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HomeMy WebLinkAbout2017 Kenai Gas FieldHilcorp Alaska, LLC if March 13, 2018 Baum Mr. Hollis French, Chair Alaska Oil and Gas Conservation Commission 333 W. 7t' Avenue, Suite 100 Anchorage, AK 99501 4L C Re: Kenai Gas Field SIO #7 2017 Sterling Pool 6 Annual Performance Evaluation Dear Commissioner French: Post Office Box 244027 Anchorage, AK 99524-4027 3800 Centerpoint Drive Suite 100 Anchorage, AK 99503 vhughes@hilcorp.com Phone: 907/777-8445 Fax: 907/777-8310 n*( 'L-�'Cn vl-� Attached for your review is the 2017 Annual Performance Evaluation for the Sterling Pool 6 Gas Storage Reservoir according to SIO #7. This report covers the primary production and injection period through the 2017 gas storage operations. Sterling Pool 6 continues to exhibit tank like behavior with neither influx of other fluids nor loss of storage gas based on the evidence shown in the exhibits below. Injection wells continue to act as expected based on an injectivity index. Real time downhole pressure monitoring is possible with shut in tubing pressures of KU 34-31 corrected to reservoir pressure. For the annual period ending 12/31/2017 the total volume injected into Sterling Pool 6 was 9,214 MMSCF and total production was 4,913 MMSCF. The total native gas withdrawn from Pool 6 was 1,296 MMSCF with a native gas balance of 0 MMSCF. The native gas was determined to be fully depleted as of November 2017. All Pool 6 gas production after this date is considered 100% storage gas. The maximum reservoir pressure recorded in Pool 6 based on the KU 34-31 monitoring well SITP (shut in tubing pressure) was 260 psi or a reservoir pressure of 287 psi. This pressure is expected to be distributed consistently throughout the productive area of Pool 6 and is below the maximum reservoir pressure of 300 psi as established by rule #4 of SIO 7. Regar , ony McConkey Reservoir Engineer Exhibit #1 — List of wells and service Exhibit #2 — KU 34-31 Monitoring Well SITP during 2017 Exhibit #3 — Monthly Production and Injection Volumes for 2017 Exhibit #4 — P/z plot for Injection Period 2017 LO 0 N m ca a _U .5 L In 1.0 _ _0 O CL O •� ._ X X L O E `-� 0 of O c l0 O X ' m r-, 0 ,n N m t -6r-1 O m I� O lD O N m (,D0 0 4-j+� m d- N r l+ O -t N� m m �t r- i r -I a-+ ` S m rH N cin lD � w O 0 a. r -i N m -4 -O Ln lD Il 00 0) r -I r -I N r -I Tubing Pressure (psi(a)) / Static Run Depth Pressure (psi(a)) f Calculated Sandface Pressure (psi(a)) 0 0 0 0 0 0 0 0 C. 0 0 O 00 co 7 N O 00 (D Y N O O O O O M N N N N N — 00 (D -e N o I � L E d U d O d .a E d O Z d a 0 O m a E a) CL m Co y N d IL rn y .0a F- a' mF- C (7 .......__. 7 7 O N d C 7 7 N N d m w �U C 14 f0 ' `L m � o (DE L O 'C CL — O OD U L U I (0 � P a m LL Z' 7 (0 7 LO w 0 c7 N co a - Oto 0 N .I -- L) U (O O O C O E O L N d d c O U 'O 0 �f CD N 0 (D C _D \O C O U m C C cB C O U D .0 O d T c O 21 co *t L X W N Gi E O m I- 0 0 Ln N ,m V 0 O CL 0 N (psw) uoi;:)npoad ION 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 o n o 00 0 0 Ln O `. I m Q ti c 0 0 0 0 0 0 0 0 C 0 0 C C C 0 0 0 0 0 0 0 0 0 0 C 0 0 0 C 0 0 0 0zr m Ocn rev o o (PSW) dIJ 9 loud Lo 0 a) 0) c6 IL LM o m M N N LnO N (elsd) Z/d 9 100d 0 0 0 0 0 Go O O 0 0 O 0 10 0 0 0 C v oa N O N 0 0 0 0 0 0 0 v Z lD O O a LO O LO N CD ca d