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162-020
~ ~ ~ ~ ~- - July 27, 2009 Mr. Dan Seamount, Chairman Alaska Oil and Gas Conservation Commission 333 W. 7`h Ave., Ste. 100 -- --. - Anchorage, AK 99501 RE: Wolf Lake Gas Field CIRI Lease No. C-061504 and Lease No. C-061569 T7N-R9W, Sections 29, 30, 31 and 32 ~.., .,~} ~ ~;-~ ~+ ~h °~° ~~[i~ sx'~cr.'9, ~~~4r ~~ U Kenai Peninsula, Alaska Dear Mr. Seamount: Cook Inlet Region, Inc, ("CIRI") holds mineral rights within the Wolf Lake Gas Field drilling area ("Drilling Area") near the following wells ("Wells"): ~ 1~~ '~~' jWolf Lake No. 1 -~ ;~ ~'~,~ U3:,~11Vo1 f Lake No. 1 RD °` ~~~{ ~a'~~ j Wolf Lake No. 2 -~ : ~ ~ ~ J I-~-:Z. Wolf Lake No.~ ~ ~~-~'-'i '? :.~ ~~ ~ ----~~~~~~~',~Soldotna Creek Unit No. 22-32 --_ , ~,~,---~3~Soldotna Creek Unit No. 22-A-32 CIRI sold a portion of its Wolf Lake mineral interests in 2000 and another interest in 2003. CIRI continues to own the mineral interests between the Hemlock and Matanuska Formations (appraximately 12,456' to 12,080') in addition to the minerals lying beneath the Hemlock Formation (approximately 13,635' to the center of the earth). CIRI also continues to hold the rights to any other non-oil and gas subsurface estate within the boundaries of the leases and resource sales. The well paths for the above referenced Wells pass through CIRI mineral acreage. The purpose of this fetter is to request that the AOGCC notify CIRI of any and all applications and actions involving the listed Wells or the Drilling Area. CIRI is interested in protecting its correlative rights as a significant mineral owner within the Drilling Area. As of August 26, 2003, CIRI has no active leases or integration of interests with other interest owners within the Drilling Area. z525 "C" STREET, SUITE 500 ~ P.O. BOX 93330 ~ ANCHORAGE, ALASKA 99509-3330 (907) 274-8638 ~ FAX (907) 279-8836 ~ Web Sice: www.ciri.com ~ • AOGCC Notice of Drilling July 27, 2009 Wolf Lake Gas Field Page 2 Please send notifications pursuant to this request to: Kim Cunningham Director, Land and Resources Cook Inlet Region, Inc. 2525 C Street, Suite 500 Anchorage, AK 99503 Thank you for your assistance and please let us know if you have any questions or concerns. Yours truly, Cook Inlet Region, Inc. Chris Gay ~ Land and Resources cc: Kim Cunningham, CIRI Tom Maunder, Petroleum Engineer, AOGCC Charles A. Underwood, Marathon DEPT. OF ENVIRONMENTAL CONSERVATION TONY KNOI/~LE$, GOVERNOR DIVISION OF ENVIRONMENTAL HEALTH SOLID WASTE PROGRAM 410 WILLOUGHBY AVE JUNEAU, ALASKA 99687 http://www.state.ak.us/dec/deh Mr. Charles R. Moxley ChevronTexaco P.O. Box 1635 Houston, Texas 77251 April' 5, 2002 Telephone: (907) 465-5162 Fax: (907) 465-5362 RECEIVED APR 9 200 Reference: Issuance of Permanent Closure Approval for Inactive Reserve Pits located at West Fork Unit 233-16,-SOMOtna~Creel~22-32, Falls Creek 43-06, North Fork Unite 11-04, Falls Creek 2 and Mink Creek Unit 14-20 .' Dear Mr. Moxley: '~ : . v ... \ , The .Alaska Department of Environmental Conservation (ADEC) has completed review'..and,public notice .*,'or permanent closure approval of the inactive reserve pits locatedat the abdve reference sites located on the Kenai Peninsula. The closure applications provided the required information describing the history of the reserve Pit(s), the present condition of the reserve pits(s), results of any required water sampling and an assessment of the potential risks posed by' the drilling waste to human health and the environment. ADEC coordinated field inspections and review of the closure plans with the appropriate landowners or land managers. ADEC has determined that the backfilled reserve pits at these sites do not present a material or probable risk to the public health or the environment. Public notice requesting comments on the closure requests was published February 21 and 22, 2002 in the Anchorage Daily News and posted on the state web site February 21, 2002. No public comments objecting to closure approval were received in response to this public notice. ADEC has determined that the reserve pits at these sites meet the closure requirements of 18 AAC 60.440. Closure Approval Well Name West Fork Unit 233-16 Soldotna Creek 22-32 Fall Creek 43-06 North Fork Unit 11-04 Falls Creek 2 Mink Creek Unit 14-20 API Number 50-133-10018-00 50-133-10022-00 50-133-20249-00 50-231-20002-00 50-133-10006-00 50-133-20209-00 MTRS Section 16, T6N, R9W, SM Section 32, T7N, T9W, SM Section 6, T1N, R12 W, SM Section 4, T4 S, R 13W, SM Section 23, T1N,R13W,SM Section 20, T7N,R9W, SM Landowner USFWS USFWS Private Kenai Peninsula Borough Private USFWS Terms and Conditions This permanent closure approval is subject to the following terms and conditions: 1) In accordance with 18 AAC 60.440(1), the Department will require additional investigation, assessment, monitoring or remediation if new information regarding conditions at the reserve pit facilities indicates that further actions, are necessary to protect human health or the environment. ..._ · 2) The approval granted by this letter is for the inactive drilling waste reserve pit(s) only. Closure for the pad as a whole (if required) must be coordinated between the owner/operator and the appropriate land owner/manager. .... : ...- . . · . . Any person who disagrees with ~any portion of this':.decision may request an adjudicatory hearing in accordance with 18 AAC 15.200-310. The request should be mailed to the Commissioner of the Department of Environmental Conservation, 555 Cordova Ave. Anchorage, AK 99501. If a hearing is not requested within thirty (30) days of the date of this letter, the right of appeal is waived. If an adjudicatory hearing is requested and granted, this decision remains in full effect during the adjudicatory process. Sincerely, Heather Stockard Solid Waste Program Manager Heather Stockard @ envircon.state.ak.us cc.' Tom Maunder, AOGCC, Anchorage Chick Underwood, Marathon Oil Company, Anchorage Roy Dudley, Kenai Peninsula Borough, Soldotna Harold and Lee Pederson, 925 R Street, Anchorage, AK 99501 Claire Caldes, USFWS, Soldotna Marion E. Oskolkoff, P.O. Box 39008, Ninilchik, AK 99639-0008 lc-apfm 10jan95 LOCATION CLEARANCE REPORT State of Alaska OIL AND GAS CONSERVATION COMMISSION PTD No. ~ ~dg~O Lease Memorandum To File: API No. Well Name Operator Location Spud: ~/~9/6~, TD: /~.5-5-~° , Completed Note casing size, wt, depth, cmt vol, & procedure. Long Csg: ~;~ "' Z3/Z6/'Zg/~ ~;~.~ {~f. ~_~ .0,3 i;'oc_3 ~a Liner: ~ Review the well file, and comment on plugging, status, and location clearance - provide loc. Plugs: ~q~7~ ' L~S-~ Well head cut off: - Marker post.or plate: Location Clearance: well head clear, code. Code 4 Signed Date June Mr 'Allen E. Brown AR(X) Exploration Co', Inc. P. O. Box 360' Anchorage. Alaska ..- 995 10 Geologic Slides and Analyses Prepared from State Well : Samples and Core Chips, Dear,,~ Mr. Brown :. The'.enclosed list reflects various geologic slides and analyses that have been recently added to the State's library of special materials prepared from well sar~ples and core chips filed with the Commission. The materials listed are in addition to those tabulated in the 1980 Statistical Heport and those reported in the February, March and April monthly bulletins. Please photo-copy and distribute copies of this list to appropriate persona.within your company.,.. You'are the °nly person in your c~pany.,to'-.~whom .:.the. I i st has been sent. In the event publication of the Commission's monthly bulletin is not resumed, the next listing of newly received geologic materials will be distributed approximately September 1, 1982. For current information on newly' received materials please call the COmmission office at any-time, weekdays 8:00 A!.~ to 4~30 P?~, A I a aka n T tree, Rnclosure . ~VA i be Amer i t'anGe - Kawik' ~:.#.1 rmal '-Maturat ion,:Re ~ ~,:~ ~.<..-.. :::,., :.::,....~<?~ .,:: ,.?.:~?:..::~..? .. -.::.~,?:~::. :%.....". .... ..::..,:,.. ,:::.:'~" ::: .:..:-.:: ...:.. ·:.-. .~ .,., . . . ~.~ . ~.. :~- ',:Wc~ . . : ~. ~ '- · ..- ~ . :, . ~, ~ . .,:'.~ . ;. - .-.., .. '~ ~. ':'.' ' * '. r ~ ' 8"'' -'-" :-, .'- '-' 2 ,"...'.-'-: - . ...-: .. .... ... . ,. ,+.,, ;.. June .-. 1 ,..?.198 ..:.'.,. ?:. - : '-"::":.:-E V" D:"' '0L ":""T' 'A ': -. ....... ~-:':~ ....... , .... ,::<" 'RECENT~.R CEI E ..:GE OC.IC ~A ER'I LS::'-::.":',":.':::.:'-:~:, :"::'::<: .... , ."::1:;::', ~ ::-.:. , ..... . .~:~, -.. , . ..,. ,.. . ,.. .. ~ ,~ , . .- . · .... . , ...-. . 'materiil.S'..<.have.'::been::.'. recently-added':.to, the . - -':.... ~pee ial :?.::::.~.~ er.i-~l S'.. pne'pared-' ·.from:' ~e 11.,-' :.' ':..:':' ri'lied ::in:?the:;' state; :::·':·'These- materials '::' abu.1 a.t ~'d:::::i'h. ::.t he ~ .~:~S,t a t t st:ical"..RepOr t;:: · . ..,-: :,.177,, .:. . z. . [. -,,. ~-.: ...:~: :~: ,.., ~. ,-.:., .~ .. ~. .; . . · . ; · , ~ . , ,,,. . ~ ./~, ~ .. '.'. ?'~'-~ .ln t e tva 1.. :.......:::. -:.,<';~-" ,.. '. t.."'~ . ;:.T'.,".: :.-":,:. "i: '"'" ' '~ ' 't ~i ':' .4 [: ' ~' ' ' -...: ::'::' ,..,:,,~?~,.,? .:.'..: ...:, 5 o~:.,~.;:~:;~i ~ ;-3 60'"':. .. :U [: :~- , :' %;: ~ ~::: :.,'..:. :,. , - ...... ~, ~-~., .':: ..... . ..:: .... ::1. -. ' ""?':0o0 .' ":..s.:;:: ~":::':..: ?.,:~"1'3:; 640,...':w' ;1,4 ,-560:.':":. -:: :"",":';~:'"':':;'::' F":::::3 :' :'5 .::'. '"'. ~ " '.,. -.::::~(:" ..'. :::' .,:. ": :, ,,:.~ _ ..- '~ '~1~'? :' " -' ' - 'F. - . . ... - ~.' "-"~: ':" :::: .. '1 :~: 6.0 ~; ?': '6 :':" ':: ::'; :4: 0 ~' 1,5 ~ 22 ;,:: ,<~'.' .. ':, 1::3(~, 640 .. ~'?'1'4 ;560' ':":1' · ,~,,:,,. ~::' , :., .':::::'..:.:: .,:- "'" o44'.-:.~.,',.96~5':" ,;::/,'.. ~.'i~;~ "i":" ~ '~.'.' ?'~ ~'i '. ~ ':'" ' ' - .?,.,.. 221.0 '~ 88!0:;" :~' .. ..... : ::.:,:.:: ::':::::2 02 8 o 'r .;8 z s o-':.?,::,~::.:~ a¢:a"!ve..~:~:~ '?' ~.::::;:.. ~ ::':~: ::,..' ::.:3'~.s o::.; ' s o5 0'?:::::'::' ::.:..~?..,:J', .~... ~.:~..:.: .; . ::::?:,, 1::::.{' :?: :?. :::'.::::..', ':: '::: . :.::::,,, ,':-. ?.,--'., .:..'.::~.:.:~, :.:.' . ..r?; v':' -: ,::.~;,. ..... . ,. ~ .... ,,. ,.. .... ..,. ,,, .: ':'i ':';:': :" ~:"';"- ' ':;'?1020;,: 1'3';':150 ":'_ ~.. ......... ."1590 ~?'-:16.,5~0.:":~,'-.: ::' ,::::~:::-4 4 'f.C'.}":t?: :: :' ' "~' "' ......... 9"":.,:',"-':':"::":' :" :' .~0~0,-.--'":':10; '::::::.:~75 60 ::. 9500 ":'" ':~'? :%' "~" · .. . . .... : .~.::' ,:,. 5 0 '."-",.'5 2.50 , : ' ,..,-:/' 53,0.'~::;,6..500.:,:,":: .-.; ~- -: . , ;.. ,, . . .~.~.... ~_ .~< ,..... ,:. :.:;~v:;.." ":',.' .... J".: "'"'.:'" :J~:r:" .... ":':'" '135.9'.::.ana 1 yse s',. '::' · -.- ::..:, , . . ,: ::. '.:': -- te'.Re'fleetaneet 1 ~s~, ....,,-,....,.. ." .,:7: :~'e:':--:~''~ ~::w~,~ ';,.: ' :' '~' ""' ":?"'""' '~ ''~ :::No r.t:h::~"S ! '..' .... ...':' 7: ':" '.,,:'~.::}~: <'.::/ ::."::': ~: '~ :Rock-Eval da t a::::.for.. CITIES SERVICE COMPANY ENERGY RESOURCES GROUP Cities Service Building 5100 Southwest Freeway Box 27570 Houston, Texas 77027 (713) 850-6100 May 6, 1982 Mr. William Van Alen Alaska Oil and Gas Conservation Commission 3001 Procupine Drive Anchorage, Alaska 99501 Dear Bill: t~re are the palynologic slides and kerogen slides prepared ~n ~ - ' for the SOCAL Naptowne ~24-8 and the 'SOCAL ~d0~tna c~_e~ ~~wells. The kerogen slides are indicated by ~~i6~-~oc) located to the right of the index numbers on the appropriate slides. The entire sample cut from each depth interval was used due to their sparse pollen content. Two paly- nologic smears were prepared from most of the sample cuts. Screened slides were not prepared because of insufficient sample size. Cities Service greatly appreciate ~e opportunity to utilize the well materials and facilities provided by the Alaska Oil and Gas Conservation Conm~ssion. We look forward to further interaction with the Conmtission in the future. Thanks again.- 'i - Sincere~ly, . 'Joe Davidson Staff .Geologist U. S. Offshore Frontier Region JDD/jed EnClosures cc.: Mr. Mike Oliveira File March 12, 1982 Mr. Joe P. avidson U.S. Offshore Frontier Region Cities ~ servi~e Company ' P;O~'BoX 27570 ' Houston, Texas 77027 Re: Preparation of Palynologic/Eerogen Slides from Well Samples and Core Chips in the State Library Col lectien rear Joe, In' confirmation of our discussions during your~visit to our office February 19, 19~2, permission has been granted to Cities Service Company to extract a maximum 1 cc. of sample material ~.~er sample envelope or 1 cc. of core material per foot of core from the State's set of samples and ~core chips for the sole purpose of preparing palynologic and kerogen slides at i00 foot composite depths within the designated intervals in the following wells, subject to the conditions set forth below: SAMPLE ~ET ~O. ~'~'E LL IMTERVAL 109 39 C C.~7r!T I Ot<?S SOCAL Naptowne Unit #24-8. Cuttings: 14,600'-15,226' Core: 14, 856 ' Cuttings: 13,640'-14,560' Cuts of the sample and/or core material by ClTCO from the State collection have been extracted only from those individual envelopes or bags in which total content of cuttings or core r~aterial was greater than 10 cc. (No cuts were extracted where the volume of material in the individual envelope was les____~s than l0 CC. ) 'CITCO has provided the State with a list of the specific sample and core footages from which w~terial was extracted. Ome composite set and one screened set of f.~alyno, logic slides and one set of kerogen slides are to ~e ~repared for the above well. ..... "~ Mr. Joe Davidson ;,-~cch 12, 1982 All slides prepared are to be received by the Commission by approxir, ately June 1, 1982 and are to be tran~.~tttud direct to the Commission and not examined by outside pattie s. 5. . All residue and exces~ material is to be returned to the Ccz~mission and no slides or sample materials are to be retaiDed by CITCO. No petrograp, hic or other slides are to be prepared nor analyses made without s~..ecifi¢ consent from thc Cc~amission. 7. CITCO shall bear all costs entailed. we are pleased to work with you in this beneficial project' and look foz~ard t© your company's continued exercise of care and good judgement in the handling of this limited quantity of well material. I know we k. oth understand that the State's well sample library is public property and that granting CITCO permission to extract portions of material from this library, for the purpose of preparing the indicated slides enhances the value of the library and is in tho public interest. $incere,.!Y, . William Van Alen Petroleum Geologist WVA/glh of' ~~. if ~atl I~:~-~ pl~ a~d ~ ~~ld STATE OF ALASKA SUBMIT IN DU~- .... ,.TE* i See other in- reverse side; OIL AND GAS CONSERVATION COMMITTEE I I_ I I III WELL cOMPLETION OR RECOMPLETION REPORT AND LOG* ,,,. ~,,,'i,E o~' ,,.'~:,.~: o,,. EZ] ,,As E3 ~ W ELL ~¥ ELL DR ~' Other b. TYPE OF COMPLETION: .X'F,W ~-~ WOBK ~ DEEP- [] PL~(; ~] DZF~. [] WELI. OVER EN BACK RESVR. Other __ ,, , , ,, 2. NAME OF OPERATOR 3. ADDRESS OF OPERATOR 4. f, oc^woN or WrLL' (Report location clearly and in accordance with any State requiremeuts)* At surface 5. API NUIKERICAL CODE 6. LEASE DESIGNATION AND SERL~L NO. 7. IF INDIA. N, ALLOTTEE OR TRIBE NA/VI.E 8. UNIT,FA.H.M OR L.F~kSE NAME 9. WELL NO. 10. FIELD AND POOL, OR WILDC~kT 11. SEC., T., R., M., (BOTTOM HOLE OBJECTIVE) At top prod. Interval reported below At total depth 13. DATE SPUDDED 14. DATE T.D. RF_,ACHlgD 15. D;A_TE co,M-P SUSP OiR ABAND. 16. ELEVATIONS (DF, RKB, · : I-IOW 1VIANY* ROTARY TOOLS 22. PRODUCING INTERVAL(S), OF THIS COMPLETION--TOP, BOTTOM, NAME (1VID AND TVD)* 12. PIgRJVIIT NO. BT, GR, ETC)* 117. ELEV. CASINGHEAD INTERVALS DR[I,I,ED BY '! CABLE TOOLS 23.WAS DIRECTIONAL SURVEY MADE 1 24. Thee ELECTRIC AND OTHEI:I,' LOGS RUN , iim~. I -- I ! i i ' CASING RECORD (Report all strings set in well) · C;~SIiqG SIZE WEIGHT, LB/FT. f GR~DI~ ~ AMOUNT PULLED ' /~ ' '. r , ',~,~ I /,% 2~ '" ' , ' ,,' ' , ' t - , ' ,, , , SIZ~ - TOP (MD) EOTTO)5 (MD) ISACt(S CEM~T* SCEE~ fA(D) SIZE ' DEPTH SET (MD) I PACKER SET (MD) ~. P~OR.ATiONS OP~ TO PRODU~ON ([atcrval size and number) 29. ACID, SHOT, Fi~AC~URE, C~',IENT SQUEeZe, TC ~-,~"~/~7-/f/~t~ t4~ ~,~' -" I~-I~ II L 30, PRODU~ION DATE FIRST Pf~ODUCTION ~ t DATE 0F T~ST, HOURS TEST~ 'lCliOIiE SIZE PROD'N FOR FLOW, ~rEING CA~NG PRESSURE ICkL~T~ OI~BBL. !~SS. 31. DmrOS~T~0~ Or o,S (Sold, used Ior ]uel, v~nte~, etc.) DEP//i I,%TE~V.4~L (MD) FI%ODUCT1ON MEIt{O'D (Fiowi~g, gas lift, pumping--size and type of pump~ AMOUN£ AND I'L!ND OF MATE?,/AL USED I VvELL STATUS (Producing or bnuL-in) ' 32. cmT o~' OIL--J~DL. G.~kS---~CF. ~V/Ji'EII~-BBL. I GAS-OIL IL%TIO GAS--NiCF. WATER--BBL. I OIL GRAVITY-APl (CORR,) tTEST WITNE[18ED BY"' 33. I hereby certify that the foregoing and attached information ts complete and correct as determined from all-available 'r'ecords SIGNED (~O'F f_~ r~c'f ~/~ TITLE DATE J~ ~--~~,~----- ...... I II I I I I I *(See Instructions and Spaces for Additional Data on Reverse Side) INSTRUCTIONS General: This form is designed for submitting a complete and correct well completion report and log on all types of lands and leases in Alaska. Item: 16: Indicate which elevation is used as reference (where not otherwise shown) for depth measure- ments given in cther spaces on this form and in any attachments. Items 20, and 22:: If this well is completed for separatc prcduction from more th~n one ~nterval zone (multiple completion), so state in item 20, and in item 22 show the prcJuci~,r0 interval, or intervals, top(s), bottom(s) and name (s) (if any) for only the intervc~l re~}orted in ite~ 30. Submit a separate report (page) on this form, adequately identified, for each additional ir~te~val to be seperately produced, show- ing the adlditional data pertinent to such interval. Item26: "Sacks Cement": Attached supplemental records for this well should show the details of any mul- tiple stage cementing and the location of the cementing tool. Item 28: Submit a separate complelion report on this form for each interval to be separately produced. (See instruction for items 20 and 22 above). '~{~" FOFLMATION TE, STS IN('LUI)IN(; INTEtq. VAL TE~TED, PHI%e,~URE DATA ~-~COVERI~' OF OIL. GAS.- 35, G~GIC MARK~ WAT~ AND MUD . ,~TA. A'I~'ACJi ~,IRIEF fDmCR!~I~ONS' OF :UITIIOLO'GY. ~POR~SiTY. 'AND LI)E'PEc~Ei.) 'SiiOW'S: OF OIL, ,O~ {OR , COMPLETION REPORT - ~EW WELL STANDARD OIL COMPANY OF CALIFORNIA - WESTERN OPERATIONS INC. - OPERATOR AREA: Kenai Peninsula, Cook Inlet Area, Alaska PROPERTY: Soldotna Creek Unit LAND OFFICE: Anchorage Lease No. A-028998 WELL NO. SCU 22A-32 Section 32, Township 7 North, Range 9 West, Seward B&M FIRST REDRILL OF SCU 22-32. LOCATION: Surface: 2115' South and 2080' East from Northwest Corner of Section 32. Bottom Hole: ELEVATION: 287' K.B. DATE: June 4, 1963 (Projected) 646' North and 535' East from surface location. Original K.B. is i~' above ground. · ., C~ V. CHATTERTON, District Superint'ende-nt DRTTJ.W.D BY: Reading & Bates Drilling Company Rig ~6. DATE COMMENCED DRILLING: December 22, 1962. DATE COMPIETED DRI~NG: April 22, 1963. DATE OF INITIAL PRODUCTION: None. Well plugged and abandoned. S~ TOTAL DEPTH: 14, 796' JUNK: Sidetracked 337' of fish. Top at 13, 507', bottom at 13,844'. CASING: 20" cemented at 31' 13 3/8" cemented at 2008' 7" PLUGS: Surface - 270' Halliburton DC bridge plug at 11650' !11,740' - 12,087' ±13, 670' - 14,060' Baker model K cast iron bridge plug set at 12, 202' in 7" casing in original hole. cemented at 14,234 in original hole with milled out section ll, 966' - 12, OlO'. Redrllled from ll, 992' · STAN~..AED. OIL .O.O..Mp~ C~ CALIFORNIA - WES~ ,.OPERATI .ONS., INC. - OPERATOR ~ . i i ~H I L I I I lJlll I II . _ , . , ONFIDENTIAI. COMPLETION REPORT - NEW WELL AREA, Kenai Peninsula, COok Inlet Area~ Alaska ..LAND OFFICE: Anchorage _:,-:-~-LEASE NO: A-028998 PROPEE~Y: Soldotna Creek Unit NO.- SCU 22-32 SECTION 32, T. 7 N~, R. 9 Wo,~ SEWARD LOCATION: Surface.: 2115' South and 2080' East from Northwest Corner of Section 32, T. ? No, R, 9W., Seward B &M. ELEVAT ION ~ 287 ' K ~B. DATE: December 20, 1962 vr CHA ~ZRT ON, District Superintendent DRILLED BY: Reading & Bates Drilling Company, Rig #7 DATE COMMENCED DRILLING: April 29, 1962 DATE COMPLETED DRILLING: September 21, 1962 DATE OF INITIAL PRODUCTION: None. Well plugged and suspended ~b~Y TOTAL DEPTH: 14,550' JUNK~ None. PLUGS: 0 - 190 ~ .~ 4800 - 5022' ~ 9735 - 9960' ~13974 - .14200' 14223 - 14250' 14250 - 14330' CASING: 20" cemehted at 315 13 3/8" cemented at 2008' with 2000 sacks cement. 7" cemented at 14234' with 700 sacks cement around shoe and through D.V. collar at 7717" with 3,100 sacks cement. CON FI D-ENTIAL FEE 7 i983 Division of i'~;m~:~ and Minerals Alaska Dept. of Naturai Re~ourc~ PERFO~ IONS Page 2~ 5 - mT" holes at 14147' - 14148' (W~O) 4 -~',tt holes per foot at 14152' - 14175' 4 -- holes per foot at 14175' - 14200! (Reperforated) 2 - ~" holes per foot at 14175' - 1420Ot 2 _5/8" holes per foot at 14175t - 14200' (Reperforated) 5 ~ -~" holes at 14203' - 14204' (WSO) 5 - ½" holes at 14204' - 14205' (Squeezed) 1. Schlumberger Induction-Electrical log, interval 2. Schlumberger Sonic log, interval 3. Schlumberger Microlog-Caliper, interval 4. Schlumberger C.D.M., interval 5o ' - 14550' 50' - 14231' 50' - 55o' 2008' - 14230' DRILL STEM TESTS HFT #1, open hole 14510' - 14550' HFT #2, open hole 14507' - 14550' HFT #3, open hole 14234' - 14250' HCT #4, perfs at 14204' - 14205' HCT #5, perfs at 14203' - 14204' HCT #6, perfs at 141~7' - 14148' HOT #7, perforated interval 14175' - 14200~ HCT #8, perforated interval 14152' - 14200' HCT #9, perforated interval 14152' - 14200 ' (WNSO, Squeezed) C0 STION EPoRT SOEDOTNA CBw. W.K UN~2 22-32 S~ection 32, T. 7 N., R. 9 ~., Seward B & M STANDARD OiL COMPANY OF CA~0RNIA- '~" 0'. 'I.'~'L ?age 3. ApriI 29,,. 196~ Spudded at 12:01 A.M.~ April 29, 1962. Drilled 12¼" hole to 2000'. Core Lab mudlogging unit commenced lo~ing at 1:30 PM. 74-,.80 pcf mud Depth 1000'. April 30, 1962 Drilled 12~" hole to 2010' and ran Schlumberger Induction-Electrical log 2013 t _ 50', Sonic log 2003t - 50' and Microlog-Caliper 2005t - 50'. Opened 12{" hole to 18 5/8" from 0 - 1275'. 80-81 pcfmad Opened 12{" hole to 18 5/8" to 2010' and drilled 18 5/8" hole to 2015'. Ran and cemented 13 3/8" casing. CEMENTING DETAIL : : ,,, i J ~ Cemented 13 3/8" casing at 2008' with 2000 sacks of cement. Used 1 top rubber plug. Pumped 50 bbls. of water ahead, mixed 2000 sacks of cement in 60 minutes using Halliburton truck, displaced in 29minutes using rig pumps. Average slurry weight 116~.. Bumped plug with 1600 psi. Full circulation. Hookload weight of casing: Before cementing 90,000~ After cementing before landing casing ?1,000~ CASING DE,AIL I J I I J_ , I 58 joints 13 3/8", 54.5~' J-55 cemented at .May 2,~,, 1962 Cement in place at 1:35 AM. Installed and ~ested BOPEwith 2000~ - O.K. Ran 12¼" bit and located top of cement at 1977'. Drilled out float collar and cement to 2008'e 1962 Drilled out shoe at 2008' and cleaned out te 2015'. Drilled ahead 12{" hole to 3072' and 10 5/8" hole to 3658'. 87-91 pcf mud COMPLET ION REPC~T SOLDOTNA CREEK UNIT 22-32 Section .32, T, 1.7. N., R. 9 W,.,.. S.e..w..ard..B.,& M STANDARD OIL COMPANY OF CALIFORNIA, W.O.Io i bPER/T6~ Page h. Drilled 10 5/8" hole to 6374' · 89-95 pcf mud May !5, 196.2. Drilled 10 5/8" hole to 6508' and 9 7/8" hole to 6511'. 95-98 pcf mud May 1,6 - 23, ,!96~ Drilled 9 7/8" hole to 7988' 93-98 pcf mud Ma7 24, 1962 Ran Schlumberger Induction-Electrical log 7988' - 2007', Sonic leg 7987' - 2007'~ Microlog-Caliper 79891 - 2009' and Continuous Dipmeter 7989' - 2008'.. 95-96 pcf mud Drilled 9 7/8" hole to 12065'. 92-96 pcf mud Ju~..e..24~, 1962_ Drilled 9 7/8" hole to 12167' did not function. . Ran Schlumberger Induction-Electrical log. Tool J.une .2..5¢ 1962 Ran Schlumberger Sonic log 12163' - 70OO'. Reran Induction-Electrical log 12168! - 7000'. Ran Microlog-Caliper 12168~ - 7000' and Continuous Dipmeter 12160t - 7988'. Cune 26 - 3,. Drilled 9 7/8" hole to 12982'. 93-96.5 pcf mad Ran Schlumberger Induction-Electrical leg 12988' - 12168', Sonic leg 12985t - 12163~, Microlog-Caliper 12990' - 12168'. Drilled 9 7/8" hole to 12984'. 96-97 pcf mad Drilled 9 7/8" hole to 13184'e COMPLETION REPORT SOLDOTNA CREEK UNIT 22-32 Section 32~ T..7, N-,R~ ~ W.~ Seward B & M STANDARD OIL COMPANY OF 'C]~LI~ORNIA, W. O. i'; 'i OPERATOR Page 5. Drilled 9 7/8" hole to 13250' and lost three cones off bit. .July 8, 1962 Ran new bit and drilled on junk. Pulled. Ran Bowen magnet and recovered ~ cone and 6 bearings. Ran in with Junk basket~ July 9, 1962 Drilled with junk basket to 13253t. PUlled ~and recovered one complete cone, 4 pieces of cone and 3 bearing pins. Ran 9 7/8" bit with. junk sub and drilled to 13273 '. Pulled. Recovered 3 small pieces of cone, 25 roller bearings and 6 ball bearings in junk sub. 96 pcf mud Jul7 10 - 11.~ 19.62 Drilled 9 7/8,, hole to 13371'. Chsnged to 9" bit at 13371' July 12 - 16, .1962 Drilled 9" hole to 13655'. July 17, 1962 Drilled 9" hole to 13674'. Jul7 18~. Cored 7 5/8" hole.. 13,674' - 13,692' Core #1: 13,674' - 13,692' . Cut 18' 18' Cored , recovered 9t. 1962 94-95.5 pcf mud July 20, 1962 Drilled 9" hole to 13780~. 95-97 pcf mud 95-95.5 pcf mud 96 pcf mud 95-96.5 pcf mud 95 pcf mud Opened 7 5/8" hole to 9" 13674' - 13692' and drilled 9" hole to 13747' COMPLETION REPORT SOLDOTNA CREEK UNIT 22-32 Section 32, Te 7 N,, .R..9 W., ~eward B & M . Oiz' W'"-O, i',. OP T0 Page July 2!,~ 1962 . Ran Schlumberger Induction-Electrical log 13784' -12988', Sonic log 13783' - 12800'. Circulated and conditioned m~d~ Ran Microlog-Caliper 13785' - 12800'. Attempted to run Continuous Dipmeter. Hit tight hole at 1330Ot. Pulled. 95 pcf mud Reamed 9" hole 13300t - 13456'. Ran to bottom. Circulated and conditioned mud. Ran Continuous Dipmeter 13400' - 12160'. Unable to get to bottom. Ran Schlumberger Sidewall Sample gun #1. Took 30 samples of the interval 13770' - 12884'. July 23, 1962 Ran Schlumberger Sidewall Sample gun #2. Took 16 samples of the interval 12878' - 12607 '. Ran 9" bit with junk sub and drilled to 13808'. 95-96 pcf mud Drilled 9" hole to 13926t. 95-96.5 pcf mud Jul~ .26,_ .1962 Drilled 9" hole to 13998'. Pulled. Tight hole 13922' - 13579'. Circulated. Pulled. Ran 9" bit. Reamed tight hole 13720' - 13730'. 27, 1962 Pulled to 13300'. Circulated and conditioned mud 11 hours. Reamed 13300' - 13709I. Circulated and conditioned mud. J,,ul7 28~ 1962 Ran 9 7/8" bite - 13740'. Reamed tight hole 12254' - 13371'~ Opened 9" hole to 9 7/8" 13371' 95-96.5 pcf mud Opened 9" hole to 9 7/8" te 13863' 95 pcf mu~ July 30, 1962 Opened 9" hole to 9 7/8" to 13922' hole to 14005'. Reamed 9" hole 13922' - 13998' and drilled 9" 95 pcf mud cOMPLETION REPORT SOLDOTNA CREEK UNIT 22-32 Se~ti°n 32~ T. 7 N.~ R. 9 W.. Seward. B &tM ST~ARD O~ c'~MI~AN~ ~ II~L~~', W. '~. I' I'- -- ~T O~ Page 7e Drilled 9" hole to 14167t. 93-96 pcf mud August 2. 1962 Drilled 9" hole to 14203'. 94-96 pcf mud August 3, ,1962, Cored ? 5/8" hole. 14203' - 14228" 25' Cored Core #2: 14203t -14228'. Cut 25', recovered 8'. 96 pcf mud August 4, 19~,2 Opened 7 5/8" hole to 9" 14203' - 14228'. Gas and oil cut mud weight to 90~. Pull- ed 5 stands. Circulated and conditioned mud~ Ran to 14228'. Circulated a~d condit- ioned mud. Pulled. August 5' 19,.6..2 Ran Schlumberger Induction-Electrical log 14233' - 13761l, Sonic log 14231~' - 13400~, Microlog-Caliper 14236~l - 13400'. Continuous Dipmeter 14230' - 13400'. Ran 9" bit to 10500'. Circulated. Ran to 14033'. Circulated and conditioned mud to run 7" casing. I00.5-98 pcf mud August 6..1962 Ran 120 joints 7" casing~ 97 pcf mud August.,7. 1962 Ran and cemented 7" casing.. CEMENTING DETAIL Il , I I Il , I I Cemented 7" casing at 14234' in 2 stages with 1800 sacks of treated cement treated with 0.3% HR-4~ Used I top and i bottom rubber plug, COMPLETION REPORT SOLDOTNA. CREEK UNIT 22-32 Section 32, T. ? N.~ Re 9 W., Seward B & M Page 8 1st Stage arounA shoe with 700 sacks of cement. Pumped 50 bbls. of water ahead, mixed 700 sacks of cement in 25 minutes using HaLliburton truck, dis- placed in 53 minutes using rig pumps. Average slurry weight 116~. Bumped plug with 2500~ psi. Full circulation. Cement in place at ll:50A.M.. 2nd Stage through DV at 7717'. Dropped DV bomb, opened DV ports in 25 rains. Pumped' 50 bbls of water ahead, mixed 1100 sacks of cement in 55 minutes using Halliburton truck, displaced in 32 rains, using rig pumps. Average slurry weight 116~. Closed DV ports with 2~OO~ psi. Full circulation. Cement in place at 2:32P.M.. Hookload weight of ca~ before cementing 248,000. (While running in hole) after cementing before landing casing 210,000 at time of landing casing 208,000 CASING D ~AIL K.B. Depth 17 joints 7", 32#, L8R, PllO 713.48' Cut and recovered 7.43' 706.O5' 55 joints 7", 29#, LSR, PllO 2273.12' 2979.17' X-over 7.70 ' 2986.87' 39 joints 7", 23~, BT, N-80 1620.80' 4607.67' 45 joints 7", 26~, BT, N-80 1913.93' 6521.60' X-over 6.86 ' 6528.46 ' 28 joints 7", 26~, L8R, P210 1186.44' 7714.90' D .V. collar 2.14 ' 7717.04 ' 35 joints 7"' 26~, L8R, PllO 1500.11' 9217.15' 68 joints 7", 29#, L8R, PllO 2809.32' 12026.47' 47 joints 7", 32#, LSR, Pll0 1973.11' 13999.58' Marker joint 14.55' 14014.13' 4 joints 7", 32#, LSR, PllO 171.84' 14185.97' Float collar 2.20' 14188.17' 1 joint 7", 32#, L8R, PllO 42.89' 14231.06' Shoe 2.45' 14233.51' Casing cemented at 14233.51 ' August 8, 1962~ Reinstalled BOPE. Tested with 3500~ psi. August 9, 1962 Picked up 3½" drill pipe and located top of cement at 7685 '. Drilled out cement and D.V. collar at 7709' and tested D.V. with 2~50~ psi - O.K. COMPLETION REPORT $OLDO~NA CREEK UNI2 22-32 ~ection 32~ T. 7 N.~ R. 9 W.~ Seward B & M ~TANDABD~' ~IL COMPANY OF CALIFORN~, W. O. ~'. -'"bP'~RATOR Page 9e Located top of cement at 140305 and drilled out cement and float collar to 14220t 88-97 pcf mud ~ugust . .1._~..,. 1962 Drilled out cement and shoe at 14234' and drilled 6" hole to 14235'. Cored 6" hole. 14235' - 14242' August 12. ,1962 PUlled out to check for wash-out. Core #3: 14235' - 14242'. Cut 7' Found wash-out in bumper sub. Cored 6" hole. 14242' - 14259' ?' Cored , recovered 3'. Changed bumper sub. 17' Cored August 13. 196~2 Cored 6" hole. 14259' - 14285' August 14~, ,1~96~2 Cored 6" holee 14285' - 14299' Core #4: 14242' - 14299'. Cut 57' Ran 5 7/8" core head to 14131'. i,u st Cored 5 7/8" hole. 14299' - 14355' August, 16,, 1962 Cored 5 7/8" hole. 26' Cored Ran to 14242'. 14' Cored , recovered 3 t. Circulated and conditioned ~_d. 96-97 pcf mud 56' Cored Circulated, 101-102 pcf mud 101-102 pcf mud 101-104 pc f mud COMPLE~ I0N REPORT SOLDOTNA CR~ UNIT 22-32 Section 32~. T. 7 N.~ R. 9 w.~ Seward B &M STANDARD OIL COMPANY OF CALIFORNIA, W. O. I.' --oPERATOR Page 11 August 21, 1962 Circulated and conditioned mud. Cored 5½" hole. 14508' - 14536' . August 22, 19~ Cored 5½" hole. 14536 ' - 14540' 28' Cored 4' Cored Core #9: 14508' - 14540'. Cut 32', recovered 9'. Circulated and conditioned mud at 14540'. Cored 5½" hole. 14540'~- 14541' 1' Cored A. ugusb. 23a. 1.9.62 Cored 5½" hole. 14541' - 14550' 9' Cored Core #10: 14540' - 14550'. Cut and recovered 10'. 103e5-104.5 pcf mud 104 pcf mud Cirm~ated ~d conditioned mud. Core Lab mudlogging unit released, 103-104 pcf mud Ran Schlumberger Induction-Elec'trical log to 14245~, Hit tight spot. Pulled, Ran 5 5/8" bit to 14550'. Circulated and conditioned mud. Reran Induction- Electrical log~the interval 14554' - 14233'. Ran Microlog-Caliper 14556' - 14236'e A~ugust 25_, !962 Rau 5 5/8" bite Circulated and conditioned mud, Prepared to run formation teste Ran HFT #1~ intervsl 14510' - 14550' Tool Assembly: 1 ~tside BT recorder, 34' of 3 3/4" perf'd tail pipe, left hand safety joint, two 5" type expanding shoe packer, VR safety Joint, hydraulic jars, 1 inside BT recordist, hydrospring tester and dual closed in pressure valve~ COMPLETION REPORT SOLDOTNA CREEK UNIT 22-32 Section 32~ T, 7 N:~, R. 9 W.~ Seward B & M 'STANDA~ O~ COMPANY 'OF 'CALi~6RNI~, W. '0~ "I~ ' OP~AT~[~ Page 10 14355" 14357' 2' Cored Core #5: 14299' - 14357'. Cut and recovered 58'. Cored 5 7/8" hOle. 14357 ' - 14389' August 17, 1962 32' Cored 102-104 pcf mud Cored 5 7/8" hole. 14389" - 14415' 26' Cored Core #6: 14357' - 14415'. Out and recovered 58'. Cored 5 7/8" hole. 14415' - 14416, A,u~st ~,8,, Z~ Cored 5 7/8" hole. 1' Cored 102 pcf mud ~4~16' - 14452' 36' Cored Salt water entered mud system while coring at 14452 104# to lOll. Conditioned mud. Au~ust 19~, 1962 Mud weight dropped from 101-104 pcf mud Circulated and conditioned mud. Built up mud weight to 104.5# pcf. Pulled core. Core #7: 14415' - 14452". Cut 37', recovered 29'. Circulated and conditioned mud at 14452'. Cored 5 7/8" hole. 14452' - 14476' Au~s,t ,2~ 196___~2~ 24' Cored 104.5 pcf mud Cored 5 7/8" hole. 14476' - 14508' 32' Cored Core #8: 14452' - 14508". Cut and recovered 56'. Circulated and conditioned mud. 103.5-104 pcf mud ~-~ COMPLETION REPORT SOLDOTNA CREEK UNIT 22-32 Section 3~2~. T~ ? N~.~ R..9 .W.., S?.ward B & M ~TANDAHD OIL COMPANY OF ~A~O~N~, W' O,-~i' '-~ $PERAT~R Page 12. Ran ca 14362' of 3½" 13.35 Grade E drill pipe ahd 85t of 4 5/8" drill collars. Used 14375' of water cushion. (Hydrospring tester valve to surface. ) Set packer at 14503' - 14510' with 45t of tail to 14555te Weigh% on hook before setting packer = 130~000~. 10:55 AM, tool opened. With surface valve closed and water cushion to surface, surface pressure = 200 psi, opened surface valve and pressure bled off to 0 psi immediately with flow of 1 gal.~ of water, then dead. 11:18 AM: Pulled packer loose with 145~000~. 11:22 AM: Reset packer and opened tool with surface valve closed and water to surface, surface pressure-= 1OO psi. Opened surface valve, bled off pressure to 0 psi immediately (1 gal. ~ Flow), then dead. ll:28AM: Rotated to shut-in then immediately reopened. Surface pressure = 0 psi with surface valve closede 11:33 AM: Shut in at dual closed in valvee 11:48 AM: Pulled packer loose with 148~O00~e Did not back-circulate, pulled ~ri%h water cushion in p~ee Recovered 40~.+ drilling fluid on bottom grading to dirty water, remainder was water cushion. Final Pressure Data: , ,.' I J , I [ r L ~ Depth Gauge IH IF FF FSI F~ Inside ' 1.4~493 107-~3 6~'~O 6~2 - ~-P~e~s. Heco~er Outside 14~550 10782 6679 6590 6682 1058~ dem,.ged b~ h~.gJa' preesuree qoncl si Tool functioned OK. No plugging.. Test inc. onclusive~ Ran 5 5/8" bite Circulated and conditioned made August 27.- 28, 1962 94,5 pcf mud Circulated and conditioned mud. Pulled~ Ran HFT #2' interval 14507' - 14550'. Tool assembly: 1 outside BT recorder 37' of 3 3/4" perf'd tail pipe, left hand safety joint, two 5" type expanding shoe packer, VR safety joint, hydraulic jars, 1 inside BT recorder, hydrospring tester and dual closed in pressure valve. Ran on 14359' of 3}" 13.35 grade E drill pipe and 85' of 4 5/8" drill collars. Used 7480' of water cushion. Set packer at 14500' - ]4507', ~,~th 48' of tail to 14555~. Opened tester at 8:45 PM for 4 min. pressure r~lease. Faint intermittant blow (surging of cushion in pipe). Shut in tester at 8:49 PM for 1 hre 7 min.. ISI pressure period. Opened tool to surface at 9:56 PM for 1 hr~ 14 min.. flow test. No noticeable blow. Shut in tool at 11~10 P.M.~ for 1 hre. FSI pressure. Pulled packer loose at 12:10 PMe Weight on hook befor~ setti~.~g packer - 118,000#. Weight ~u hook to open b~pass valve - 148,000~.~ Weight on hook to pull packer loose - 140,000~. COMPLE~ION REPCRT SOLDOTNA CREEK UNIT 22-32 Section 32, T. 7 N.~ Re 9 W.~ Seward B & M STANDARD '~'~OMPANY' 0~'" CALIFORNIA, 'W. o.' 'I' - OPERATOR Page 13. Did not open back circulating port. Pulled pipe with cushion. Recovered cushion of water plus lOt to 30' of drilling fluid on bottom (105 pcf). Final Pressure Data: .... ~ ' ' - Depth Gauge_ ___~ ISI_ IF FF FS.!' FH Inside 14,490 10726 6488 3~5 3437 4133 10726 Outside 14,551 10762 6513 3505 3495 4181 10599 3489 3477 Conclusion: Tool operation OK. Test conclusive~ no fluid entry. Ran 5 5/8" bite Circulated and conditioned mud. Pulled. pipe. Ran open ended drill 104 pcf mud Cemented through drill pipe hung at 14330t with 50 sacks cement. Cement in place at 3:15 AM. Pulled 5 stands. Unable to break circulation. Pulled out with wet pipe. 14 joints of drill pipe and 12 joints tubing plugged with cement. Ran 5 7/8" bit and casing scraper.. Located top of cement, at 14198t. Drilled out cement to 14216'. Laid down casing scraper. Ran 5 7/8" bit. August 30-~31, 1962 Drilled out cement 142161 - 14250'. Pulled Ran EFT #3, interval 14234' - 14250'. Tool assembly: 1 outside BT recorder, 4t of 2 7/8" perf'd tail pipe, "C" type hookwall packer, VR safety joint, hydraulic jars, 1 inside BT recorder, hydro.spring tester with 3/8" fixed bean on top of hydrospring tester. Ran on 14022' of 3~" drill pipe. Used 6192' of water cushion. Set packer at 14134' with 13' of tail to 14147'. Hookload 114,O00~. Set packer 85,O00~. Opened tester at 5:54 PM for pressure release. Shut-in tester at 5:54 PM for 92 min. ISI pressure period. Tubing pressure buildup to 1875 psi. Opened tool to surface at 7:26 PM for 3 hrs. 13 mine. flow test. Shut-in tool at 10:41 PM for 126 min. FSI pressure. Pulled packer loose at 12:47 AM with 150~O00# or 36~000~ over weight of pipe. Cushion to surface at 7:28 PM (2 min.) 900~ tubing pressure gradually decreasing. Salty rat hole mud to surface at 8:40 PM (72 min.)~lO0 psi tubing pressure. Muddy salt water to surface at 9:05 PM (25 min.) gradually becoming murky, gray salt water testing as follows: 9:15 PM - O.21 ohm/m at 70° = 1800 G/G, 9:30 PM - O.18 ohm/m at 70° = 2200 G/G, 9':40 - 10:40 PM- 0.17 chum at 70° = 2400 G/Ge Shut-in at 10:41 PM for 126 min. FSI. Dropped 2 rods to open backscuttle valve - unsucessful. Pressure up to 6000 psi to open backscuttle ports - unsucessful (using Halliburton trucks). Pulled drill pipe - wet, Sample at tool tested Final Pressure Data: D_epth GauEe IH ISI IF FF FSI FH Inside 14'124" - 102~7 ~3 81~1 6~4 79~8 10~'~6 ~tside ~,~' 103~ 8625 8307 6724 8071 10196 Conclusion: Tool functioned OK, Ran in to 14250t. Circulated and conditioned mud. Pulled. 104 pcf mud COMPLETION REPORT SOLDO~NA CREEK UNI2 22-32 Section 32, T. 7 N'~ R. 9 W..~ Seward B &M STANDARD '0IL C'OMPANY 6F CAL~ORNIA, W~ '~. 'I". -'OfERkTOR Page 14. SeRtembe ,r, ,,1, 1962 Ran open ended drill pipe to 14250'. with drill pipe hung at 14250 '. scraper. Circulated at 9500'. to 140381 and circulated. S.e. Ptember 2, 19,,6,2 Circulated. Equalized 50 sacks of cement Pulled. Ran in with 5 7/8" bit and 7" casing Ranin and located top of plug at 14084'. Pulled 104 pcf mud Circulated. Drilled out cement 14083~ - 14223~. Circulated and conditioned mud at 14223'. Ran Schlumberger Neutron Collar log 14229~ - 13229t and 7800' - 7600t (Schlumberger measurements ). ~eptember 3, 1962 Ran Schlumberger Cement Bond log 14226' - 1~1}!00' and 8420~ -1720' (Schlumberger measurements). Ran Schlumberger Carrier Gun and jet perforated 5 - ½" holes 14204' - 14205'. Septe .m~e. r 4, 1962_ Ran HCT #4, WSO test of perforations 14204' - ]4205~. Tool assembly: 1 outside BT recorder, 4' of .2 7/8" pe~f'd tail pipe~ "C" type hookwall packer' VR safety joint, hydraulic jars, 1 inside BT recorder, hydrospring tester and dual closed in valve 90' above hydrospring tester. Ran on 14016! of 3~" drill pipe. Use~ 6192' of water cushion. Set packer at 14134~ with 13~ of tail to 14147'. Set packer at 1:33 AM~ Shut in tester at 1:35 AM for 60 min. ISI pressure period. No pressure at surface. Opend tool to surface at 2:35 AM for 12 hrs. flow test. Shut in tool at 4:35 AM for 30 min. FSI pressure. *Reopened tester (see below). Pulled packer loose at 2:46 PM. Opened at 2:35 AM - faint puff and faint blow for 10 min.. Appeared dead until 4:35 AM - no blow at pig.- Shut in at 4:35 AM. Surface pressure started building up at 4:50 AM - built up to 1875 psi. Opened to surface at 5:05 AM. Cushion to surface at 5:07 AM. Cushion out at 9:15 AM (9.6 B/hr. or 230 B/D rate). Salty rat hole mud out at 9:30 AM. Flowed muddy salt water with a trace of oil at .9.6 B/hr. or 230 B/D rate. Salt water tested 0.20 ohm/m at 70° - 1800 G/G; 10:00 AM - .18 ohm/m at 7Q° - 2200 G/G; 10:15 AM - ,18 ohm/m at 70° - 2200 G/G; 10:30 AM - .18 chum at 70~ - 2200 G/G. Shut in tool at surface at 10:37 AM for 135 min. FSI. *Started backsCuttle at 12:55 PM - opened bypass at 2:35 PM. Pulled packer loose at 2:46 PM - 190,000~ - 35,000~ over weight of pipe. (Dual closed in valve ran in open position - rotated to backscuttle position at 2:35 PM). Final Pressure Data: Depth,, ,Gauge, IH ISI IF FF FSI FH Top inside 14,124 10057 - - 6462 Bottom outside 11,144 10150 3495 6582 9065 Chart time ex- 9121 9986 pired. Conclusion: W.N.S.O. Ran 5 7/8" bite COMPLETION REPORT SOLD OTNA CREEK UNIT 22-32 ..Section 32~ T, 7 .N.~R. 9. W.~ Seward B & M STAN~'ARD "0~ 'COMPANY 'OF 'l';: 6P am oa Page 1Se September .5,, 1962 Circulated and conditioned mud at 14215t. Pulled, Set Halliburton DM cement retainer at 14030-t and broke down formation with 4800# psi. Formation took fluid at 12 cu. ft,/min, at 3300~ psi,. Pumped in 40 cu, ft. of water. Mixed and pumped in 200 sacks of cement treated with~ e3% retarder followed by l0 cu. fi, of water and 330 cu. ft, of drilling fluid, Squeezed 185 sacks through holes at 14204' - 14205t. Left 15 sacks of cement inside casing. Working pressure 3000~ psi, final pressure 8000~ psi. Cement in place at 4:22 PM, Unable to backscuttle out cement. Pulled out and laid down 43 joints of cemented drill pipe. Standing cemented. Located top of cement at 14028t, Drilled out cement and retainer ~o 14215t. Circulated and conditioned mud. 100-102 pcf mud September ? - 8~. 1962 .. Ran Schlumberger Carrier Gun s_ud jet perforated 5 - ½" holes at 14203' - 14204 te Ran HCT #5, WSO test of perforations 14203' - 14204' and squeezed perfs ~4204' - 14205'. Tool assembly: 1 outside BT recorder, 4' of 2 7/8" perf'd tail pipe, one 5 3/4" type C hookwall packer, VR safety joint, h~ydraulic Jars, 1 inside BT recorder, hydrospring tester, 85' 4 5/8" drill collar, dual closed in valve, and impact reversing sube Nad difficulty last two stands above packer setting point because of drag in hole, pulled 170, O00~ to free tools. Ran on 14031' of 3½" 13. ~ E Drill Pipe. Used 6192' of water cushion. Weight on hook before setting packer 118,000~. Set packer at 14144', with 13' of tall to 14157. Weight on hook with packer set 96,000~. No initial shut-in period. Opened tool to surface at ll:55P.M, for 4HR 17 Min. flow test. Faint blow throughout test. Shut in tool at 4:12A.M. for 2 Hr. 16 min. FSI pressure. Pulled packer loose at 6:28A.M. Weight on hook - 150, O00~ max pull to free packer. Lost about 3 cubic feet drilling fluid in annulus while attempting to set packer. Lost about Eydrospring valve opened with packer binding in casing. Lost about 9 cubic feet drilling fluid in annulus mt steady rate during flow period. Pulled and Recovered: 355' of drilling fluid (lO4 pcf) below water cushion. (270' of 3½" D.P. + 85' D.C., about 12 cu. ft. total vol.)Bottom 100' was thick mud. Packer rubbers were badly torn and damaged. Steel body of packer had g~uge J apparently cut by sm~ll metal fragment. Slips were packed with cement. Pressure data: Depth Gauge IH ISI IF FF FSI FH To~ inside 14,134' 10,199 - - 3079 3397 9061 10167 Bottom outside 14,154 10,264 - - 3309 3502 9077 10214 COMPI~TION REPORT SOLDOTNA CREEK UNIT 22-32 Section 32, T....TN..~ R. 9 W.~ Sewar.d..~B & M STANDARD 0Zt C0m~AN~ OF CALZFORNIA, W. 0. '~.~' 6~.R~TO~- Page 16 Conclusion: * FST pressure probably caused b~, mud leaking around packer, not true formation pressure build-up. Slow leak of mud around packer. Test conclusive WS0 - OK. Ran 5 7/8" bit and 7" casing scraper. Circulated and conditioned mud at 14,215'. Pressure tested casing ~th 2600~ psi for 30 minutes. O.K. Pulled. ~eptember 9~..1962. Ran junk basket on Schlumberger wire line. Stuck at 12,100' pulled junk basket free and pulled out. Ran open ended drill pipe to 14,210'. Circulated and conditioned mud. Pulled. Reran junk basket on Schlumberger wire line. September ..10, 1962: Pulled junk basket. Set Baker drillable cast iron bridge plug 14,217' - 14,220' (wire line measurement) . Ran Schlumberger Carrier Gun and shot holes 14,147' - 14,148' (Schlumberger I-ES Depth) Ran HCT ~6. WS0 - Test of perforations at 14,147 - 148', 14203 - 204' and 14,204 - 205' (sq.) * All Schlumberger I-ES measurement. Tool assembly: ~ " ~ I outsi'd~ BT..recorder~ ~'" "~' '8" pip~ 5 3/4" ~e' C~ Hookwali .. of.~"2~:!7/~ perf' d tail one packer, VR ~afety joint, hydraulic jars~ 1 inside BT recorder~ hydro~prinE 'teste,r, '85:' or 4 5/8" drill collars, ..and dual .clo~ed in .val.~e, and impact reversin~ sub. Ran on 13767' of 3½;'~ 13.3~ E Drill Pipe. Used 6192' of water cushion. Set packer at 14080', with 13' of tail to 14093'. Opened tool to surface at 6:57P.M. for 2 hrs. 8 min. flow test. Shut in tool at 9:05P.M. for 1 hr. 55 min. FSI pressure. Pulled packer loose at ll:OOP.M. Max Pull=160,000~ No blow during flow period. Pulled and found top of water cushion about 3' above original point of pill when cushion was installed; found slight amount of mud' at dual closed-in valve (possibly washed down forom inside of drill pipe); and found drill collar comple- tely dry. (Dual closed-in vlave run in open position~ dry drill collar may be result of air pocket created when cuahion put in). Pre s sure Data: DEPTH GAUGE IH ISI IF FF FSi FH Inside 14,070" 9657 - - 2769 2787 7600 9586 Outside 14,090' 9735 - - 2891 2905 7622 9667 Conclusion: Tool operation - OK Test Conclusive, WSO OK. COMPLETION REPORT SOLDOTNA CREEK UNIT 22-32 Section 32, T.___7 N. R. 9 W.,Seward B & M STANDARD OIL CO~T~ OF CALIFORNIA, W. O. I. - OPERATOR Page 17 ~eptember 11~-t962 Ran open ended drill pipe· Circulated and conditioned mud. Locate~ top of cast iron plug at 14,206'. (Drill pipe measurement.) RanSchlumberger Carrier gun an~:?perforated the interval 14,200 - 14,175' with 4 - ½" holes per foot. September 12,~ 1962 Ran HCT ~7, of the interval 14,175 - 14,200'. Tool assembly: i outside BT recorder, 4' of 2 7/8" perf'd tail pipe, 7" type "C" Hookwall packer, VR safety joint, hydraulic jars, i inside BT recorder, hydrospring tester, 85' 4 5/8" D.C., Dual Closed-in valve and impact reversing valve. Ran on 13,997' of 3½" drill pipe. Used 6192' of water cushion. Set packer at 14,110', with 13' of tail to 14,123' at 6:05 A.M. with llS,000~ on hook. Opened tool to surface at 6:08A.M. for l0 hrs. 45 min. flow te~t. Shut in tool at 4:53 P.M. for 2 hr. 2 min. FSI pressure and backscutted ~.ise. Pulled packer loose at 6:55 P.N. with 178,000~. Immediate weak blow decreasing to dead at 4:40P.M. Backscuttled rise and recovered approxmately ~00' net rise (Calc. from flow pressure increase). Approxmately i6 gallons (.150') oil on top of water cushion and 150' drilling fluid below water cushion (Include 85' of mud in drill Collar). Oil Corr. Gravity 23.0° cut 12~ Total, 2~2%.water, ~.0~ emulsion, 5.8~ sand and mud. Salinity of cushion ~5c/c (0.7520H~S~ 100~...?¢~ n~ud. Pressure Data: Depth Gauge IH ISI IF FF FSI FH Inside l~,lO0' 10340 - - 2773 3083 6840 . lOll6 Outside l~, 120' 10389 - - 2909 3189 6873 10361 Conclusion: Charts indicate tool functioned properly. Test Questionable. .September 13~ 1962 Ran open ended drill pipe· Circulated at 14,217'. Attempted to perforate. Schlumberger failure. Ran open ended drill pipe. Circulated and conditioned mud at 14,217'. Pulled. September 14~ !962 Ran Schlumberger Carrier gun and shot 2 ~ holes / foot 14,175 - 14,200' and lit · 4 W holes / foot 1~,152 - 14,175' R~n HCT ~8 of all perforations 14~152 - 14,200'. Tool Assembly: I outside BT recorder, 4' of 2 7/8" perf'd ta~l pipe, "C" .Holk- wall packer, VR safety joints, hydraulic jars~ i inside BT recorder, hydrospring tester 85' drill collars and dual c&sed in pressure valve and impact reversing sub. COMPLETION REPORT SOLDOTNA CREEK UNIT 22-32 ~ectio~~n 32., T. 7 N. R. 9 W. ,Seward B & M ---RDSTA~ OIL CU~NM OF UALiFoRN~A' W. O. ~. Page 18 Ran on 13985' of 3½" drill pipe. Used 6192' of ~ater cushion. Set packer at 14080', with 13' of tail to 1409~'. Free weight =120,000~, after setting pack- er 96,000~. Opened tester at 4:05P.M. for 4 min pressure release. Faint blow of air. Shut in tester at 4:09 P.M. for 61 min. ISI pressure period. Opened tool to surface at 5: iOP.M, for l0 hrs. 21 min. flow test. Shut in tool at 3:31 A.M. for 159 min. FSI pressure. Pulled packer loose at 6:iOA.M. with 150,000~ pull (30,000~ over weight pipe) Faint bubbly blow gradually decreasing to very faint bubbly blow. Well did not die. Recovered 690'net rise (7 Stands and 2 singles) Recovered ~882' gross rise. Top 2 singles of oil (22 gallon~) of 29° oil-clean - 0% cut. Backscuttled rise. Slight scum of oil at firSt, them slightly oily water cushion (fresh) then slightly oily rat' hole mud. No salt water during backscuttle. Bottom 85' rise in drill collars above tool was salty slightly oil clabbered drilling mud - filtrate tested 0.2740R~iS'. at 50° = 1700G/G Final Pressure Data~ Depth Gauge IH ISI IF FSI FH ' 66 s Inside 14,070 10397 8561 28~7/ Outside 14,090' 10439 8619 3022/~ ~ 6756 10389 ~uee. C~eula~ea an~ eondig~one~ Ran open ended drill pipe. September 1.67 1962 Circulated. Pulled. Ran McCullough Super F~rmation jets on Schlumberger line. Positioned gun and attempted to fire. Unsuccessful. Pulled gun and found two damaged sections on line. Sept,emb ,er ,, ,17,,, 1962 Repaired Schlumberger line. Reran McCulloBgh Super Formation jets and shot 2 5/8" holes / foot 14,200 - 14,175'. ~irculated and conditioned mud. S. eptember 18 & !9~ 1962 Circulated and conditioned mud. HCT ~9 of interval 14152 - 14200 . '~ .~-'~ Tool ass.e,~bl[: One outside BT, recorders' 4' of 2[~8" perf'd tail pip~ one 5 3/4" t~e C look~ll packer, VR safety joint, hydraulic jars, 1 inside BT recorder, hyd~spring tester, 85' 4 5/8 drill collar (I.D~, dual closed-in valve, and i~act ~versing sub. Ran on 13965' of o~ 13.3~ E Drill Pipe. Used 6192' of water cushion. Set packer mt 14078', with 13' of tail to 14091. Opened tester at 6:54P.M. for 8 min. COMPLETION REPORT SOLDOTNA CREEK UNIT 22-32 Section 3L2. ,~.._T._~7~_~_ R. 9 W., Seward B & M STANDARD OIL COMPANY OF CALIFORNIa, W. O. I. - ~R~TOR Page 19 pressure release. Faint blow ~2 of water over bubble hose kills blow) Shut in tester at ?:02P.M. for 2 hr. 16 min, ISI pressure period. Opened tool to surface at 9:18P.M. for 7 hr. 49 min. flow test. Faint blow (~" water kills blow) until 5:02A.M., then dead. Shut in tool. 5:O7A.M.~for 4 hr. 54 min. FSI pressure. Pulled packer loose at lO:O1 A.M. Pulled and recovered 360' net rise. Top 20-30', on top of water cushion was oil (6-8Gal. Total Vol) Bottom 330' Below water cushion, was salt water (2400~G at tools) (85 Gal. Total Volume. Pressure D~ta~ Inside 14,068 10433 8939 6989 10149 Outside 14,088 10436 8978 ~/ / 7015 10,296 Cohclusion: Tool operation. OK _ Test Conclusive Ran open ended drill pipe. Circulated and conditioned mud. September..20, 1962 ~emented plug ~1 thru drill pipe hung at !4,200' with 35 sacks cement. Pulled 5 stands. Circulated. Pulled to 13,195 ' and circulated. Pulled to 9960'. Estimated top of cement at 13,974. Cemented plug ~ thru drill pipe hung at 9960' with 40 sacks of cement. Estimated top of plug at 9735'. Pulled to 5022'. Cemented plug ~3 thru drill pipe hung at 5022' with 20 sacks cement. Estimated top of plug at 4800'. L~id do~ drill pipe. ~eptember.. 21~ 1962 Cemented surface plug with 35 sacks of cement, thru drill pipe hung at 190'. Rig released and well suspended at 12:OOP.M., September 21, 1962: Depth 120 ' 372 ' 2010 ' 3073' 3666 ' 4322 ' 4636' 4900 ' 5056 ' 5156' 5229' 5301' 5462' 5518' 5643' 5698' 5749' 5834' 5898 ' 6064' 6122 ' 6348' 6408' 6508' 6658' 6798' 6917' 7068' 7215 ' · 7340' 7450' 7570' 7683' 7795' 7899' 7988' 8096' 8125 ' 8289' 8517' 8755' 888o, DEVIATION DATA Degrees 0o45 0© 30 0030 0° 30 0o30 0° 30 0o30 0045 0° 30 0© 30 0o15 0°45 lO00 0© 0° 30 0045 lO00 lO00 lO00 0045 0045 0o45 0°45 0045 0030 0045 2000 lo00, lO07, 2o00, 2o07, 2007, 1045' 1© 15 ' 1000, 1° 30 ' 1°37' lO30, lO07, 1045, 1045' 1° 30 ' t ;~-~ - ~ Al~rovol exphe~ UNITED STATES ~.u om~ ..~C~Pr~ DEPARTMENT OF THE INT~IOR ~ ~..~~9~8.__~~~.~ LESSEE'S ~ONTHLY".REP~'RT OF OPERATIONSA"~h°~g~' OCT 1~ ~62 , . , . . .. ~'~g~ (If (If drone, ~th: ff .hut down. 2[ .'::i: ' ' - ~203'~- ~Oh', -~:~ ~, ~0 - 0~. 8e~ "{ ho!e,/[oot~175' - ~~', ~ RC~ ~. 10 hfs, h~ ~, to ver~ f~at bl~. '~o~ered~690~ ~ rise, includt~ ~rf}ra~$ inte~ ~I?~' -~2~'~th 2 ~/8" holes/foot ut~ ~cC~~h ~r{ casing Jets.. ~ HOT ~9 of ~ ~. at-996p' ~{h ho sa~slce~nt.] sst~a~ t~ o~ pl~ at 9735'.{ C~ted .~ug ~3 ~ ~-r. h~ at 5022' vt~ ~ -{ stet ~%e~ runs or ~ales of off; _= .... :!-'.=~..~:_.:__5[:. ......................... M cu. ft. of gas sold; .......... ~- .... : .............. ~ .......... '.m~18 'or ~,los of 8asoliue du~ th~ mog~h.. :{W~ "no" whero appli~blo.) ~o~,~Report oa::thh form. is ~'qnir~ for~ch ~lendar month, ~g~ ~ ~ status ,of operations, and m~t be ~ed in . duphca~ ~th the supe~isor: by the 6th of the suc~diug month, un~ o~he~ise' d~ted by the superv~or. .; Mine~ah - . - / lm~ Appm~,e~. - ' . ~.,a o,b. An~lmora~.. Bremcn ........................ · ' " of Natu;a: i.:.~.:.,.~l~ Ne. .............. ~'.4'_"'. .... DEPA~T~£NT OF TH£ GEOLOGICAL SURVEY SUNDRY NOTICES AND REPORTS ON WELLS NOTICE OF' I~ TO D~ILL ................................. NOTIC~ OF INI~NTION TO ~ PLANS ....................... NOTICE OF INTENTION TO ~ WATER SHUT-OFF .............. NOTICE OF IN'I~{N~ TO RE-DRILL OR REPAiR.WELL ......... NOTICE OF I~ON TO SNOOT OR A~IDIZE .................. NOTi¢~ OF' I~ TO PULL OR AL/IR CASING .............. NC)'TK~ OF I~ TO A~ANDON ~ ...................... i; MARK NATURE Ol· RIKPO~T, NOTICL OR OTHU2¢ DATA) ABOVE BY CH~7.K i,u ...... II '"--"-' ....................... / ..... ...... II '~""~""" ..,o.,, o, .,,,.o.,~ .......................... / ..... W ted __2__1~__~ .... it. from__ line and ._~... it. from line of sec .... ~ .... ...... -~'~. ~'~'N;3 .............. ~.) ............ ~'~ ................-~'~'~3' .......... _.W~_~ .................................. ~~__~~ .................... ~m~ .......... (~) ' (~x od s~i,~.) ......... 2~ ~'~'~3 .... K.B. DETAI~ OF ~OH i~ ~n~ ~ nil otb truant ~ ~)(~~~~ ~n~~*on ~~nt h~z ~ lk,~' Plus. lk, 3~' - ~n~n - ~tMy 9/19/~) ' 7" ~ lk, l~' l~,~'t ~ ' i" ~s/f~t 1~,17~' ' lk,~(~~), a ~ ~/8_ 1~,~'; ~ - '" ~ at 1~,~' - lk,~'. ~ onnt tv,.. lk 20~a 1l~-211' .btam6 ~o permeability. Tes~; or open ~o~e ~.,~,~.~ .~s~f ~l~d ~n ~ ~Mo of oll ~ nit mMr. ~ o~r in~~ of ~~st for.~~ Title Work oontlmied on Pa~ 2. ~o ,,-07, Sundry Notices and ~eportl on Welle U.S.G.S. Form 9-331A September 21, 1962 Page 2. Details of Work (continued) 1. Plug with cement 14,223' - 14, O25'-+ with 1OO sacks const, cement. 2. Locate top of plug near 14,025' and abandon hole below 14,025~. 3. Place 1OO sacks running plugs (approx. 200 lineal feet) from 10,OO0' - 9800' a 5,O00' - 48OO'. 4. Place 1OO sacks plug from 200' to s~rface. 5. Bolt steel plate on casing head & place well on suspended s~atus for possible reentry at later date for redrill to more f~vor~ble structural position. UNITED STATES DEPARTMENT OF THE INTERIOR ' GEOLOGICAL SURVEY . LESSEE'S .MONTHLY REPORT OF OPERATIONS . Budge~ Bureau No. Approval expire~ 12-/11-60. LA.. omc~__..A..n..c.h o~age ......... ~.. ..... ~old~n~..Creek.~ State ........... Alaska ..........6'o~n~7/::._Ke~&i..P.e~l~.. Fie'~d _.~on.~.v. er .................................... Tke foHo~ is ~ correct repo;r~ of opera~ions and production (i~ch.~dir~ drillin~ a~d produ, cin~ wells) for t~e mo~t?~ of ........... ~~% ...................... 79_~ .......... ~9~9~...Creek U~t ............................. ~'~o~ '. ~':7~1 ~'~ '~n~'~ tit~e Dia~ric~ ~~~..m~au~ ....... SEC. ANt) (~ tho~) RECOVEaED none, 8o s~te) sou 14083" - 14228' - at 7717' · to 14235 14203 '. 14234' · . eemente an~ 1100 Tested Drilled Cored Ran % · TeSt ~o~ 32 ih~o7 mud, at (If drilling, depth; if shut down, da~ ~nd result of t~.at~ for Cored ~203' - 14228~. Ran I-E~, Sonic log, Microlog ! 7" casing at 14234' with 700 sacks ti · ]th 245( out oe~ 14235' ~st #i, o: Lnconcl~ ~rough DV at 7717'. ~- O.K. Locate~ ~nt and shoe at 14234 '. ,14550' ToD. Ran ,en hole test of the ire. Ran test #2, 145~01. No ff.udi entry. Circulated ~ ..ed 5!_ sacks (ement at 1433Ogo Loc- '. Drilled out '~..ement' to 14250'. of th~ interv~l 14234' - 14250'. i Equalized ? sacks cement at ement atl 14083'/ Drilled out cement [ Al, Pefrole~. Branch [vision-of MM e~ and Minerals ~ko DelX. of Natural. bsourill No?~.--Th~e were .......................... . .......... ~ or sales of oil; ............................................... M ea. ft. of gas sold; _ ............................................. runs-or s~ies of gasoline during the month. ' (Write "no" where applicable.) No~E.--Report on this form is reqUired~or each calendar month, ~dless of tho status of operations, ~nd must be filed in duplicate with the supervisor by the '6th of t~he succeeding month, unless otherwise directed by the supervisor. (January ~g~0) - PRODUCING DEPARTMENT TELEPHONE BR. 7--6201 C. V. CHATrERTON DISTRICT SUPERINTENDENT P. 0 BOX 7 8 · - 39 ° ANCH~~ . · . o. ~~ ?-';:~X~:l ...'.,'.'-,.'.- ":...' "-":'..:". ,. . ':. ' -':':' -.:: -'.: ,... ~ i- .. -'- ' ~. ~... ..~'~ . :'.':. ~" ' -.. -:.~.:...,..-':~~-:-.........._ _-~:. ,.. >~.~~ ~~...~ · ... ,~::L~'~-:'""~'::':,"' - "'.';"¥. - ~.'-' ~' "i '. . :: ~ -' · -'~ _ ' ' . '-~:i ..-" -' :.:?~.:::, L,.:.. :" ~' . : ~J: I ..... ! ! ' '... ' .' ' ~~ .:: .....~~~ - "-' ' ::" "-:. 2 ':>:-,': ."> :,-~~ -I '-. ' - .-.: UN~ ~A~ · · ' ~~I~ ' ~" - ' "--L.-I--~,.4 '-' ~'~' '" · "'~ !' ! - ' ': ' ' ~,-. ::.,~-',:..SUNDRY'- NOTICe'". AND. . RE~RTS. ON ~L~ . .. ~.. .-.. .... ~z . ~ ' '- ' :' "~ ...... I "~ ~ ~ ~-'- ...... L ...... ~- ..... L ............... -~- ~~ ~ ~ m~ ~~ ...................... ~1'~"' ~=.~..,~~ ~ ~..~ .... _~ .......... :..~ .... Z-Il ~ :->:-~"...-: ~: ~ -. ,~ -.~ -'- ~-----~ .... ' ...... 4~-~'~ ~ ' '~ -' ...................... -r'- . . .:~~..~~~~~~~ ..... ~_..:~.:.~_~~-~.~~~ .......... ~ , ':: :~ .-'~ ...... ~' ~ ~ ~~ ~ ~'~'~'~.~- ................ ::---~1~ ~ o. ~.~..' ......... . .... -.-~---:' -. [~:.~. ~.. . ..... ~=~7=--r-- ' ............. ~ .... (~m~ ..... ' ..... ~~ .... ~ .............../~ I ~ ~ ~, ~ ~ ~ ~Ta) . ' : . . . ~. , . . . .. ~....,.. ,... . ~.- . ~ .-.. ..-.. ........~ ........ : ........ : ............ : .......... ~?---~ ......... , -~ . . / ,:'-....',.': :-:'~, .: .,.".. . - .. . . . - . I.'. =. .... ' ' "'- ' '' :' ' ' ' N ~":'>~",:':'. ,:":'.: ~ . ". ~" ~~ ~ ~_~:-' ~: ' ..... ~ - '. ~S: ':-: ~- :..'.-'..'.' ...: "-.':~~~: ..... :---:',-, ..... ~:~'~" ::--Y~i. '" ' ~ ' ' ' ' k ' " ' ' ': ' , f>. ..- :..., . :=-,--~~:,,:-: ..... ,..:--:.-~.-.-:---.--~-~~ ......................... ...: ::....: ._.-,.~ · ....~.......... :.-~~.-.~~ .. . - . . ... i -??:~-";,:~ , :.-' '_,. - ' .- : -..' ,-~. . ' " · ,., S and Minerals ' ~ - .".:~, ........ : .. · , - - ' DI~ion ~ ~me . - ~ - ;:':'::~, ...... -' ' DETAI~ OF ~O~ ~. ,~ ,~f .Natural Resource, --.y ..::, ,-,.., '. ', .. : -.. - I~~, ~ ~ arm ~~ : . ._' .-. [ ..:>:..::::.-.:. ... .. ~ ~.~ ~. ~-.~_ ~~,~-_ ~.. .. ~,-: ~,, ,~ ~.~., .. ' . . . . '"":::: ..... :':~6. ~~ ~"" ' ::-:" '~: "~e~ti~ ~l?~".---~b~ ~ ~e~. -' - ·, .~ ::.::-,-:,:.:::, , . .-.. ...._¥..~..:: .- ... . .- .. ': "::" ,.-..':~:.-- i~-~i~~~:~.~~=~~~~~~~~--~~~ . ---: :.::.;-::?. ::: :....~ ~.... ~~ ~.-~~_.~..~~,._m~__~m~~.,...~.,[ .............. ::~ --,. ::4~:.' ...--.~:-_: :.'.... ,.-: . ,:.,...:..,, '_' ....... : .... , -, .. ~ :..%,.Y?.'.?:: ,:....:.:. : .,~ .... ~:. ,- , . .. :'..' ... _:. , .. .-:_-_ UNIT 1 2 2 13:371' '. m%d . [er REMARKS (If drllUn& d~pth; if Abut down, csm; d~t~ -n~I ~t of t~t for f~o~ * I-E S~ic log ~ -'. h~e 12~8~ ' + 13371'. Dri~ ~ [-~, S~c log, Mterol~- . ,' D~l~lon of Mlne~ and Ml~rals - _.. ~ ~' ~ ~'tura/ R~r. , --, ~ ~.. ~,~ = .- . . . . . _ ,: ..... ; ..... ~ ~ - STATE OF ALASKA DIVISION OF MINES 6; MINEBAL~ 329 SF'"CE3ND AVENIJEi;; SUNDRY NO,.iCES AND REPORTS ON WELI~ i i i . u i. i! iii . . i . i ii -- · o~_. ,.~,~. ~ ~~-'-)-~i ......... ~-~ ..... l"*--Il ~""~~"t~°~ ~. ~.~ ~ ~~ ............... I ..... -.~~ ~~ ~ ~"~ ~~ .... :----q--:---Ii ~~-~ ~ ~~ ~ ....................... I ..... ~-'~ ~-'~~_~~-~---~ .... ! ...... !1~~ ~ ~ ~~ ~ ~" ............. fl ..... '~ ~ ~ ~-~~ :-~-- ..... :-:-1---~ ~~. ~ ~ ~~ ......................... 1 ..... ~"~" ~''~ ~ ..... ..... --I-~:'~t~'~ ~ ~": ................................ 1'-- ~'~'-~~ .... ~'" ......... -1 ..... 1 ..................... ~ .................................................. ] ..... : . . :. ...... ~ ...................... Jl .............. , ......................... ; ............... n ................ -~- ~. A~s~ ~ 19..~ x~--~- ll! '~' ~ ] - ~''~ ~} '~' ~ - .... ~-'- ~_~.~,~...~ . ~..:_.s~,__~-..~.?'_.. ~-~ ........ -- ~?~ .......... ~.) ~) .............. ~~~- ...... ~ ~. ~~~_..~ ......... ...... ~ ..... :' ~ii'~ ~u~v~) ......... i~'~'~~ .............. ~.~ ~ e~a~ of'the ~~ e ~ .level ~ .~ ..... ,~~: ~, ~/a -,~,~"~ ~' RECEIVED ~o ~/~" ~e .~ eSc8' ~ ~2 ~/~" .o~ ~ ~ ~' AUG ~ 9' ~'~e ~ ~~' ~~:'. ~ D~islon of Min~ and Mlne~b ~l~a .Dept. ~ Natural R~ur~ 1. ~nt Tn cabin;-&t 1~' In ~vo s~s iPO ! 14~7 4 CONFIDENTIAL UNITED STATES DEPARTMENT OF THE INTERIOR GEOLOGICAL SURVEY LESSEE'S MONTHLY REPORT OF OPERATIONS State ......... ~_l._~..s.__~__ .............. County ..... _~_en__ai._Penin ~..~__ Field ..... Swanson .P~.y~ ............. Tl~e follow~nE is a correct report of operation,s, and prodz~ctior~ (iT~cluJin,d drillin~ and producing wells)for the mo.th of J~ f9 6~ S~do~a Creek Unit ..................................................................... ST~ ~ OIL-C~T A~_c~ages _ A!as~a S~ed Phone ............................. --' -- ~ '"'' '~ ' I ~:--:-'-- ' ' '~ ' , 12167 i - 70~ ~ ~ ~crolo[ 1216~ ~ - 7~ ~ and CDM 12167' - 7~00 ~. D~q_l.' li~ she scl} u.s.o.s. - M. R~, t~eld - C. ril~s: Produ, 12167' - 1: · S~ter - Do D. Brue~ W. Perry R. R~tter :lng , _~782'. ,UL 11 1962 l~etroleum Sranch Dlvldoni of Mines Alaska I~lept. of biatU~O, NoTE.--ThoI~ were ..................................... runs or sales of off; ................................................. M cu. ft. of gas sold; ............................................. runs or sales of gasoline during the month. (Write "no" where applieable.) No~.--Repor~ on this form is required for each calendar month, regardless of the s~a~us of operations, and must be filod in dupheate with the supervisor by the 6th of the succeeding month, unioas otherwise directed by the supervisor. (J~anuary 1950) 10---~I~766-8 u. ~. aowqa~*~ *~ls'r~ o~lc! . CONF ENT., .L ' DEPARTMENT OF THE INTERIOR .~ I -, G,..O,..OG,CAL SURVEY LESSEE'S MONTHLY REPORT OF v., = RATIONS St~;e ..........Alaska ....... Cou. n.¢~ ._Kenai per~nsula... F, Ccld.. Swanson River ]'lz.e fo[IoaJt'~,~ i~7 ~: correc¢ report of u.,c~,Q for tl~e m.o~th ~;,r I'~y ;V 6~ Soldotna Creek ';nit ........... ' ................. STA~ARD OIL CO~A~ OF' CAL~. P, 0o Box 7-8~9 .... Com. pa.y Western (.,perations~ Inc. - ................... Z- ;,.,:,;,.,' . ....................... ~R..7~201 . . ...~ct~;'s z. itZc Distric t Superin~nden.t - . .......... =:__. - .... ~, _ . L'~' FY. o~' ~;.t8 i (}AS,)L~NE ~,'.~':1.,; '~' ,1< d.~.', .~..',-"',, · .h /~,,~- 32 7N ~4 SW NE ~ casi~ a~ 200~- ~ ~-~t~ 2000 sacks~ cement.' BOPE, : t : Drilled 12~" hole 2 ,0~0' - 3072'. I Drilled 10 5/~" holel 3072' - 6508'. I DriP.ed 9 7/fl" hole 6508' - 79,88'. ; Drilled 9 7/g'' hole 7988' - 9032~. Dri]lin~ U.S.G.S. -M. H. Soyster Alaska 0~..0,- G C :C - D'. D. B~uce Richfield - C. :W. Perry, R. R. Files: Produdng, Land R~tter i ; - 2OO8'. RECEIVED' M ¢u. ft. of ga;s sold; NOTE.---There were ......................................... runs or sales of oil; ............................................ ................................................. runs or sales of gasoline during the month. (Write "no" where applicable,) Nor~m~Report on this form is reqtdred for each calendar month, regardless of iht; si'atu.; of operatiotxs, and mu~t L,e filed in duphcate with tho supervisor by the 6th of the succeeding ntonth, unless otherwise dir,zcted by tho supervisor. ~'orm 9-~29 ~anuary 1950) PRODUCING DEPARTMENT TELEPHONE BR. 7--6m01 C. V. CHATTERTON DI~rTRICT SUPERINTENDENT P. O. BOX 7-839 · ANCHORAGE · May ll, 1~62 Mr. John B. Hakala United States Department of the Interior Fish & Wildlife Service P. O. Box 500 Kenai, Alaska Dear Sir: SOUTH SOLI~ CR~.W.K UNIT WELL 22-32 Please refer to our letter of March 30, 1962 concerning construction of road and location at South Soldotna Creek Unit Well 22-32. The location and road have been completed and surveyed. The attached copy of the surveyor's drawings is for your information and files. The well coordinates 1,re. ye been determined to be 2115 feet south and 2080 feet east of ~he northwest corner of Section ~2, Township 7 north, .Range 9 west, Seward Meri- dian. Very truly you rs, D. V. Ci-iATTERTOI~' C. V. CHATTERTON Attachment IINITED STATES DEPARTSI:~''''r~_,..,. OF THE INTERIOR GEOLOGICAL SURVEY LAND C~ ;!:~ Anchorage ,~:, Soldotna Creek LESSEE t 'IONTHLY REPORT OF OPERAq ,)NS Alaska ................. 6'ou, nty~ Kenai Peninsula ._ p'ir~M_ Swanson River Tl~e,?ollo~c[;~c~, is a correct revert o/ wells)y~r ti~e ~?~o~,th o/' Ap~I . /~62 Soldot~ Creek ~tCOMPANY OF CALIF. ............................................. STA~A~ .4~..~t s addr~x~ _ P.O. B~ 7-839. Compa~.!t Weste~ ~erati~s, .Inc, ............................ ~ohorage, .Alaska Phoneme ............................ ~_7~01 ................... Zgcn, t'.~ tgglc Dis_~t .Superintendent .~o , ~,.,~-~.,I._.~~ ~ , 32 7N ~ ~~ SW ~ Sp~ed April 29, 1~2o Drilled 12~" h61e 0 - 2010'. ~ ~-~, So~$ log ~d I UoS.6.S. -Mo N. Soyster Alaska 0 & G C C -Do D. Bruce Rich,~ield - C. W. Perry, R. R. Files: ProducJ.ng Land ~g. - 1900' o Ritter 'RECEIVED Dlvlslo~ of MinesI and Minerals Dept. Alask~ of Nptural Resources I I i No~..--There were ..................................... runs or sMes of oil; .......................................... M cu. ft. of gas sold; ................................................ runs or sales of gasoline during the month. (Write "no" where applicable.) No?}s.~Report on this form is required for each e&lendar month, regardless of thc Jtr[t. us of operations, and taus0 be filed in dupheate with the supervisor by the 6th of tho succeeding month, unless otherwi3e directed by thc supcrw.sor. · ~om 9-3~9 APPLICATION"FOR PERMIT TO DRILL, DEEPEN OR PLUG BACK ..... ~.. ....... APPLIC-.AT~ION TO DR}LL_~ DEEPEN [] PLUG BACK [] NAME OF '-C(~"MP-~:N~-' ~)R OPERA~'0R .... ..... ~ :' ' ' DATE Address ' ~-~' "- ...... ' ~ : "- - ': -'' :- City~ w- State .. d..' ..-. r: ........ : ' Dti~SCRIPTION OF -WE~I~i~: AND LEASE '~~'Name of ]ea~;- ; '" ' "~" ;Q:'M ~ .... · ' ;. :.- _ '- .r~'.~,: - ''- ' ' '[t '~'ell~",,]" n~mb~~~r~. [ 'iii'' ' Elevation (ground) X¥ell location (give footage'from section lines) Section--township--range or block & survey Field & resergoJv~ (!f-.wil.~toat,. s,o-~ta~te)~- ~:' : . :;: :.. [.C~unty ; . . . Distance, in miles, and direction from nearest town or post office Nearest distance from proposed location Distance from proposed location to nearest drilling, to property or lease line: completed or applied~for well on the same lease: feet Proposed depth: Rotary or cable tools Approx. date work will stare Number of acres in lease: Number of wells on lease, including this well, completed in or drilling to this reservoir: If lease, purchased with one or more wells drilled, from whom purchased: Name Status of bond Address Remarks: (If this is an application to deepen or plug back, briefly describe work to be done, giving present producing zone and expected new producing zone) ., APR 1"7 1982 petroleum Branch DivisiO'n of N[ines and Minerals Alaska Dept. of Natural Resourc~ (company), and that I am authorized by said company to make this report; and that this report was pre- pared under my supervision and direction and that the facts stated ther~a ~r~ tr~e, eorrec~and complete to ungmm s~gneo the best of my knowledge. C.V. C~LkTTERTON Permit Number: Approval Date: A'B'lOfi q q FI _ '[962. /7 Chief, Petroleum Branch Notice: Before Sendku~ in-this form be sure that ~oU have ~iven aH information requested. Much unnecessarY correspond- ence will thus be avoided. See Instruction on Reverse side o~ Form Signature Alaska Oil and Gas Conservation Commission Application to Drill, Deepen or Plug Back Form No. P-1 Authorized by Order No. 1 Effective October 1, 1958' (SUBMIT IN TRIPLICATE) UNITED STATES DEPARTMENT OF THE INTERIOR GEOLOGICAL SURVEY ~-:' :..--. SUNDRY NOTICES AND REPORTS ON WELLS . . .i ~'' ........ ; · ..... ~;~E OF INTENTION :. NoTIC~ OF INTENTION NOTICE OF INTENTION ' NOTICE OF INTLrNTION . * :: !~NOTICE OF INTENTION · llIOTICE OF INTENTION NOTICE OF INTENTION TO i~llLL ................................. l-_Ill SUBSEQUI~T REPORT OF WATF-J;I SHUT-O~F TO:c~GE ~S .................... } ..... { SUB~QUENT ~PORT Of ~TING TO'T~ WA~R SH~FF ........... i- _J: SU~OUENT ~PORT OF AL~RING ~ING .... TO RE-DRILL OR R~AIR ~L ........ ] SU~EQUENT RE~RT OF RE-DRILLING OR REPAIR .............. TO S~T OR AC~DIZE ................ SUBSEQ~ RE~RT OF ABANDONME~ TO PULL OR ~ C~ING ........ H SUP~EMENTARY WELL H~ORY ....................... , .... [,- ~ ............. :--_ (INOICAT[ A~OVE BY CHECK MARK NATURE OF R~ORT. NaTl.. OR O~ER DATA) ....................... ~r~ ._1~_. ....................... 19_~ ~PP~°xl~telY ~, line and _~ _2l.~__. ft. from ~I line of sec. ~._ Well No. ~.___~_?.'_.~. is located/. ~_~_. ft. from__ ;' ~ !~roJ. See. ~. ~. Z.I., a. 9_.W. _ ............... ~..v~.~___~_ ..... --', - ~'~V~-~. ~.) ........... ....... ~(',,unt}' ,,r .{ubdivlslOn} Thc elevation DETAI~ OF WORK (~t~t~ 3, .. names of and exi~ct~cl depths to obj~ctlve ands I show s|zas, weights, and lengths of propo~d casl alEsi i~dlcate mudding jobs, lng I~ints, and all other important pro~! work) ~ 'RECEIVED' .. APR 17 1~ Petroleum Branch Division of Mines and Minerals ~:q~ Dep~ al Nmural gesourc~ that tli~ plnn of weak. ~,u.t.. ,'~.ehm ~pp~oval in wrttlne h, the a.oio~ic.I Survey befor~ ~p. rations m,,, be comn. nc~i. PRODUCING DEPARTMENT TELEPHONE BR. 7--6201 C. V. CHATTERTON DISTRICT SUPERINTENDENT :_ P. O. BOX 7-839 ° ANCHORAGE ° ALASKA PRODUCING DEPARTMENT TELEPHONE BR. 7--6201 C. V. CHATTERTON DISTRICT SUPERINTENDENT P. O. BOX 7-839 ° ANCHORAGE ° ALASKA II II II