OIL AND GAS Case Status: 35 ISSUED Status Date: 09/30/1969 Total ~1c~•es: 2469.000 Date Initiated: 08/11/1969 Office of Primary Responsibility: DOG D1V OIL AND GAS Last Tr•ansuctrora Date: 12/28/2007 Case .Suhdype : :^~ NORTH SLOPE Lust Transaction: CHNGTEXT CHANGE LEGAL TEXT I~1e17[~/(/{7' U TOIb'flsll/~~: O ~ ~ ~ Ran,~~c': 012E ~SeCtlon: 0~ ~CC'!Il)/I ,~C/'t'S.~ ~)~~) :tis_'dt'C~~ ~i~,y tllc rig/r~ u~: L Totinnship: 0 l 1 N Rnr~,~c: 012E Section: U6 S'~ ~~ ~ir~ir . I rr~ ~: ~9 ME'Y7~~Rl/1: ~ TObVn.S121JJ: O I ~ ~' ~~t711~C.~ 012E ~'c'C'!lu/l.~ O .ti~c'c'l1U71 rIC7'C,~'.~ 596 R~Tc~i~ich~m.~ t, Towftsh~ip: O I I N R~in;~~ : 012E S~°~~ti~~~i: Oti 5'r~~~inn 1cr~~s.~ (,~Il Leba1 nescriptiou 08-11-1969 ~'~'*SALE NOTICE LEGAL DESCRIPTION*'k~ C23-035 T11N-R12E-UM GENERAL 05 640.00 ALL 06 59 x.00 ALL 07 596.00 ALL OS 640.00 ALL TOTAL ACRES - 2469.00 t k 1= >;c ;k ;k ,14 ;i= ~= ~ =f~ k a: =k >k ;k =k =k ~ ~ k ;k ~ -;< ;k ~; ;k ;k ;k 'k 'k ~= :;='k 'k ;k * =1- :k :k x ;i: ;ic a: ;k :i: ;i: ;k ;k ~;: ;{: ;f: ;k 'c '',: ~I= ~= >k h: < %1- `I= 04-OI-1977*~'UNITIZED LEASE AND PARTICIPATING AREA LEGAL DESCR[PITION{"k LEASED COMMITTED IN ITS ENTIRETY TO THE PRUDHOE BAY UNIT AND OII, RIM AND GAS CAP PARTICIPA"LING AREAS http://www. dnr.state. ak.us/las/Case_Summary. cfm?FileType=ADL&FileNumber=47450&... 9/ 18/2008 Alaska Department of Natural Resources Land Administration System Page 1 of ~ f -,: ~ ~,:; . .. ~ ;:' .i , ~" t arr~rrj~€'`S ~°c3t"C}~ ~J~r"It~ Cabins ~1.11"~! 3r~;E1PS !_AS Mania ~ Case Abstract ~ Case Detail ~ Land Abstract File: ADL 2820 '~~"` Search for Status Plat Updates ~ car lly lSi2U(18 Customer: 000107377 BP EXPLORATION (ALASKA) INC PO BOX 1.96612/900 E. BENSON BL ATTN: LAND MANAGER- ALASKA ANCHORAGE AK 995 1 966 1 2 Cus'e Tvpe: ~ OIL & GAS LI/ASE COMP DN12 Uniz: 780 OIL AND GAS File Location: DOG DIV OIL AND GAS CaSL' Statars: 35 ISSUED Status Date: 09/1/1965 Total Acres: 2560.000 Daze h~~itiuted.~ 05/28/1965 Office of Primajy Responsibility: DOG DIV OIL AND GAS Last Transaction Daze: 12/0/2006 Case Subtype: ~ NORTH SLOPE Lust Transaction: AA-NRB ASSIGNMENT APPROVED ~/e~~rclfcrat: l i 7rnr~isfri/,.~ U I I N Rca~t~~~'.~ O1 I E :~~~>rliun.~ (1 ] 1~c~clf~»t : lc~r~~s.~ 640 `~ea~ch Gi:'_~S Mericli~ui.~ l ~ To~~tz~~/zip: O1 I N I~c~n,Lre.~ 011E S'c~c~li~,n: U2 .ti~rc/run _1~~~~e~~: (, 1O Meridi~nt.~ l_~ Toirn~hip: O1 I N K~mL,c.~ Ol 1 E ti'ec~~ruir: I 1 .~'~z~lir~n : lrr~-~~: (~-(I) Mei~icliun.~ C_! Totiti~n~{~i~,.~ U I I \ l~~rn~e: 01.1E ti~r~~liun.~ I ~ S'~>~~tiun :lc~r~~s: 6~0 Legal Descrihtinu 0>-28-19<~ '~*~TSALENOTICF. LECTAL DESCRIPTIOr'~'*** C1~-19 OIIN-011E-UM 1,2,11,12 260.00 0=/-01-1)77 **UNI`117ED,LE.ASEAND PARTICIP.~ITING:~REA LEGAL DESCRIPTION** LEASE COMMITTED IN ~NTIRETI' TO PR UDHOE BA Y UNIT AND OIL RIM GAS C I P I'_~1 PR UDHOF 13A I' UNIT http : //www. dnr. state. ak. us/las/Case_Summary . cfm?FileType=ADL&F ileNumber=2 8240&... 9/ 18/200 8 TRANSMITTAL LETTER CgECT{LIST WELL NAME _ ~ ~ f/•~/9 1~TD# boy-/~~ __ Development / Service __ Exploratory Strati _Non-Conventional Wett ---.-_ graphic Test FIELD: ~.e't/.D~,/D~' /t~,~~ POOL: .,~/Ort~ - Cirde Appropriate Letter /Paragraphs to be Included in Transmittal Letter CHECK ADD-ONS WHAT (OPTIONS) TEXT FOR APPROVAL LETTER APPLIES MULTI LATERAL The permit is for a new wetlbore segment of existing well (If last two digits in Permit No. API number are APC No. SO-____. between 60-69) Production should continue to be reported as a function of the original API number stated above. PILOT HOLE In accordance with ZO AAC 25.005 acquired for the pilot hole must be (clearly differen~ fisted inn bad well name ( PI-~ and API aumber (S~ = :_) fc+om records, data and logs acquired for welt SPACING The permit is approved subject to full compliance with ZO AAC EXCEPTION 25.055. Approval to perforate and aroduce / intact is contingent upon issuance of a conservation order approving a spacing exception. assumes the liability of any protest to the spacing exception that may occur. ~.-... ~+a s \,.R Alt dry ditch sample sets submitted to the Commission must bC in SAMPLE no greater than 30' sample intervals from below the from where samples are first caught and JO' samplemint >s throw h et tunes. Non-Conventional please note the following special condition of this permit: Well production or production testing of coal bed mejhane is mot allowed for [name of w~ until after [Coraoanv Vame) has designed and implemented a water well testing program to provide baseline data on water quality and quantity, _(Comounv N9fne) must contact the Commission to obtain advance approval of such water well testing program. Rev: i!i iR008 PERMIT CNECKUST Field & Pool PRUDHDE BAY, ORION SCHR BL OIL - 640135 11YEL1 Well Name: pRUDHOE BAY UNGRIN V-219 Program SER Well bore sag ^ . PTD#:2081420 Comparry BP EXPLORATION (ALASKA INC Initial Class/Type SER I PEND GeaArea 890 Unit 11650 OnlOff Shore ~n Annular Disposal ^ Administration 1 Petmikfee attached- - - - - - - - - - - - - - - - - - ~- - - - - - - - - - - - - - - - - - - - - - - - - - - - - 2 Leas®numDer appropriate - - - - - - - - - - - - Yes - - - - - - - - - - - - - - - - - - - 3 Un(quewellnameandnumber -- --- -- - - -- - ------ Yes - -- - ---- - --- -- -- ; -- - - - - -- -- -- --- 4 Wflli-located in a_definedpool_________._-_--__-------_-- ---------Yes- ----Orion!Schraderl3luff._-________________-_------------------- - -- -- 5 -Vllelllocatedproperdistancefromdnllingunit_boundary._____________ ________Yes _-____-_____-.------ -- --- 6 WeII IQCated Proper distanCal[om Rtherwells- - - - - - - - - - - - - - - -Yes - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - 7 Sufticientacreageayailable(ndriUingun)t----------------------- ----_-__Yes- ------1560acrea.-__--__---_--_-------------- -- - - -- - --- -- 8 If deviated, is_v-ellbor@ Piat_included - - - - - - - - - - - - - - - - -Yes - - - - - - - - - - - - - - - - - - - - - - - - - - - - - 9 Ope[atoloniyafteciedParfY- -- --- -- -- -- -- -- ---- ---Yes -- -- -- --- -- ---- - ----- - - -- ------- ------ --- 10 Ope[atorbaia_app[oprlatebondinforce-.-------------------- ---------Yes- --.--.QlanketBond#6184193------------------------------------- - --- -- 11 Pe[mitcaDbe'tssuedwlthQUtconserYati0n4rdBr------------------- ---------Yes- ---------------------------- ------------- -- - - -- --~ -- --- --- Appr Date 12 PemliteanbelssuedwithQUiadmioiatrative_approval---------------- ---------Yes- ---------.----.---------------------- -- -- --- - - - - --- --- 13 Can permit be aPRrGVed 4efore 15-daY v/ait - - - - - - - ~ - - - - - - - - Yes - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - ACS 9H812008 14 .WelUocated within area and_slrata authorized by Injection Order # (put Ip# in.comments)_ (For_ Yes _ _ _ _ _ _ AIQ16- - - - - - - - - - - - - - - - _ _ _ _ _ _ _ - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - ~ - - 15 Allwelia_v~ithin1l4_mileateaof[eyieMrjdent)fled(Foraerviceweli4rlly)------ ---------Yes- -------------------------- - --- -- ---- ----- -- - -- - ---- --- 16 Pre-Aroduced injector, duration of preproduction teas than 3 months-(For service well only) _ _ -NA _ _ _ - - _ _ _ - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - 17 NonGOnvan,9as_c9nf4r[natRAS31,05,030U.1.A),ILZ.A-D}-- ----- - -- -- ----~-- - -----~ --~---- - -- -- -- --- --- -- -- -- ---- - -- ---- Engineering 18 Cond4ctorstnng_provlded- -- -- --- - - - - ------- Yes- -- --- - -- - - -- - ---- -- - - --- -- - ------- ~ -- --- 19 Su[face.caaing_protectsall knownUSDWa---------------------- --------- ~A-- ------Allaquifera exempted,40CFR_147.102_(b}(3)andAEQ1•---------------------------------- 20 CMT-voladequate_tocirculate_onconductot&surf-csg--------------- --------Yes- ---------------------------- -- ------ --- --- -- ----- ------- 21 CMT-vol aequate_ t9 tie-in IQng string to surf cs9- - - - - - - - - - - - - - - -~o- - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - 22 CMLwillcoveraliknawn_p>~ductivebarizons--------------------- --------Yes ----------.------------------- -- ----- -- - --- -- --- --- --- 23 Casing des~ns adequate for G, ? 6 &_p®[mafrost - - - - - - - - - - - -Yes - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - 14 Adequate tankage-or reserve pit _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ Yes _ _ _ _ _ Rig equipped wish areal pits. No_reserve pit planned•_ All waste_to approved disposalwell(s). - . _ _ - _ _ _ _ _ _ _ - 25 rs-drill,bas-at0.403foreband9nment keenapR~Ved------------ Ifa -------- NA- -------------------------------------- -- - - ------ ------ -- 26 _ Adequate_wellfpfflaeparation-proposed_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ Yes _ . _ _ _ . _ P[oximrfy analysis performed, T[ayeling cylinder path calculated, Gyros likely_in surface hole. _ _ - . _ _ - _ _ _ _ _ 27 Ifdiverterrequired,duea~meetregulations---- - - - -- - - -- --- Yes -- -- -- - - -- -- - - ------------- - -- -- --- ---- -- Appr Date 28 Drilling Buidprogram schematic_& equip listadequate_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _Yes _ _ _ _ _ _ _ Maximum expected formation pressure 6,7-EMW.- MW Planned up to 9,5_ppg._ _ _ _ _ _ _ . - _ _ - - _ _ _ - _ _ _ _ _ TEM 101312008 29 BOPEs,_dotheymeetre9ulation- --- --- -- - - -- -Yes - -- ---- -- --- --- - - ----- --- - -- -- - --- --- 30 BOPE_prQSS rating appropriate; test to_(put prig in comments)_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ Yes _ _ _ - _ _ _ MASP calculated at 1&17 psi, 4000_psi_BOP testplanned. _ _ _ _ _ - - _ - - _ _ - . _ _ _ _ _ - . _ _ _ - _ - _ _ 31 Choke_manifckl cornplies wlAPl_RP-53 (May $4) - - - - - - - - - - -Yes - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - 32 1NQrkwillscourwithoutoperationsbutdovm---------------------- ---------Yes ----------------------------- ----- -- -- -- - - -- --- -- 33 - la presence of H1S gas probable _ _ _ _ _ _ _ __ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _Yes _ - - _ _ _ . H1$ is repoded_at Vpad• _ Mud should precit~de_H2S on rig._ Rig has sensors and_alarms. _ _ _ _ - _ _ _ - - _ _ _ _ 34 -Mechanical-condition of wells within AOR ver~'ied (.For serv)ce well only} _ _ _ _ _ _ _ _ _ _ _ _ _ _ Yes _ _ _ - _ _ _ V-107 newly_driUad in AOR._ No issyes identified. _ _ _ _ . _ _ _ - _ _ _ . _ _ _ - - _ _ - _ _ _ - - _ - _ _ - . _ _ _ - _ Geology 35 Permitcan be issued wlo hydtogensulTide measures - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ No. _ _ _ _ Max Ievels_H2S wells V-122=30ppm_(3-31.07}; V-117=120ppm-(8-3.07). _ _ _ - _ _ .. _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ 36 Data_presentedonpotentialoverpressurezones_-_-____----_-- -.------- NA __--_____.-__------------------ -- -- ---- - -- -- ----- - Appr Date 37 Se(smic anaysis of shallow gas zones- - - - - - - - - - - - - - - NA - - - - - - - - - - ~ - - - - - - - - - - - - - - - - - - - - - ACS 9!1812006 38 Seabed-conditionsurt+ey_(if off-sho[e)------------------------ --------- NA. --------------------------------------------------------- ----------------- 39 Contact namelphone for weekly_prggress repor#s [exploratory only] - - - - - - - - - - - - - - - -Yes - _ _ _ - - Amanda l2eboi - 564c5543• - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - Geologic Engineering Date C Date: Date Commissioner: o er Commissioner: /0•3 -0~9