Department of Commerce, Community, and Economic Development
Alaska Oil and Gas Conservation Commission
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HomeMy WebLinkAbout2020 Kuparuk Undefined Pool
Greater Kuparuk Area
2020 Undefined Pool Report
Ugnu Formation
Reporting Period
January 1 to December 31, 2020
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Carlotta Chernoff
Manager, GKA Asset Development
Greater Kuparuk Area
ConocoPhillips Alaska, Inc.
ATO-602
PO Box 100360
Anchorage AK 99510-0360
Phone (907) 263-4692
March 25, 2021
Ms. Jessie Chmielowski, Commissioner
Alaska Oil and Gas Conservation Commission
333 West 7th Ave. Suite 100
Anchorage, Alaska 99501
Re: 2020 Undefined Oil Pool Reservoir Report
Dear Commissioner Chmielowski,
In compliance with Title 20 AAC 25.517, ConocoPhillips Alaska, Inc., operator of the Kuparuk River Unit, is hereby
submitting the Plans of reservoir development and operation for Undefined Oil Pools. This report documents
the required information pertinent to the field development and enhanced recovery operations from January
through December 2020. The following is an outline of the information provided:
Ugnu Formation – 2020 Report Operations Review (Attachment 1)
If you have any questions concerning this data, please contact Jeff Stine at (907) 263-4735.
Sincerely,
Carlotta Chernoff
Manager, GKA Asset Development
Greater Kuparuk Area
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Attachment 1
Ugnu Formation
2020 Report Operations Review
UGNU PILOTS/ STUDIES
The Kuparuk River Unit working interest owners re‐started the Ugnu Heavy Oil pilot and established stabilized oil
flow from well 1H‐401 during December 2013. A down hole heater was used to lower the oil viscosity sufficiently to
allow viscous oil to flow via a progressive cavity pump installed in the well. The well was online for approximately 10
cumulative months until it was shut in March 2016 due to a failed pump. In 2017 and 2018, elastomer studies were
completed to redesign a downhole pump more appropriate for the fluid chemistry and downhole conditions. A new
pump design was installed in April 2019. The well was online for two weeks before the motor failed. Evaluating rig
workover alternatives to bring the well back on production.
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