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HomeMy WebLinkAbout209-078STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION REPORT OF SUNDRY WELL OPERATIONS - o . m- s tv "?4 MAY 2 8 2019 1. Operations Abandor❑ Plug Perforations ❑ Fracture Stimulate ❑ Pull Tubing ❑ Operations shutdown 1-6 Performed: Suspenr❑ Perforate ❑ Other Stimulate ❑ Alter Casing Q Change Approved Program ❑ Plug for Redril❑ :rforate New Pool ❑ Repair Well ❑ Re-enter Susp Well ❑ Other: ❑ 2. Operator Name: ConocoPhillips Alaska, Inc. 4. Well Class Before Work: 5. Permit to Drill Number: ❑ Ex lorato Development + Exploratory ❑ Stratigraphic❑ Service ❑ 209-078 3. Address: P. O. Box 100360, Anchorage, Alaska 6. API Number: 99510 50-029-22714-62-00 7. Property Designation (Lease Number): 8. Well Name and Number: ADL 25638, ADL 25649 KRU 1C -11L1-02 9. Logs (List logs and submit electronic and printed data per 20AAC25.071): 10. Field/Pool(s): N/A Kuparuk River Field / Kuparuk River Oil Pool 11. Present Well Condition Summary: Total Depth measured 13,031 feet Plugs measured None feet true vertical 6,636 feet Junk measured None feet Effective Depth measured 13,029 feet Packer measured 5203, 10141 feet true vertical 6,636 feet true vertical 3518, 6143 feet Casing Length Size MD TVD Burst Collapse CONDUCTOR 80 feet 16 121' MD 121' TVD SURFACE 6,903 feet 95/8" 6,945' MD 4439' TVD .5" SCAB LINER 5,108 feet 3 1/2 " 10,271' MD 6231' TVD PRODUCTION 10,438 feet 7 10,466' MD 6372' TVD LINER 1,021 feet 5 11,300' MD 701 1'TVD CTD LINER 2,308 feet 2 3/8 " 13,030' MD 6636' TVD Perforation depth: Measured depth: 10660-10716 feet True Vertical depth: 6517-6559 feet Tubing (size, grade, measured and true vertical depth) 3.5" L-80 5,193' MD 3,512' TVD Packers and SSSV (type, measured and true vertical depth) PACKER- FHL Retrievable Packer 5,203' MD 3,518' TVD PACKER - BAKER PREMIER Packer 10,141' MD 6,143' TVD SSSV - TRMAXX w/2.813 X -Profile 2,297' MD 1,994' TVD 12. Stimulation or cement squeeze summary: Intervals treated (measured): N/A Treatment descriptions including volumes used and final pressure: 13. Representative Daily Average Production or Injection Data Oil -Bbl Gas-Mcf Water -Bbl Casing Pressure Tubing Pressure Prior to well operation: 180 393 1481 1000 300 Subsequent to operation: 1880 3379 4135 1200 300 14. Attachments (required per 20 AAC 25.070, 25.071, 8 25.283) 15. Well Class after work: Daily Report of Well Operations O Exploratory ❑ Development 21 Service ❑ Stretigraphic ❑ Copies of Logs and Surveys Run ❑ 16. Well Status after work: Oil O Gas ❑ WDSPL ❑ Printed and Electronic Fracture Stimulation Data ❑ GSTOR ❑ WINJ ❑ WAG ❑ GINJ ❑ SUSP❑ SPLUG❑ 17. 1 hereby certify that the foregoing is true and correct to the best of my knowledge. Sundry Number or N/A if C.O. Exempt: 319-126 : Contact NameWilliam Long Authorized Name: James Ohlin er Contact Email: William.R.Long@cop.com Authorized Title: Staff CTD Engineer Contact Phone (907) 263-4372 Authorizetl Signature: Date: Form 10-4r4Revised 4/2017 ' P,L 4l -fl/ 91411', "4BDMS—df4VMAY 2 9 9019 5ubmit Original Only KUP PROD WELLNAME 1C-11 WELLBORE 1C -11L1-02 ''Irya' + -' ' Well Attributes Max Angle & MD _ TO t` FIeMN WNIWIe YPY11yA Wellnare 5trlu5 ncll'1 MOIRNB) Ac191m lnl(al Alaska, Il 1KDPARDKRIVER UNIT 15002922]1462 IPRDD 630 To 9(Z70`7 130910 In. 11 um. 5424019 2'.56:19 PM Last Tag v«w w+n.mcesDwl nnnwmn oepm mna) End om w.11mre LsslMm ey .........._.. __.............. ....... ... .__ Last Tap: 1 -11 L1-02 Imosbor NANpur E2 Last Rev Reason ......•••..••..............•••........_.................. .... Annurran End Daa, Mm,I,m LesLModey Rev Reason GLV CIO 511412013 1C -11L1-02 bargee casing Strings Ceslnp De:<r11x1on oD llnl ID 11nI TopmRI set Delun MKel sal Depm (rvRL. wIstm O...pmae TTTnreed coaoocloa. al olvo LINER IC -117 23/8 200 10,2d0.8 13,030.0 6,635.9 0.60 L-80 SbL Liner Details NomDmllo Top nnel TOP(rv01(Uce) Taplmir) lwm Des cam 11n) 10,240.8 6,2WS 46.47 PACKER BAKER HYD KB LINER TOP PACKER 1730 SAFETY VLV 22srI4 10246.4 6.213.5 4630 SEAL 6seal assembly stung iniadeployment s@eve 1730 10,2479 6214.5 46.25 DEPLOY Deployment sleeve with Seal bore 2250 GsSUFT.al93.9 111125.4 6,5657 41.51 NIPPLE RSEALING Nipple 1710 10,151.8 6,589.9 43.35 Swell Packer TAM mail packer. Top of elem.M M 17,760' 1 680 10885.1 6,6348 90.40 DEPLOY 3" GS DEPLOYMENT Sleeve 1.992 ens uFT:4.z124 129922 6.621.3 8].23 O-RING 0 -RING SUB 1,710 13,024.9 6,633.9 61.20 INDEX TOOL Raker Oil Toot R B R INDEXINTOOL 1.680 uF05'11''a Perforations& Slots snot Tap (1vD1 elmtrvRl ISentint LOCATOR:E,.E TOPM.' BlmptlLe) MR) RIK81 L1n4tl Zone pN¢ I Type Lom 11,3864 12,9922 6,618) 6,621.3 ]2]2009 32.0 SLOTS 4 pii BLOTTED UNER I 1C-iiL1-02 MAL:slns Frac Summary &art Dab 6202008 pnppm[Oe5pI1M (ID) Proppanl In Fmmatlon(m) 1F1011 sMs srad Dale TOP pePIn MK, atm lnKel L sysmm va clean leap TI vnlswmy tDa) 1 612012008 6600 10,]160 Notes: General & Safety Ena oam Arra.- n ]1262009 NOTE.MULTI-LATERAL iC-11,1U-11L1, 1C -11L1 -01,1C -11L1-02 SURFACE', 42a4,W2� INN LINER1G11L 10,2124 15,19A0 JSSELINIU ER,5,IS3,y louro 56LL ASSY'. ism: 2W CTD LINER: 1023]0 PRODUCTION: Wirt asE ll RPERF:10a®D10.920D FRAC: I0.YY1.0 (PERF: Vial10T80 WHIPSTOCI(1a684041 WHIPSTOCK:10.147.0 LINER: 10.218.4-11... sL.:11.vse-12s92.2—J LINER 1411 LI -0Z 10,74 (I- ..0 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Time End Time Dur (hr) Powe Op Code Activity Code Time P -T -X Operation Start Depth (RKB) End Depth (RKB) 3/26/2019 3/26/2019 1.50 MIRU MOVE MOB P Continue RD checklist, Trucks on 0.0 0.0 20:00 21:30 location, load shop, secure stairs and landings, secure BOP's, Complete RD checklist 3/26/2019 3/27/2019 2.50 MIRU MOVE MOB P PJSM, Pull utility module away from 0.0 0.0 21:30 00:00 rig and line up for move, trouble getting up hill to get off pad, hook up cattdozer, work over hill, pull drilling sub off well. 3/27/2019 3/27/2019 2.00 MIRU MOVE MOB P Install Jeeps, ready to move, PJSM 0.0 0.0 00:00 02:00 3/27/2019 3/27/2019 3.50 MIRU MOVE MOB P Begin move from 3F -Pad to 1C -Pad 0.0 0.0 02:00 05:30 3/27/2019 3/27/2019 1.00 MIRU MOVE MOB P Park at 1 Q for changeout, walkaround 0.0 0.0 05:30 06:30 3/27/2019 3/27/2019 3.25 MIRU MOVE MOB P Continue move to 1C 0.0 0.0 06:30 09:45 3/27/2019 3/27/2019 1.00 MIRU MOVE MOB P Arrive on location, remove jeeps, prep 0.0 0.0 09:45 10:45 well location for rig 3/27/2019 3/27/2019 2.25 MIRU MOVE MOB P Spot sub & pits over well, lay mats, 0.0 0.0 10:45 13:00 drop stairs 3/27/2019 3/27/2019 2.00 MIRU MOVE RURD P Begin RU checklist, get COMMS up, 0.0 0.0 13:00 15:00 set -down shop & lay mats, install scaffolding & platform around well 3/27/2019 3/27/2019 3.00 MIRU MOVE RURD P Continue RU checklist, spot tiger -tank 0.0 0.0 15:00 18:00 & MU hard-line, begin NU BOPE, MU PUT2, grease tree valves & Tangos, complete NU BOP " Rig Accept: 18:00 3/27/2019 3/27/2019 2.50 MIRU WHDBOP RURD P Complete rig up check list, Air test TT 0.0 0.0 18:00 20:30 line, Obtain RKB Measurments, Service tree and stack, Valve crew here. Prep for BOPE test 3/27/2019 3/27/2019 1.00 MIRU WHDBOP ROPE P PJSM, Fill stack and bleed aire out of 0.0 0.0 20:30 21:30 system. Shell test BOPE, Swap out 0 - Ring on riser 3/27/2019 3/28/2019 2.50 MIRU WHDBOP BOPE P Start full initial BOPE test, Test 0.0 0.0 21:30 00:00 witness waived by Adam Earl, AOGCC, No Fail pass through midnight test #9 3/28/2019 3/28/2019 2.50 MIRU WHDBOP BOPE P Continue full BOPE test, on test 9 0.0 0.0 00:00 02:30 3/28/2019 3/28/2019 0.50 MIRU WHDBOP BOPE P Pull test joint, Make up nozzle stab on 0.0 0.0 02:30 03:00 injector. Pressure test inner reel iron and pack offs, End BOPE test 3/28/2019 3/28/2019 1.00 SLOT WELLPR RURD P PJSM, Rig down BOPE test 0.0 0.0 03:00 04:00 equipment. PT PDL's TT line 3/28/2019 3/28/2019 0.75 SLOT WELLPR RURD P Normal up rig, Blow down TT line, 0.0 0.0 04:00 04:45 Open Tango valves. WHP=175 PSI 3/28/2019 3/28/2019 2.75 SLOT WELLPR PULD P M/U PD, BHA #1, fishing assembly 0.0 68.5 04:45 07:30 3/28/2019 3/28/2019 0.50 SLOT WELLPR PULD P Surface test Coil (good -test), Tag up 68.5 68.5 07:30 08:00 reset counters 3/28/2019 3/28/2019 2.00 SLOT WELLPR TRIP P RIH 68.5 9,745.0 08:00 10:00 3/28/2019 3/28/2019 0.3o SLOT WELLPR DLOG P Log formation correction of plus 3.5' 9,745.0 9,779.0 10:00 10:18 3/28/2019 3/28/2019 2.00 SLOT WELLPR CIRC P Continue RIH, park @ 10,200', obtain 9,779.0 10,200.0 10:18 12:18 static, 8.5-8.7 ppg, bring pump on-line circ bottoms up. PUW 40 k Page 1135 Report Printed: 5/28/2019 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Time End Time Dur(M) Phase Op Code Activity Coda Time P -T -X Operation Start DepM (WB) End Depth(VB) 3/28/2019 3/2812019 0.75 SLOT WELLPR CIRC P Vac out tiger tank, 10,200.0 10,200.0 12:18 13:03 3/28/2019 3128/2019 1.50 SLOT WELLPR JAR P RIH, pumping .46 bpm latch into fish 10,200.0 10,245.0 13:03 14:33 @ 10,245', hit jars x 25, jaring at 25k (57k), straight pull to 70 k, with no success 3/2812019 3/28/2019 1.75 SLOT WELLPR CIRC P Pump off fish, circulate 8.8 ppg drilling 10,245.0 10,200.0 14:33 16:18 1 fluid around 3/28/2019 3/28/2019 0.50 SLOT WELLPR CIRC P ppg all the way around, shut down 10,200.0 10,200.0 16:18 16:48 1 pump, perform flow check, flow at the 18.8 valve, shut back in and montior, slowly built up to 116 psi, 3/28/2019 3/2812019 0.30 SLOT WELLPR TRIP P RBIH, pumping 0.46 bpm latch into 10,200.0 10,245.0 16:48 17:06 fish, pump 1.5 bpm at 3,451 psi, no returns 3/2812019 3/28/2019 0.30 SLOT WELLPR JAR P Perform 5 jar hits @ 25 k PU over 10,245.0 10,245.0 17:06 17:24 PUW 30 k, straight pull to 70 k 3/28/2019 3/2812019 1.30 SLOT WELLPR OWFF P Unlach fish, PUH to 10240. Observe 10,240.0 10,240.0 17:24 18:42 well for flow, WHP 40 PSI and slowly climbing 3/2812019 3/28/2019 0.10 SLOT WELLPR OTHR P Take static pressures. Annular @ 10,240.0 10,240.0 18:42 18:48 1 2934, Bore @ 2928 PSI. 3/28/2019 3/2812019 0.10 SLOT WELLPR OTHR P Slowly stab on and latch fish, 3K 10,240.0 10,245.0 18:48 18:54 1 down, Annular 2925, Bore 2935, WHP=40 312812019 3128/2019 0.40 SLOT WELLPR OTHR P Set down 6K, Annular 2932, Bore 10,245.0 10,245.0 18:54 19:18 2929, WHP=40 PSI. Annular down to 2896 after 20 min. Bore at 2925 3/28/2019 3128/2019 0.10 SLOT WELLPR OTHR P Put fish in tension, DHWOB=-3K, 10,245.0 10,245.0 18:18 19:24 Annular 2864, Bore 2923, WHP=41 3/28/2019 3/28/2019 0.20 SLOT WELLPR OTHR P Pull fish harder, DHWOB=-7K, Annualr 10,245.0 10,245.0 19:24 19:36 2883, Bore 2924, WHP=41 3/28/2019 3128/2019 0.30 SLOT WELLPR OTHR P Pull fish up to 60K, Annular 2858, 10,245.0 10,245.0 19:36 19:54 Bore 2945. 3/28/2019 3/28/2019 1.30 SLOT WELLPR OTHR P Bring on pumps 1.5 BPM, release 10,245.0 10,200.0 19:54 21:12 from fish PUW=35K, PUH, Open EDC. Wait on 9.0 PPG fluid 3/2812019 3/28/2019 1.20 SLOT WELLPR KLWL P Start pumping 9.0 PPG down CT .9 10,200.0 10,200.0 21:12 22:24 BPM with .15 BPM returns. Slow pump down to .6BPM. returns holding @ .15 -.2 BPM. Jog coil to help shear fluid up to 9595 @ 80 FPM them back down to 10,200. CT displaced to 9 PPG. 3/28/2019 3/28/2019 0.90 SLOT WELLPR KLWL P Consult town, Bull head 60 BBIs 9.0 10,200.0 10,200.0 22:24 23:18 Fluid, 1.5 BPM @ 1400 PSI WHP 3/28/2019 3/29/2019 0.70 SLOT WELLPR KLWL P Shutdown and monitor well. Would 10,200.0 10,200.0 23:18 00:00 not go to no flow,2900 PSI 6045.6 ND, @ 9.26 PPG 3/29/2019 3/29/2019 1.60 SLOT WELLPR TRIP P POOH pumping 9.0 down CT 10,200.0 90.0 00:00 01:36 3/2912019 3/2912019 0.90 SLOT WELLPR OWFF P At surface, Flow check well. Fluid 90.0 90.0 01:36 02:30 coming out of whity valve. Open up choke and blow down to pits. No flow for 12 minutes then started. 3/29/2019 329/2019 1.00 SLOT WELLPR PULD P Tag up and space out. PUD BHA#1. 90.0 0.0 02:30 03:30 wHP up to 30 PSI. Bleed down came right back up. Lay down fishing BHA 3/29/2019 3/29/2019 1.50 SLOT WELLPR ELNE P Shift to running a -line with lubricator. 0.0 0.0 03:30 05:00 Rigging up a -line grease head 3/29/2019 3/29/2019 0.60 SLOT WELLPR ELNE P PJSM, with Pallard &Rig crew for e- 0.0 0.0 05:00 05:36 line ops, crew change Page 2135 Report Printed: 5/2812019 ' Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Sfart Time EM Time Der(m) Phase Op Cade Actnity Code Time P -T -X Operemon S art Depth (WB) End Depth(flKB) 3/29/2019 3/29/2019 3.00 SLOT WELLPR ELNE P RU a -line 0.0 0.0 05:36 08:36 3/29/2019 3/29/2019 0.45 SLOT WELLPR ELNE P Stab on lubricator, PT with rig pump, 0.0 0.0 08:36 09:03 4,000 psi, good test, bleed off pressure 3/29/2019 3129/2019 1.10 SLOT WELLPR ELNE P RIH, with 5/8" string shot, weight bar, 0.0 0.0 09:03 10:09 firing head (16.03' BHA), WHP=312 3/29/2019 3/29/2019 0.50 SLOT WELLPR ELNE P Log CCL for depth control on the way 0.0 0.0 10:09 10:39 in the hole, no-go on nipple at 10,725', obtain log of previous cut depth, looks to be clean. fire string shot 10,713'- 10,725'. 3129/2019 1.20 SLOT WELLPR ELNE P POOH, w/e-line 0.0 0.0 10:39 11:51 13/2912019 Note: Operator shut in well 1C-17 MI Injection well. 3/29/2019 3/29/2019 0.50 SLOT WELLPR ELNE P MU Jet cutter to a -line, stab on 0.0 0.0 11:51 12:21 lubricator PT, grease head small leak, -1 add addtional grease, re -PT 3/29/2019 3/29/2019 00 SLOT WELLPR ELNE P RIH, w/Spectra2 Jet Cutter 1.68" OD, 0.0 0.0 12:21 13:21 3/29/2019 3/29/2019 0.40 SLOT WELLPR ELNE P Tie into K1 10,427.5', Log CCL while 0.0 0.0 13:21 13:45 RIH, log across seal bore and 15 joints. fire cutter on depth 10,722'. PUH free, RBIH past cut depth, temporily detained, RBIH, PUH w/mcreased speed, Pull free 3/29/2019 3/29/2019 1.00 SLOT WELLPR ELNE P POOH 0.0 0.0 13:45 14:45 3/29/2019 3/29/2019 1.00 SLOT WELLPR ELNE P PJSM, LD cutter and pressure 0.0 0.0 14:45 15:45 equipment, RD a -line unit and release 3/29/2019 3/29/2019 0.70 SLOT WELLPR CTOP P PJSM, move INJH cart forward, RIH 0.0 0.0 15:45 16:27 with coil into mouse hole inspecting coil, found flat spots at 10' and 15', Prep coil and cut 20 3/29/2019 3/29/2019 0.80 SLOT WELLPR CTOP P Prep CT, Install CT connector. Pull lest 0.0 0.0 16:27 17:15 35K 3/29/2019 3/29/2019 1.00 SLOT WELLPR CTOP P Head up BHI UOC / test wire - Good. 0.0 0.0 17:15 18:15 Pressure test UOC CTC to 4400 PSI - Good 3/29/2019 3/29/2019 2.00 SLOT WELLPR PULD P M/U and PD BHA#2 Fishing BHA with 0.0 81.3 18:15 20:15 Accelorator, weight bars, Up down jars, and sealed GS spear 3/29/2019 3/29/2019 1.80 SLOT WELLPR TRIP P Trip in hole BHA#2. Sputtering small 81.3 9,760.0 20:15 22:03 gas bubbles on trip in 3/29/2019 3/29/2019 0.20 SLOT WELLPR DLOG P Log K1 for -2.5", Close EDC 9,760.0 9,798.0 22:03 22:15 3/29/2019 3/29/2019 0.30 SLOT WELLPR TRIP P Continue in hole, Pull weight check @ 9,798.0 10,248.0 22:15 22:33 1 10,200' PUW=36K 3/29/2019 3/29/2019 0.70 SLOT WELLPR JAR P Latch fish, Jar up - down X5. Jar up 10 10,248.0 10,248.0 22:33 23:15 times 25K over PUW. No movement. 3/29/2019 3129/2019 0.20 SLOT WELLPR CIRC P Start pumping to establish circulation. 10,248.0 10,248.0 23:15 23:27 Remain latched to fish. .5 BPM @ 3478, Annular 3096. Unable to move fluid to surface 3/29/2019 3/29/2019 0.45 SLOT WELLPR JAR P Go back to jarring up on fish X15. No 10,248.0 10,211.0 23:27 23:54 movement. Pump on to release from fish 3/29/2019 3/30/2019 0.10 SLOT WELLPR CIRC P Pump on to establish returns 10,211.0 10,211.0 23:54 00:00 3130/2019 3/30/2019 0.30 SLOT WELLPR CIRC P Continue circulating with open EDC 10,211.0 10,211.0 0000 0018 Page 3/35 Report Printed: 5/28/2019 Operations Summary (with Timelog Depths) IC -11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log start Time EM Time our (hr) Phase OpCMe Apivily Coee Time P -T -X O eraeon p Start Depth (fiKB) End Depth (WS) 3/30/2019 3/30/2019 0.50 SLOT WELLPR PRTS P Get static pressure test. BHP=3193, 10,211.0 10,211.0 00:18 00:48 TVD=6154.5, EMW=9.97 3/30/2019 3/30/2019 1.30 SLOT WELLPR CIRC P Circulate bottoms up 1.6 BBL/Min with 10,211.0 10,211.0 00:48 02:06 full returns. 3/30/2019 3/30/2019 1.80 SLOT WELLPR TRIP P Trip out of hole, lost 4 MIS on trip out 10,211.0 72.0 02:06 0354 3/302019 3/30/2019 1.50 SLOT WELLPR PULD P Tag up and space out, PJSM. PUD 72.0 0.0 03:54 0524 1 BHA#2 3/30/2019 3/30/2019 1.50 SLOT WELLPR ELNE P Prep rig floor for eline ops, standby for 0.0 0.0 05:24 0654 SLB eline travel to rig 3/30/2019 3/30/2019 0.75 SLOT WELLPR ELNE 3 SLB on location, PJSM, spot in unit 0.0 0.0 06:54 07:39 3/30/2019 3/30/2019 0.30 SLOT WELLPR ELNE P PJSM with dg crew and SLB 0.0 0.0 07:39 07:57 3/30/2019 3/30/2019 5.00 SLOT WELLPR ELNE P RU, SLB pressure equipment to the 0.0 0.0 07:57 12:57 rig floor 3/30/2019 3/30/2019 2.00 SLOT WELLPR ELNE P PT SLB a -line lubricator 0.0 0.0 12:57 14:57 3/30/2019 3/30/2019 5.80 SLOT WELLPR ELNE P RIH, w/Shammas Chem Cutter 0.0 0.0 14:57 20:45 1.8675" OD, 2 x centralizers, CCL, Gamma. Log Kt. Run CCL. Appears liner has moved uphole -15'. Attemp to log R nipple. Set down @ 10725. right where nipple should be. CCL 13' from bottom of a -line tool string. Log K1 to ensure we are on depth. POOH 3/30/2019 3/30/2019 1.10 SLOT WELLPR ELNE P At surface with a -line. PJSM to lay 0.0 0.0 20:45 21:51 down chem cutter. Swap out to 1 3/8" loolstring for logging ops 3/30/2019 3/30/2019 0.50 SLOT WELLPR ELNE P PIU Next a -line run. Stab on well 0.0 0.0 21:51 22:21 3/30/2019 3/312019 1.65 SLOT WELLPR ELNE P Trip in hole with a -line unit with 1 3/8" 0.0 0.0 22:21 00:00 logging tools 3/31/2019 3/31/2019 1.30 SLOT WELLPR ELNE P Continue tripping out with a line 0.0 0.0 00:00 01:18 logging tools 3/31/2019 3/31/2019 3.25 SLOT WELLPR ELNE P E -line at surface. PJSM. Pull logging 0.0 0.0 01:18 04:33 tools from well. Rig down a -line unit 3/31/2019 3/31/2019 0.70 SLOT WELLPR CTOP P PJSM, Position injector on rig floor. cul 0.0 0.0 04:33 05:15 off UQC. Boot wire, 3/31/2019 3/31/2019 0.25 SLOT WELLPR CTOP P Install CT cutter, Trim 300' of coiled 0.0 0.0 05:15 05:30 tubing from reel 3/31/2019 3/312019 1.50 SLOT WELLPR CTOP P Trim 300' of coiled tubing, String 0.0 0.0 05:30 07:00 #52794, Reel #20709 3/31/2019 3/31/2019 0.30 SLOT WELLPR CTOP P RD, cutting equipment operation 0.0 0.0 07:00 07:18 3/31/2019 3/31/2019 0.75 SLOT WELLPR CTOP P Install CTC, and pull test 35 k 0.0 0.0 07:18 08:03 3/31/2019 3/31/2019 0.45 SLOT WELLPR CTOP P Re -head BHI upper quick(77.5 0.0 0.0 08:03 08:30 1 1 meg/ohms, >2000) 3/31/2019 3/31/2019 0.25 SLOT WELLPR CTOP P PT re -head 4,500 psi 0.0 0.0 08:30 08:45 1 3/31/2019 3/31/2019 0.50 SLOT WELLPR CTOP P Stab into stump and pump 1 coil 0.0 0.0 08:45 09:15 volume forward @ 1.83 bpm at 3,299 psi, IA=110, OA=26, unstab INJH, park cart out of the way. 3/31/2019 3/31/2019 1.00 SLOT WELLPR PULD P PD fishing assembly 0.0 0.0 09:15 10:15 3/31/2019 3/31/2019 0.30 SLOT WELLPR PULD P Stab INJH, surface test BHI CoilTrak 0.0 81.3 10:15 10:33 tools (good -test) 3/31/2019 3/31/2019 1.75 SLOT WELLPR TRIP P RIH 81.3 9,760.0 10:33 12:18 Page 4135 Report Printed: 5/2812019 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Time End Time our (hr) Phase Op Code A Aty Code Time P -T -X Operadon Start Depth (ftKB) End Depth (WB) 3/31/2019 3/31/2019 0.20 SLOT WELLPR DLOG P Log formation correction of minus 4.0' 9,760.0 9,781.0 12:18 12:30 3/31/2019 3/31/2019 0.30 SLOT WELLPR TRIP P Continue IH 9,781.0 10,200.0 12:30 12:48 3/31/2019 3/31/2019 0.50 SLOT WELLPR CIRC P Circulate bottoms up @ 1.5 bpm at 10,200.0 10,200.0 12:48 13:18 3,100 psi, Diff -16 psi, WHP=36, BHP 3,651, IA=114, OA=27 3/31/2019 3/31/2019 0.50 SLOT WELLPR PRTS P Shut down pump, obtain static bottom 10,200.0 10,200.0 13:18 13:48 hole pressure 30 min - 10.09 ppg/3226 AP/W HP=235/6148.28' TVD, PUW 37 it 3/31/2019 3/31/2019 0.60 SLOT WELLPR JAR P RIH latch fish @ 10,235', jar down x1, 10,200.0 10,240.0 13:48 1424 jar up on fish x 1, jar down on fish x2, jar up on fish x 4, Pull up to 64 k, pump 1.9 bpm -10 bbl, Could not establish returns 3/31/2019 3/31/2019 2.90 SLOT WELLPR JAR P Continue to jar on fish. Stop every 5 10,240.0 10,199.0 14:24 1718 cycles and attempt to get circulation. Jar a total of 45 cycles, release fish 3/31/2019 3/31/2019 0.10 SLOT WELLPR TRIP P PUH to tie in 10,199.0 9,760.0 17:18 17:24 3/31/2019 3/31/2019 0.20 SLOT WELLPR DLOG P Log K1 for+7.5' 9,760.0 9,502.0 17:24 17:36 3/31/2019 3/31/2019 0.10 SLOT WELLPR TRIP P RIH to tag lop of fish @ 10,225'. 9,502.0 10,225.0 17:36 17:42 Release off fist 3/31/2019 3/31/2019 1.80 SLOT WELLPR TRIP P POOH 10,225.0 76.0 17:42 19:30 3/31/2019 3/31/2019 1.10 SLOT WELLPR PULD P At surface, Tag up and space out. 76.0 0.0 19:30 20:36 PJSM. PUD BHA#3 and lay down 3/31/2019 3/31/2019 0.80 SLOT WELLPR CTOP P PJSM. Lock out E -line. Remove UQC. 0.0 0.0 20:36 21:24 Boot wire. Stab on well. Perform slack mgmt 3/31/2019 3/31/2019 1.10 SLOT WELLPR CTOP P Unstab injecor.P/U hydraulic tubing 0.0 0.0 21:24 22:30 cutter. Trim CT for fatigue mgmt. Find e -line @ 38'. Trim 100' total 3/31/2019 3/31/2019 1.40 SLOT WELLPR CTOP P Test wire- good. Prep CT and install 0.0 0.0 22:30 23:54 connector. Pull test to 35K 3/31/2019 4/112019 0.10 SLOT WELLPR CTOP P Head up UQC 0.0 0.0 23:54 00:00 4/1/2019 4/1/2019 0.90 SLOT WELLPR CTOP P Complete reheading UQC. PT 0.0 0.0 00:00 00:54 connector to 4300 PSI 4/1/2019 4/1/2019 1.00 SLOT WELLPR PULD P PJSM, M/U and PD BHA #4 fishing 0.0 81.0 00:54 01:54 BHA. Check packoffs. Surface test BHA 4/1/2019 4/1/2019 2.00 SLOT WELLPR TRIP P RIH SHA#4, EDC open, pumping 1.5 81.0 9,760.0 01:54 03:54 BPM from surface 4/1/2019 4/1/2019 0.10 SLOT WELLPR DLOG P Log k1 for -4.5' correction, Close EDC 9,760.0 9,791.0 03:54 04:00 4/1/2019 4/1/2019 0.10 SLOT WELLPR TRIP P Continue in well 9,791.0 10,220.0 04:00 04:06 4/1/2019 4/1/2019 3.00 SLOT WELLPR JAR P Set down @ 10,220'. Did not latch up 10,220.0 10,220.0 04:06 07:06 first time. Bring pumps on. BPM and run in faster. Set down and latch. Jar up 3X. Paint red flag @ 51 K PUW. Line up to pump down backside. Go up to 1100 PSI WHP. Pull up to fire jars and dump pressure. No good. Jar 5X. Stop and pump 5 BBIs down coil. No circulation. Jar 5X up and down 4/1/2019 4/1/2019 0.50 SLOT WELLPR PULL P Continue jadng total of 30 cycles@ 10,220.0 10,195.0 07:06 07:36 10,199', hold in tention 60 k, 10,195', notice weight falloff slightly Page 5135 Report Printed: 5/2812019 - Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Time End Time Our (hr) Phase Op Code Activity Cada Time P -T -X Operation Start Depth (WB) End Depth (fm B) 4/1/2019 4/1/2019 0.50 SLOT WELLPR PULL P Continue working fish towards surface 10,195.0 9,753.0 07:36 08:06 75 k @ 3-5 fpm, notice weight change @ 10,145', continue pulling up to 9,975', 15-30 fpm, fish is pulling free 4/1/2019 4/1/2019 3.75 SLOT WELLPR PULL P Park with fish, discuss with town team, 9,753.0 9,753.0 08:06 11:51 plan forward to kill well, call out 10.5 ppg completion fluid. 10.5 ppg on location load into pits 4/112019 4/1/2019 1.20 SLOT WELLPR PULL P Second brine truck headed to the dg, 9,753.0 9,729.0 11:51 13:03 start displacing coil to 10.5 ppg kill fluid w/open EDC holding one for one 45 bbls, , shut down and close EDC, slowly PUH circulating 0.25 bpm 2 bbls, shutdown open EDC, bullhead 1.4 bbl, WHIP increased to 1,500 psi, shutdown pump, bleed pressure off, pull up hole to confirm fish is free, fish Ps free, Close the EDC, 4/1/2019 4/1/2019 0.50 SLOT WELLPR PULL P PU slow, pumping down the coil 0.2 9,729.0 9.699.0 13:03 13:33 bpm at 48 psi, CTSW=36.5 k, DHWOB=-2.2 k, close choke WHIP built to 1,000 psi shutdown pump, park and discuss with town team further. 4/112019 4/1/2019 0.20 SLOT WELLPR PULL P Attempt to RIH w/1000 psi WHIP, stack 9,699.0 9,717.0 13:33 13:45 out 5k CTSW, bleed pressure off WH 4/1/2019 4/1/2019 0.15 SLOT WELLPR PULL P Open EDC, PUH @ 2 fpm, seems fish 9,717.0 9,693.0 13:45 13:54 is still on. 4/1/2019 4/1/2019 1.00 SLOT WELLPR OWFF P Park, bleed pressure off, perform flow 9,693.0 9,693.0 13:54 14:54 1 1 check, well still flowing, 4/1/2019 41112019 0.30 SLOT WELLPR PULL P RBIH to tag @ 9,713' (Fish 9,693.0 9,71-3 0 14:54 15:12 depth=10,287') 4/1/2019 4/1/2019 1.50 SLOT WELLPR PULL P Circulate bottoms up, gas cut brine at 9,713.0 9,713.0 15:12 16:42 surface, take returns to tiger tank, bring back inside, 411/2019 4/1/2019 1.30 SLOT WELLPR OWFF P Perform flow check (no -flow) 9,713.0 9,713.0 16:42 18:00 4/112019 4/1/2019 2.00 SLOT WELLPR TRIP P Close EDC, pump 2 bbls down the 9,713.0 557.2 18:00 20:00 coil, shutdown, open EDC, circlulate through the EDC, 1.19 bpm at 1,477 psi, 0.80 bpm returns, POOH 4/1/2019 4/1/2019 0.60 SLOT WELLPR OWFF P PJSM, Check well for flow (no -flow) 557.2 557.2 20:00 20:36 4/1/2019 4/1/2019 1.25 SLOT WELLPR PULD P Brake down BOT fishing tools, check 557.2 444.9 20:36 21:51 the hole (good) 4/1/2019 4/112019 1.20 SLOT WELLPR PULD P LD, fish 2-318" solid liner no 444.9 0.0 21:51 23:03 centrilizers. 4/1/2019 4/2/2019 0.95 SLOT WELLPR PULD P PJSM, MU cleanout assembly, Stab 0.0 23:03 00:00 on well, Surface test tool 4/2/2019 4/2/2019 0.10 SLOT WELLPR PULD P Complete surface test tool 51.3 51.3 00:00 00:06 4/212019 4/2/2019 1.80 SLOT WELLPR TRIP P Trip in hole, BHA#5 Clean out BHA 51.3 9,730.0 00:06 01:54 with straight motor and D-331 4/212019 412/2019 0.20 SLOT WELLPR DLOG P Log gamma tie in for -2', Close EDC 9,730.0 9,769.0 01:54 02:06 4/2/2019 4/2/2019 0.30 SLOT WELLPR TRIP P Continue in well 9,769.0 10,220.0 02:06 02:24 4/2/2019 4/2/2019 1.30 SLOT WELLPR CIRC P 10220'. Displace to 8.8 PPG milling 10,220.0 10,210.0 02:24 03:42 fluid slowly recip up hole 4/2/2019 4/2/2019 0.20 SLOT WELLPR TRIP P 102101, Wt check @ 35K, RIH min 10,210.0 10,276.0 03:42 03:54 rate. Tag dill @ 10,276 Page 6/35 ReportPrinted: 5128120119 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log I Sten DepthDePth startTime End Time our (ho Phase Op Corte Aalvly Cale Time P -T -X Operation End 4/2/2019 4/2/2019 1.80 SLOT WELLPR OTHR P Bring(0,2) pumps on 1.85 BPM @ 3629 10,276.0 10,442.0 10,4 2.0 03:54 05:42 PSI FS. Start clean out. Taking 25' bites. Parafin coming across shaker at first bottoms up 4/2/2019 4/2/2019 0.50 SLOT WELLPR OTHR P Washing down set down @ 10442. 10,442.0 10,442.0 05:42 06:12 PUH slowly to 10356. RBIH and tag up 10442. DHWOB=2K. 4/2/2019 4/2/2019 0.90 SLOT WELLPR OTHR P Pump sweeps, PUH slowly circ 10,442.0 10,442.6 06:12 07:06 bottoms up 4/2/2019 4/2/2019 0.50 SLOT WELLPR MILL P Hole circulated clear, Bring pumps on 10,442.6 10,443.0 07:06 07:36 1.88 BPM @ 3635 PSI FS, BHP=3540, DHWOB=2K 4/2/2019 4/2/2019 0.30 SLOT WELLPR MILL P Pick up off bottom to reset. to hard to 10,443.0 10,443.0 07:36 07:54 be fill. Reset. Set back down 2.51K DHWOB, 1.88 BPM @ 3635 PSI FS. BHP=3540 4/2/2019 4/2/2019 0.50 SLOT WELLPR MILL P 10443, Metal on shaker, PUH consult 10,443.0 10,444.0 07:54 08:24 town eng. RBIH dry. Set down @ 10444 attempt to move down. Set 8K. 4/2/2019 4/2/2019 2.80 SLOT WELLPR TRIP P Trip out of well 10,444.0 46.0 08:24 11:12 4/2/2019 4/2/2019 1.20 SLOT WELLPR PULD P At surface, PJSM, PUD BHA#5, Lay 46.0 0.0 11:12 12:24 down motor. Mill out 2.80 NO Go 4/2/2019 4/2/2019 1.30 SLOT WELLPR SLKL P Move in / spot up slickline unit 0.0 0.0 12:24 13:42 4/2/2019 4/2/2019 2.40 SLOT WELLPR SLKL P PJSM, R/U slickline unit, full pressure 0.0 0.0 13:42 16:06 control equipment on dg floor 4/2/2019 4/2/2019 1.90 SLOT WELLPR SLKL P PT slick line lubricator to 2500 PSI - 0.0 0.0 16:06 18:00 RIH with 2.47 LIB, POOH after tagging @ 10,462' SL depth 4/2/2019 4/2/2019 0.50 SLOT WELLPR SLKL P PJSM, pop off lubricator, LD LIB, 0.0 0.0 18:00 18:30 Picutes on S: Drive, confer w/ SL supervisor & town, decision made to to run non -retrievable spear. 4/2/2019 4/2/2019 0.40 SLOT WELLPR SLKL P PU non -retrievable spear 0.0 0.0 18:30 18:54 4/2/2019 4/2/2019 2.10 SLOT WELLPR SLKL P RIH w/ spear, attempt to spear into 0.0 0.0 18:54 21:00 fish, spang dawn for -45 min, unable to latch into fish, POOH to inspect tool 4/2/2019 4/2/2019 0.60 SLOT WELLPR SLKL P LD tools, small scratches on face of 0.0 0.0 21:00 21:36 grapple, decision made to run 1-1/2" braided line brush "Test non -retrievable spear on 4' piece of liner at surface to ensure engagment is possible, engages as designed 4/2/2019 4/2/2019 0.70 SLOT WELLPR SLKL P MU braided line brush 0.0 0.0 21:36 22:18 4/2/2019 4/2/2019 0.20 SLOT WELLPR SLKL P PU braided line brush, stab on 0.0 0.0 22:18 22:30 lubricator, PT 4/2/2019 4/2/2019 1.20 SLOT WELLPR SLKL P RIH w/ braided line brush, run tool into 0.0 0.0 22:30 23:42 fish, see overpull of brushes in PU's 4/2/2019 4/3/2019 0.30 SLOT WELLPR SLKL P Begin POOH (to PU non -retrievable 0.0 0.0 23:42 00:00 spear) 4/3/2019 4/3/2019 0.10 SLOT WELLPR SLKL P Complete POOH 0.0 0.0 00:00 00:06 4/3/2019 4/3/2019 0.20 SLOT WELLPR SLKL P Pop off lubicalor & LD tools, tattle tails 0.0 0.0 00:06 00:18 bent back, marking on 2.20" swedge at -5' up tool, appear to have engaged fish, retrieved 2 small steal fish pieces Page 7135 ReportPrinted: 5/26/2019 Operations Summary (with Timelog Depths) 1c-11 16 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Stert Time End Time Dur ht ( ) phase Op Cade Activity Code Tme P -T -X Operation Sten Depth en(WEI)De End Depth (flKa) 4/3/2019 4/3/2019 1.30 SLOT WELLPR SLKL P PU non -retrievable spear, PT, RIH, 0.0 0.0 00:18 01:36 latched into fish, jarred up -25 times, sheared off spear (GR), no movement of fish 4/3/2019 4/3/2019 0.60 SLOT WELLPR SLKL P POOH 0.0 0.0 01:36 02:12 4/3/2019 4/3/2019 2.50 SLOT WELLPR SLKL P PU 3" GS, RIH, latch into fish, jar on 0.0 0.0 02:12 04:42 fish for 1.25 hrs, unable to move fish, shear off fish ••BOT on the way to fish on coil 413/2019 4/3/2019 0.60 SLOT WELLPR SLKL P POOH 0.0 0.0 04:42 05:18 413/2019 4/3/2019 1.10 SLOT WELLPR SLKL P At surface, Bleed off lubricator. Lay 0.0 0.0 05:18 06:24 down slick line equipment. Put lubricator in pipe shed 4/3/2019 4/3/2019 1.40 SLOT WELLPR PULD P M/U BHA#6. Fishing BHA with weight 0.0 67.0 06:24 07:48 bars, accelorator, Jars, and GS spear. Pressure deploy. make up to coil and surface test. Tag up and set counters 4/3/2019 4/3/2019 1.80 SLOT WELLPR TRIP P Trip in hole, EDC open 67.0 9,745.0 07:48 0936 4/3/2019 4/3/2019 0.10 SLOT WELLPR DLOG P Log Gamma tie in for -3' 9,745.0 9,770.0 09:36 09:42 4/3/2019 4/3/2019 0.10 SLOT WELLPR TRIP P Continue in well, Close EDC @ 10225 9,770.0 10,441.0 09:42 09:48 4/3/2019 4/3/2019 0.50 SLOT WELLPR JAR P Set down and lift off fish. Set back 10,441.0 10,050.0 09:48 10:18 down and latch. PIU to 50K and fire jars. Pull up to 59K and start moving fish uphole 4/3/2019 4/3/2019 2.00 SLOT WELLPR TRIP P 10,050 stop, open EDC. See slight 10,050.0 59.0 10:18 1218 overpull @ 10,189 milled nipple. Hang up in SSSV @ 2308. Shut EDC. Work down out of SSSV. Bring control pressure up to 5K PSI. Work free down. PUH and hung up in SSSV. Cock jars down. PUH jars fire @ 43K continue out of hole 413/2019 4/3/2019 2.30 SLOT WELLPR PULD P Al surface tag up and space out. PUD 59.0 0.0 12:18 14:36 BHA #6. Have fish. Length 20.38'. Jet cut end Flared to 2.752. Overall fish recovered 465.28' 4/3/2019 4/3/2019 1.00 SLOT WELLPR PULD P PJSM, Complete HES slickline rig 0.0 0.0 14:36 15:36 down. Remove spear from fish 4/3/2019 4/3/2019 1.40 SLOT WELLPR PULD P PJSM. P/U BHA #7 FCO with straight 0.0 51.3 15:36 17:00 motor and D331 mill and PD. Chek pack offs - Good 4/3/2019 4/3/2019 1.70 SLOT WELLPR TRIP P RIH BHA#7 51.3 9,730.0 17:00 18:42 4/3/2019 4/3/2019 0.20 SLOT WELLPR DLOG P Log Kt for -2' correction, close EDC 9,730.0 9,760.0 18:42 18:54 4/3/2019 413/2019 1.60 SLOT WELLPR TRIP P Continue FCO, PUW = 37 @ 10,200', 9,760.0 10,717.0 18:54 20:30 1.85 bpm, FS = 290 psi, circ = 3656 psi, WHP = 20 psi, significant asphaltenes over shaker, pump 5x5 sweeps, taking bites & picking up, drop in MW out, begin taking returns to tiger -tank (pinch in choke), cleans up, begin taking returns back inside Page 8135 Report Printed: 5/2 812 01 9 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Depth Stmt Time End Time Dur (hr) phase Op Code Activity Cale Time PJA Operation (flKB) Ertl Depth (flKB) 4/3/2019 4/3/2019 1.40 SLOT WELLPR CIRC P Continue FCO, clean down to 10,717' 10,717.0 10,425.0 20:30 21:54 & hard tag, PUW = 37K, pump 5x5 sweeps, recip WS setting area, circulate 2 bottoms up, asphallenes clean-up over shakers PJSM w/ LRS for hot diesel flush 4/3/2019 413/2019 0.30 SLOT WELLPR DLOG P Log K1 for O' correction, RIH to bottom 10,425.0 10,690.0 21:54 22:12 4/3/2019 4/4/2019 1.80 SLOT WELLPR CIRC P Begin circulating 100 bbl of 180° 10,690.0 10,690.0 22:12 00:00 diesel (1.5 bpm) 4/4/2019 4/4/2019 0.30 SLOT WELLPR CIRC P Complete diesel circulation, chased w/ 10,690.0 10,690.0 00:00 00:18 DuoVis, 4/4/2019 4/4/2019 2.00 SLOT WELLPR TRIP P POOH, tag up, open EDC failed, 10,690.0 51.0 00:18 02:18 PJSM undeploy w/ failed checks 4/4/2019 4/4/2019 1.40 SLOT WELLPR PULD P PUD BHA#7 & LD tools, mill came out 51.0 0.0 02:18 03:42 2.80" no-go, PJSM 4/4/2019 4/4/2019 0.70 SLOT WELLPR PULD P PU BHA #8 Caliper (HES real-time), 0.0 24.0 03:42 04:24 slide in cart, check pack -offs, MU to coil, tag up, set counters 4/4/2019 4/412019 2.20 SLOT WELLPR TRIP P RIH wl BHA#8 24.0 10,707.0 04:24 06:36 4/4/2019 4/4/2019 0.50 SLOT WELLPR DLOG P 10,707', Line up across the top, Open 10,707.0 10,130.0 06:36 07:06 caliper finger. Log up 25 FPM 4/4/2019 4/4/2019 0.10 SLOT WELLPR TRIP P Close finger. RBIH 10,130.0 10,350.0 07:06 07:12 4/4/2019 4/4/2019 0.20 SLOT WELLPR DLOG P Open fingers. relog 10,350 to 10,121 10,350.0 10,121.0 07:12 07:24 for comparison 4/4/2019 4/4/2019 1.70 SLOT WELLPR TRIP P Close caliper fingers. Trip out of hole 10,121.0 22.0 07:24 09:06 4/4/2019 4/4/2019 0.70 SLOT WELLPR PULD P At surface, PJSM, Shut swab. Unstab 22.0 0.0 09:06 09:48 injector. Lay down caliper and camera adapter 4/4/2019 4/4/2019 2.20 SLOT WELLPR CTOP P Pull floats from UQC. Stab injector on 0.0 0.0 09:48 12:00 well. Jet stack roll CT to water. Unstab injector. Fluid pack BOPE obtain shell test 4/4/2019 4/4/2019 6.00 SLOT WELLPR BOPE P Start full BOPE test, perform draw- 0.0 0.0 12:00 18:00 down test, test IRV. Test witness waived by Matt Herrera, AOGCC, " 250 low / 3500 high 4/4/2019 4/4/2019 1.20 SLOT WELLPR CTOP P Roll coil to drilling fluid, pop off 0.0 0.0 18:00 19:12 injector, install checks in UQC, load BOT tools onto ng, bring tools to rig Floor, PJSM 4/4/2019 414/2019 0.90 SLOT WELLPR PULD P PD BHA #9 Haily Under -Reamer 0.0 66.0 19:12 20:06 (4.10" & 4.7" blades), slide in cart, check pack -offs, MU to coil, tag up, set counters 4/4/2019 4/4/2019 1.90 SLOT WELLPR TRIP P RIH wl BHA#9 66.0 10,435.0 20:06 22:00 41412019 4/4/2019 0.10 SLOT WELLPR DLOG P Log K1 for 4correction, close EDC, 10,435.0 10,474.0 22:00 22:06 I PUW = 35K 4/4/2019 4/4/2019 0.20 SLOT WELLPR TRIP P Continue RIH, RIW = 12.2K 10,474.0 10,660.0 22:06 22:18 1 Page 9135 ReportPrinted: 5/28/2019 - Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Time EM Time Dur(hn Phase Op Code Activity Cotle Time P -T- 0 peradon Sten Depth rt De End Depth (WO) 4/4/2019 4/4/2019 1.00 SLOT WELLPR UREM P Under -reaming, start at 1 fpm, 1.87 10,660.0 10,681.0 22:18 23:18 bpm, dp = 1420 psi, annular = 3658 psi, pump = 4610 psi, CWT = 11.51K, WOB = 0.6K, vibrations into red Stall at 10,679', PUW = 38K, out rate dropped (from 1,8 bpm to 1.64 bpm), rate out continues to drop to 1.36 bpm, stall at 10,681', PUW = 37K, annular increasing, packing off, significant cement over shakers 4/4/2019 4/5/2019 0.70 SLOT WELLPR UREM P Continue under -reaming, reduce 10,681.0 10,687.0 23:18 00:00 speed to .2 fpm, dp = 1313 psi, annular = 3973 psi, pump = 4781 psi, annular dropped & rate out increased back to 1.8 bpm 4/5/2019 4/5/2019 1.80 SLOT WELLPR UREM P Continue under -reaming from 10,687' 10,687.0 10,700.0 00:00 01:48 @ 0.2 fpm, dp = 1283 psi, 1.84 bpm in, 1.79 bpm out, annular = 3619 psi, pump = 4341 psi, CWT = 8.5K, WOB =1K Stall at 10,690', 10,694', 10,699', again at 10,698' getting to bottom, ream to 10,700' 4/5/2019 4/5/2019 0.40 SLOT WELLPR UREM P Back -ream up to 10,600'@ 5 fpm, 10,700.0 10,600.0 01:48 02:12 PUW = 39K 4/5/2019 4/5/2019 1.10 SLOT WELLPR UREM P Under -ream from 10,600', dp = 1275 10,600.0 10,660.0 02:12 03:18 psi, pump = 4387 psi, 98% returns, start at 0.2 fpm, walk up to 0.5 fpm, then 1 fpm, vibrations to 4, pump 5x5 sweeps 4/5/2019 4/5/2019 0.30 SLOT WELLPR UREM P Back -ream @ 5 fpm, PUW = 38K 10,660.0 10,600.0 03:18 03:36 4/512019 4/5/2019 2.30 SLOT WELLPR TRIP P Open EDC, POOH 10,600.0 66.0 03:36 0554 4/5/2019 4/5/2019 1.10 SLOT WELLPR PULD P PJSM, PUD BHA *9. All under reamer 66.0 7-0- 05:54 0700 blades intact 4/5/2019 4/5/2019 0.90 SLOT WELLPR PULD P M/U HES caliper, Stab on and surface 0.0 22.7 07:00 0754 test. 4/5/2019 4/5/2019 2.10 SLOT WELLPR TRIP P RIH BHA#10 22.7 10,704.0 07:54 1000 4/5/2019 4/5/2019 0.30 SLOT WELLPR DLOG P 10,704'. Open caliper arms. Log 10,704.0 10,148.0 10:00 10:18 uphole. Close caliper arms 4/5/2019 4/5/2019 1.70 SLOT WELLPR TRIP P Trip out of well 10,148.0 22.0 10:18 12:00 4/5/2019 4/5/2019 0.50 SLOT WELLPR PULD P PJSM. Pull BHA #10 from well 22.0 0.0 12:00 12:30 4/512019 4/5/2019 1.20 SLOT WELLPR PULD P M/U Whipstock in pipe shed/ Plan 0.0 0.0 12:30 1342 change reset motor back to 0" and pick up under reamer 4/5/2019 4/5/2019 1.30 SLOT WELLPR PULD P PJSM, PDBHA#11 Underreameron 0.0 66.0 13:42 15:00 straight motor, Make up injector and surface test. 4/5/2019 4/5/2019 1.70 SLOT WELLPR TRIP P RIH BHA#11, EDC open. Pumping 66.0 9,730.0 15:00 16:42 min rate 4/5/2019 4/5/2019 0.10 SLOT WELLPR DLOG P Log gamma lie in for 4.5 9,730.0 9,770.0 16:42 16:48 I 4/5/2019 4/5/2019 0.30 SLOT WELLPR TRIP P Continue RIH to 10,600' 9,770.0 10,660.0 16:48 17:06 Page 10135 ReportPrinted: 5/28/2019 Operations Summary (with Timelog Depths) T Y'FW" 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Depth Start Time End Time Dur (hr) Phase Op Code Activity Code Time P -T -X Operation (W[3) End Dept (ftK8) 4/5/2019 4/5/2019 1.50 SLOT WELLPR UREM P Under -reaming, dp = 1249 psi, annular 10,660.0 10,700.0 1706 1836 = 3610 psi, pump =4368 psi, 1 fpm from 10,660'to 10,700', back -ream to 10,680', under -ream down to 10,700' @ 0.5 fpm " Cement over shakers (trace asphaltenes, very little metal) 4/5/2019 4/5/2019 0.30 SLOT WELLPR UREM P Back -ream up to 10,600' (5 fpm) 10,700.0 10,600.0 18:36 18:54 4/5/2019 4/5/2019 1.80 SLOT WELLPR UREM P Under -ream from 10,600'to 10,660' (1 10,600.0 10,680.0 18:54 2042 fpm), slow to 0.5 fpm from 10,660' to 10,680' "Stall @ 10,668', PUW = 37K 4/5/2019 4/5/2019 0.30 SLOT WELLPR UREM P Back -ream 10,680'to 10,600' (5 fpm), 10,680.0 10,600.0 20:42 21:00 PUW = 37K 4/5/2019 4/5/2019 1.60 SLOT WELLPR UREM P Under -ream from 10,600'to 10,700' (1 10,600.0 10,700.0 21:00 2236 fpm), pump 5x5 sweeps, open EDC 4/5/2019 4/6/2019 1.40 SLOT WELLPR TRIP P Begin POOH, PUW = 36K 10,700.0 2,600.0 22:36 00:00 4/6/2019 4/6/2019 0.60 SLOT WELLPR TRIP P Complete POOH 2,600.0 66.0 00:00 0036 4/6/2019 4/6/2019 1.20 SLOT WELLPR TRIP P PJSM, PUD BHA #11, LD tools 66.0 0.0 00:36 01:48 4/6/2019 4/6/2019 1.10 PROD1 RPEQPT PULD P PD BHA#12 WS Assembly, slide in 0.0 75.0 01:48 02:54 cart, check pack -offs, MU to coil, tag up, set counters 4/6/2019 4/6/2019 1.80 PROD1 RPEQPT TRIP P RIH w/ BHA #12 75.0 10,420.0 02:54 04:42 4/6/2019 4/6/2019 0.20 PROD1 RPEQPT CLOG P Log K1 for -3.5' correction 10,420.0 10,476.0 04:42 04:54 4/6/2019 4/6/2019 0.20 PROD1 RPEQPT TRIP P Continue RIH, arrive at setting depth, 10,476.0 10,697.0 04:54 05:06 PUW = 35K, close EDC, RBIH, bring up pump, shear off at 3700 psi, set - down 5K WOB, TOWS -10,684' 4/6/2019 4/6/2019 1.80 PROD1 RPEQPT TRIP P POOH w/ BHA #12, PUW = 35K 10,697.0 69.0 05:06 0654 4/6/2019 4/6/2019 1.10 PROD1 RPEQPT PULD P Tag up and space out. PJSM PUD 69.0 0.0 06:54 08:00 1 1BHA#12 Whipstock setting tools 4/6/2019 4/6/2019 1.30 PRODi WHPST WPST P M/U BHA#13 with .6° AKO motor, 0.0 74.7 08:00 09:18 2.80 DSM, 2.79 String reamer, and 10' pup. Pressure deploy. Make up to coil and surface test 4/6/2019 4/6/2019 1.90 PROD1 WHPST WEST P RIH BHA#13 74.7 10,440.0 0918 1112 4/6/2019 4/6/2019 0.20 PROD1 WHPST WEST P Log K1 for -4.5', Close EDC, 10,440.0 10,477.0 11:12 11:24 PUW=36K 4/6/2019 4/6/2019 0.20 PROD1 WHPST WPST P Continue in well, Dry tag @ 10688. 10,477.0 10,688.0 11:24 11:36 1 1 IPUH 4/6/2019 4/6/2019 4.20 PROD1 WHPST WPST P PUH bring pump on 1.9 BPM @ 4024 10,688.0 10,692.8 11:36 1548 PSI FS, BHP=3668, Ease onto tray call pinch point 10,688.5. 4/6/2019 4/6/2019 2.20 PROD1 WHPST WPST P DHWOB fall off. Call bottom of 10,692.8 10,695.8 15:48 1800 window. Continue time milling for string reamer exit 4/6/2019 4/6/2019 0.90 PROD1 WHPST WPST P Begin pushing on it w/ string reamer 10,695.8 10,711.0 18:00 1854 out, milling rat -hole, CWT = 11.8K, WOB = 1.3K, pump = 4114 psi, annular = 33722 psi, WHP = 18 psi Page 11135 ReportPrinted: 5128/2019 Operations Summary (with Timelog Depths) IC-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Depth Start Time End Time our(hr) Phase Op Code Acdelry Cade rima P.T-x Operadon (aKB) End Depth(ftKB) 4/6/2019 4/6/2019 1.80 PRODt WHPST REAM P Dress window (HS, 30R, 30R, & 10,711.0 10,711.0 1854 20:42 180°), 1 fpm, dry drift window up & down, clean, tag TD of rat-hole, pump sweeps, PUW = 36K 4/6/2019 4/6/2019 1.90 PROD1 WHPST TRIP P Open EDC, POOH w/ BHA #13, PJSM 10,711.0 75.0 20:42 22:36 4/6/2019 4/6/2019 1.00 PRODi WHPST PULD P PUD BHA#13, mill came out 2.80" no- 75.0 0.0 22:36 23:36 go, string reamer came out 2.79" po- go 4/6/2019 4/7/2019 0.40 PROD1 DRILL PULD P Begin PD BHA#14 Build/Turn 0.0 72.0 23:36 00:00 Assembly (2.2" AKO motor, RB Dynamus bit) 4/7/2019 4/7/2019 0.70 PRODt DRILL PULD P Complete PD BHA#14 Build/Turn 0.0 72.0 00:00 00:42 Assembly (2.2" AKO motor, RB Dynamus bit), slide in cart, check pack -offs, MU to coil, tag up, set counters 4/7/2019 4/7/2019 2.20 PROD1 DRILL TRIP P RIH w/ BHA #14 72.0 10,425.0 00:42 02:54 4/7/2019 4/7/2019 0.20 PROD1 DRILL DLOG P Log K1 for 4correction, close EDC, 10,425.0 10,463.0 02:54 03:06 1 PUW = 35K 4/7/2019 4/7/2019 0.10 PROD1 DRILL TRIP P Cotninue RIH 10,463.0 10,711.0 03:06 03:12 4/7/2019 4/7/2019 1.20 PROD1 DRILL DRLG P Drilling, FS = 535 psi @ 1.9 bpm, 10,711.0 10,805.0 03:12 04:24 CWT = 10.5K, WOB = 2.31K, annular = 3788 psi, WHIP = 79 psi, pump = 4161 psi, 98% returns, pump 5x5 sweeps, begin losing -0.1 bpm @ 10,799', drill to called TD of 10,805' 4/7/2019 4/7/2019 0.20 PROD1 DRILL TRIP P PUH to log K1 & RA, PUW = 38K 10,805.0 10,425.0 04:24 04:36 4!7/2019 4/7/2019 0.40 PRODi DRILL DLOG P Log K1 for 0' correction, log RA at 10,425.0 10,725.0 04:36 05:00 10,691' TOWS = 10,684', BOW = 10,692, RA = 10,691.5' 4/7/2019 4/7/2019 1.80 PROD1 DRILL TRIP P POOH, PUW=37K 10,725.0 67.0 05:00 06:48 4/7/2019 4/7/2019 1.30 PRODt DRILL TRIP P At surface, Tag up and space out. 67.0 0.0 06:48 08:06 PJSM. PUD BHA#14 Build section BHA 4/7/2019 4/7/2019 0.80 PROD1 DRILL OTHR P M/U Nozzle. Slab on well. Jet stack. 0.0 0.0 08:06 08:54 Flush micro motion. Pull off well. Change out floats in UQC 4/7/2019 4/7/2019 1.20 PROD1 DRILL PULD P PJSM. M/U Mill, Motor, and FVS and 0.0 78.2 08:54 10:06 scribe. PD BHA #15 lateral BHA with .5" AKO motor, agitator, and RB HYC A3 bicenter. Make up to coil and surface test 4/7/2019 4/7/2019 2.10 PRODt DRILL TRIP P RIH, Shallow test agitator @ 300'. 78.2 10,445.0 10:06 1212 1 1 1 Continue in well 4/7/2019 4/7/2019 0.10 PROD1 DRILL DLOG P Log Kt for 4.5', Close EDC, 10,445.0 10,464.0 12:12 12:18 PUW=36K 4/7/2019 4/7/2019 0.20 PRODi DRILL TRIP P Continue in well, Clean pass through 10,464.0 10,803.0 12:18 12:30 window 4/7/2019 4/7/2019 0.80 PROD1 DRILL DRLG P 10803', Drill ahead, 1.9 BPM @ 5057 10,803.0 10,864.0 12:30 13:18 PSI FS, BHP=3833. New mud @ bit 10,844' 477/2019 4/7/2019 0.10 PROD1 DRILL WPRT P Pull BHA wiper, PUW=35K. 10,864.0 10,864.0 13:18 13:24 4/772019 4/7/2019 1.90 PROD? DRILL DRLG P New mud around, 1.9 BPM @ 10,864.0 11,000.0 13:24 15:16 1 4634PSI FS, BHP=3807. RIW=10.5K, DHWOB=1.5K Page 12135 ReportPrinted: 512812019 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Stan Deem Start Time End Time Our (hr) Pha&e Op Code Activity Code Time P -T -X Operation (HKB) End Oepm(f1KB) 4/7/2019 4/7/2019 2.40 PROD! DRILL DRLG P Start continuous rotating drilling 11,000.0 11,205.0 15:18 17:42 11,000'- 11,155', 1.9 BPM @ 4634 PSI FS, BHP=3840 4/7/2019 4/7/2019 0.20 PROD1 DRILL WPRT P Wiper up -hole, PUW = 37K 11,205.0 10,813.0 17:42 17:54 4/7/2019 4/7/2019 0.20 PROD1 DRILL WPRT P Wiper in-hole, RIW = 13K 10,813.0 11,205.0 17:54 18:06 4/7/2019 40/2019 1.70 FROM DRILL DRLG P Drilling, FS = 1303 psi at 1.9 bpm, 11,205.0 11,290.0 18:06 19:48 CWT = 11.5K, WOB = 1.6K, annular = 3846 psi, WHP = 114 psi, pump = 4955, -100% returns, avg ROP = 50 fph Drilling a bit ratty, clays/sands in samples, 50K PUW from 11,241', increase to 6% KCI 4/7/2019 4/7/2019 1.50 FROM DRILL DRLG P Continue drilling from 11,290, CWT= 11,290.0 11,370.0 19:48 21:18 8.1 K, WOB = 2.85K, annular = 3855 psi, WHP = 119 psi, pumps 5x5 sweeps, 1 00'wiper from 11,357', PUW = 39K, PUW = 45K from 11,370', avg ROP = 53 fph Holding -87° Inc in attempt to acquire the Ct prior to Fault 1 crossing (per geology) 4/7/2019 4/7/2019 1.70 FROM DRILL DRLG P PUW =45K from 11,370', pull heavy to 11,370.0 11,467.0 21:18 23:00 52K break -over Drilling, CWT = 10.8K, WOB = 1.91K, annular = 3851 psi, WHP = 78 psi, PU's as required, avg ROP = 71 fph 4/712019 4/8/2019 1.00 FROM DRILL DRLG P Continuous rotation drilling, CWT = 11,467.0 11,511.0 23:00 00:00 1 OK, WOB = 1.71K, annular = 3875 psi, WHP = 69 psi, avg ROP = 44 fph 4/8/2019 4/8/2019 1.50 FROM DRILL DRLG P Continuous rotation drilling from 11,511.0 11,600.0 00:00 01:30 11,511', CWT =7.4K, WOB =2.5K, annular = 3877 psi, WHP = 66 psi, pump sweeps, avg ROP = 60 fph 4/8/2019 4/8/2019 0.30 PRODt DRILL WPRT P Wiper up -hole, PUW =40K 11,600.0 10,800.0 01:30 01:48 4/8/2019 4/8/2019 0.60 PROD1 DRILL WPRT P Wiper in-hole, will stacked at 11,400', 10,800.0 11,600.0 01:48 0224 no WOB, PUW = 50K, reduce rate to get through & bring back up quickly, RIW = 9.9K 4/8/2019 4/8/2019 1.60 PROD? DRILL DRLG P BOBD (non oscillating to acquire 11,600.0 11,697.0 02:24 04:00 targets) FS = 1190 psi @ 1.85 bpm, CWT = 10.21K, WOB = 1.31K, annular = 3892 psi, WHP = 20 psi Confer w/ town geology, decsion made drop to 84° Inc (target deeper in C1 prior to fault crossing) 418/2019 4/8/2019 0.60 PROD1 DRILL WPRT T Rig Link crashed, PU off bottom, PUW 11,697.0 11,697.0 04:00 04:36 = 43K, pulled heavy to 63K at 11,620' (at 7 fpm), pump 5x5 sweeps, reboot, resolve issue, RIW = 8.71K 4/8/2019 418/2019 3.00 FROM DRILL DRLG P Drilling, FS = 1107 psi @ 1.9 bpm, 11,697.0 12,000.0 04:36 07:36 CWT =8.6K, WOB =1.4K, annular= 3864 psi, pump = 4784 psi, drilling break at -11,691 PUW = 41 K from 11,756' Page 13135 Report Printed: 5/28/2019 Operations Summary (with Timelog Depths) 1c-11 qW Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Depth Start Time EndTime Dur(hn Phase Op Cole ActiWy Corle Time P -T -X Operation (ftKB) End Depth(flKB) 4/8/2019 4/8/2019 1.20 PROD1 DRILL WPRT P Wiper to window with tie into RA 12,000.0 12,006.0 07:36 08:48 marker for a +7• correction. Some slight overpulls coming up. RBIH stacking multiple times. Reduce rate to gel lhroigh 11,450, 11496' 4/8/2019 4/8/2019 3.50 PROD1 DRILL DRLG P 12,006', Drill 1.9 BPM @ 4742 PSI 12,006.0 12,400.0 08:48 12:18 FS, BHP=3930, RIW=7.2K, DHWOB=2K. 12059' start working rotation 4/8/2019 4/8/2019 0.30 PROD1 DRILL WPRT P 12,400', 800 foot wiper with 5 X 5 12,400.O 11,592.0 12:18 12:36 sweeps, PUW=44K 4/8/2019 4/8/2019 1.80 PROD1 DRILL WPRT P RBIH, Stack out @ 11,941. Unable to 11,592.0 12,400.0 1236 14:24 get past at various rates and speeds. P/U heavy at 68K and dragging. -12K DHWOB. Pump more sweeps and circ bottoms up. Normal material on shakers at bottoms up Work through bad area 11940 to 12,070. Min rate, Continue to bottom at full rate 4/8/2019 4/8/2019 0.50 PROD1 DRILL DRLG P 12400 Drill, 1.84 BPM @ 4722 PSI 12,400.0 12,450.0 14:24 14:54 FS, BHP=3937, Goto rotation @ 10430'. 4/8/2019 4/8/2019 2.70 PROD1 DRILL DRLG P 12450'. Increase inclination to 100° 12,450.0 12,628.0 1454 17:36 turn up to cross cut. 1.84 BPM @ 4722 PSI FS, BHP=3954, 4/8/2019 4/8/2019 0.70 PROD1 DRILL WPRT P Pull wiper to 12,400. Staking, 12,628.0 12,628.0 1736 18:18 PUW=53K 4/8/2019 4/8/2019 3.20 PROD1 DRILL DRLG P 12628', Drill, 1.89 BPM @ 4918 PSI 12,628.0 12,796.0 1818 21:30 FS, BHP=3970, RIW-.8K, DHWOB=I.8K. Hard to get drilling 4/8/2019 4/8/2019 0.70 PROD? DRILL WPRT P 12796', Wiper trip to 12,300'. 12,796.0 12,795.0 21:30 22:12 PUW=55K 4/8/2019 4/8/2019 0.60 PROD1 DRILL DRLG P 12795', Drill, 1.84 BPM @ 4810 PSI 12,795.0 12,822.0 22:12 22:48 FS, BHP=3978 4/8/2019 4/9/2019 1.20 PROD1 DRILL DRLG P 12822, Drill, 1.84 BPM @ 4810 PSI 12,822.0 12,860.0 22:48 00:00 FS, BHP=4025, New mud going down coil 4/9/2019 4/9/2019 0.60 PROD? DRILL DRLG P Difficulty starting drilling, WOB w/ no 12,860.0 12,880.0 0000 00.36 motorwork, drilled to called TD of 12,880', pump 10x10 sweeps 4/9/2019 4/9/2019 2.90 PROD1 DRILL TRIP P POOH, PUW = 38K, open EDC in 12,880.0 78.0 00:36 03:30 cased hole, PJSM, pre -load DS PDL 4/9/2019 4/9/2019 1.00 PROD1 DRILL PULD P PUD BHA#15, bit came out a 1-1 78.0 0.0 0330 04:30 " UT coil (thinnest @ .165"), inspect injector 4/9/2019 4/9/2019 2.00 PROD2 STK PULD P PU/PD BHA#16 OH Anchored Billet, 0.0 72.0 04:30 06:30 failed checks, PUD, & redeploy, check pack -offs " Crew chage 4/9/2019 4/9/2019 2.10 PROD2 STK TRIP P RIH w/ BHA #16 72.0 10,445.0 06:30 08:36 4/9/2019 4/9/2019 0.40 PROD2 STK DLOG P Log K1 for +1 5'correction, clean 10,445.0 10,495.0 0836 0900 counter wheel, PUW = 37K Page 14135 Report Printed: 5/28/2019 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Depth Stan Time End Time our thin Phase Op Cotle Activity Cone Time P -T-% Operation (WS) End Depth (WS) 4/9/2019 4/9/2019 0.80 PROD2 STK TRIP P Continue RIH, park at window, Gose 10,495.0 11,050.0 09:00 09:48 EDC, RIH & stack weight 10,744', PUW = 40K, dragging -3.7K WOB, RBIH, setdown at 10757'10760', 10762', continue working through 10,802' Arrive at setting depth, PU 36K, bring on pumps, shear off at 4200 psi, set down 4K WOB, TOB -11,050', oriented HS 4/9/2019 4/9/2019 1.80 PROD2 STK TRIP P POOH, open EDC, PJSM 11,050.0 78.0 09:48 11:36 4/9/2019 4/9/2019 1.00 PROD2 STK PULD P PUD BHA #16, bit came out a ... 78.0 0.0 11:36 12:36 4/9/2019 4/9/2019 0.40 PROD2 STK BOPE P Suck out stack, PU test jnt, function 0.0 0.0 12:36 13:00 test BOP'S, LD test jnt 4/9/2019 4/9/2019 1.30 PROD2 STK PULD P PD BHA#17 KO/Drilling Assembly 0.0 78.0 13:00 14:18 (Agitator, 0.5° AKO motor, new HYC A3 bit), slide in can, chaged out pack - offs, MU to coil, tag up, space out, set counters 4/9/2019 4/9/2019 2.20 PROD2 STK TRIP P RIH w/ BHA #17, test agitator, 1.9 78.0 10,435.0 14:18 16:30 bpm, pump = 4650, FS = 1203 psi (verify on transducer) 4/9/2019 4/9/2019 0.10 PROD2 STK DLOG P Log Kl for -4' correction 10,435.0 10,473.0 16:30 16:36 4/9/2019 4/9/2019 0.40 PROD2 STK TRIP P Continue RIH, PUW = 36K, clean 10,473.0 11,050.1 16:36 17:00 through window, dry tag TOB at 11,051', PUW = 39K, bring up pump & RBIH 4/912019 4/9/2019 1.20 PROD2 STK KOST P Milling off billet 330" ROHS, FS = 11,051.1 11,052.1 17:00 18:12 1 1 11242 psi @ 1.9 bpm, lfph for 1 ft 4/9/2019 4/9/2019 0.40 PROD2 STK KOST P Milling off billet 330° ROHS, FS = 11,052.1 11,053.1 18:12 18:36 1242 psi @ 1.9 bpm, 2fph for 1 It 4/9/2019 4/9/2019 0.20 PROD2 STK KOST P Milling off billet 330° ROHS, FS = 11,053.1 11,054.1 18:36 18:48 1242 psi @ 1.9 bpm, 3fph for 1 ft 4/9/2019 4/912019 0.40 PROD2 DRILL DRLG P Off billet drilling ahead -10 ft/hr, WOB 11,054.1 11,058.0 18:48 19:12 <1 k lbs. 4/9/2019 419/2019 1.20 PROD2 DRILL DRLG P Past OH anchered billet slips, Drill 11,058.0 11,150.0 19:12 20:24 ahead with unresticted WOB. CT W18.6 k lbs, WOB 2.5 k lbs, ROP 89 ft/hr 4/9/2019 419/2019 0.20 PROD2 DRILL WPRT P PU Wt 30 k bs, PUH to dry drift billet. - 11,150.0 11,003.0 20:24 20:36 1 k WOB tug as the bit pased the top of billet. 4/9/2019 4/9/2019 0.10 PROD2 DRILL WPRT P RBIH, CT Wt 10 k lbs, billet clean. 11,003.0 11,149.0 20:36 20:42 4/9/2019 4/10/2019 3.30 PROD2 DRILL DRLG P CT 5027 psi @ 1.87 by in and 1.86 11,149.0 11,422.0 20:42 00:00 bpm out, free spin diff 1248 psi, BHP 3808 psi holding 11.1 ppg EMW, BOBD, cT Wt 8.8 k lbs, WOB 2 k lbs, 11,271' PU 40 k lbs - MM out acting up, bypass, flush/blowdown, drive gain back to normal. Average ROP over interval drilled - 83 ft/hr 4/10/2019 4/10/2019 0.30 PROD2 DRILL DRLG P OBD- 11,422.0 11,450.0 00:00 00:18 4/10/2019 4/10/2019 0.10 PROD2 DRILL WPRT P PU W142 k lbs Wiper# 1 to just below 11,450.0 11,112.0 00:18 0024 I I the billet Page 15135 Report Printed: 5/2812019 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Sten Tme End Time Dur (hr) Phase Op Code Activity Cade Tens P -T -X Operation Sten Depth (WIS) End Depth (flKB) 4/10/2019 4/10/2019 0.20 PROD2 DRILL WPRT P RBIH, RIH Wt 8.8 k lbs - Wellworc 11,112.0 11,450.0 00:24 00:36 estimates 0.2 bbls cuttings returned. 4/10/2019 4/10/2019 5.50 PROD2 DRILL DRLG P CT 4841 psi @ 1.88 bpm in and 1.87 11,450.0 11,850.0 00:36 06:06 bpm out, free spin diff 1300 psi, BHP 3880 psi holding 11.1 ppg @ the window. WH 87 psi, IA 122 psi, OA 34 psi. CT Wt 5.8 k lbs, WOB 2.7 k lbs, 11,545' PU - 45 k lbs 11,646' PU -43 k lbs free spin 1313 psi 11,667' PU - 42 k lbs 11,720' PU - 43 k lbs Pump sweeps 4/10/2019 4/10/2019 0.30 PRODt DRILL WPRT P Wiper up -hole, PUW = 43K, clean up 11,850.0 11,100.0 06:06 06:24 to 11,100' 4/10/2019 4/10/2019 0.30 PROD2 DRILL WPRT P Wiper in-hole, slack CWT at 11,267', 11,100.0 11,850.0 06:24 06:42 no WOB indication, PUW = 51 K, then got by, RIW = 10K 4/10/2019 4/10/2019 3.00 PROD2 DRILL DRLG P Drilling, FS = 1336 psi, CWT = 7.2K, 11,850.0 12,043.0 06:42 09:42 WOB = 2K, annular = 3860 psi, WHP = 46 psi, pump = 5292 psi, pump 5x5 sweeps, avg ROP = 64 fph 4/10/2019 4/10/2019 2.00 PROD2 DRILL DRLG P Drilling, CWT =5.5K, WOB =2K, 12,043.0 12,138.0 09:42 11:42 annular = 3920 psi, WHP = 44 psi, pump = 5320 psi, begin continuous rotation drilling, avg ROP = 48 fph 1 00'wiper from 12,080', PUW = 44K PUW = 41 from 12,126' Drilling break at 12,114' 4/102019 4/10/2019 1.10 PROD2 DRILL DRLG P Drilling, CWT = 1.3K, WOB = 2.5K, 12,138.0 12,250.0 11:42 12:48 annular = 4007 psi, WHP = 18 psi, pump sweeps 4/10/2019 4/10/2019 1.20 PROD2 DRILL WPRT P Wiper to tubing tail, PUW = 45K, pull 12,250.0 10,325.0 12:48 14:00 heavy at 10,915'(55K), RBIH, PUH, pull heavy at 10,795', RIBH, stack -9K WOB, pull -13K WOB, begin packing off, work free, PUH, RBIH to surge BHA prior to pulling through window 4/10/2019 4/10/2019 0.20 PROD2 DRILL DLOG P RBIH & Log K1 for+6.5' correction 10,325.0 10,467.0 14:00 14:12 (circulate bottoms up from window at surface) 4/102019 4/10/2019 1.30 PROD2 DRILL WPRT P Wiper in-hole, sweeps timed to exit at 10,467.0 12,250.0 14:12 15:30 EOB, clean through build, PUH to 10,710', RBIH, slack weight at 11,677' 4/10/2019 4/10/2019 2.60 PROD2 DRILL DRLG P Drilling, FS = 1200 psi @ 1.9 bpm, 12,250.0 12,420.0 15:30 18:06 CWT = 1.5K, WOB = 1 K, annular = 4113 psi, WHP = 18 psi PUW = 47K from 12,350' Average ROP over section - 65 fUhr 4/10/2019 4/10/2019 1.10 PROD2 DRILL DRLG P PU post crew change, CT Wt 62 k Ilbs, 12,420.0 12,496.0 18:06 19:12 RBIH CT 5396 psi @ 1.90 bpm in and 1.86 bpm out, Free spin 1398 psi, BHP 3991 psi, open choke, WH 16 psi, IA 124 psi, OA 42 psi CT Wt 6 k to -5 k lbs, WOB -1.8 klbs, More and more frequent pick ups, CT Wt - 55-60 k lbs Average ROP over section - 69 ft/hr Page 16135 Report Printed: 5t28/2019 . - Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Stan Depth stat Time End Time our (m) Phase Op Code Acllvity Code Time P-T-X Operabon (ftKB) End DWh(fd(S) 4/10/2019 4/10/2019 0.40 PROD2 DRILL DRLG P Last PU 69 k lbs, 100' short BHA 12,496.0 12,526.0 19:12 19:36 wiper. RBIH, Drill ahead, start preparing for mud swap. Small short lived pack off event, 4/10/2019 4/1012019 0.30 PROD2 DRILL WPRT P PU 52 k lbs, 100' BHA wiper, pump 12,526.0 12,526.0 19:36 1954 5x5, RBIH 4/10/2019 4/10/2019 0.80 PROD2 DRILL DRLG P PU 69 k lbs, 100'short BHA wiper. 12,526.0 12,620.0 19:54 2042 RBIH, Drill ahead, start preparing for mud swap. Small short lived pack off event, 4/10/2019 4/10/2019 0.40 PROD2 DRILL WPRT P PU , 55 k lbs, new mud started down 12,620.0 12,620.0 20:42 21:06 the coil, Slowly PUH timing out new mud to the bit while RBIH. 4/10/2019 4/10/2019 0.60 PROD2 DRILL DRLG P CT 4944 psi @ 1.9 bpm in and 1.89 12,620.0 12,738.0 21:06 21:42 bpm out. FS diff 1352 psi, BHP 4049 psi. CT Wt 5 k lbs, WOB 1.5 k lbs Average ROP over section - 148 ft/hr New Mud at the bit 12,620' 4/10/2019 4/10/2019 0.50 PROD2 DRILL WPRT P PU Wt 50 k lbs - Wiper trip #1 12,738.0 11,940.0 21:42 22:12 Trouble turning around, reduced rate to 1.5 bpm, 4/10/2019 4/10/2019 0.80 PROD2 DRILL WPRT P Multiple set downs while RBIH, 11,940.0 12,738.0 22:12 23:00 11,965, 11,984, 11,989, 11,982'-Hot gamma areas, - 140 API 0.4 bbls of cuttings returned per WW 4/10/2019 4/11/2019 1.00 PROD2 DRILL DRLG P CT 4785 psi @ 1.89 bpm in and 1.85 12,738.0 12,878.0 23:00 00:00 bpm out, Free psi diff 1303 psi, BHP 3940 psi, targeting 11.1 ppg EMW @ the window. WH 73 psi, IA 122 psi, OA 38 psi. CT Wt5to-5klbs, WOB 1.2 to 0.3k lbs. Average ROP over section - 140 ft/hr 4/11/2019 4/11/2019 0.20 PROD2 DRILL DRLG P CT 4785 psi @ 1.89 bpm in and 1.85 12,878.0 12,889.0 00:00 00:12 bpm out, Free psi diff 1303 psi, BHP 3940 psi, targeting 11.1 ppg EMW @ the window. WH 79 psi, IA 122 psi, OA 38 psi. CT Wt 5 to -5 k lbs, WOB 1.2 to 0.3 k lbs. Average ROP over section - 55 ft/hr 4/11/2019 4/11/2019 4.80 PROD2 DRILL DRLG P On something hard, Geo thinks 12,889.0 12,964.0 00:12 0500 siderite CT 5127 psi @ 1.9 bpm, BHP 3898 psi, CT Wt 5.8 k lbs, WOB 3 k lbs. 12,946' PU Wt 40 k lbs RBIH CT 5000 psi @ 1.90 bpmfree spin diff 1335 psi, BHP 3947 psi, WH 117 psi, Ct Wt 7 k lbs, WOB 3 k lbs Average ROP over section - 15 ft/hr 4/11/2019 4/11/2019 2.00 PROD2 DRILL DRLG P Drilling, CWT =7.3K, WOB =3.2K, 12,964.0 12,986.0 05:00 07:00 annular = 3933 psi, WHIP = 117 psi, slow drilling wl siderite in samples 4/11/2019 4111/2019 3.50 PROD2 DRILL DRLG P Drilling, CWT =6.3K, WOB =3.4K, 12,986.0 13,035.0 07:00 10:30 annular= 3948 psi, WHIP = 125 psi, pump = 5271 psi, PUW = 43K from 13,012', Continued low ROP w/ Siderite in samples, avg ROP = 14 fph 4/11/2019 4/11/2019 2.30 PROD2 DRILL DRLG P Drilling, CWT =7.9K, WOB =2.5K, 13,035.0 13,050.0 10:30 12:48 1 1 1 annular = 3942 psi, WHP = 104 psi 4/11/2019 4/1112019 0.30 PROD2 DRILL WPRT P Wiper up-hole, PUW = 43, clean 13,050.0 12,250.0 12:48 13:06 1 I Page 17135 Report Printo 1: 512812019 Operations Summary (with Timelog Depths) ru- 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Depth StartTime End Tare our (Inn Phase Op Code Activity Code 11me P -T -X Operation (WB) End Depth (flKB) 4/11/2019 4/11/2019 0.30 PROD2 DRILL WPRT P Wiper in-hole, RIH=6.8K, dean 12,250.0 13,050.0 13:06 13:24 4/11/2019 4/11/2019 1.10 PROD2 DRILL DRLG P Drilling, FS = 1304 psi @ 1.88 bpm, 13,050.0 13,058.0 13:24 14:30 CWT = 9.6K, WOB = 2.9K, annular = 3940 psi, WHP = 97 psi, pump = 5306 psi 4/11/2019 4/11/2019 1.90 PROD2 DRILL DRLG P Drilling break at 13058', CWT= 7.2K, 13,058.0 13,200.0 14:30 16:24 WOB = 1.3K, annular = 3952 psi, begin snubbing, PUW = 50K, pump 5x5 beaded sweeps to good effect (39K PUW wl beads out) Grab new parameters: FS = 1325 psi 4/11/2019 4/11/2019 2.10 PROD2 DRILL DRLG P Driling, CWT= 1.6K, WOB= 1.8K, 13,200.0 13,310.0 16:24 18:30 annular = 3961 psi, WHP = 82 psi avg ROP = 52 fph 4/11/2019 4/11/2019 1.20 PROD2 DRILL WPRT P PU Wt 52 klbs - Bit trip 13,310.0 10,650.6- 18:30 19:42 13,137-13,048' light WOB tugs -300 lbs 12,250-12,218 firm WOB tugs - 680 lbs 11,962 - 11,934 heavy WOB tugs 2.5 - 3klbs 10,788'-S k WOB lug, believe it was a tool orientation issue not a hole issue. Window dean -150 lb WOB tug 4/11/2019 4/11/2019 2.00 PROD2 DRILL TRIP P Park, open EDC, Online @ 1.95 bpm, 10,650.0 65.0 19:42 21:42 POH Saw coil weight swing and a small pack off event when passing the Mule shoe @10,331'. Preloaded drillers side PDL in order to swap our Res tool per town request. 4/11/2019 4/11/2019 1.40 PROD2 DRILL PULD P PUD BHA 17 65.0 0.0 21:42 23:06 Lowest WH 690 psi, estimate BHP @ 10.8-10.9 ppg or lower. Inspected pipe, 0.174, 0.175, 0.109, 0.175" -low reading from long shallow gouge, sliding across the window or something similar. 4/11/2019 4/11/2019 0.50 PROD2 DRILL PULD P PU/PD BHA 18 0.0 65.0 23:06 23:36 Re highside motor post resistivity tool swap, 4/11/2019 4/1112019 0.30 PROD2 DRILL PULD T PHASE 3 called - no email from 65.0 0.0 23:36 23:54 security, radio announcement, CPF 1&2 Phase 3, CPF 3 Phase 2. Pulled BHA above swab closed same. Lined up on managed pressure 4/11/2019 4/12/2019 0.10 PROD2 DRILL WAIT T Wait on weather 0.0 0.0 23:54 00:00 Phase 3 4/1212019 4/12/2019 6.00 PROD2 DRILL WAIT T Waiting on weather while pumping 0.0 0.0 00:00 06:00 managed pressure. Phase 3 4/12/2019 4/12/2019 12.00 PROD2 DRILL WAIT T Waiting on weather, pumping 0.0 0.0 06:00 18:00 mangaged pressure, -16 bbl lost to formation, Phase 3 'Weather prediction calls for decreasing winds by midnight tonight. Page 18135 ReportPrinted: 5/28/2019 Operations Summary (with Timelog Depths) IC -11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Time End Time Our (hr) Phase Op Code Activlly Code Time P -l -x Operation Start Depth (ftKe) End Depth(ftO) 4/12/2019 4/13/2019 6.00 PROD2 DRILL WAIT T Convoy crew change @ 19:30. 0.0 0.0 18:00 00:00 PJSM, unstab DSPDL, LD /agitator/motor. Set PDL in dedicated mount, lower blocks below windwalls, straighten mast and insert pins. -standby Weather has improved drastically, can see the shop stationed at the other end of the pad. No change in Phase conditions. Waiting on weather, pumping mangaged pressure, 4/13/2019 4/13/2019 4.50 PROD2 DRILL WAIT T Waiting on weather while pumping 0.0 0.0 00:00 0430 managed pressure. - Phase 3 Weather has improved drastically, can see the shop stationed at the other end of the pad. Phase2 called @ 4:15, Rousted crew, called R&P to confirm our access road was clean 4/13/2019 4/13/2019 1.50 PROD2 DRILL PULD P PJSM, PU agitator and motor, PD 0.0 68.0 04:30 06:00 BHA #18, 0.5 °AKO motor over a P104 BH bit, replace checks, check pack offs. 4/13/2019 4/13/2019 2.10 PROD2 DRILL TRIP P R I H w/BHA #18, shallow test agitator, 68.0 10,435.0 06:00 08:06 1.87 bpm, dip = 1265 psi, pump = 5181 psi Many various alarms on HMI, park at 9054', evaluate, VFD room door open, possibly cold conditions causing issue 4/13/2019 4113/2019 0.20 PROD2 DRILL DLOG P Log K1 for -5.5' correction, PUW = 10,435.0 10,473.0 08:06 08:18 37K 4/13/2019 4/13/2019 0.30 PROD2 DRILL DLOG P Confirm 11.1 ppg kills well, trap 3795 10,473.0 10,676.0 08:18 08:36 psi SBHP: MD = 10,676 psi, annular = 3677 psi, TVD sensor= 6492, 10.9 ppg EMW (stopped once hitting 10.9 ppg) 4/13/2019 4/13/2019 1.20 PROD2 DRILL TRIP P Continue RIH, 2K WOB bobble at 10,676.0 13,310.0 08:36 09:48 10,685' (window) Stack WOB 11,805', PUW = 42K, -3K WOB, & 11,785' Stack CWT at 12044' (no WOB indication) Annular increasing, PU, slack CWT at 12,711' Stack CWT at 13,088' 411312019 4/13/2019 1.20 PROD2 DRILL DRLG P Drilling, FS = 1275 psi @ 1.87 bpm, 13,310.0 13,426.0 09:48 11:00 CWT = 5K, WOB = 1.6K, annular = 4285 psi, annular higher than expected w/ choke fully open (11.8 ppg at Mindow, dropping as mud shears, cheesing over shakers), 4/13/2019 4/13/2019 1.00 PROD2 DRILL DRLG P PUW =42K from 13,426', stacking 13,426.0 13,520.0 11:00 12:00 CWT getting to bottom, annular = 4115 psi, pump = 5419 psi, pump 5x5 sweeps (1% LoTorq /2% 776), -98% returns 4/13/2019 4/13/2019 0.50 PROD2 DRILL DRLG P Hard spot 13,520', rate out fell to 1.3 13,520.0 13,558.0 12:00 12:36 bpm( -70% returns), annular = 3944 psi, BHA wiper, PUW = 58K, rate out falls to 1.15 bpm (-62% returns) Page 19135 Report Printed: 5/28/2019 Operations Summary (with Timelog Depths) IC -11 ol Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Sun Depth Stan Time End Time our (hr) Phase Op Co4e Activity Cotte Time P -T -X Operation (fl(B) End Depth (ftKB) 4/13/2019 4/13/2019 0.40 PROD2 DRILL DRLG T Unable to PU off bottom, differentially 13,558.0 13,558.0 12:36 13:00 stuck, work pipe, pull to 70K+ multiple times, pull free @ 79.5K 4/13/2019 4/13/2019 0.30 PROD2 DRILL WPRT P Wiper up -hole, load LVF to rig & begin 13,558.0 12,753.0 13:00 13:18 warming 4/13/2019 4/13/2019 0.30 PROD2 DRILL WPRT P Wiper in-hole, work a bit to get dawn 12,753.0 13,558.0 13:18 13:36 beginning at 13,326' 4/13/2019 4/13/2019 1.20 PROD2 DRILL DRLG P Drilling, CWT =OK, WOB =1.2K, 13,558.0 13,640.0 13:36 14:48 annular = 4000 psi, 1.87 bpm in, 1 bpm out, drilling ahead, rate out continues to drop (.85 bpm), 61 K PUW from 13,623', 68K PUW from 13,626', pumped 5x5 sweeps, difficulty drilling, stacking weight 4/13/2019 4/13/2019 0.30 PROD2 DRILL WPRT P Pull 300'wiper, PUW =46K 13,640.0 13,640.0 14:48 15:06 4/13/2019 4/13/2019 3.70 PROD2 DRILL DRLG P Drilling, rate out increased to 1.15 13,640.0 13,894.0 15:06 18:48 bpm, sweeps exiting bit w/ 4K CWT, WOB = 1.32K, annular = 4008 psi, nuetral to snubbing CWT, returns climb to 1.4 bpm PUW = 50K from 13,711' PUW = 47K from 13,769' PUW = 48K from 13,827' 4/13/2019 4/13/2019 0.20 PROD2 DRILL WPRT P PU Wt 54 k lbs, wiper trip 13,894.0 1,349.0 18:48 19:00 4/13/2019 4/13/2019 0.20 PROD2 DRILL WPRT P RBIH 1,349.0 13,984.0 19:00 19:12 4/13/2019 4/14/2019 4.80 PROD2 DRILL DRLG P OBD CT 4481 psi @ 1.89 bpm in and 13,984.0 14,055.0 19:12 00:00 1.70 bpm out. Free spin diff 1340 psi, BHP 3970 psi. CT Wt 4 k Is, WOB 2.8 klbs. .• Drilled out the top into Kuparuk D, average 165 API, max 180. 4/14/2019 4/14/2019 0.60 PROD2 DRILL DRLG P Ct 5424 psi @ 1.86 bpm in and 1.69 14,055.0 14,070.0 00:00 00:36 bpm out BHP 4023 psi, CT Wt -3 k lbs 2.4 k lbs WOB. Gamma - 160 +API ROP - 25 ft/hr 4/14/2019 4/14/2019 3.30 PROD2 DRILL DRLG P Gamma dropping below 160 API, ROP 14,070.0 14,208.0 00:36 03:54 increasing to - 80 ft/hr CT 5326 psi @ 1.88 bpm in and 1.69 bpm out, BHP 4069 psi, CT Wt -5.5 k Ib, WOB 600 lbs, ROP 80 ft/hr, pump 5x5 beaded lubed sweep - 1 ppb beads, no noticible effect on weight transfer. 4/14/2019 4/14/2019 2.10 PROD2 DRILL WPRT P PU Wt 45 k lbs, 14,208.0 10,330.0 03:54 06:00 13,779' Baker surface read out glitched, bore pressure shot up to 22k psi, artifact, continue wiper fallowing tripping schedule, tools return normal read-outs, MWD feels confident RIH to contiinue drilling, Annular appears to be correct. Fault transitio(s) - clean Saw 4-5 k CT Wt over pull and -1 k WOB across hot gamma 11995-11915' billet clean, jog 5" up to mule -shoe 4/14/2019 4/14/2019 0.10 PROD2 DRILL WPRT P Log K1 for+13.5' 10,330.0 10,468.0 0600 06:06 1 Page 20/35 Report Printed: 512 812 01 9 Operations Summary (with Timelog Depths) IC -11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Time End Time Dur(hd Phase Op Cod. Activity Code Time P -T -X Operabon Stan Depth (ftKB) End Dept (%KB) 4/14/2019 4/14/2019 1.60 PROD2 DRILL WPRT P Wiper in-hole, bore pressure spikes to 10,468.0 14,208.0 0606 0742 21K psi, WOB at 15K (faulty readings from DPS) beginning at 12,962' (similar issue as wiper up - hole), VWD's trouble -shoot issue, perform power cycle, returned to normal values, continue in-hole, watching closely Stack at 14,009', continue in-hole w/ negative CWT through high gamma interval, reduce rate to 0.6 bpm, bring rate up as soon a possible, stacking working to bottom, PUW = 44K, pump 5x5 sweeps, 4/14/2019 4/14/2019 1.50 PROD2 DRILL DRLG P Drilling, FS = 1260 psi @ 1.87 bpm, 14,208.0 14,288.0 07:42 09:12 CWT -6K, WOB =0.6K, annular= 4128 psi, pump 5440 psi, rate out 1.7 bpm Bring HiVis to 2 ppb beads with lubes, pump 13 bbl pill, no significant improvement, PUW = 47 from 14288', Avg ROP = 53 fph 4/14/2019 4/14/2019 1.80 PROD2 DRILL DRLG P Drilling, CWT= -8K, WOB 6K, 14,288.0 14,352.0 09:12 11:00 annular = 4007 psi, pump = 5097 psi, pump 15 bbl, 2ppb pill to limited effect, 4/14/2019 4/14/2019 0.50 PROD2 DRILL DRLG P Drilling, CWT = -8K, WOB = 0.5K, 14,352.0 14,365.0 11:00 11:30 continue struggling w/ weight transfer, continue pumping beaded pills to limited effect, unable to transfer weight to bit effectively, continual PU's 4/14/2019 4/14/2019 0.20 PROD2 DRILL WPRT P 500' wiper up -hole, PUW = 46K, clean 14,365.0 11:30 1142 pulling through high gamma interval 4/14/2019 4/14/2019 0.30 PROD2 DRILL WPRT P Wiper in-hole, losing CWT through 13,865.0 14,365.0 11:42 1200 high gamma interval, reduce running speed 4/14/2019 4/14/2019 2.00 PROD2 DRILL DRLG P Drilling, attempt 15 bbl 2% Drill Zone / 14,365.0 14,467.0 12:00 14:00 2% Screen Kleen pill to good effect, increased weight transfer & able to drill, continue pumping Drill Zone / Screen Kleen pills binging active to —1 %, avg ROP = 51 fph PUW = 65K from 14,375' PUW = 63K from 14,403' PUW = 52K from 14,412' 4/14/2019 4/14/2019 2.00 PROD2 DRILL DRLG P Drilling, CWT = -3K, WOB = O.SK, 14,467.0 14,565.0 14:00 16:00 annular = 4081 psi, pump = 5546 psi, 85% returns, continue to struggle w/ weight transfer, pumping pills to keep weight to the bit, avg ROP = 49 fph PUW = 54K from 14,565' 4/14/2019 4/14/2019 3.60 PROD2 DRILL DRLG P Drilling, CWT= -1.8K, WOB =0.5K, 14,565.0 14,734.0 16:00 1936 annular = 4117 psi, pump = 5620 psi, continue pumping pills as required PUW = 60K from 14,579', turn into BHA wiper Average ROP over interval drilled - 47/hr Page 21/35 Report Printed: 5/28/2019 Operations Summary (with Timelog Depths) 1C-11 og: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log stag Depth Stat Time End Time our (hr) Phase Op Code Activity Code Time P -T -X Operation (flKir) End Depth (fll(B) 4/14/2019 4/14/2019 0.40 PROD2 DRILL WPRT P PU Wt 45 k Is, Wiper #2 - 1000' 14,734.0 13,676.0 19:36 20:00 chasing sweep up hole Clean hole, CT puling weight smooth at 39k while POOH, slight increase to 41 k @ /after 13,848' 4/14/2019 4/14/2019 0.40 PROD2 DRILL WPRT P RBIH, -preemptively reduced rate to 1 13,676.0 14,734.0 20:00 20:24 bpm and running speed to 30 filmin From 13,800 - 14,173, back on pump 4/14/2019 4/15/2019 3.60 PROD2 DRILL DRLG P CT 5654 psi @ 1.90 bpm in and 1.78 14,734.0 14,905.0 20:24 00:00 bpm out, Free spin dff 1287 psi, BHP 4149 psi, 11.2 EDC at the window, ( targeting 11.1 choke is full open). WH 21 psi, IA 124 psi, OA 34 psi. OBD Ct wt -5 k Ibs WOB 0.67 k lbs, ROP 117 - 20 Average ROP over interval drilled - 47.57hr 4/15/2019 4/15/2019 2.10 PROD2 DRILL DRLG P OBD CT 5655 psi @ 1.88 bpm in and 14,905.0 14,980.0 00:00 02:06 1.77 bpm out, BHP 4175 psi, 11.26 EDC at the window, ( targeting 11.1 choke is full open). WH 17 psi, IA 125 psi, OA 39 psi. Cl wt -6 k bs WOB 0.58 k lbs, ROP -50 ROP and weight transfer fell off @ 14,945', sweeps not helping Average ROP over interval drilled - 377hr 4/15/2019 4/15/2019 2.20 PROD2 DRILL WPRT P PU Wt 47 k lbs, Wiper trip to the 14,980.0 10,430.0 02:06 04:18 window for tie in. CT weight stepped up from 37 k t 43 k lbs @ 13,670'. Weight slowly fell off over the remainder of the trip up hole. Saw hot gamma spot @ 11,934' on CT wt, 450 lbs WOB, and motor torqued up. Billet clean, window clean. Jog 5" 4/15/2019 4/15/2019 0.20 PROM DRILL DLOG P Tie into the K1 for +10'correction, set 10,430.0 10,476.0 04:18 04:30 counters, 4/15/2019 4/15/2019 0.30 PROD2 DRILL TRIP P RIH, window, build and billet clean, 10,476.0 11,100.0 04:30 04:48 4/15/2019 4/15/2019 1.80 PROD2 DRILL TRIP P Continue to RIH, begin pumping new 11,100.0 14,980.0 04:48 06:36 mud system #4 4/15/2019 4/15/2019 2.40 PROD2 DRILL DRLG P Drilling, FS = 1150 psi @ 1.8 bpm, CT 14,980.0 15,110.0 06:36 09:00 = 3K, WOB = 0.7K, annular = 4240 psi, pump = 5712 psi. new mud at bit 15,006', avg ROP = 54 fph 4/15/2019 4/15/2019 2.50 PROD2 DRILL DRLG P Drilling, CWT = -1.5K, WOB = 7K, 15,110.0 15,215.0 09:00 11:30 annular = 4004 psi, pump = 5053 psi, begin increasing active system to 2% LoTorq 12% 776 (per town request), avg ROP = 42 fph .. Intermitent DPS glitches sending faulty readings to surface. Continue to watch closely 4/15/2019 4/15/2019 2.50 PROD2 DRILL DRLG P Drilling, CWT= -6K, WOB 0.5K, 15,215.0 15,336.0 11:30 14:00 annular = 4114 psi, pump = 5244 psi PUW = 44K from 15,266' 4/15/2019 4/15/2019 0.80 PROD2 DRILL DRLG P Drilling, additional lube all the way 15,336.0 15,380.0 14:00 14:48 around, modest results 4/15/2019 4/15/2019 0.30 PROD2 DRILL TRIP P Wiper up -hole, RUIN =45K, pump 15,380.0 14,555.0 14:48 15:06 DrillZone pill to aid trip to bottom Page 22135 Report Printed: 6/2812019, Operations Summary (with Timetog Depths) Q� 113-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Dept Start Time End Time our (m) Phase OP Code ActivityCade Time P-T-X operation (fixe) Entl Depth (RK8) 4/1512019 4/15/2019 0.60 PROD2 DRILL TRIP P Wiper in-hole, struggl to bottom, 14,555.0 15,380.0 15:06 15:42 squatting up to -10K CWT, PU, continue in-hole, reduce rale to .75 bpm to reach bottom 4/15/2019 4/15/2019 2.30 PROD2 DRILL DRLG P Drilling, FS = 1233 psi @ 1.9 bpm, 15,380.0 15,437.0 15:42 1800 CWT = -8.5K, WOB = 0.61K, annular = 4070 psi, pump = 5542 psi PUW = 42K from 15,387' PUW = 53K from 15,426' 4/15/2019 4/15/2019 1.20 PROD2 DRILL DRLG P Drilling, CWT=-3K, WOB=1.8K, 15,437.0 15,458.0 18:00 19:12 annular = 4078 psi, pump = 5557 psi, drill to called TD of 15,458', pump 10 x 10 sweeps 4/15/2019 4/15/2019 0.50 PROD2 DRILL CIRC P Wait for sweeps to exit bit 15,458.0 15,458.0 19:12 19:42 4/15/2019 4/16/2019 4.30 PROD2 DRILL WPRT P Wiper to swab, PUW = 44K, pump 15,458.0 137.0 19:42 00:00 10x10 sweeps timed for EOB, jog 5", park at 4861' & reboot Orion 4/16/2019 4/16/2019 0.20 PROD2 DRILL WPRT P Continue out of hole, tag up, reset 137.0 78.0 00:00 00:12 1 counters. 4/16/2019 4/16/2019 1.80 PROD2 DRILL TRIP P RBIH 78.0 10,430.0 00:12 02:00 4/16/2019 4/16/2019 0.20 PROD2 DRILL DLOG P Tie in for -3.5' correction 10,430.0 10,470.0 02:00 02:12 4/16/2019 4/16/2019 0.20 PROD2 DRILL DLOG P Park @ 15458.74' CTMD, 6473.88' 10,650.0 10,650.0 02:12 02:24 TVD, trap psi and observe bleed down. Time Pressure EMW Initial 3765 11.18 imin 3748 11.13 2min 3695 10.98 3min 3634 10.79 5 min 3606 10.71 4/16/2019 4/16/2019 3.80 PROD2 DRILL TRIP P Continue to RIH 10,650.0 15,462.0 02:24 06:12 Some CT Weight bobbles and motor work sliding by 11,900. CT Wt set downs @ 13,770' and 13,852'. Reducet pump rate to 1 bpm @ 13,950', increased to 1.48 bpm @ 14,100'. Continue in hole. SID 14,204', PU 45 k lbs, continue in hole, reduce RIH speed to 25 ff/min @ 14518, reduce running speed to 14 fi/min @ 14,740'. 8 ft/min @ 14,800'. PU @ 15,120' for a restart, 40 k lbs, Continue in hole, 0.71 bpm & 7 f lmin. Stall out 15428, pump liner running pill, RIH on LRP, tag bottom with 5-6 k lbs CT Wt. 4/1612019 4/16/2019 3.70 PROD2 DRILL TRIP P POOH laying in LRP. 15,462.0 72.0 06:12 09:54 Park and paint Yellow flag @ 13570.75' Park and paint White flag @ 9378.29' Continue out of hole Top of beaded liner running pill 4/16/2019 4/16/2019 1.10 PROD2 DRILL PULD P LD BHA#18,over a dead well. Inspec 72.0 0.0 09:54 11:00 coil and CTC 4/16/2019 4/16/2019 0.40 COMPZ2 CASING PUTB P Prep floor for running liner. 0.0 0.0 11:00 11:24 4/16/2019 4/16/2019 1.90 COMPZ2 PUTB P PU / MU jointed pipe, 12-01 first run, 0.0 1,212.0 11:24 13:18 40 joints with a solid bullnose under a 1 1 JCASING shorty deployment sleeve. ( Liner 1212.44' LOA 1213.69') Page 23135 Report Printed: 512812019 . Operations Summary (with Timelog Depths) r.: IC -11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Time EW Time Dur(hr) Phase Op Code Activit' Code Time PJA Operation Stert Depth (WB) Ertl DepN(RKB) 4/16/2019 4/16/2019 0.70 COMPZ2 CASING PULD P PJSM, PU BHA#19, 12-01 lower 1,212.0 1,265.0 13:18 14:00 completion BHA. 4/16/2019 4/16/2019 4.10 COMPZ2 CASING TRIP P RIH with 1-2-01 liner. Tie into flag for- 1,265.0 15,462.0 14:00 18:06 10.68'. PU Wt 38 k WOB -6 k lbs. Contiune in hole, drive by the K1, + 6'. No correction made. Continue in hole SID 11,648'- PU 49 k bs. 4/16/2019 4/16/2019 0.85 COMPZ2 CASING CIRC P Line up to 40 beaded LRP, recap pipe 15,462.0 14,457.0 18:06 1857 4/16/2019 4/16/2019 1.50 COMPZ2 CASING TRIP P POOH, while laying in beaded LRP 14,457.0 10,670.0 18:57 20:27 4/16/2019 4/16/2019 1.90 COMPZ2 CASING TRIP P Pull through the window, continue 10,670.0 44.2 20:27 22:21 POOH 4/16/2019 4/16/2019 0.50 COMPZ2 CASING OWFF P At surface, check well for flow, PJSM 44.2 44.2 22:21 22:51 4/16/2019 4/16/2019 0.25 COMP72 CASING PULD P LD liner running tools 44.2 0.0 22:51 23:06 4/16/2019 4/16/2019 0.60 COMPZ2 CASING PUTB P Prep RF for liner ops, inspect 0.0 0.0 23:06 23:42 Traveling Blocks, inspect INJH 4/16/2019 4/17/2019 0.30 COMPZ2 CASING PUTB P Start PU upper liner segment 0.0 151.7 23:42 00:00 4/17/2019 4/17/2019 1.50 COMPZ2 CASING PUTB P Continue PU upper liner segment, 151.7 2,970.0 00:00 01:30 filling the hole every 10 jts, Joint #40 @ 01:30 ,Joint #80 @ 03:10,Joint #99 @ 04:00 4/17/2019 4/17/2019 3.30 COMPZ2 CASING PUTB P Continue picking up upper 12-01 2,970.0 3,497.0 01:30 04:48 completion. 4/17/2019 4/17/2019 0.90 COMPZ2 CASING PULD P PU BHA # 20, Lower 1-2-01 BHA. 3,497.0 3,541.0 04:48 05:42 4/17/2019 4/17/2019 1.50 COMPZ2 CASING RUNL P RIH with upper 1-2-01 competion. 3,497.0 10,599.0 05:42 07:12 4/17/2019 4/17/2019 0.10 COMPZ2 CASING DLOG P Tie into fag, note flag painted without 10,599.0 10,554.0 07:12 07:18 tying in prior to painting, it showed as a -17.2' correction, we arbitrarily set the correction t0 -4.5 to better reflect typical corrections. PU Wt 45 4/17/2019 4/17/2019 6.60 COMPZ2 CASING RUNL P Continue to RIH, first SD @ 11,438', 10,554.0 14,246.0 07:18 13:54 multiple set downs after ROP slowed @ 12,977' and really slowed down @ 13,695' Fight liner to bottom. Multiple S/D's @ 14,245' up to -25 k lbs CT Wt. Hard bottom. consult with town, Pump off liner PU 38 k WOB -5 klbs. Guestimate top @ 10747.7 Drive by of K1 showed -4.5' correction drive by of the RA tag showed -3' correction. 4/17/2019 4/17/2019 2.00 COMPZ2 CASING TRIP P PUH, park, reset counters. POOH 14,246.0 58.0 13:54 15:54 4/17/2019 4/17/2019 0.80 COMPZ2 CASING PULD P LD BHA 20 over a dead well. 58.0 0.0 15:54 16:42 Losses 4 bbpVhr 4/17/2019 4/17/2019 1.25 PRODS STK CIRC P Skid cart, pull checks, stab on, flush 0.0 0.0 16:42 17:57 stack.test inner reel valve, inner reel iron, and stripper. 4/17/2019 4/17/2019 1.50 PRODS STK CTOP P Prep RF for testing operations, grease 0.0 0.0 17:57 19:27 crew on location service tree valves and tango's. 4/17/2019 4/18/2019 4.55 PROD3 STK BOPE P Start bi-weekly BOPE test, low 250 0.0 0.0 19:27 00:00 psi/High 3,500 psi, Annular 2,500 psi, , witness waived by AOGCC (Adam Earl) Page 24/35 Report Printed: 5/2812019 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Siert rime End Tim our (hr) Phew op COW Activity Code Time P -T -X Operation Start Depth (fixe) Ed Depth(ftKe) 4/18/2019 4/18/2019 2.50 PRODS STK BOPE P Continue bi-weekly BOPE test, low 0.0 0.0 00:00 02:30 250 psi/High 3,500 psi, Annular 2,500 psi, witness waived by AOGCC (Adam Earl), call out grease/valve crew re -test Tango #1 (pass). FaiVpass=Swab #2 Fail/pass=Tango #1 Fail/pass=R3 4/18/2019 4/18/2019 0.50 PROD3 STK CTOP P Coil Mangement (flat spot @ 0.0 0.0 02:30 03:00 7' (WT=0.120"), Slide cart forward, remove UQ, cut/remove CTC, trim coil (9.0') 4/18/2019 4/18/2019 1.00 PROD3 STK CTOP P Install CTC 0.0 0.0 03:00 04:00 4/18/2019 4/18/2019 0.80 PRODS STK CTOP P Re -head BHI UQ, PT UQ to 4,500 psi 0.0 0.0 04:00 04:48 1 (good -test) 4/18/2019 4/18/2019 0.30 PRODS STK CTOP P Install QTS, MU build assembly 0.0 0.0 04:48 05:06 4/18/2019 4/18/2019 1.20 PROD3 STK PULD P PU BHA#21, turn build assemble, 2.2 0.0 90.0 05:06 06:18 ° AKO motor over a rerun P14 BH bit with an agitator. 4/18/2019 4/18/2019 2.00 PRODS STK TRIP P Bump up, set counters, RIH. 90.0 10,435.0 06:18 08:18 Shallow agitator test, 1.9 bpm diff 1451 psi, strong vibrations. Continue in hole, star turning the coil over to mud. 4/18/2019 4/18/2019 0.20 PROD3 STK CLOG P Tie into the K1 for a -3.5' 10,435.0 10,468.0 08:18 08:30 4/18/2019 4/18/2019 1.10 PROD3 STK TRIP P Open EDC, circulate well to mud. 10,468.0 10,625.0 08:30 09:36 Mud to surface, Cose EDC, PU Wt 35k lbs. 4/18/2019 4/18/2019 0.10 PROD3 STK TRIP P RIH, window clean, dry tag billet @ 10,625.0 10,706.0 09:36 09:42 10743' PU W137 k lbs 4/18/2019 4/18/2019 0.20 PR0D3 STK KOST P Set rate, RBIH, CT 5118 psi @ 1.90 10,706.0 10,742.4 09:42 09:54 bpm in and 1.81 bpm, Free spin 1025 psi, CT Wt 11.37 k lbs, 4/18/2019 4/18/2019 1.00 PROD3 STK KOST P Tag TOB start time milling @ 1 ft/hr 10,742.4 10,743.6 09:54 10:54 4/18/2019 4/18/2019 0.60 PROD3 STK KOST P Increase ROP to 2 ft/hr 10,742.4 10,744.6 10:54 11:30 4/18/2019 4/18/2019 0.10 PRODS STK KOST P Increase ROP to 3 ff/hr 10,744.6 10,745.2 11:30 11:36 4/18/2019 4/18/2019 0.30 PROD3 STK KOST P Gradually target 1 k lbs WOB 10,745.2 10,752.0 11:36 11:54 CT Wt 13 k lbs, WOB 0.8 k lbs - 50 fUhr 4/18/2019 4/18/2019 0.60 PRODS DRILL DRLG P Drilling ahead, 10,752.0 10,800.0 11:54 12:30 CT 4844 psi @ 1.88 bpm in and 1.83 bpm out BHP 3787 psi, 11.1 ppg EMW at the window. CT Wt 11.79 k lbs, WOB 1.61 It lbs ROP 62 ft/hr 4/18/2019 4/18/2019 0.20 PRODS DRILL WPRT P PU Wt 39 k lbs, PUH for dry drift. 10,800.0 10,800.0 12:30 12:42 RBIH Window clean 4/18/2019 4/18/2019 4.20 PROD3 DRILL DRLG P Ct 4776 @ 1.88 bpm in and 1.84 bpm 10,800.0 11,018.0 12:42 16:54 out, free spin diff 837 psi, BHP 3823 psi, WH 16, IA 121 psi, OA 26 psi, OBD, CT Wt 11.7 k lbs, WOB 3.8 k lbs, ROP 50 Page 25135 Report Printed: 512 812 01 9 -, Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Depth Start Time End Time our (hr) Phase Op Code AaVity Code Time P-T-X Operabon (tlKB) End Depth (N(B) 4/18/2019 4/18/2019 1.10 PRODS DRILL DRLG P Ct 4776 @ 1.88 bpm in and 1.84 bpm 11,018.0 11,070.0 16:54 18:00 out, free spin diff 837 psi, BHP 3823 psi, WH 16, IA 121 psi, OA 26 psi, OBD, CT Wt 11.7 k lbs, WOB 3.8 k lbs, ROP 50 4/18/2019 4/18/2019 0.20 FROM DRILL TRIP P Pull up hole allowing sweep to exit the 11,070.0 10,684.0 18:00 18:12 bit, PUW 39k, continue pulling to the window, jog the 5 inch. 4/18/2019 4/18/2019 0.20 PROD3 DRILL TRIP P At the TOW, shut down pump, open 10,684.0 10,684.0 18:12 18:24 EDC 4/18/2019 4/18/2019 1.60 FROM DRILL TRIP P POOH, pumping 2.0 bpm at 3,822 psi 10,684.0 1,584.0 18:24 20:00 4/18/2019 4/18/2019 0.20 FROM DRILL TRIP P Active choke plugged off (B) 900 psi 1,584.0 1,389.0 20:00 20:12 WHP line up to choke (A), choke (A) plugging off, cycle choke to advoid plugging off, continue POOH slowly, clearing choke (B) @ 35 fpm 4/18/2019 4/18/2019 0.60 PROD3 DRILL TRIP P Continue POOH taking returns 1,389.0 69.0 20:12 2048 through choke (A) 4/18/2019 4/18/2019 0.15 FROM DRILL PULD P At surface, space out 69.0 69.0 20:48 20:57 4/18/2019 4/18/2019 1.10 FROM DRILL PULD P PUD build section assembly 69.0 0.0 20:57 22:03 4/18/2019 4/18/2019 0.60 FROM DRILL PULD P Crew change (Nabor's), Tools OOH, 0.0 0.0 22:03 22:39 LD motor and brake off agitator 4/18/2019 4/18/2019 0.75 PRODS DRILL CTOP P MU Nozzle and jet BOPE stack and 0.0 0.0 22:39 23:24 flush choke (B) 4/18/2019 4/19/2019 0.60 FROM DRILL PULD P MU & PD Lateral Drilling Assembly, 0.0 17.2 23:24 00:00 w/0.5° ako motor and RB bi-center bit 4/19/2019 4/19/2019 0.30 FROM DRILL PULD P MU & PD Lateral Drilling Assembly, 17.2 78.3 00:00 00:18 w/0.5° ako motor and New A3 HYC, bi-center bit, stab onto tools, perform surface test (good-test), check pac- offs (good-test) 4/19/2019 4/19/2019 2.00 PROD3 DRILL TRIP P Tag up, reset counters, RIH 78.3 10,430.0 00:18 02:18 4/19/2019 4119/2019 0.20 PRODS DRILL DLOG P Log formation (K1) for depth control 10,430.0 10,463.0 02:18 02:30 minus 2.0' 4/19/2019 4119/2019 0.38 FROM DRILL TRIP P Continue IH 10,463.0 11,070.0 02:30 02:52 4/19/2019 4/19/2019 3.00 FROM DRILL DRLG P OBD, 1.87 bpm at 4,057 psi, 11,070.0 11,470.0 02:52 05:52 Diff--1,250 psi, WHP=14, BHP=3,920, IA=120, OA=22, avg ROP 133 ft/min, 4/19/2019 4/19/2019 0.10 PROD3 DRILL WPRT P PU Wt 35 k lbs, Wiper#1 tojust below 11,470.0 11,070.0 05:52 05:58 the build - 400' 4/19/2019 4/19/2019 0.20 PRODS DRILL WPRT P RBIH 11,070.0 11,470.0 05:58 06:10 4/19/2019 4/19/2019 8.20 FROM DRILL DRLG P 1.87 bpm at 5007 psi, Free spin diff 11,470.0 11,900.0 06:10 14:22 1080 psi, WHP=14, BHP=3885psi, IA=122, OA=28, OBD CT 6 k lbs, WOB 2.8 k lbs. Ran into siderite - 11,490-11,584' and many more stringers 11,601' PU 39 k Ibs 11,777' PU 38 k lbs 11,890' PU 40 k lbs avg ROP 52 ft/min, 4/19/2019 4/19/2019 0.30 PRODS DRILL WPRT P PU Wt 40 k Ibs, Wiper #2 11,900.0 11,078.0 14:22 14:40 Page 26135 ReportPrinted: 5/28/2019 Operations Summary (with Timelog Depths) IC -11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Stan Depth start Time End Tane our (hr) Phase Op Code Activity Calle Time P -T -x Operation (ftKB) End Depth (MKS) 4/19/2019 4/19/2019 0.20 FROM DRILL WPRT P RBIH 11,078.0 11,900.0 14:40 14:52 S/D 11634'- CT Wt -3 k Is, WOB 1.7 k lbs, PU and continue in hole 11,779 WOB spike to 700 lbs, 11,797' WOB spike to 8351bs 4/19/2019 4/19/2019 2.20 PRODS DRILL DRLG P 1.86 bpm at 5951 psi, Free spin diff 11,900.0 11,984.0 14:52 17:04 1034 psi, WHP=15, BHP=3944 psi, IA=124, OA=29, CT 1 k lbs, WOB 2.11 k lbs. 11,935' PU 41 k lbs avg ROP 38 ft/min, 4/19/2019 4/19/2019 1.50 PRODS DRILL DRLG P OBD, 1.86 bpm at 4,107 psi, 11,984.0 12,057.0 17:04 18:34 Diff --1,100 psi, WHP=13, BHP=3,922, IA=125, OA=32 4/19/2019 4/19/2019 0.90 PRODS DRILL WPRT P Ratty Drilling, with increased weight 12,057.0 10,430.0 18:34 19:28 on pickup's, pull early wiper up hole, pull through window, jog the 5inch. RIH to log Kt marker 4/19/2019 4/19/2019 0.20 PRODS DRILL DLOG P Log formation (K1), correction of plus 10,430.0 10,463.0 19:28 19:40 4.0' 4/19/2019 4/19/2019 0.60 PRODS DRILL WPRT P Continue wiper IH 10,463.0 12,057.0 19:40 20:16 4/19/2019 4/19/2019 2.15 PRODS DRILL DRLG P BOBD, 1.87 bpm at 4,078 psi, 12,057.0 12,156.0 20:16 22:25 Diff=1,048 psi, WHP=14, BHP=3,910, IA=122, OA=28 New mud at the bit @ 12,110' 4/19/2019 4/19/2019 0.20 PRODS DRILL DRLG P PUH, obtain new pumping 12,156.0 12,156.0 22:25 22:37 parameters, PUW 40 k 4/19/2019 4/19/2019 0.20 PRODS DRILL DRLG P BOBD, 1.87 bpm at 4,078 psi, Diff -1, 12,156.0 12,173.0 22:37 22:49 psi, WHP=222, BHP=3,897, IA=122, OA=289 4/19/2019 4119/2019 0.50 PRODS DRILL DRLG P Hard spot, PUW 38 k, restart, BOBD, 12,173.0 12,184.0 22:49 23:19 1.87 bpm at 4,078 psi, Diff=1,060 psi, WHP=222, BHP=3,897, IA=122, OA=289 4/19/2019 4/19/2019 0.30 PRODS DRILL WPRT P PUH, mud weight falling, MM out 0.00, 12,184.0 12,184.0 23:19 23:37 take returns outside (35 bbls), returns cleaned up, bring returns back inside. 4/19/2019 4/19/2019 0.20 PRODS DRILL DRLG P BOBD, 1.87 bpm at 4,078 psi, 12,184.0 12,195.0 23:37 23:49 Diff --1,060 psi, WHP=222, BHP=3,897, IA=122, OA=289 4/19/2019 4/20/2019 0.18 PROD3 DRILL WPRT P PUH, PUW 51 k, pull short wiper up 12,195.0 11,795.0 23:49 00:00 hole, pumping BU 4/20/2019 4/20/2019 0.25 FROM DRILL WPRT P Wiper back in hole, RIW 6 k 11,795.0 12,195.0 00:00 00:15 4/20/2019 4/20/2019 0.50 PRODS DRILL DRLG P BOBD, 1.86 bpm at 4,050 psi, 12,195.0 12,198.0 00:15 00:45 Diff --1,049 psi, WHP=227, BHP=3,910, IA=122, OA=26 4/20/2019 4/20/2019 1.10 PROD3 DRILL WPRT T HOT has failed, circulate 5x5 sweep 12,198.0 10,684.0 00:45 01:51 and chase to the window 4/2012019 4/20/2019 0.25 PRODS DRILL WPRT T Jog the 5inch xi, Open EDC, POOH 10,684.0 10,348.0 01:51 02:06 4/20/2019 4/20/2019 2.00 PRODS DRILL TRIP T Shut down the pump, open EDC, 10,348.0 67.0 02:06 04:06 POOH pumping 2 bpm 4/20/2019 4/20/2019 1.50 PRODS DRILL PULD T LD BHA #22 67.0 0.0 04:06 05:36 4/20/2019 4/20/2019 1.50 PRODS DRILL PULD T PU BHA#23 0.0 72.0 05:36 07:06 4/20/2019 4/20/2019 1.20 PROD3 DRILL TRIP T RIH, shallow tested agitator, 940 psi 72.0 10,440.0 07:06 08:18 free spin diff Q 1.83 bpm Page 27135 Report Printed: 5128/2019 Operations Summary (with Timelog Depths) IC -11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Depth StartTune End Tune Our (hr) Phase Op Code Actively Code Time P -T -X Opermon (flKB) End Depth (ftKB) 4/20/2019 4/20/2019 0.20 PROD3 DRILL DLOG T Tie into the K1 for a -5' correction 10,440.0 10,464.4 08:18 08:30 4/20/2019 4/20/2019 0.50 PRODS DRILL TRIP T PU Weight 35 k lbs, continue to RIH. 10,464.4 12,198.0 08:30 09:00 Window and billet clean, SID @ 10,669', both CT Wt and WOB, PU dean continued to RIH, we were oriented as drilled on both runs. 4/20/2019 4/20/2019 0.10 PRODS DRILL DRLG P CT 4522 psi, @ 1.86 bpm in and 1.82 12,198.0 12,207.0 09:00 09:06 bpm out, free spin diff 1005 psi, OBD, CT Wt 0 k lbs, WOB 2.3 k lbs. ROP 90 fl/hr 4/20/2019 4/20/2019 3.20 PROD3 DRILL DRLG P OBD, CT 4726 psi, @ 1.86 bpm in and 12,207.0 12,332.0 09:06 12:18 1.82 bpm out, BHP 3896 psi, CT Wt 0 k lbs, WOB 1.9 k lbs. " Faulted into the D, -180 API rock ROP 40 ft/h 12,327' PU 40 k lbs 12,332' PU 40 k lbs Average ROP 39 ft/hr 4/20/2019 4/20/2019 0.90 PROD3 DRILL WPRT P PU 42 k lbs, PUH on BHA wiper, 12,332.0 11,079.0 12:18 13.12 12,225' CT wt increased from 37k to 44 k lbs, Some -tk WOB tougs up to 12,147' RBIH SID @ 12,184'2.6 k WOB. PUH, -6 k WOB 54k CT Wt, slight pack off event pump 5x5, slow pull UH whie sweep exits, tum around once sweep in cased hole " 1253' wiper #1 4/20/2019 4/20/2019 0.40 PRODS DRILL WPRT P RBIH, 11,079.0 12,332.0 13:12 13:36 Saw spot @ 12,230', dropped pump rate bumped through 4/20/2019 4/20/2019 1.30 PROD3 DRILL DRLG P CT 4573 psi, Q 1.86 bpm in and 1.85 12,332.0 12,361.0 13:36 14:54 bpm out, BHP 3899 psi, CT Wt -1.6 k lbs, WOB 2.6 k lbs. Diff pressure jumpingg, assuing plugged nomle(s) cleared. 12,339' PU 40 k lbs 12,355' PU 40 k lbs 12,355' PU 40 k lbs Average ROP 22 ftlhr 4/20/2019 4/20/2019 0.60 PROD3 DRILL DRLG P Required the sand 12,361.0 12,439.0 14:54 15:30 CT 4893 psi @ 1.85 bpm on bottom diff 1304 psi, BHP 3905 psi, WH 99 psi, IA 125 psi, OA 29 psi CT Wt 4 k lbs, WOB 1.8 k lbs, ROP 220 R/hr in between siderite stringers. Average ROP ft/hr 4/20/2019 4/20/2019 0.40 PROD3 DRILL WPRT P PU 41 k Pull up above the fault, 12,439.0 12,439.0 15:30 15:54 12,151' RBIH, set down @ fault 3 times, tried reducign rate and orienting. Made it through by orienting TF to low side and droping the pump. 4/20/2019 4/20/2019 1.10 PROD3 DRILL DRLG P CT 4633 psi, @ 1.85 bpm in and 1.83 12,439.0 12,581.0 15:54 17:00 bpm out, BHP 3896 psi, CT Wt -2 k lbs, WOB 2. k lbs. Average ROP ftlhr 4/20/2019 4/20/2019 1.00 PROD3 DRILL DRLG P OBD, 1.86 bpm at 4,050 psi, 12,581.0 12,700.0 17:00 18:00 Diff=1,049 psi, WHP=227, BHP=3,910, IA=122, OA=26 4/20/2019 4/20/2019 0.35 PRODS DRILL WPRT P Wiper up hole, PUW 38 k 12,700.0 11,700.0 18:00 18:21 4/20/2019 4/20/2019 0.20 PROD3 DRILL WPRT P Wiper back in hole, RIW 10 k 11,700.0 12,183.0 18:21 18:33 Page 28135 Report Printed: 512812019 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Stan Depth Start Time End Time Dur(hr) Phase op Code ANvity Code Tema P -T -X Operation (M(9) End Dept (4)(B) 4/20/2019 4/20/2019 0.20 FROM DRILL WPRT P Work pipe past Kuparuk D, PUW's 38- 12,183.0 12,183.0 18:33 18:45 40 k, minipulaling pump rate 4/20/2019 4/20/2019 0.25 FROM DRILL WPRT P Continue IH 12,183.0 12,700.0 18:45 19:00 4/20/2019 4/20/2019 3.50 FROM DRILL DRLG P OBD, 1.86 bpm at 4,050 psi, 12,700.0 13,115.0 19:00 22:30 Diff -1,049 psi, WHP=227, BHP=3,910, IA=122, OA=26 4/20/2019 4/20/2019 1.25 FROM DRILL WPRT P Wiper up hole, PUW 38 k, pull through 13,115.0 10,324.0 22:30 23:45 window, jog the 5 inch, w/sweep 4/20/2019 4121/2019 0.25 PRODS DRILL WPRT P RIH to log formation 10,324.0 10,361.0 23:45 00:00 4/21/2019 4/21/2019 0.10 PRODS DRILL WPRT P Continue IH 10,361.0 10,430.0 00:00 00:06 4/21/2019 4/21/2019 0.20 PROD3 DRILL DLOG P Log formation (K1), correction of plus 10,430.0 10,458.0 00:06 00:18 8.0' 4/21/2019 4/21/2019 1.00 FROM DRILL WPRT P Continue wiper back in hole, RIW 10,458.0 12,300.0 00:18 01:18 4/21/2019 4/21/2019 0.50 FROM DRILL WPRT P Work pipe through rough area 12,300.0 12,371.0 01:18 01:48 maniplulating pump rate, one pickup, PUW 43 k, continue IH 4/21/2019 4/21/2019 4.20 FROM DRILL DRLG P BOBD, 1.89 bpm at 4,950 psi, 13,115.0 13,205.0 01:48 06:00 Diff --1006, WHP=77, BHP=4,017, IA=125, OA=32 4/21/2019 4/21/2019 6.70 PRODS DRILL DRLG P Post crew change Pick up. CT Wt 43 13,205.0 13,494.0 06:00 12:42 lbs CT 5002 psi @ 1.89 bpm in, 1.83 bpm out, BHP 4124 psi, free spin diff 1010 psi Cl Wt -5 k Ibs, WOB 1.1 k lbs WHP=96, IA=131, OA=48 13307' PU 48 k lbs 13342' PU 46 k lbs 13377' PU 49 k lbs add 1 pbb beads to the high vis 5x5 sweep pumped with good results. 4/21/2019 4/21/2019 0.40 FROM DRILL WPRT P PU Wt 45 k lbs, Wiper#1 - 1000' 13,494.0 12,495.0 12:42 13:06 4/21/2019 4/21/2019 0.80 FROM DRILL WPRT P RBIH Wt 9 k to 5 k CT @ 50 fVmin 12,495.0 13,494.0 13:06 13:54 Stack out CT Wt 12896, reduce rate and running speed, struggle to bottom. 4/21/2019 4/21/2019 3.10 FROM DRILL DRLG P CT 4767 psi @ 1.79 bpm in and 1.73 13,494.0 13,679.0 13:54 17:00 bpm out, Free spin diff 884 psi, BHP 413 psi, OBD, CT Wt -7.7 k Ibs, WOB 0.5 k Is, ROP 70-30 ft/hr 13,632' PU W153 k lbs 4/21/2019 4/21/2019 4.50 PRODS DRILL DRLG P OBD, 1.80 bpm at 4,814 psi, 13,679.0 13,910.0 17:00 21:30 Diff --1,100 psi, WHP=214, BHP=4,123, IA=135, OA=46 4/21/2019 4121/2019 0.40 PRODS DRILL WPRT P Wiper up hole PUW 45 k, leave 13,910.0 13,110.0 21:30 21:54 beaded sweep in hole 4/21/2019 4121/2019 0.60 FROM DRILL WPRT P Wiper back in hole, RIW 6 k 13,110.0 13,910.0 21:54 22:30 4/21/2019 4/22/2019 1.50 PROD3 DRILL DRLG P OBD, 1.86 bpm at 4,050 psi, 13,910.0 13,955.0 22:30 00:00 Diff --1,100 psi, WHP=163, BHP=3,910, IA=122, OA=26 4/22/2019 4/22/2019 4.50 FROM DRILL DRLG P OBD, 1.86 bpm at 4,050 psi, 13,955.0 14,045.0 00:00 04:30 Diff --1,100 psi, WHP=163, BHP=3,910, IA=122, OA=26 4/22/2019 4/22/2019 0.30 FROM DRILL WPRT T Unable to achieve DLGS to stay within 14,045.0 14,045.0 04:30 04:48 the polygon PUH, PUW 46 k, Circ beaded sweep 4/22/2019 4/22/2019 0.70 PROD3 DRILL WPRT T POOH, laying 8.76 ppg beaded pill 14,045.0 12,543.0 04:48 05:30 Page 29/35 Report Printed: 5/28(2019 Operations Summary (with Timelog Depths) 1c-11 NIQW Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Depth Sten Time End Time Dur (hr) Phase Op Code Activity Code Time P -T -X Operation (RKB) End Depth(0Ka) 4/22/2019 4/22/2019 0.20 PROD3 DRILL WPRT T Pulled 10 k over CT WT and up to -8 k 12,543.0 12,132.0 05:30 05:42 WOB. Motor stalled, bit stuck, worked pipe over interval, pulled free. 4/22/2019 4/22/2019 2.80 PROD3 DRILL TRIP T Continue to POOH, Billet and window 12,132.0 65.0 05:42 0830 clean, Jog the 5', POOH, bump up 4/22/2019 4/22/2019 1.40 PROD3 DRILL PULD T PUD BHA 23, checks not holding, 65.0 0.0 08:30 0954 close EDC, follow new PUD procedure. Bit graded out 1-1 4/22/2019 4/22/2019 1.20 PROD3 DRILL PULD T PD BHA 24, 1.VAKO, over RR 0.0 64.0 09:54 1106 P104 BH bit. Swap checks post pumping beads, check pack offs, stab injector, tool test good, bump up and space out. 4/22/2019 4/22/2019 2.00 PROD3 DRILL TRIP T RIH, shallow test agitator. 64.0 10,440.0 11:06 13:06 4/22/2019 4/22/2019 0.20 PROD3 DRILL DLOG T Tie into the K1 for -3.5' correction 10,440.0 10,469.0 13:06 13:18 4/22/2019 4/22/2019 0.20 PROD3 DRILL DLOG T Continue to RIH. Park at 10,469.0 10,679.0 13:18 13:30 10,679.18CTMD - 6494.82 TVD and measure BHP. Trapped 3860 psi and watched it climb to 3987, bled off 20 psi, observed pressure climb back to 3987 - 11.82 EMW 4/22/2019 4/22/2019 1.20 PROD3 DRILL TRIP T PU Wt 33 k Is, continue to RIH, 10,679.0 12,175.0 13:30 1442 window and billet clean. 12,175' observe gas at surface, export returns to the tiger tank. S/D 3 K WOB @ 12,295', PUH, pulling -5 k WOB @ 12,215' Clean after 12,179' 4/22/2019 4/22/2019 0.40 PROD3 DRILL TRIP T PUH whil holding 12 ppg EMW @ the 12,175.0 12,225.0 14:42 1506 window and exporting returns to the tiger tankturn around @ 11,596', Atempt to RBIH. Returns cleaned up, brought back inside ( 100 bbls to the tiger tank) 4/22/2019 4/22/2019 0.60 PROD3 DRILL TRIP T S/D 12,220'11 times, varied running 12,225.0 12,395.0 15:06 1542 speed, pump rates, TF until popping through to 12,306 varied parameters 3 times popped through 4/22/2019 4/22/2019 1.30 PROD3 DRILL TRIP T Continue to RICH. Struggling W poor 12,395.0 14,045.0 15:42 1700 weight transfer, pump 20 bbl bead sweep, ride to bottom on beads. 4/22/2019 4/22/2019 1.80 PROD3 DRILL TRIP T On bottom drilling, rammped up pum 14,045.0 14,074.0 17:00 1848 as we kissed bottom, no free spin diff. CT 5562 psi @ 1.78 bpm, OR diff 1245, BHP 4381 argeting 12 ppg at the window. CT -5 k lbs, WOB 2.55 k lbs ROP 20 f /hr 4/22/2019 4/22/2019 1.70 PROD3 DRILL TRIP T "New mud at the bit 14,074' 14,074.0 14,100.0 18:48 2030 New mud all the way around @ 19:30 -14,085', PU Wt 44 k lbs, CT 4984 psi @ 1.81 bpm in and 1.71 bpm out, Free spin Diff 1141 psi, BHP 4339 psi holding 12.1 ppg @ the window. CT Wt -8 k Ins, WOB 2.2 k Its, ROP 15 ft/hr 14,108' PU Wt 47 k lbs 4/22/2019 4/23/2019 3.50 PROD3 DRILL TRIP T Reaquired sand 14,100.0 14,285.0 20:30 00:00 OBD, CT 5294 psi, @ 1.86 bpm, BHP 4357 psi, CT -8.4 k lbs, WOB 1.64 k Ibs, WH 357 psi, IA 124, OA 50 psi Page 30135 Report Printed: 5/28/2019 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Time End Time Dur (hr) Phase Op Code Activity Code Time P -T -X Operation Sfart Dept (flKB) End DepN (flKB) 4/23/2019 4/23/2019 4.00 PRODS DRILL DRLG P OBD, 1.87 bpm at 5,446 psi, 14,285.0 14,447.0 00:00 04:00 Diff=1,150 psi, WHP=347, BHP=4,388, IA=133, OA=54 Osculating: 14,302'-14309' 14,333'-14,416' 14,438'-14,447' 4/23/2019 4/23/2019 0.50 PROD3 DRILL WPRT P Wiper up hole to 13,447', PUW 47 k 14,447.0 13,647.0 04:00 04:30 4/23/2019 4/23/2019 0.40 PRODS DRILL WPRT P Wiper back in hole, RIW 04k CTSW 13,647.0 14,447.0 04:30 04:54 4/23/2019 4/23/2019 1.90 PRODS DRILL DRLG P OBD, 1.87 bpm at 5,446 psi, 14,447.0 14,577.0 04:54 06:48 Diff ---1,150 psi, WHP=347, BHP=4,388, IA=133, OA=54 "` Osculation 14,447'-14,574' 4/23/2019 4/23/2019 0.60 PRODS DRILL WPRT P 800' wiper up hole, 55 k 14,577.0 14,577.0 06:48 07:24 4/23/2019 4/23/2019 6.00 PRODS DRILL DRLG P OBD, 1.87 bpm at 5,446 psi, 14,577.0 14,850.0 07:24 13:24 Diff=1,150 psi, WHP=347, BHP=4,388, IA=133, OA=54, (average DLGS 4° while osculating) Osculation 14,613'-14,644' 14,668'-14,717' 4/23/2019 4/23/2019 0.40 PROD3 DRILL WPRT P 800' wiper up hole, PUW 47 k 14,850.0 14,050.0 13:24 13:48 4/23/2019 4/23/2019 0.60 PROD3 DRILL WPRT P Wiper back in hole,RIW 0.0-2.Ok 14,050.0 14,850.0 13:48 14:24 4/23/2019 2.50 PRODS DRILL DRLG P OBD, 1.87 bpm at 5,446 psi, 14,850.0 14,942.0 14:24 16:54 Diff --1,150 psi, WHP=347, 14/23/2019 BHP=4,388, IA=133, OA=54, (average DI -GS 4' while osculating), Heavy PU @ 14,920' 4/23/2019 4/23/2019 0.20 PRODS DRILL WPRT P 14942, BHA wiper, PUW=62K 14,942.0 14,942.0 16:54 17:06 4123/2019 4/24/2019 6.90 PRODS DRILL DRLG P 14942', Drill, 1.8 BPM @ 4970 PSI 14,942.0 15,152.0 17:06 00:00 FS, BHP=4430. RIW=-7.1K, DHWOB=.9K, ROP=45-25 FPH. Oscillate from 15017. Pump sweeps with BHa wipers as needed 4/24/2019 4/24/2019 1.60 PRODS DRILL DRLG P Continue drilling, 1.8 BPM @ 5207 15,152.0 15,190.0 00:00 01:36 PSI FS, BHP=4417 PSI, RIW=-5.5, DHWOB=1.1 K, ROP=33 FPH 4/24/2019 4/24/2019 0.50 PRODS DRILL CIRC P Call TD @ 15190'. PUH for sweeps 10 15,190.0 15.1-0-0 01:36 02:06 low vis 50 Hi vis with beads. PUW=47K 4/24/2019 4/24/2019 2.30 PROD3 DRILL WPRT P Start swab wiper. See ratty area 15,190.0 10,437.0 02:06 04:24 12,300' to 12,100' with light over pulls. Did not have to RBIH. See RA marker - 20 off. PUH and jog 5" tubing. Continue up hi=ole 19 4/24/2019 0.10 PRODS DRILL DLOG P Log K1 for +17.5 10,437.0 10,455.0 04:24 04:24 04:30 4/24/2019 4/24/2019 2.00 PRODS DRILL WPRT P Continue swab wiper 10,455.0 78.3 04:30 06.30 4/24/2019 4/24/2019 1.70 PRODS DRILL TRIP P Tag up reset counters, RBIH 78.3 10,435.0 06:30 08:12 4/24/2019 4/24/2019 0.20 PRODS DRILL DLOG P Log formation (K1), correction of plus 10,435.0 10,467.0 08:12 0824 2.0' 4/24/2019 4/24/2019 0.20 PRODS DRILL TRIP P Continue IH 10,467.0 10,680.0 08:24 08:36 Page 31135 Report Printed: 5/28/2019 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Stan Time End Time our (hr) Phase Op COtle Activity Code Tura P -T -X Operation Stan Depth (111(13) End Depth (I") 4/24/2019 4/24/2019 0.50 PRODS DRILL OWFF P Obtain static hole pressure @ 10,680', 10,680.0 10,680.0 08:36 09:06 6495.91' TVD, 11.806 ppg (3,984 psi AP), 973 WHP, weight check 4124/2019 4/24/2019 1.50 PROD3 DRILL TRIP P Continue IH through window exit, S/D 10,680.0 15,201.0 09:06 10:36 12,238', and 14,607', confirm TO @ 15,201- 4/24/2019 4124/2019 0.50 PROD3 DRILL TRIP P Circulate 12.1 ppg completion fluid, 15,201.0 15,201.0 10:36 11:06 PUH slowly 4/24/2019 4/24/2019 4.50 PRODS DRILL TRIP P POOH, laying in 12.1 ppg beaded liner 15,201.0 78.3 11:06 15:36 running pill, painting EOP flags 13,960' (yellow) 4/24/2019 4/24/2019 0.50 PRODS DRILL OWFF P At surface, check well for flow, PJSM 78.3 78.3 15:36 16:06 4/24/2019 4/24/2019 0.50 FROM DRILL PULD P LD drilling assembly on a dead well. 78.3 0.6- 16:06 16:36 4/24/2019 4/24/2019 2.80 PROD3 DRILL CTOP P Test coil for flat spot wall thickness 0.0 0.0 16:36 19:24 @.100. Trim 14' of CT Prep CT install connector. Pull test CTC to 35K. Rehead E -line to UQC. Test wire @ +2000 / 75.6. Pressure lest to 450OPS1 4/24/2019 4/24/2019 0.60 FROM DRILL BOPE P Perform Bi weekly BOPE function test 0.0 0.0 19:24 20:00 4/24/2019 4/24/2019 2.20 COMPZ3 CASING PUTB P PJSM, Prep floor for liner pick up. P/U 0.0 1,223.1 20:00 22:12 12-02 lower liner segment withnon ported bullnose, 41 joints 2 318" slotted liner, and shorty deployment sleeve 4/24/2019 4/24/2019 0.70 COMPZ3 CASING PULD P M/U coil trek to liner. MIU injector and 1,223.1 1,267.0 22:12 22:54 1 surface test. Check pack offs 4/24/2019 4125/2019 1.10 COMPZ3 CASING TRIP P Trip in hole, BHA#25 1,267.0 7,450.0 22:54 00:00 4/25/2019 4/25/2019 0.60 COMM CAS I -NG TRIP P Continue in hole with BHA#25 1-2-02 7,450.0 10,567.0 00:00 00:36 1 lower liner segment, First pick up @ 10,490' start working liner in hole 4/25/2019 4/25/2019 0.10 COMPZ3 CASING DLOG P Stop and correct to flag + 13.5' 10,567.0 10,580.0 00:36 00:42 4/25/2019 4/25/2019 0.80 COMPZ3 CASING RUNL P Continue in hole with liner. Working 10,580.0 11,635.0 00:42 01:30 liner with headway 4/25/2019 4/25/2019 0.20 COMPZ3 CASING DLOG P Log K1 for -22' 11,635.0 11,685.0 01:30 01:42 4/25/2019 4/25/2019 5.40 COMM CASING RUNL P Continue working liner to bottom 11,685.0 12,185.0 01:42 07:06 4/25/2019 4/25/2019 2.30 COMPZ3 CASING TRIP T Unable to get liner to bottom, POOH 12,185.0 1,267.0 07:06 09:24 4/25/2019 4/25/2019 0.50 COMPZ3 CASING OWFF T At surface, check well for flow (no- 1,267.0 1,267.0 09:24 09:54 flow), 5 bbl static losses 4/25/2019 4/25/2019 0.50 COMPZ3 CASING PULD T LD, CoilTrak tools 1,267.0 1,222.8 09:54 10:24 1 4/25/2019 4/25/2019 2.50 COMPZ3 CASING PULL T PJSM, lay down liner segment #1 1,222.8 0.0 10:24 12:54 4/25/2019 4/25/2019 0.70 COMPZ3 CASING PULD T MU cleanout assembly 0.0 68.4 12:54 13:36 4/25/2019 4/25/2019 1.80 COMM CASING TRIP T Tag up, reset counters, RIH with BHA 68.4 10,430.0 13:36 15:24 #26, surface lets agitator, 1.8 bpm at 1,050 psi, 4/25/2019 4/25/2019 0.20 COMPZ3 CASING DLOG T Log formation (K1) correction of minus 10,430.0 10,469.2 15:24 15:36 4.5' 4/25/2019 4/25/2019 0.30 COMPZ3 CASING TRIP T Continue IH 10,469.2 10,859.0 15:36 15:54 Page 32135 Report Printed: 5/28/2019 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Depth De Start Time End Imre ouch (� Phase O Code p Activity Code y Time P -T- X Operation (k EM Depth (kKe) 4/25/2019 4/25/2019 0.60 COMPZ3 CASING TRIP T Set down @ 10,859', PUH, PUW 38 it, 10,859.0 12,193.0 15:54 16:30 adjust TF RBIH, popped through, continue IH to next SO @ 12,193' 4/2512019 4/25/2019 1.10 COMPZ3 CASING CIRC T PUH slowly displacing well to drilling 12,193.0 10,700.0 16:30 17:36 fluid 4125/2019 4/25/2019 1.20 COMPZ3 CASING REAM T Clean out 10,700'to setdown @ 10,700.0 12,190.0 17:36 18:48 12,190 4/25/2019 4/25/2019 2.90 COMPZ3 CASING REAM T Set down@ 12,190, Start working 12,190.0 12,365.0 18:48 21:42 area 12,190 to 12,365 with 100' bites and wipers up to 11,800'. Good amount of material over shaker. Circulate multiple Bottoms up. 4/25/2019 4/25/2019 0.90 COMPZ3 CASING REAM T 12,365 able to run in hole @ 1.8 BPM. 12,365.0 13,800.0 21:42 22:36 25 FPM with minor stacking untill 13,800 4/2512019 4/26/2019 1.40 COMPZ3 CASING REAM T 13,800'. Loose surface weight, 13,800.0 15,170.0 22:36 00:00 Continue to work pipe to 15170 with multiple attempts to get there. Multiple BHA wipers. Get gas cut mud at surface. Ship returns to tiger tank. Send 60 BBIs out. 4/26/2019 4126/2019 1.10 COMPZ3 CASING REAM T Pick up from 15170 to 15127. Unable 15,170.0 15,170.0 00:00 01:06 1 1 to get back to 15170. RIW=-8K. 4/26/2019 4/26/2019 2.00 COMPZ3 CASING REAM T Back at 15,165. Trip up to tie into RA 15,170.0 10,700.0 01:06 03:06 for hole assessment. Good trip up. Some slight overpulls 12,250 to 12,150. Looks goad coming up Pumping 1.8 BPM 4/26/2019 4/26/2019 0.10 COMPZ3 CASING DLOG T Log RA in for+13' 10,700.0 10,721.0 03:06 03:12 4/26/2019 4/26/2019 1.30 COMPZ3 CASING REAM T RBIH 50 FPM, 1.86 BPM. Set down 10,721.0 14,125.0 03:12 04:30 12,284, P/U went right through. Clean down to 12,354'. Pick up and went right through. Continue in. Set down 13034 No DHWOB. Pick up went right through 4/26/2019 4/26/2019 1.30 COMPZ3 CASING REAM T Lost surface weight, RIW=-6K, Slow 14,125.0 15,186.0 04:30 05:48 run in speed 4/26/2019 4126/2019 1.70 COMPZ3 CASING TRIP T PUH laying in beaded 8.8 ppg LRP 15,186.0 10,684.0 05:48 07:30 4/26/2019 4/26/2019 1.60 COMPZ3 CASING TRIP T Above window, continue POOH 10,684.0 1,500.0 07:30 09:06 pumping beads, encountered gassed up returns, set out 12 bbl of fluid to tiger tank, returns cleaned up, continue POOH 4/26/2019 4/26/2019 0.20 COMPZ3 CASING TRIP T Perform jog back in hole 1,500.0 2,186.0 09:06 09:18 4/26/2019 4/26/2019 0.60 COMPZ3 CASING TRIP T Continue POOH 2,186.0 68.4 09:18 09:54 4/26/2019 4/26/2019 2.00 COMPZ3 CASING TRIP T Tag up, reset counters, RIH 68.4 10,435.0 09:54 11:54 4/26/2019 4/2612019 0.30 COMPZ3 CASING DLOG T Log formation (K1) correction of minus 10,435.0 10,680.0 11:54 12:12 45, continue IH to check pressures 4/26/2019 4/26/2019 0.15 COMPZ3 CASING OWFF T Obtain static pressure above window 10,680.0 10,680.0 12:12 12:21 6502.79' TVD, 11.852 ppg, 864 psi WHP, 4,004 AP 4/2612019 4/26/2019 0.50 COMPZ3 CASING TRIP T Continue IH to 10,900', PUH slowly 10,680.0 10,900.0 12:21 12:51 1 I I circulating 12.1 ppg beaded completion fluid down roil. 4/26/2019 0.80 COMPZ3 POOH, laying in beaded 12.1 ppg 10,900.0 7,640.0 14126/2019 12:51 13:39 LRP, encounter gas cut returns 8,670', ICASING-TIP IT I send out to the tiger tank. Paint EOP flag 13,180' Page 33135 ReportPrinted: 6/2812019 Operations Summary (with Timelog Depths) 1c-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log start Depth Start Tune End Time Dur (hr) Phase op Code Activity Cade Tune P -T -X operation (flKB) End Depth (BXa) 4126/2019 4/26/2019 0.50 COMPZ3 CASING TRIP T Stop moving OOH, continue 7,640.0 7,640.0 13:39 14:09 displacing well to completion fluid. 4126/2019 4/26/2019 1.25 COMPZ3 CASING TRIP T Continue POOH, paint EOP flag 7,640.0 68.4 14:09 15:24 7,639.3' 4/26/2019 4/26/2019 0.50 COMPZ3 CASING PULD T Check well for flow (no -flow), PJSM 68.4 68.4 15:24 15:54 4/26/2019 4/26/2019 0.50 COMPZ3 CASING PULD T LD cleanout BHA on a dead well. 68.4 0.0 15:54 16:24 **" Note: 2.80 no-go 4/26/2019 4/26/2019 0.50 COMPZ3 CASING BHAH T Prep RF for liner ops 0.0 0.0 16:24 16:54 4/26/2019 4/26/2019 3.00 COMPZ3 CASING PUTS T PU 66 joints of slotted (liner 0.0 1,973.0 16:54 19:54 4/26/2019 4/26/2019 1.40 COMPZ3 CASING PULD T P/U Coiltrak tools. Make up to liner. 1,973.0 1,018.0 19:54 21:18 M/U coil and surface test tools 4/26/2019 4/26/2019 1.60 COMPZ3 CASING TRIP T Trip in well, EDC shut 1,018.0 10,627.0 21:18 22:54 4/26/2019 4/26/2019 0.10 COMPZ3 CASING DLOG T Tip into EOP flag for -97, PUW=38K 10,627.0 10,618.0 22:54 23:00 4/26/2019 4/27/2019 1.00 COMPZ3 CASING TRIP T Continue in well. Initial setdown with 10,618.0 12,247.0 23:00 00:00 PIU @ 12047'. Work pipe down to midnight depth @ 12,247 4/2712019 4/27/2019 1.90 COMPZ3 CASING RUNL T Continue working liner to bottom 12,247.0 12,580.0 00:00 01:54 4/27/2019 4/27/2019 0.10 COMPZ3 CASING RUNL T Pump down coil in compression, .5 12,580.0 12,580.0 01:54 02:00 BPM 4/2712019 4/27/2019 1.10 COMPZ3 CASING RUNL T SID pump. Continue to work liner 12,580.0 12,713.0 02:00 03:06 4/2712019 4/27/2019 0.10 COMPZ3 CASING RUNL T Roll pump in compression, .5 BPM 12,713.0 12,713.0 03:06 03:12 4/2712019 4/27/2019 0.60 COMPZ3 CASING RUNL T Work liner towards bottom 12,713.0 12,767.0 03:12 03:48 4/2712019 4/27/2019 0.10 COMPZ3 CASING RUNL T Roll pump 12,767.0 12,767.0 03:48 03:54 4/27/2019 4/27/2019 1.20 COMPZ3 CASING RUNL T Continue wiorking liner, 12,878 tough 12,767.0 12,901.0 03:54 05:06 spot. Pump 1 BPM in compression. No returns. 4/2712019 427/2019 1.65 COMPZ3 CASING RUNL P Continue IH, setting down 15,188', 12,901.0 15,201.0 05:06 06:45 42712019 4/27/2019 0.20 COMPZ3 CASING CIRC P Bring pump up to 1.9 bpm and 1,230 15,201.0 13,214.0 06:45 06:57 psi diff, PUW 35 k 42712019 4/27/2019 3.75 COMPZ3 CASING TRIP P Remove liner length from counters, 13,214.0 10,900.0 06:57 10:42 circulate 8.8 ppg drilling fluid around to clear annulus of mixed fluids, PUH laying in beaded 8.8 ppg LRP up to 10,900' 4/27/2019 4/27/2019 0.25 COMPZ3 CASING TRIP P Continue POOH, laying in 12.1 ppg 10,900.0 10,420.0 10:42 10:57 beaded LRP 4/2712019 427/2019 0.20 COMPZ3 CASING DLOG P Log formation (K1) for depth control 10,420.0 10,458.0 10:57 11:09 plus 11.0 4/27/2019 427/2019 2.00 COMPZ3 CASING TRIP P Continue POOH, laying in 12.1 ppg 10,458.0 44.2 11:09 13:09 beaded LRP 4/2712019 4/27/2019 0.50 COMPZ3 CASING OWFF P Tag up, check well for flow (no -flow), 44.2 44.2 13:09 13:39 PJSM 4/27/2019 4/27/2019 0.75 COMPZ3 CASING PULD P LD setting tools 44.2 0.0 13:39 14:24 4/27/2019 4/27/2019 0.50 COMPZ3 CASING PUTB P Prep RF for liner OPS 0.0 0.0 14:24 14:54 Page 34/35 Report Printed: 5128/2019 Operations Summary (with Timelog Depths) IC-11 Rig: NABORS CDR3-AC Job: DRILLING SIDETRACK Time Log Start Tme End Time Dur (hr) Phase Op Code Activity Code Time P-T-X Operabon Start Depth (ftKB) End Depth (1i 4/27/2019 4/27/2019 4.40 COMPZ3 CASING PUTB P Start picking up liner segment #2 with 0.0 2,976.3 14:54 18:18 large ported, 1.25" bullnose, 99 its slotted liner and shorty deployment sleeve 4/27/2019 4/27/2019 0.90 COMPZ3 CASING PULD P PJSM, P/U Coiltrak, M/U to liner and 2,976.3 3,020.6 19:18 2012 hang in deployment rams. Change out floats in UQC. Inspect packoffs. M/U coil and surface test. Strip on. Tag up and set counters 4/27/2019 4/27/2019 1.60 COMPZ3 CASING TRIP P RIH BHA #28, EDC closed pumping 3,020.6 10,628.0 20:12 21:48 j min rate 4/27/2019 4/27/2019 0.10 COMPZ3 CASING DLOG P Tie into flag for-8.1', PUW=37K 10,628.0 10,619.0 21:48 21:54 4/27/2019 4/27/2019 0.30 COMPZ3 CASING RUNL P Continue in well, Initial stack out @ 10,619.0 11,415.0 21:54 22:12 11,415 4/27/2019 4/28/2019 1.80 COMPZ3 CASING RUNL P 11,415, Working liner to bottom 11,415.0 12,305.0 22:12 0000 4/28/2019 4/28/2019 3.40 COMPZ3 CASING RUNL P Continue working 1-2-02 liner to 12,305.0 13,213.0 00:00 03:24 bottom 4/28/2019 4/28/2019 0.10 COMPZ3 CASING RUNL P Hard tag @ 13213, PUW=62K. 13,213.0 13,195.6 03:24 0330 Repeat twice. Same spot. Bring pumps online 1.5 BPM @ 3145 PSI. Release liner PUW=32K 4/28/2019 4/28/2019 0.40 DEMOB WELLPR PRTS P PUH to 13195. Remove liner length 13,195.6 10,219.2 03:30 0354 left in hole 2976.34. Perform static test, Sensor depth TVD 6184.98', Pressure stabilized @ 3882 PSI, EMW=12.07 25 Minute test 4/28/2019 4/28/2019 2.00 DEMOB WELLPR CIRC P Dispace well to seawater 10,219.2 10,219.2 03:54 0554 4/28/2019 4/28/2019 1.20 DEMOB WELLPR TRIP P POOH 10,219.2 2,500.0 05:54 0706 4/28/2019 4/28/2019 1.00 DEMOB WELLPR FRZP P LRS on location, PJSM, move unit in, 2,500.0 2,500.0 07:06 08:06 RU, and PT hose to 4,000 psi, Freeze protect well from 2,500' with 32 bbls of deisel 4/28/2019 4/28/2019 0.55 DEMOB WELLPR TRIP P Continue POOH 2,500.0 44.2 08:06 08:39 4/28/2019 4/28/2019 1.25 DEMOB WELLPR PULD P At surface, PUD and LD setting tools 44.2 0.0 08:39 09:54 FTP 1,200 psi 4/28/2019 4/28/2019 2.00 DEMOB WELLPR CTOP P MU Nozzle, stab onto stump, flush 0.0 0.0 09:54 11:54 stack and surface lines to tiger tank, vac truck on location remove returns from tank 4/28/2019 4/28/2019 6.10 DEMOB WELLPR RURD P RDMO 0.0 0.0 11:54 18:00 Rig Release 18:00 hrs Page 35135 ReportPrinted: 5/28/2019 PTO209-©%-8 Loepp, Victoria T (DOA) From: Long, William R <William.R.Long@conocophillips.com> Sent: Friday, March 22, 2019 1:37 PM To: Loepp, Victoria T (DOA) Cc: Ohlinger, James J Subject: RE: [EXTERNAL]KRU 1C-11 L1-02(PTD 209-078) Follow Up Flag: Follow up Flag Status: Flagged The 1C -11L1 laterals will remain producing. The whipstock will allow flow past. Thanks, William R. Long Staff CTD Engineer ConocoPhillips 907-263-4372 (office) 281-723-6000 (cell) William.R.Long@ConocoPhillips.com From: Loepp, Victoria T (DOA) <victoria.loepp@alaska.gov> Sent: Friday, March 22, 2019 1:23 PM To: Long, William R <William.R.Long@conocophillips.com> Subject: [EXTERNAL]KRU 1C-11L1-02(PTD 209-078) William, Are the 1C-111-1 laterals producing? Is the whipstock to be set a flow through whipstock? Thanx, Victoria Victoria Loepp Senior Petroleum Engineer State of Alaska Oil & Gas Conservation Commission 333 W. 7th Ave Anchorage, AK 99501 Work: (907)793-1247 Victoria. Loeooftalaska.00v CONFIDENTIAUIY NOTICE: This e-mail message, including any attachments, contains information from the Alaska Oil and Gas Conservation Commission (AOGCC), State of Alaska and is for the sole use of the intended recipient(s). It may contain confidential and/or privileged information. The unauthorized review, use or disclosure of such information may violate state or federal law. If you are an unintended recipient of this e-mail, please delete it, without first saving or forwarding it, and, so that the AOGCC is aware of the mistake in sending it to you, contact Victoria Loepp at (907)793-1247 or Victona.Loeoo@alaska.aov THE STATE °fALASKA 11. GOVERNOR MIKE DUNLEAVY James Ohlinger Staff CTD Engineer ConocoPhillips Alaska, Inc. P.O Box 100360 Anchorage, AK 99510-0360 Re: Kuparuk River Field, Kuparuk Oil Pool, KRU 1C -11L1-02 Permit to Drill Number: 209-078 Sundry Number: 319-126 Dear Mr. Ohlinger: Alaska Oil and Gas Conservation Commission 333 West Seventh Avenue Anchorage, Alaska 99501-3572 Main: 907.279.1433 Fax: 907.276.7542 www.aogcc.olaska.gov Enclosed is the approved application for the sundry approval relating to the above referenced well. Please note the conditions of approval set out in the enclosed form. As provided in AS 31.05.080, within 20 days after written notice of this decision, or such further time as the AOGCC grants for good cause shown, a person affected by it may file with the AOGCC an application for reconsideration. A request for reconsideration is considered timely if it is received by 4:30 PM on the 23rd day following the date of this letter, or the next working day if the 23rd day falls on a holiday or weekend. erely, Daniel T. Seamount, Jr. Commissioner a DATED this 2'2 day of March, 2019. RB0MSL^1 MAR 2 7 2019 STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION APPLICATION FOR SUNDRY APPROVALS 20 AAC 25.280 FI P M 1. Type of Request: Abandon ❑ Plug Perforations ❑ Fracture Stimulate ❑ Repair Well ❑ Operations shutdown ❑ Suspend ❑ Perforate ❑ Other Stimulate ❑ Pull Tubing ❑ Change Approved Program ❑ Plug for Redrill ❑ Perforate New Pool ❑ Re-enter Susp Well ❑ Alter Casing ❑� Other: ❑ . 2. Operator Name: 4. Current Well Class: 5. Permit to Drill Number: ConocoPhillips Alaska, Inc. Exploratory ❑ Development ❑� . Stratigraphic ❑ Service ❑ 209-078 3. Address: 6. API Number: PO Box 100360, Anchorage, AK 99510 50-029-22714-62-00 ' 7. If perforating: 8. Well Name and Number: What Regulation or Conservation Order governs well spacing in this pool? N/A KRU 1 C-11 L1-02 ' Will planned perforations require a spacing exception? Yes ❑ No ❑� 9. Property Designation (Lease Number): 10. Field/Pool(s): ADL 25638, 25649 Kuparuk River Field / Kuparuk River Oil Pool 11. PRESENT WELL CONDITION SUMMARY Total Depth MD (ft): Total Depth TVD (ft): Effective Depth MD: Effective Depth TVD: MPSP (psi): Plugs (MD): Junk (MD): 13,031 6636' 13,029 6636 2955 N/A N/A Casing Length Size MD TVD Burst Collapse Structural Conductor 80, 16" 121' 121• Surface 6902' 9-5/8" 6943' 4439' Production 10,386' 7" 10,427' 6344' Liner 1029' 5" 11,300' 7011' Scab Liner 5108' 3-1/2" 10,271' 6231' CTD Liner 2782' 2-3/8" 13,030' 6636' Perforation Depth MD (ft): Perforation Depth TVD (ft): Tubing Size: Tubing Grade: Tubing MD (ft): 10,660'- 10,716' 6517'- 6559' 3-1/2" L-80 5193' Packers and SSSV Type: Packers and SSSV MD (ft) and TVD (ft): FHL Retdev, Baker Premier, Carrico SSSV 5203',10,141', 2297-13518', 6143',1994- 143',1994'12. 12.Attachments: Proposal Summary 0 Wellbore schematic 13. Well Class after proposed work: Detailed Operations Program ❑ BOP Sketch ❑ Exploratory ❑ Stratigraphic ❑ Development ❑� * Service ❑ 14. Estimated Date for 15. Well Status after proposed work: Commencing Operations: 18 -Mar -79 OIL ❑� WINJ ❑ WDSPL E] Suspended El GAS ❑ WAG ❑ GSTOR ❑ SPLUG ❑ 16. Verbal Approval: Date: Commission Representative: GINJ ❑ Op Shutdown ❑ Abandoned ❑ 17. 1 hereby certify that the foregoing is true and the procedure approved herein will not be deviated from without prior written approval. Authorized Name: James Ohlinger Contact Name: William Long Authorized Title: Staff CTD Ener Contact Email: William. R. Lon COP.com ,. /y/-7 Contact Phone: 907-263-4372 Authorized Signature. Date: Ji/� COMMISSION USE ONLY Conditions of approval: Notify Commission so that a representative may witness Sundry Number: G Plug Integrity ❑ BOP Test ❑ Mechanical Integrity Test ❑ Location Clearance ❑ Other: RBDMS±"/ MAR 2 7 2019 Post Initial Injection MIT Req'd? Yes ❑ No 4 Spacing Exception Required? Yes ❑ No V Subsequent Form Required: /O_ 4,0 &* APPROVED BY Approved by: COMMISSIONER THE COMMISSION Date: l ` SUDmtt corm and Form 10-403 Revised 4/2017 Approved appli0a �apa ro� o s�rfom the date of approval. Ahachm nts in Dupli e oa�312411 V7-1- 3/22//9 V L ,0#- 3; �9 ConocoPhillips Alaska P.O. BOX 100360 ANCHORAGE, ALASKA 99510-0360 March 13, 2019 Commissioner - State of Alaska Alaska Oil & Gas Conservation Commission 333 West 7th Avenue Suite 100 Anchorage, Alaska 99501 Dear Commissioner: ConocoPhillips Alaska, Inc. hereby submits sundry application to set a whipstock and applications for permits to drill three laterals out of the KRU 1 C-11 (PTD# 196-172) using the coiled tubing drilling rig, Nabors CDR3-AC. --Also included in this submission is a sundry application to cut and remove liner from KRU 1C-11 L1-02 (PTD# ✓ 5 d 209-078) to gain access to the kick o point inn11 CC -11. CTD operations are scheduled to begin in late March 2019. The objective will be to drill thre laterals, KRU 1 C- 11 L2, 1C-111-2-01, and 1C-111-2-02, targeting the Kuparuk C -sand interval. To account for geological uncertainties, ConocoPhillips requests a variance from the requirements of 20 --- AAC 25.015 to allow the actual kick-off point to be anywhere along the length of the parent lateral instead of being limited to 500' from the original point. Attached to the sundry applications are the following documents: - Sundry Application Forms (10-403) for 1C-11 and 1C-11 L1-02 - Operations Summary in support of the 10-403 Sundry Applications - Current Wellbore Schematic - Proposed CTD Schematic Attached to permit to drill applications are the following documents: - Permit to Drill Application Forms (10-401) for 1C-11 L2, 1C-111-2-01, and 1C-111-2-02 - Detailed Summary of Operations - Directional Plans for 1C-11 L2, 1C-11 L2-01, and 1C-111-2-02 - Current Wellbore Schematic - Proposed CTD Schematic If you have any questions or require additional information, please contact me at 907-263-4372. Sincerely, William R. Long Coiled Tubing Drilling Engineer ConocoPhillips Alaska KRU 1 C-11 (PTD: 196-172) KRU 1C-11 L1-02 (PTD: 209-078) CTD Summary for Sundry Summary of Operations: KRU well 1C-11 is a Kuparuk C -Sand producer equipped with 3-1/2" tubing and 5" production casing. The CTD sidetrack will utilize three laterals to target the C -sands to the north and north-east of 1 CA 1. The laterals will increase C -sand resource recovery and throughput. Prior to CTD rig up, the CTD liner landed in the 1C-11 L1-02 will be cut CDR3-AC will pull the cut liner and set a mechanical thru tubing whipstock inside the 5" casing at the planned kick off point of 10,684' MD. The 1C-11 L2 lateral will exit through the 5" and drill to a planned TD at 13,000' MD, targeting the C sand to the north. The lateral will be left unlined. An aluminum billet for kicking off will be set at 12,490' MD. The 1C-111-2-01 lateral will kick off at 12,490' MD and drill to a planned TD of 15,800' MD targeting the C sand to the north. It will be completed with 2-3/8" slotted liner from TD up to 10,780' MD with an aluminum billet. The 1 C-111-2-02 lateral will kick off at 10,780' MD and drill to a planned TD of 15,600' MD targeting the C sand to the north-east. It will be completed with 2-3/8" slotted liner from TD up into the 5" casing at 10,600' MD with a deployment sleeve. CTD Drill and Complete 1C-11 Laterals: Pre -CTD Work c)1P 1. RU wire line: Change out GLV's, record SIBP, and drift 2-3/8" liner. Pull 2-3/8" x 3-1/2" liner top packer. Cut 2-3/8" Liner 2. Prep site for Nabors CDR3-AC. Rig Work 1. MIRU Nab s CDR3-AC rig using 2" coil tubing. NU 7-1/16" BOPE, test. 2. Prep wellbore fo idetrack a. Pull 2-3/8" slotte liner above cut b. Set Thru-Tubing Stock in 5" Casing 5� 7k 5 3. 1 C-11 L2 Lateral (C sand - h) �0 a. Mill 2.80" window at 10,68 D. Q b. Drill 3" bi-center lateral to TD 13,000' MD. c. Run an aluminum billet with ope hole anchor at 12,490' MD. 4. 1C-111-2-01 Lateral (C sand -North) a. Kick off the aluminum billet at 12,490' b. Drill 3" bi-center lateral to TD of 15,800' c. Run 2%" slotted liner with an aluminum bille from TD up to 10,780' MD. Page 1 of 2 3/14/2019 5. 1C-11 L2-02 Lateral (C sand - North-East) a. Kick off of the aluminum billet at 10,780' MD. b. Drill 3" bi-center lateral to TD of 15,600' MD. c. Run 2%" slotted liner with deployment sleeve from TD up to 10,600' MD. 6. Obtain SBHP, freeze protect, ND BOPE, and RDMO Nabors CRD3-AC. Post -Rig Work 1. Return to production Page 2 of 2 3/14/2019 1C-11 L1, L1-01, L1-02 Actual CTD Sidetrack Update: 07/27109 ConocoPhillips Alaska 10,24,' on T'26# L-80 shoe 10,427- MID C -sand parts (sgfd) 10,660' - 10,716' MD :er 3.5"x5" TTWS at 10,747'MD set 15 deg LOHS - 2.80" Window Fail 18# L-80 liner at 10,271' - 11,300' MD ZXP liner -lop packer at 10,271' Fish a1 10,990' (failed IBP) Hole in 7" casing at 5466'MID (5/26/08) P" /I L T -P D = 1.71" ,ell packe = 1 aa^ ID = 1.00" Camco TRMAXXSE SCSSV @ 2297' MD Minimum ID = 2.813"(X -profile) Camco KBMG gas lit mandrels @ 3194',4217',5118' L-80 EUE and Tubing to surface 8040 seal assembly @ 5172' MD Muleshoe at 5193' MD Scab Liner (5163--10271'MD FHL Retrievable Decker at 520T N Baker Premier packer at 10,149' MD D -nipple at 10,189' MD Milled out to 2.80" (414/09) 5.75" OD Locator at 10,259' MD Muleshoe Jnt at 10,260-10,266' MD, inside of 5.25" ID tieback ID = 4.40", OD = 5.2" Fish - 8040 Seal Assembly, 10266'- 10313' (5/25/2008) Length = 46.55'. ID = 3.00" Muleshoe at 10,313' MD 1C-11 L"2:11,407- -13,031' MD 2-3/8" liner 10,248' - 13,030' slotted 11,386'- 12,992 - IC -111-1: 2,992' lV-nll-0l: 11,/5U'-11,675 MD /// za/e"nnerll,aor-11,eoz' anchor billet at 11,40T MD d� 1C-11Ltrll,75'-13,3,369- J 2J/8"liner 11,750'-13,389' aluminum billet at 11,750' MD 9-518" 400 L-80 shoe @ 6943' MD 7" 26# L-80 shoe @ 10,427' MD KOP @ 10,684MD _ Baker 3.5"x5'TTWS - C -sand pert. (said) 10,660'- 10,716MD _ 2-3/8" R -Nipple at 10725' MD D = 1.71" ' @ 10,747' MD er 3.5"x 5" TT WS at 10,747' MD set 15 deg LOHS - 2.80" Window Etit 5", 180 L-80 liner at 10,271' -11,300' MD ZXP liner -top packer at 10,271' 1C-11 Proposed CTD Schematic Hole in 7" casing at 5466' MD (5126/08) 1C-111-2 Plan TD: 13,000' MD Top of Billet. 12.490' MD Updated: 13 -Mar -2019 WRL 3-1/2" Camco TRMAXX-5E SCSSV Q 2297' MD Minimum ID = 2.813" (X -profile) 3-1/2" Camco KBMG gas fig mandrels @ 3194', 4217',5118- 3-112" 217',5118'3-1/2" 9.30 L-80 EUE 8rd Tubing to surface Baker 8040 seal assembN� 5172' MO 3-1/2" muleshoe at 5193' FFAA 3-1/2" Scab Liner 15163'-10271' MIN BAker FHL Retrievable packer of 5203' MD Baker Premier packer at 10,149' MD D -nipple at 10,189' MD Milled out to 280" (414/09) Behind 2-318" Liner & LinerTo Packer ocator al 10,258' M Muleshoe Jnl at 10,260-10,266' MD, inside of 5.25" ID tieback sleeve It) =4,40",OD=5.2' Fish - 8040 Seal Assembly 10266' -10313' (5/25/2008) Length = 46.55', ID = 3.60" Muleshoe at 10,313' MO Plan TO Plan : 15 15,800' MD Top of Billet 10,760' MD iC-111,2-02 Plan TD: 15.600' MD Top of liner: 10,600' MD -------------- -------------- ---------------------- 1C-11 Lt -02: 11,407 -13,031' MD 1G-11 L1-01: 11,750'- 12,875' MD 2J/8' liner 11,407 - 11,802' anchor billet at 11,407' MD 1C -11L1: 10,750' -13,385' MD 2-3/8" liner 11,750'- 13,369' aluminum billet at 11,750' MD Loepp, Victoria T (DOA) From: Long, William R <William.R.Long@conocophillips.com> Sent: Friday, March 22, 2019 11:28 AM To: Loepp, Victoria T (DOA) Cc: Ohlinger, James 1 Subject: 1C-11 L1-02 Pre -CTD Sundry to Cut 2-3/8" Liner Victoria, We submitted an Application for Sundry Approvals last week to cut the previous 2-3/8" CTD liner in X-111-1-02 (PTD: 209-078). We plan to make the cut pre -CTD with wireline. Wireline would like to potentially schedule the work for this weekend. What is the approval status of this sundry? Thanks, William R. Long Staff CTD Engineer ConocoPhillips 907-263-4372 (office) 281-723-6000 (cell) William.R.Long@ConocoPhillips.com Loepp, Victoria T (DOA) From: Long, William R <William.R.Long@conocophillips.com> Sent: Friday, March 22, 2019 1:37 PM To: Loepp, Victoria T (DOA) Cc: Ohlinger, James J Subject: RE: [EXTERNAL]KRU 1C-11L1-02(PTD 209-078) The 1C-111-1 laterals will remain producing. The whipstock will allow flow past. Thanks, William R. Long Staff CTD Engineer ConocoPhillips 907-263-4372 (office) 281-723-6000 (cell) William.R.Long@ConocoPhillips.com From: Loepp, Victoria T (DOA) <victoria.loepp@alaska.gov> Sent: Friday, March 22, 2019 1:23 PM To: Long, William R <William.R.Long@conocophillips.com> Subject: [EXTERNAL)KRU 1C-11L1-02(PTD 209-078) William, Are the 1C -11L1 laterals producing? Is the whipstock to be set a flow through whipstock? Thanx, Victoria Victoria Loepp Senior Petroleum Engineer State of Alaska Oil & Gas Conservation Commission 333 W. 7th Ave Anchorage, AK 99501 Work: (907)793-1247 Victoria LOepp O(ialaska oov CONFIDENTIALITY NOTICE: This e-mail message, including any attachments, contains information from the Alaska Oil and Gas Conservation Commission (AOGCC), State of Alaska and is for the sole use of the intended recipient(s). It may contain confidential and/or privileged information. The unauthorized review, use or disclosure of such information may violate state or federal law. If you are an unintended recipient of this e-mail, please delete it, without first saving or forwarding it, and, so that the AOGCC is aware of the mistake in sending it to you, contact Victoria Loepp at (907)793-7247 or Victoria.Loeop@alaska.gov