Department of Commerce, Community, and Economic Development
Alaska Oil and Gas Conservation Commission
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HomeMy WebLinkAbout2018 Kuparuk Undefined Pool
Greater Kuparuk Area
2018 Undefined Pool Report
Ugnu Formation
Reporting Period
January 1 to December 31, 2018
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ConocoPhillips Kazeem Adegbola
Manager, GKA Base
Production & Optimization
Greater Kuparuk Area
ConocoPhillips Alaska, Inc.
ATO-1376
PO Box 100360
Anchorage AK 99510-0360
Phone (907) 263-4027
March 29, 2019
Ms. Jessie Chmielowski, Commissioner
Alaska Oil and Gas Conservation Commission
333 West 7th A e. Suite 100
Anchorage, Alaska 99501-3539
Re: 2018 Undefined Oil Pool Reservoir Report
Dear Commissioner Chmielowski,
In compliance with Title 20 AAC 25.517, ConocoPhillips Alaska, Inc., operator of the Kuparuk River Unit,
is hereby submitting the Plans of reservoir development and operation for Undefined Oil Pools. This
report documents the required information pertinent to the field development and enhanced recovery
operations from January through December 2018. The following is an outline of the information provided:
a. A summary of reservoir development and operation for the Ugnu Undefined Oil Pool
(Attachment 1).
If you have any questions concerning this data, please contact Kazeem Adegbola at (907) 263-4027.
Sincerely,
Kazeem Adegbola
Manager, GKA Base
Production and Optimization
Greater Kuparuk Area
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Attachment 1
Ugnu Formation
2018 Report Operations Review
UGNU PILOTS/ STUDIES
The Kuparuk River Unit working interest owners re‐started the Ugnu Heavy Oil pilot and established
stabilized oil flow from well 1H‐401 during December 2013. A down hole heater was used to lower the oil
viscosity sufficiently to allow viscous oil to flow via a progressive cavity pump installed in the well. The well
was online for approximately 10 cumulative months until it was shut in March of 2016 due to a failed pump.
In 2017 and 2018, elastomer studies were completed to redesign a downhole pump more appropriate for
the fluid chemistry and downhole conditions. A new pump design has been selected and plans are in place
to restore the well to production in early 2019.
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