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HomeMy WebLinkAboutPBU CGF B / BP Exploration STATE OF ALASKA AOGCC GAS DISPOSITION FILES YEAR: 2004 FACILITY: PBU CGF B OPERATOR: BP EXPLORATION ., CENTRAL GAS FACILITY ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Operator Field(s) Month/Year of Disposition BP EXPLORATION, ALASKA EASTERN OPERATING AREA-PBU 01/2004 Facility Disposition Volume MCF* *Indicate contribution of each pool to total. 1. Sold 2,782,435 Pool Name Code Percent 2. Reinjected 11,060,787 PRUDHOE 640150 100.00% 3. Flared or vented less than 1 hour. 1 ,449 4. Flared or vented greater than 1 hour (Supplemental report required - See 20 AAC 25.235) 2,810 5. Pilot and Purge 25,545 6. Used for lease operations Fuel Assist 3,445,893 41 ,737 7. Other Lift Gas, Off Field MI to GPMA o 2,267,374 TOTAL items 1 - 7 19,628,030 1. Safety ~ ß\ D MCF <{¡sf?- 8. NGL gas equivalent produced 2,782,435 2. Lease Use MCF 9. Purchased gas o 3. Conserv. Purposes MCF 11. Transferred to: FS1, FS2, FS3 1,747,526 10. Transferred from: CCP 21,375,556 Remarks: Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. Signature: Form 10-422 (Revised 4/95) Title: SUPERVISOR BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT January 2004 Page 1 Unplanned Events less than or equal to 1 hour 1/7/2004 1/24/2004 1600-1700 1122-1212 1,161 Not required for unplanned events which 98 are less than or equal to 1 hour Not required for unplanned events which are less than or equal to 1 hour TOTAL 1,259 Unplanned Events greater than 1 hour See attachments See attachments TOTAL o Iplanned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT 6< CAUSE 1/7/2004 1507 -1537 190 See attachments ACTION TAKEN TO ELlMINATI!: CAUSE See attachments TOTAL 190 1/7/2004 0557-0811 2,810 See attachments See attachments TOTAL 2,810 Unplanned Events < 1 Hour Unplanned Events> 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME 1,259 o 190 2,810 71,541 2/6/2004 10:42 AM REPORT NO: 04-0008 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 07 Jan 2004 SYSTEM 1. Flare/Relief Valve 2. Flare/Relief Valve 3. Flare/Relief Valve TIME OF FLARING Black Start Stop Duration Intermittent Smoke Planned VOLUME 05:57 08:11 2Hrs 14 Mins 0 0 ~ 2,810 MSCF 15:07 15:37 OHrs 30Mins 0 0 ~ 190 MSCF 16:00 17:00 1 Hrs OMins ~ 0 0 1;161 MSCF TOTALVOLUJI/IE 4,161 ~MSCF First Determination of Cause: 1. Shutdown MI#2 for maintenance MTR#660 2. Shut down tandem #4 for maintenance. MTR#618 3. Had to BESD MI#2 3 times to straighten out logic. Volume indicated by meter#618 Action Taken to Stop Flaring: 1. Adjusted plant operations. 2. Completed blowdown of tanden compressor. 3. Blowdown completed. Tuesday, January 20,2004 Page 1 of 1 1l7/04 CGF Flaring Event To: Steve McMains, AOGCC steve mcmains@admin.state.ak.us 907-793-1241, fax 907-276-7542 From: Hal Tucker, GPB Prod Optim Team Leader, 907-659-4472 or 907-659-5566 Two flaring events (in excess of one hour) occurred at CGF on January 7, 2004. The first event occurred when MI compressor 1855 was shut down to repair an integrity concern. When the MI compressors are shut down MI is backed out of the system gradually to allow the plant to adjust to changing process temperatures and levels, thus avoiding a more severe plant upset. Total duration and volume for this event were 2 hours and 14 minutes and 2,180 MSCF. / The second event was during restart of the same machine. Logic problems caused 1855 to require four restart attempts. Three times the machine had to be shutdown and blown down before logic was fixed and a successful restart was achieved. Total duration and volume for this event were 1 hour and 1,161 MSCF. Please call or email if you need additional clarification. Thank you, Hal Tucker Greater Prudhoe Bay production Optimization Team Leader "'I of 1 1/12/20047:26 AM Facility ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Operator Field(s) Month/Year of Disposition BP EXPLORATION, ALASKA EASTERN OPERATING AREA-PBU 02/2004 CENTRAL GAS FACILITY Disposition Volume MCF* 1. Sold 2,721,478 2. Reinjected 10,276,505 3. Flared or vented less than 1 hour. 3,691 4. Flared or vented greater than 1 hour 0 (Supplemental report required - See 20 AAC 25.235) 5. Pilot and Purge 23,924 6. Used for lease operations Fuel 3,329,507 Assist 34,432 7. Other Lift Gas, Off Field 0 MI to GPMA 2,119,266 TOTAL items 1 - 7 18,508,803 8. NGL gas equivalent produced 2,721,478 9. Purchased gas 0 10. Transferred from: CCP 20,165,352 11. Transferred to: FS1, FS2, FS3 1,656,549 Remarks: I hereby ce(j. that t! foregoi1 is true and correct to the best of my knowledge. Signature: .n. .A U·i\. iJ. Title: SUPERVISOR Form 10-422 (Revised 4/95) "Indicate contribution of each pool to total. Pool Name Code Percent PRUDHOE 640150 100.00% 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner Date Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT February 2004 Page 1 ~Unplanned Events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE 2/18/2004 0120-0135 328 Not required for unplanned events which 2/18/2004 0120-0219 3,173 are less than or equal to 1 hour 2/28/2004 2203-2235 190 TOTAL 3,691 ACTION TAKEN TO ELIMINATE CAUSE Not required for unplanned events which are less than or equal to 1 hour ~Unplanned Events greater than 1 hour DATE· TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE See attachments TOTAL o Iplanned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mef DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE See attachments TOTAL o ~Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT 6< CAUSE See attachments TOTAL o Unplanned Events < 1 Hour Unplanned Events> 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist 3,691 o o o TOTAL FLARED VOLUME 62,047 ACTION TAKEN TO ELIMINATE CAUSE See attachments ACTION TAK¡::N TO ELIMINATE CAUSE See attachments ACTION TAKEN TO ELIMINATE CAUSE See attachments 3/5/2004 2:07 PM .. Facility CENTRAL GAS FACILITY Disposition 1. Sold 2. Reinjected 3. Flared or vented less than 1 hour. ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Operator Field(s) Month/Year of Disposition BP EXPLORATION, ALASKA EASTERN OPERATING AREA-PBU 03/2004 Volume MCF* 2,916,192 11,025,940 1,464 4. Flared or vented greater than 1 hour (Supplemental report required - See 20 AAC 25.235) 5. Pilot and Purge 6. Used for lease operations 7. Other TOTAL items 1 - 7 8. NGL gas equivalent produced 9. Purchased gas 10. Transferred from: CCP 11. Transferred to: FS1, FS2, FS3 Remarks: 25,387 25,767 Fuel Assist 3,578,758 46,671 Lift Gas, Off Field MI to GPMA o 2,310,955 19,931,134 2,916,192 o 21,669,978 1,738,844 Signature: Form 10-422 (Revised 4/95) is true and correct to the best of my knowledge. Title: SUPERVISOR "Indicate contribution of each pool to total. Pool Name Code Percent PRUDHOE 640150 100.00% 1. Safety z~ 387 MCF 3ß.e../ 2. Lease Use MCF MCF Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT March 2004 3/20/2004 3/20/2004 3/20/2004 3/20/2004 0631-0711 0845-0902 0850-0910 0855-0907 0858-0911 TOTAL 300 Not required for unplanned events which 195 are less than or equal to 1 hour 195 387 387 1,464 Page 1 Not required for unplanned events which are less than or equal to 1 hour lunplanned Events ~reater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE 3/18/2004 2138-2359 1,500 See attachments 3/20/2004 0855-1240 23,887 TOTAL 25,387 ACTION TAKEN TO ELIMINATE CAUSE See attachments Iplanned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE See attachments TOTAL o Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf See attachments TOTAL Unplanned Events < 1 Hour Unplanned Events> 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME o 25,387 o o 99,289 ACTION TAKEN TO ELIMINATE CAUSE See attachments See attachments 4/8/2004 3:09 PM REPORT NO: 04-0083 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 18 Mar 2004 TIME OF FLARING Black SYSTEM Start Stop Duration Intermittent Smoke Planned VOLUME 1. Flare/Relief Valve 21 :3.8.. 23:59 2.Hrs 21 Mins ~ 0 D. J~50D..MSCF TOTAL VOLUME 1,500 MSCF First Determination of Cause: 1. 57 P72BSV Relief valve lifting early. Action Taken to Stop Flaring: 1. Blocked in for maintance. Tuesday, March 30, 2004 Page 1 of 1 REPORT NO: 04-0094 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 20 Mar 2004 TIME OF FLARING Black SYSTEM Start Stop Duration Intermittent Smoke Planned VOLUME 1. FlarelRelief Valve 08:45 09:02 OHrs 17 Mins 0 0 0 t95,MSCF 2. Flare/Relief Valve 08:50 09:10 OHrs 20 Mins D 0 0 195 MSCF 3. Flare/Relief Valve 08:55 09:07 OHrs . 12Mins 0 0 0 387 MSGF 4. FlarelRelief Valve .08:55... 12:40 3Hrs 45Mins ~ 0 0 23,88.7 MSCF 5. Flare/Relief Valve 08:58 09:11 OHrs 13Mins 0 0 D 387 MSCF TOTAL VOLUME 25,051 MSCF First Determination of Cause: 1. TIC 1801 SO ONLOW'GG·{) L'PRE~SURE 2. TIC 1802 SO ON LOSS OF N2 SPEED SIGNAL 3. T/C 1805 RECYCLE TRIPPED DUE TO PROCESS UPSET 4. PROCESS UPSET DUE TO LOSS OF TIC 1805 & T/C 1855 5. T/C 1855 RECYCLE TRIPPED DUE TO PROCESS UPSET Action Taken to Stop Flaring: 1. TIC 1801 BLEWDOWN AND WAS STARTED 2. TIC 1802 BLEW DOWN AND WAS STARTED 3. TIC 1805 COMPLETED BLOWDOWN 4. STARTED TIC 1805 & TIC 1855 + WARMED UP CHILLERS AND L TS TEMPS 5. TIC 1855 BLEW DOWN Tuesday, March 30, 2004 Page 1 of 1 ... Facility ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Operator Field(s) Month/Year of Disposition BP EXPLORATION, ALASKA EASTERN OPERATING AREA-PBU 04/2004 CENTRAL GAS FACILITY Disposition Volume MCF* 1. Sold 2,740,803 2. Reinjected 10,058,439 3. Flared or vented less than 1 hour. 3,182 4. Flared or vented greater than 1 hour (Supplemental report required - See 20 AAC 25.235) 18,080 5. Pilot and Purge 24,875 6. Used for lease operations Fuel Assist 3,346,743 56,696 7. Other Lift Gas, Off Field MI to GPMA o 2,148,602 TOTAL items 1 - 7 18,397,420 8. NGL gas equivalent produced 2,740,803 9. Purchased gas 10. Transferred from: CCP 20,036,123 11. Transferred to: FS1, FS2, FS3 1,638,703 Remarks: I hereby certify that the fore oing is true and correct to the best of my knowledge. " ~ - '2.. 'l -0 V Title: WrCFfli 150P! v--c-t, *Indicate contribution of each pool to total. Pool Name Code Percent PRUDHOE 640150 100.00% 1. Safety \'6 I (Jò 0 MCF crBl- 2. Lease Use MCF o Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT April 2004 Page 1 lunplanned Events less than or equal to 1 hour ..... .. DAT!;. ......... .'1'IME .. . . VOLUME . .·DESCRtPTION O¡:tNCIDENT~ CAUSE ... 4/14/2004 1635-1728 133 Not required for unplanned events which 4/27/2004 0910-0925 328 are less than or equal to 1 hour 4/27/2004 1431-1443 0 4/27/2004 1834-1910 14 TOTAL 475 lunplanned Events greater than 1 hour . DATE> TIME .. . VOLUMEDESCfllPTIONOFINCIDENT 6< CAUSE· 4/27/2004 0910-1046 14,139 See attachments 4/27/2004 1414-1520 3,554 4/27/2004 1414-1620 387 TOTAL 18,080 . .... ACT!9NTAKEN TO i:.LIMINATE CAUSE· Not required for unplanned events which are less than or equal to 1 hour ACTION TAKEN TO ELIMINATE CAUSE See attachments ACTION TAKEN TO ELlMINATEÇAUSE See attachments I 1.~I~n~e~..~~:~t~..L:ss.,.~~n~~~~ual..1. ~~~r~ND .~otE~ce.eding.50?? .~Cf ..··..··>DA:Tta...···· . . ·fJ'IMS··'········ ··.....VO!4U.M§ ·.......>~§SçR!E'mIOI\l>9!7).JN.ÇID§I\I;J:f~fÇA:!;!·S§ 4/9/2004 0035-0111 400 See attachments 4/9/2004 1305-1314 30 4/9/2004 1447-1451 30 4/10/2004 0020-0056 400 4/11/2004 0027-0059 430 4/11/2004 0338-0343 20 4/11/2004 0354-0400 1 0 4/11/2004 1716-1722 30 4/11/2004 1906-1956 30 4/12/2004 0033-0113 400 4/12/2004 0805-0816 30 4/26/2004 0332-0400 510 4/26/2004 0337-0352 387 TOTAL 2,707 RECEIVE MAY 2 7 2004 Alaska Oil & Gas Cons. Anchorage 5/27/2004 9:17 AM BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT April 2004 Page 2 ~Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf <QAT~··· ..... . TIME . . VOLUME ·DESCRIPTIONOFINCIDENT&CAUSt:..···. See attachments TOTAL Unplanned Events < 1 Hour Unplanned Events> 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME 475 18,080 2,707 102,833 o o . . ACTION TAKEN TO ELlMINA TECAUSE See attachments 5/27/2004 9:17 AM REPORT NO: 04-01 06 BPXA FLARE REPORT PRUDHOE SAY FACILITY: CGF DATE: 09 Apr 2004 SYSTEM 1. Flare/Relief Valve 2. FlarelRelief Valve 3. Flare/Relief Valve TIME OF FLARING Black Start Stop Duration Intermittent Smoke 00:35 01 :11 OHrs 36Mins D 0 13:05 13:14 OHrs 9Mins D 0 14:47 14:51 OHrs '4Mins D 0 Planned .. VOLUME ~ ~ ~ TOTAL VOLUME ,400-MSCF 30 MSCF ·'JO'MSCf 460 MSCF First Determination of Cause: 1. Type "B" SID on Tandem #1 forwaterwash. MTR# 618 2. Type "B" to a Type "C" on Tandem #.1 forwaterwash MTR# 618 3. PressÜred Up unit"tò80 PSIGfor rest,ai1;,logic problen'ls,;Slewdöwr'ì again with a tYpe "C"tö"O" pressure. MTR# 618 Action Taken to Stop Flaring: 1. Depressure completed 2. Depressure to "0" completed 3. Depressure completed Sunday, April 25, 2004 Page 1 of 1 REPORT NO: 04-0107 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 10 Apr 2004 TIME OF FLARING Black SYSTEM Start Stop Duration Intermittent Smoke Planned VOLUME 1. Flare/Relief Valve, 00:20 00:56 0 Hrs 36 Mins 0 0 ~400;MSGF TOT AL VOLUME 400 MSCF First Determination of Cause: 1. SID Tandem #4 for waterwash"MTR#618"Type "B" Action Taken to Stop Flaring: 1. Depressure completed Sunday, April 25, 2004 Page 1 of 1 FACILITY: CGF SYSTEM 1. Flare/Relief Valve 2. Flare/Relief Valve 3. Flare/Relief Valve 4. Flare/Relief Valve 5. Flare/Relief Valve REPORT NO: 04-0112 BPXA FLARE REPORT PRUDHOE BAY DATE: 11 Apr 2004 TIME OF FLARING Black Start Stop Durätion Intermittent Smoke Planned V01.UME 00:27 00:59 O,Hrs 32.Mins 0 0 ~ 430 MSGF 03:38 03:43 OHrs 5Mins 0 0 ~ 20 MSCF "03:54 . ·····04:00 "OHrs .' ''6'Mîns 0 0 ~ '10'MSCF 17:16 17:22 OHrs 6Mins 0 0 ~ 30 MSCF 19:06 19:56 o Hrs 50 Mins 0 0 ~ 30 MSCF TOTAL VOLUME 520 MSCF First Determination of Cause: 1. Tandem#3 Waterwash"Type "G" BESD" MTR#61B 2. Tandem #3 Waterwash MTR#618 3. Tandem #3 Waterwash MTR#618 4. Tandem#3 Waterwash MTR#618 5. 6-lntermittent, 3 min. burps, with 90 PSIG"MTR#618"Tandem #3 Waterwash job. PLC Logic problems. Action Taken to Stop Flaring: 1. Oepressure to "0" completed 2. Oepressure suffice 3. Oepressure Complete 4. Depressure complete 5. PLC Logic straightened out and waterwash started. Sunday, April 25, 2004 Page 1 of 1 FACILITY: CGF SYSTEM 1. Flare/Relief Valve 2. Flare/Relief Valve BPXA FLARE REPORT PRUDHOE BAY DATE: 12 Apr 2004 TIME OF FLARING Black Start Stop Duration Intermittent Smoke 00:33 01 :13 0 Hrs 40 Mins 0 0 08:05 08:16 0 Hrs 11 Mins 0 0 REPORT NO: 04-011 3 Planned VOLUME' ~ ,400, MSCF ~ 30 MSCF TOTAL VOLUME 430 MSCF First Determination of Cause: 1. Tandem #2 Waterwash"Type "S" S/D",MTR#618 2. Tandem #2 Waterwash"Type "C"" 80 psi to "0""MTR#618 Action Taken to Stop Flaring: 1. Depressure complete 2. Depressure'COmpiete Sunday, April 25, 2004 Page 1 of 1 bp REPORT NO: 04-0141 BPXA FLARE REPORT PRUDHOE SAY FACILITY: CGF DATE: 26 Apr 2004 TIME OF FLARING Black SYSTEM Start Stop Durâtìon Intermittent Smoke Planned VOLUME 1. Flare/Relief Valve 03:32 04:00 OHÅ’ 28Mins D 0 ~ ..5.l0..MSCF 2. FlarelRelief Valve 03:37 03:52 0 Hrs 15 Mins 0 D ~ 387 MSCF TOTAL VOLUME "897 'MSCF First Determination of Cause: 1. SID MI T/C 1805 TO PERF{:)RM MAINTENANCE AG.TIVJTIES-REPAIR HYD PUMP,WAJ-ER WASH, PSV PMoS-FLARE METER #660 2. INITIATED BESD OF MI TIC 1805 IN ORDER TO FULLY DEPRESSURE UNIT, IN'PREPARATION FOR MAINTENANCE ACTIVITIES. METER #618 Action Taken to Stop Flaring: 1. ADJUSTED, (WARMED UP) REFRIGERATION AND LOW TEMPERATURE SEPARATION PROCESS AREAS 2. UNIT FULLY DEPRESSURED AND ISOLATED Monday, May 03, 2004 Page 1 of 1 REPORT NO: 04-0144 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 27 Apr 2004 TIME OF FLARING Start Stop Dura . 1. Flare/Relief Valve . 09: 10 10:46 2. Flare/Relief Valve 3. Flare/Relief Valve 4. Flare/Relief Valve 5. Other 6. Flare/Relief Valve 09:10 09:25 OHrs 15 Mins 'P4:14- '1'5':20 .' "1 "Hrs' "ô'Mins 14:14 16:20 2Hrs 6Mins 14:31 14:43 OHrs 12 Mins 18:34 19:10 OHrs 36 Mins ~ Black Intermittent Smoke Planned 'VOLUME 0 0 0 j 4, t39 . MSCF 0 0 0 328 MSCF 0 0 0 '3;554' MSCF ~ 0 0 387 MSCF 0 ~ 0 o MSCF 0 0 0 14 MSCF TOTAL VOLUME 18,422 .MSCF First Determination of Cause: 1. T IC-1855 sId, resulting in Stab Overhead vent to flare Mtr. #660 2. T/C-1855 sId - High EGT (Plant upset- Transformer problem) Mtr.-#618 3. T/C-1805 s/d- Stabilizer Overhead vent to flare. Mtr. #660 4. T IC-1805 s/d- depressure to flare- (process gas leak on unit) Mtr. #618 5. HP Flare Blowcase controller L5-IC malfunctioned and opened the blowcase drain valve·totheBurn Pit Disposal system. Mtr.#619 (Liquids)- Volume calc as 18 gallons (.42bbls) 6. Excessive MI discharge header pressure. TIC - 1855 having trouble getiing into the header. Mtr. #660 Action Taken to Stop Flaring: 1. Restarted T IC-1855. 2. Unit depressured Monday, May 03,2004 Page 1 of 2 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 27 Apr 2004 ~ XRestarted T/C-1805 ~ % Unit depressured to zero. ~ %,Took manual control of L5-IC to close the drain valve. b /1': WOA opened up MI wells to drop pressure. Monday, May 03, 2004 '. REPORT NO: 04-0144 Page 2 of 2 FW: GPB Flaring Incident To: Steve McMains, AOGCC steve mcmains@admin.state.ak.us 907-793-1241, fax 907-276-7542 From: Hal Tucker, GPB Prod Optim Team Leader, 907-659-4472 Two extended flare events occurred on April 27, 2004 at CGF. the first event was due to a transformer failure which shut down turbine compressor (TiC) 1855 at 09:10 resulting in the stabilizer overhead venting to flare. Total duration was 1 hour and 36 minutes, total volume was 14,139 MSCF. The second event was a process gas leak on Tic 1805 at 14:14 resulting in the stabilizer overhead venting to flare. Total duration was 1 hour and 6 minutes, total volume was 3,554 MSCF. During the same period of time, Tic 1805 was depressured to 0 (via the flare). Depressuring began at 14:14 with a total duration of 2 hours and 6 minutes of intermittent flaring and a total volume of 387 MSCF. If you require additional information, please do not hesitate to call me. Hal Tucker GPB Production Optimization TL 659-4472 I 'of 1 5/3/2004 11 :31 AM ... CENTRAL GAS FACILITY ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Operator Field(s) Month/Year of Disposition BP EXPLORATION, ALASKA EASTERN OPERATING AREA-PBU 04/2004 Facility Disposition Volume MCF* "Indicate contribution of each pool to total. 1. Sold 2,740,803 Pool Name Code Percent 2. Reinjected 10,058,439 PRUDHOE 640150 100.00% ,/ 3. Flared or vented less than 1 hour. 17,321 4. Flared or vented greater than 1 hour (Supplemental report required - See 20 AAC 25.235) 3,941 5. Pilot and Purge 24,875 6. Used for lease operations Fuel Assist 7. Other Lift Gas, Off Field MI to GPMA o 2,148,602 TOTAL items 1 - 7 18,397,420 1. Safety MCF 8. NGL gas equivalent produced 2,740,803 2. Lease Use MCF 9. Purchased gas o 3. Conserv. Purposes MCF 20,036,123 Commissioner Date 1,638,703 Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. Signature: Form 10-422 (Revised 4/95) Title: SUPERVISOR BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT April 2004 Page 1 lunplanned Events less than or equal to 1 hour ······················P:~me'WF'?"··'··'fWffiffim!M.erWF"'········"'··?"ft&':~ gº¡MeFF':FF¡P:e§.'ª~!~m!~!';fW¡~!i¥W!ff:!,'ª!1!l§!';fmg~ffi,ª~º,ª§i:""""""'" 4/14/2004 1635-1728 133 Not required for unplanned events which 4/27/2004 0910-1046 14,139 are less than or equal to 1 hour 4/27/2004 0910-0925 328 4/27/2004 1431-1443 0 4/27/2004 1834-1910 14 . ""A,ª~m)f\lT~I<ENJOE,LIM'N~re'CM$E .'. Not required for unplanned events which are less than or equal to 1 hour I TOTAL 14,614 lunplanned Events greater than 1 hour . . t i:;';'FW!¡).~'J!§Hw"············;.;.;.q¡Hm!I\1!§;"'··········"?''?""";&,:~ gº·l\1!effi¡¡;ffil:;i!1?e$,ªf1flg'J!f.~JjIH~ffiffi!N,ªI!¡).eNi:¡~¡,ª~º§eFn """""'''''''iT¡WH~~T!~!SIH'J!~l<eN!rQHe g'I\1!Ifi ~m§ffi,ª~º$e:'''''' 4/27/2004 1414-1520 3,554 See attachments See attachments 4/27/2004 1414-1620 387 TOTAL 3,941 ~Planned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mef ';;,;,;·;.!¡)~m§nrrnrrFrrrrn:;¡¡¡¡¡¡@!!l\1!e;HW.rrnYF;·F'FY';'&,:Q gºM§¡¡;rr'';R!1?§§~f1f!~'J!I~:ti!:¡Q§W!!SI.,ª!!¡)eti!m;~·;,ª~,ª§§iFF;'F'" . ··F'F·FH~~rl~ti!¡m~l<eNrrmQ¡¡e gIMIfi ~m§W,ª~º§.e·· 4/9/2004 0035-0111 400 See attachments See attachments 4/9/2004 1305-1314 30 4/9/2004 1447-1451 30 4/10/2004 0020-0056 400 4/11/2004 0027-0059 430 4/11/2004 0338-0343 20 4/11/2004 0354-0400 10 4/11/2004 1716-1722 30 4/11/2004 1906-1956 30 4/12/2004 0033-0113 400 4/12/2004 0805-0816 30 4/26/2004 0332-0400 510 4/26/2004 0337-0352 387 TOTAL 2,707 5/11/2004 1 :28 PM BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT April 2004 Page 2 Planned Events Exceeding 1 Hour OR Exceedin 5000 Mcf TOTAL o Unplanned Events < 1 Hour Unplanned Events> 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist 14,614 3,941 2,707 o TOTAL FLARED VOLUME 102,833 5/11/2004 1:28 PM STATE OF ALASKA ALASKA Oil AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 0290000008 2. Facility Name PBU CCF B Disposition 3. Field PBU - EOA Volume MCF 4. Operator 5. MonthlYear of Disposition BP Ma -2004 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold 2,689,442 Pool Name Pool Code 640150 Percent 100.00% 7. Reinjected 9,768,246 PRUDHOE 8. Flared or vented 1 hour or less 430 9. Flared or vented more than 1 hour (see instr.) o 10. Pilot and Purge 25,600 11. Used for lease operations (specify in Remarks) 3,372,368 12. Other (see instructions) o Authorization> 1 hr: Safety MCF 13. TOTAL VOLUME (ITEMS 6-12) 15,856,086 \ Lease Use MCF 14. NGL Gas Equivalent 2,689,442 ' Conservation MCF 15. Purchased gas o Waste: MCF 16. Transferred from: CCP 19,558,997 17. Transferred to: (Express as a negative #) FS1, FS2, FS3 -1,620,591 Commissioner Date 18. Remarks: Block 11: Fuel Gas = 3,322,975 mscf and Assist Gas = 49,393 mscf I h,rnby ,,,,. fu" fu, ""'.'0''' tho "'" 01 my ,,,,,,,,dgo Signature Q (1, JJ.. Title Date Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 600 F. Authorit 20 AAC25.235. Printed Name Robert A. Re nolds Phone (907)564-5028 Form 10-422 Rev. 1/2004 Submit in Duplicate ...... ' BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT May 2004 Page 1 lunplanned Events less than or equal to 1 hour .... ..DATi: .... ..... 'TlI\iIE; ....... '>VOLUMEDE~RIPTIOJ\¡OFINCJQi:NT&CAI)SE . . 5/17/2004 1411-1421 430 Not required for unplanned events which are less than or equal to 1 hour . . . ACTION TAKEN TO ELII\iIINATECAI)~E . Not required for unplanned events which are less than or equal to 1 hour TOTAL 430 lunplanned Events greater than 1 hour D~TE ,.... . . ··TlI\iIE '. VOLUI\iIE; , '. ..DE~CfUPTION()F INCIDENT & C~I)SE See attachments '. ACTI()N TAKEN TO ELIMINA T¡:CAUSE . . See attachments TOTAL o Iplanned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mcf · DATE < . . . . . TIME . 'VOLUMEDESCRI'f'TION OF INCIDENT & CAUSE .,. . .... . ...... ACTION TAKEN TO ELIMINATE CAUSE . See attachments See attachments TOTAL o See attachments See attachments TOTAL o Unplanned Events < 1 Hour Unplanned Events> 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist o o o TOTAL FLARED VOLUME 75,423 6/4/2004 10:07 AM .. STATE OF ALASKA ALASKA Oil AND GAS CONSERVATION COMMISSION FACiliTY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 0290000008 2. Facility Name PBU CCF B Disposition 3. Field PBU - EOA Volume MCF 4. Operator 5. MonthlYear of Disposition BP June-2004 20. For production from multiple pools. list contribution of each pool as a percent of Total Volume. 6. Sold 2,247,479 7. Reinjected 7,673,121 Pool Name PRUDHOE Pool Code 640150 Percent 100.00% 8. Flared or vented 1 hour or less 15,948 9. Flared or vented more than 1 hour (see instr.) 15,517 10. Pilot and Purge 24,743 11. Used for lease operations (specify in Remarks) 2,877,999 12. Other (see instructions) o S8P- 13. TOTAL VOLUME (ITEMS 6-12) 12,854,807 Lease Use 14. NGL Gas Equivalent 2,247,479 15. Purchased gas o Waste: MCF 16. Transferred from: CCP 16,065,847 17. Transferred to: (Express as a negative #) FS1, FS2, FS3 -1 ,488,587 18. Remarks: Block 11: Fuel Gas = 2,826,420 mscf and Assist Gas = 51,579 mscf I hereby certify that the foregoin Signature Q . 0 . Title Date Note: All volumes must be corrected to pressure of 14.65 pSia and to a temperature of 600 F. Authorit 20 AAC25.235. Printed Name Robert A. Re nolds Phone (907}564-5028 Form 10-422 Rev. 1/2004 Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT June 2004 1.~·¡~·r~:~~:~··:~:~~~':::'~~~~~~V~1~~¡~~ ~·~;~~~!ffl1Iº~'º~§I~çl~$.~;r·~'~ \º$g¡¡.·,""""'" ······¡ \ç¡ JIºJ\I';r~$I\I]º·g""M!N \¡ J$Ç \º~$···· 6/9/2004 2054-2124 10 Not required for unplanned events which Not required for unplanned events which 6/11/2004 0547-0614 328 are less than or equal to 1 hour are less than or equal to 1 hour 6/17/2004 1415-1424 328 6/17/2004 1600-1615 387 6/17/2004 1601-1630 4,109 6/17/2004 1845-1930 9,496 6/17/2004 1845-1900 387 6/21/2004 0417-0422 3 6/21/2004 0441-0445 3 TOTAL 15,051 Page 1 lunplanned Events greater than 1 hour 'º~Tr;,·'·'···TIM!õ:'·'·············¡¡'····¥QI.lºM!õ:····· ·····QJ;:$~alf!t'QI\tQF·II\IºIQ¡;J\lT·~~~Q$¡;;··· 6/11/2004 0547-0808 5,840 See attachments 6/17/2004 1355-1600 570 6/18/2004 1636-1750 8,677 ........... .1 .. ..... ..... ACTION TAKEN. TO ELlMINAt¡;CAUSE' .... See attachments TOTAL 15,087 ~Planned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Met ·PA]g··············]!MIæ'.···················.¥Q!ltJM.IË.······gIËSÇRII:!¡ JIQti .QFI(\/CIPIËti ¡ J&.CAUSIË . . . . .. .. .··.ACTIQti TA~EN¡ JQIËIlIN1INATECAIJSE 6/5/2004 0154-0204 510 See attachments See attachments 6/9/2004 0108-0122 387 TOTAL 897 ~Planned Events Exceeding 1 Hour OR Exceeding 5000 Met ¡'.' ,DATg ¡. ...... ... II""E ", .......> ¥qI,.UME .··..J;)ESCI¡UpTlON()FINCIDENT~CA1JSr;:. ...... ...... ¡.·A:ÇTIO~TA~ENTOEUMINATECAUSE .' . 6/9/2004 0224-0358 430 See attachments See attachments TOTAL Unplanned Events <: 1 Hour Unplanned Events> 1 Hour Planned Events <: 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME 430 15,051 15,087 897 430 107,787 7/8/2004 10:00 AM REPORT NO: 04-0208 SPXA FLARE REPORT PRUDHOE SAY FACILITY: CGF DATE: 05 Jun 2004 TIME OF FLARING Black SYSTEM Start Stop Duration Intermittent Smoke Planned VOLUME 1. Flare/Relief Valve 01 :54 02:04 0 Hrs 10 Mins 0 0 ~ 510 MSCF TOTAL VOLUME 510 MSCF First Determination of Cause: 1. TIC 1801 & TIC 1802: SESD & BESD. Booster 1 & 2 Shutdown for maint. Action Taken to Stop Flaring: 1. Blowdown complete. Friday, June 18, 2004 Page 1 of 1 REPORT NO: 04-0215 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 09 Jun 2004 SYSTEM 1. Controlled Blowdow 2. Controlled Blowdow 3. FlarelRelief Valve TIME OF FLARING Black Start Stop Duration Intermittent Smoke Planned VOLUME 01:08 01:22 o Hrs 14 Mins 0 0 ~ 387 MSCF 02:24 03:58 1 Hrs 34 Mins ~ 0 ~ 430 MSCF 20:54 21:24 OHrs 30 Mins 0 ~ 0 10 MSCF TOTAL VOLUME 827 MSCF First Determination of Cause: 1. MI # 2 TIC 1855 SID For Maint. Compressor BESD on shutdown. Meter 618 2. Part of L TS #2 depressured for maint on flare valves. Meter 618 3. 51 P5001 SV NGL Recycle Pump 1504 Discharge. Relived to BPD Due to possible incorrect setting on PSV, Approximately Ten barrels of NGL Liquids. Meter 619 Action Taken to Stop Flaring: 1, Depressure Complete. 2. Depressure completed. 3. 100% Assist Gas was open at the first sign of smoke. PSV was removed from service. Friday, June 18, 2004 Page 1 of 1 REPORT NO: 04-0218 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 11 Jun 2004 SYSTEM 1. Flare/Relief Valve 2. Flare/Relief Valve TIME OF FLARING Black Start Stop Duration Intermittent Smoke Planned VOLUME 05:47 06:14 OHrs 27 Mins 0 0 0 328 MSCF 05:47 08:08 2Hrs 21 Mins 0 0 0 5,840 MSCF TOTAL VOLUME 6,168 MSCF First Determination of Cause: 1. shutdown 1855 due to a hydraulic line failure. (MTR 618) 2. MI1855 was shutdown due to a hydraulic line failure. Action Taken to Stop Flaring: 1. Completed Depressure. 2. Plant process was adjusted to compinsate for the loss of 1855 compressor. ( MTR 660) Friday, June 18, 2004 Page 1 of 1 REPORT NO: 04-0225 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 17 Jun 2004 TIME OF FLARING Black SYSTEM Start Stop Duration Intermittent Smoke Planned VOLUME 1. Flare/Relief Valve 13:55 16:00 2Hrs 5Mins 0 0 0 570 MSCF 2. FlarelRelief Valve 14:15 14:24 OHrs 9Mins 0 0 0 328 MSCF 3. Controlled Blowdow 16:00 16:15 OHrs 15 Mins 0 0 0 387 MSCF 4. Flare/Relief Valve 16:01 16:30 OHrs 29 Mins 0 0 0 4,109 MSCF 5. FlarelRelief Valve 18:45 19:30 OHrs 45 Mins 0 0 0 9,496 MSCF 6. Controlled Blowdow 18:45 19:00 OHrs 15 Mins 0 0 0 387 MSCF TOTAL VOLUME 15,277 MSCF First Determination of Cause: 1. 1884 Turbine SD due 3 times due to to underspeed caused by high ambient temperature. Flared total of 15 minutes as it depressured each time 2. 1855 MI Compressor SD while trying to take it to idle, due to high ambient conditions. 3. T/C-1805 s/d- instrumentation problem Mtr# 618 4. 1854 MI Compressor SO, unknown reason, probably ambient temp related. 5. T/C-1855 s/d- instrumentation problem- resutinging Stabilizer tower overpressure. Mtr.#660 6. T/C-1855 s/d- instrumentation problem- F&G panel troubleshoot resulted in a unit trip Mtr.# 618 Action Taken to Stop Flaring: 1. Restarted Turbine 3 times 2. Let it blowdown, no action taken 3. Unit depressured 4. Restarted 1855 compressor Friday, June 18, 2004 Page 1 of 2 bp REPORT NO: 04-0225 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 17 Jun 2004 ~ ß Took measures to decrease MI make- Opened plant by-passes, heated L TS btms. Ultimately restarted unit. b Á Unit depressured Friday, June 18, 2004 Page 2 of 2 REPORT NO: 04-0233 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 18 Jun 2004 TIME OF FLARING Black SYSTEM Start Stop Duration Intermittent Smoke Planned VOLUME 1. Flare/Relief Valve 16:36 17:50 1 Hrs 14Mins D 0 0 8,677 MSCF TOTAL VOLUME 8,677 MSCF First Determination of Cause: 1. 1805 M 11 SO on a recycle trip while loading the Booster Compressors Action Taken to Stop Flaring: 1. Restarted 1805 compressor Thursday, July 01, 2004 Page 1 of 1 GPB Flaring Incidents To: Steve McMains, AOGCC steve mcmains@admin.state.ak.us 907-793-1241, fax 907-276-7542 From: Hal Tucker, GPB Prod Optim Team Leader, 907-659-4472 Several extended flare events occurred in the past few weeks at GPB. This is a note giving you a courtesy "heads up" on the greater than one hour flare events you will be seeing in the monthly gas disposition reports prepared by the Anchorage Volume Accounting Team. * GC3 experienced three flare events on June 24, 25 and 26 due to K5500 shutting down on high lube oil temperature. Temperature probes, RTD's and switches were changed out during the three days in attempts to eliminate that root cause of the shut downs. K5500 procedures were followed to minimize flaring. Total volume for the three events was 1,261 MSCF, total duration for the three events was 7 hours and 17 minutes. * FS1 experienced one extended flare event beginning at 10:00 June 17 and ending at 02:45 June 18 when the 1801 STV/IP compressor shut down due to high ambients. Several attempts were made to restart and reload the machine. Total flare volume for the event was 8,491 MSCF over 16 hours and 45 minutes. * GC2 experienced two flare events on May 30 and 31 due to PLC malfunction in the produced water section of the plant. The production cuts resulting from the water section upset caused the skid 18, IP and LP compressors to surge intermittently due to the low GC oil rate. The compressors loaded up as GC2 oil rates returned to normal. Total volume for the two events was 920 MSCF, total duration was 5 hours and 31 minutes. * ~experienced two flare events on June 17 and 18. The first event occurred when the 1884 tandem shut down 3 times due to high ambient temperatures over a 2 hour period. Each shut down resulted in 15 minutes of flaring. This event should have been captured as three separate flaring events and should not be considered as a greater than one hour event. The second event occurred when the 1805 MI compressor shut down a recycle trip while loading the boosters. Flaring stopped when 1805 was restarted. Total duration for the 1805 event was 1 hour and 14 minutes, total volume was 8,677 MSCF. * LPC experienced one flare event on June 17 when the 1808 gas reinjection turbine shut down. Flaring stopped when 1808 was restarted. I oaf2 6/28/20047:02 AM GPB Flaring Incidents ~Gas was cut during the event to reduce flare volume. Total duration for the event was 1 hour and 16 minutes, total volume was 5,804 MSCF. * FS3 experienced two flare events on June 17 and June 20. The first event occurred when the 1801 STV/IP compressor shut down due to high ambients and plant upsets. After three failed restart attempts, the spare machine (1802) was started, ending the flare event. Total duration for this event was 1 hour and 10 minutes, total volume was 466 MSCF. The second event occurred when the 1806 gas lift machine shut down due to instrumentation problems. 1806 was secured and depressured, ending the flare event. Total duration of the event was 6 hours of intermittent flaring totaling 685 MSCF. If you require additional information, please do not hesitate to call me. Hal Tucker GPB Production Optimization TL 20,[2 6/28/20047:02 AM STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 0290000008 3. Field PBU - EOA Volume MCF 2,132,463 6,849,175 11,670 26,081 / 25,467 2,744,623 ----Õ/ 11,789,479 2,132,463 I 0 14,838,597 -1,252,178 6. Sold 7. Reinjected 8. Flared or vented 1 hour or less 9. Flared or vented more than 1 hour (see instr.) 10. Pilot and Purge 11. Used for lease operations (specify in Remarks) 12, Other (see instructions) 13. TOTAL VOLUME (ITEMS 6-12) 14. NGL Gas Equivalent 15. Purchased gas 16. Transferred from: CCP 17. Transferred to: (Express as a negative #) FS1, FS2, FS3 18. Remarks: Block 11: Fuel Gas = 2,692,702 mscf and Assist Gas = 51,921 mscf I hereby certify that the foregoin is true and correct to the best of my knowledge. Signature Title 4. Operator 5. Month/Year of Disposition BP Jul -2004 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. Pool Name PRUDHOE Pool Code 640150 Percent 100.00% .5i:L- Printed Name Robert A. Re nolds Phone (907}564-5028 Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 600 F. Authorit 20 AAC25.235. Form 10-422 Rev. 1/2004 Date Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT July 2004 ¡Unplanned Events less than or e9ual to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT" CAUSE 7/9/2004 2232-2248 387 Not required for unplanned events which 7/9/2004 2232-2248 263 are less than or equal to 1 hour 7/9/2004 2254-2312 387 7/9/2004 2254-2354 789 7/11/2004 1224-1253 32 7/11/2004 2145-2205 350 7/13/2004 0007-0022 400 7/19/2004 2010-2020 774 Page 1 TOTAL 3,382 ¡unplanned Events greater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT" CAUSE 7/19/2004 2010-2202 26,081 See attachments TOTAL 26,081 ¡Planned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mct DATE TIME VOLUME DESCRIPTION OF INCIDENT" CAUSE 7/10/2004 0143-0155 430 See attachments 7/10/2004 0315-0335 350 7/10/2004 0425-0440 430 7/10/2004 0553-0605 430 7/10/2004 0830-0930 2,850 7/10/2004 0900-0915 328 7/10/2004 1240-1258 430 7/11/2004 0200-0300 2,850 7/13/2004 1440-1452 190 TOTAL 8,288 ¡Planned Events Exceedin~ 1 Hour OR Exceeding 5000 Mct DATE TIME VOLUME DESCRIPTION OF INCIDENT" CAUSE See attachments TOTAL o Unplanned Events < 1 Hour Unplanned Events> 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME 26,081 8,288 o 115,139 ACTION TAKEN TO ELIMINATE CAUSE Not required for unplanned events which are less than or equal to 1 hour ACTION TAKEN TO ELIMINATE CAUSE See attachments ACTION TAKEN TO ELIMINATE CAUSE See attachments ACTION TAKEN TO ELIMINATE CAUSE See attachments 8/9/2004 9:53 AM REPORT NO: 04-0283 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 10 Jul2004 TIME OF FLARING Black SYSTEM Start Stop Duration Intermittent Smoke Planned VOLUME 1. FlarelRelief Valve 01:43 01:55 OHrs 12 Mins 0 0 ~ 430 MSCF 2. Flare/Relief Valve 03:15 03:35 OHrs 20 Mins 0 0 ~ 350 MSCF 3. Flare/Relief Valve 04:25 04:40 OHrs 15 Mins 0 0 ~ 430 MSCF 4. FlarelRelief Valve 05:53 06:05 o Hrs 12 Mins 0 0 ~ 430 MSCF 5. Flare/Relief Valve 08:30 09:30 1 Hrs OMins 0 0 ~ 2,850 MSCF 6. Flare/Relief Valve 09:00 09:15 o Hrs 15 Mins 0 0 ~ 328 MSCF 7. Flare/Relief Valve 12:40 12:58 OHrs 18 Mins 0 0 ~ 430 MSCF TOTAL VOLUME 5,248 MSCF First Determination of Cause: 1. 1886 tandem was shutdown due to TAPS slowdown. 2. 1857 Booster was shutdown for maintenance during TAPS slowdown. 3. 1884 tandem was shutdown due to TAPS slowdown. 4. 1883 tandem was shutdown due to taps slowdown 5. Tandem station vented for maintenance. 6. 1805 was shutdown for power supply replacement 7. 1885 tandem was shutdown for maintenance during TPAS slowdown. Action Taken to Stop Flaring: 1. TIC completed depresurization. MTR 618 2. TIC completed venting MTR618 3. TIC completed venting MTR618 4. TIC completed venting MTR618 Wednesday, July 28,2004 Page 1 of 2 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 10 Jul 2004 ~ ~Completed venting MTR618 b ,;e:- Unit completed venting to 180psi. MTR618 7 ~T/C completed depressurization. MTR 618 Wednesday, July 28,2004 REPORT NO: 04-0283 Page 2 of 2 REPORT NO: 04-0286 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 11 Jul 2004 TIME OF FLARING SYSTEM Start Stop Duration Intermittent 1. FlarelRelief Valve 02:00 03:00 1 Hrs 0 Mins 0 2. Flare/Relief Valve 12:24 12:53 0 Hrs 29 Mins 0 3. FlarelRelief Valve 21 :45 22:05 0 Hrs 20 Mins 0 Black Smoke Planned VOLUME 0 ~ 2,850 MSCF 0 0 32 MSCF 0 0 350 MSCF TOTAL VOLUME 3,232 MSCF First Determination of Cause: 1. Depressured the Tandem station piping to repair a leak. 2. Vented to reduce high plant feed pressure. Due to CCP TIC problems 3. 1857 tripped during startup. Action Taken to Stop Flaring: 1. completed venting. MTR618 2. Reduced inlet pressure while CCP and the field settled out. MTR664 3. Completed venting MTR618 Wednesday, July 28,2004 Page 1 of 1 REPORT NO: 04-0289 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 13 Jul 2004 SYSTEM 1. Flare/Relief Valve 2. FlarelRelief Valve TIME OF FLARING Black Start Stop Duration Intermittent Smoke Planned VOLUME 00:07 00:22 OHrs 15 Mins 0 0 0 400 MSCF 14:40 14:52 OHrs 12 Mins 0 0 ~ 190 MSCF TOTAL VOLUME 590 MSCF First Determination of Cause: 1. 1883 Tripped due to a loose wire that indicates fuel gas HHH suction drum level. (Type "B" shutdown> 2. 1886 Shutdown for maintenance. (Typa "A" shutdown> Action Taken to Stop Flaring: 1. Completed venting. MTR 618 2. Completed venting. MTR 618 Wednesday, July 28, 2004 Page 1 of 1 bp REPORT NO: 04-0303 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 19 Jul 2004 SYSTEM 1. Flare/Relief Valve 2. Flare/Relief Valve TIME OF FLARING Black Start Stop Duration Intermittent Smoke Planned VOLUME 20:10 20:20 OHrs 10Mins ~ 0 0 774 MSCF 20:10 22:02 1 Hrs 52 Mins ~ 0 D 26,081 MSCF TOTAL VOLUME 26,855 MSCF First Determination of Cause: 1. Both MI machines depressured indicated by meter# 618. 2. Both MI machines tripped while attempting to pressurize the EOA MI header. Meter 660 Action Taken to Stop Flaring: 1. Depressure completed. 2. Warmed Us bottom temps. to minimize flaring and restarted both compressors. Wednesday, July 28,2004 Page 1 of 1 STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 0290000008 2. Facility Name PBU CCF B Disposition 3. Field PBU - EOA Volume MCF 6. Sold 1,817,647 7. Reinjected 7,585,306 8. Flared or vented 1 hour or less 1,754 9. Flared or vented more than 1 hour (see instr.) 21,125 10. Pilot and Purge 25,523 11. Used for lease operations (specify in Remarks) 2,877,268 12. Other (see instructions) 1 ,573,605 13. TOTAL VOLUME (ITEMS 6-12) 13,902,228 14. NGL Gas Equivalent 1,817,647 15. Purchased gas o 16. Transferred from: CCP 15,380,164 17. Transferred to: (Express as a negative #) FS1, FS2, FS3 -1,477,936 18. Remarks: Block 11: Fuel Gas = 2,825,045 mscf and Assist Gas = 52,223 mscf; Block 12: MI Gas to PI. McIntyre = 1,573,605 mscf I hereby certify that the foregoin is true and correct to the best of my knowledge. Signature Title Printed Name Robert A. Re nolds Phone (907)564-5028 Form 10-422 Rev. 1/2004 4. Operator 5. Month/Year of Disposition BP Au ust-2004 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. Pool Name PRUDHOE Pool Code 640150 Percent 100.00% Authorization> 1 hr: Safety MCF (11Z6 j""&z- MCF MCF MCF Date Lease Use Waste: Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 600 F. Authorit 20 AAC25.235. Date Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT· CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT August 2004 Page 1 IUnplanned Events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT 8. CAUSE 8/14/2004 1655-1708 190 Not required for unplanned events which 8/17/2004 1418-1419 21 are less than or equal to 1 hour 8/17/2004 2052-2100 83 8/22/2004 11 30-1140 7 TOTAL 301 lunplanned Events greater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT 8. CAUSE 8/16/2004 1108-1637 21,125 See attachments TOTAL 21,125 ~Planned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mct DATE TIME VOLUME DESCRIPTION OF INCIDENT 8. CAUSE 8/16/2004 0030-0040 420 See attachments 8/16/2004 0430-0435 135 8/16/2004 0010-0016 328 8/16/2004 0350-0358 390 8/16/2004 0740-0752 80 8/16/2004 0912-0918 100 TOTAL 1 ,453 ~Planned Events Exceeding 1 Hour OR Exceeding 5000 Mct DATE TIME VOLUME DESCRIPTION OF INCIDENT 8. CAUSE See attachments TOTAL o Unplanned Events < 1 Hour Unplanned Events> 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist 301 21,125 1,453 o TOTAL FLARED VOLUME 100,625 ACTION TAKEN TO ELIMINATE CAUSE Not required for unplanned events which are less than or equal to 1 hour ACTION TAKEN TO ELIMINATE CAUSE See attachments ACTION TAKEN TO ELIMINATE CAUSE See attachments ACTION TAKEN TO ELIMINATE CAUSE See attachments 9/10/2004 11:21 AM REPORT NO: 04-0353 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 16 Aug 2004 SYSTEM 1. Flare/Relief Valve 2. Flare/Relief Valve TIME OF FLARING Black Start Stop Duration Intermittent Smoke Planned VOLUME 00:30 00:40 o Hrs 10 Mins 0 0 ~ 420 MSCF 04:30 04:35 OHrs 5Mins 0 0 ~ 135 MSCF TOTAL VOLUME 555 MSCF First Determination of Cause: 1. Shutdown TIC 1876 for scheduled maintenance 2. Shutdown T/C 1808 for scheduled maintenance Action Taken to Stop Flaring: 1. Depressured T /C 1876 2. Depressured T/C 1808 VVednesday, August 25, 2004 Page 1 of 1 REPORT NO: 04-0355 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 16 Aug 2004 TIME OF FLARING Black SYSTEM Start Stop Duration Intermittent Smoke Planned VOLUME 1. Flare/Relief Valve 00:10 00:16 OHrs 6Mins 0 0 ~ 328 MSCF 2. FlarelRelief Valve 03:50 03:58 OHrs 8Mins 0 0 ~ 390 MSCF 3. Flare/Relief Valve 07:40 07:52 OHrs 12 Mins 0 0 ~ 80 MSCF 4. Flare/Relief Valve 09:12 09:18 OHrs 6Mins 0 0 ~ 100 MSCF 5. Flare/Relief Valve 11:08 16:37 5Hrs 29 Mins 0 0 0 21,125 MSCF TOTAL VOLUME 22,023 MSCF First Determination of Cause: 1. SO MI1 for maintenance 2. 1801 1802 Booster Comp SO 3. Flaring to get DP for F221 perimeter valve test 4. Flaring to get DP for F301 ,F302 perimeter valve test 5. 1855 MI Comp SO due to process upset Action Taken to Stop Flaring: 1. Allowed compressor to blow down 2. Let compressors blow down 3. Completed test, closed flare valve 4. Completed test, closed flare valve 5. Took corrective action to get stabilizer section stable, started 1805 MI compressor when it became available. VVednesday, August 25, 2004 Page 1 of 1 · STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 0290000008 2. Facility Name PBU CGF B Disposition 3. Field PBU - EOA Volume MCF 4. Operator 5. MonthNear of Disposition BP Se tember-2004 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold 2,182,901 7. Reinjected 9,564,082 Pool Name PRUDHOE Pool Code 640150 Percent 100,00% 8. Flared or vented 1 hour or less 4,090 9. Flared or vented more than 1 hour (see instr.) 27,371 10. Pilot and Purge 24,701 11. Used for lease operations (specify in Remarks) 3,098,741 12. Other (see instructions) o f2- 13. TOTAL VOLUME (ITEMS 6-12) 14,901,886 MCF 14. NGL Gas Equivalent 2,182,901 MCF 15. Purchased gas o 16. Transferred from: CCP 17,594,515 17. Transferred to: (Express as a negative #) FS1, FS2. FS3 and GPMA PI. Mcintyre MI 18. Remarks: Block 11: Fuel Gas = 3,047,845 mscf and Assist Gas = 50,896 mscf; Block 17: Includes MI Gas to PI. McIntyre = 1,233,724 mscf -2,692,629 I hereby certify that the foregoing is true and correct to the best of my knowledge. Signature A ~ h..~ Title Mana er, State Taxes and Ro alt Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 600 F. Authorit 20 AAC25.235. Printed Name Robert A. Re nolds Phone (907)564-5028 Form 10-422 Rev. 1/2004 Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT September 2004 Page 1 IUnplanned Events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE 9/6/2004 1605-1617 400 Not required for unplanned events which 9/11/2004 1100-1110 387 are less than or equal to 1 hour 9/14/2004 1600-1610 774 9/14/2004 1858-1908 387 9/14/2004 1951-2005 387 9/14/2004 2124-2134 387 9/14/2004 2209-2220 387 9/14/2004 2248-2258 328 9/14/2004 2352-2356 100 9/15/2004 0053-0112 328 9/15/2004 1328-1345 144 9/30/2004 1858-1940 15 9/30/2004 1949-2002 7 TOTAL 4,031 ACTION TAKEN TO ELIMINATE CAUSE Not required for unplanned events which are less than or equal to 1 hour lunplanned Events greater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE 9/11/2004 1100-1335 12,256 See attachments 9/14/2004 1600-1912 14,787 TOTAL 27,043 Iplanned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Met DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE 9/30/2004 1031-1051 59 See attachments TOTAL 59 Iplanned Events Exceeding 1 Hour OR Exceeding 5000 Met DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE 9/30/2004 0901-1014 328 See attachments TOTAL 328 Unplanned Events < 1 Hour Unplanned Events> 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist 4,031 27,043 59 328 TOTAL FLARED VOLUME 107.058 ACTION TAKEN TO ELIMINATE CAUSE See attachments ACTION TAKEN TO ELIMINATE CAUSE See attachments ACTION TAKEN TO ELIMINATE CAUSE See attachments 1 0/6/2004 10:54 AM REPORT NO: 04-0423 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 11 Sep 2004 SYSTEM TIME OF FLARING Start Stop Duration Intermittent Black Smoke Planned VOLUME 0 0 -, 1\1SC~ 0 0 387 MSCF 0 0 12,256 MSCF TOTAL VOLUME 12,643 MSCF :. .¡ '--~'':''.a!:-:.' _ oJ ~~ ~<~~; ~~~!ì~. 0 11:00 11 :10 OHrs 10 Mins D 11:00 13:35 2Hrs 35 Mins 0 '.-. Flare/Relief Valve 2. i flare/Relief Valve First Determination of Cause: 1. MI # 1 Shutdown T/C-1805 Valve out of position caused compressor to B.E.S.D: Meter 618 2. MI # 1 Shutdown T/C-1805 Suction Valve out of position caused turbine to shutdown, Turbine control logic prevented turbine from starting. Meter 660 Action Taken to Stop Flaring: 1. B.E.S.D depressue was completed. 2. Repaired F-12 A V suction valve position logic to indicate open and restarted turbine. Monday, September 27, 2004 Page 1 of 1 REPORT NO: 04-0442 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 14 Sep 2004 TIME OF FLARING Black SYSTEM Start Stop Duration Intermittent Smoke Planned VOLUME 1. Flare/Relief Valve 16:00 19:12 3Hra 12.,.Ins ~ 0 0 14,787 MSCF 2. Flare/Relief Valve 16:00 16:10 OHrs 10 Mins ~ 0 0 774 MSCF 3. Flare/Relief Valve 18:58 19:08 OHrs 10 Mins ~ 0 0 387 MSCF 4. Flare/Relief Valve 19:51 20:05 OHrs 14 Mins ~ 0 D 387 MSCF 5. Flare/Relief Valve 21:24 21:34 OHrs 10 Mins ~ 0 0 387 MSCF 6. Flare/Relief Valve 22:09 22:20 OHrs 11 Mins ~ 0 0 387 MSCF 7. Flare/Relief Valve 22:48 22:58 OHrs 10 Mins ~ 0 0 328 MSCF 8. Flare/Relief Valve 23:52 23:56 OHrs 4Mins ~ 0 0 100 MSCF TOT AL VOLUME 17,537 MSCF First Determination of Cause: 1. Stabilizer upset due to power blip. Both MI trains tripped off line. 2. MI trains 1 &2 shutdown due to power blip. Both units depressured to flare. 3. Unsuccesful start attempt to MI compressor train 1855. 4. Unsuccesful start attempt to MI compressor train 1855. 5. Unsuccesful start attempt to MI compressor train 1855. 6. Unsuccesful start attempt to MI compressor train 1855. 7. Unsuccesful start attempt to MI compressor train 1855. 8. Intermittant flaring from stabilizers due to plant upset. Action Taken to Stop Flaring: 1. Volume indicated by meter 660. 2. Blowdowns completed. Estimated volume indicated by meter 618. Monday, September 27, 2004 Page 1 of 2 REPORT NO: 04-0442 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 14 Sep 2004 ~ 'Kí. Blowdown completed. Estimated volume indicated by meter 618. 'I H. Blowdown completed. Estimated volume indicated by meter 618. ;; 1Z. Blowdown completed. Estimated volume indicated by meter 618. 6 1<f Blowdown completed. Estimated volume indicated by meter 618. I )4. Blowdown completed. Estimated volume indicated by meter 618. g 1-5. Restarting MI trains and adjusting L TS trains to minimize flare. Volume indicated by meter 660. Monday, September 27, 2004 Page 2 of 2 REPORT NO: 04-0475 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 30 Sep 2004 TIME OF FLARING Black SYSTEM Start Stop Duration Intermittent Smoke Planned VOLUME 1. Flare/Relief Valve 09:01 10:14 1 Hrs 13Mins 0 0 ~ 328 MSCF 2. Flare/Relief Valve 10:31 10:51 OHrs 20 Mins 0 0 ~ 59 MSCF 3. Flare/Relief Valve 18:58 19:40 OHrs 42 Mins ~ 0 0 15 MSCF 4. Flare/Relief Valve 19:49 20:02 OHrs 13 Mins ~ 0 0 7 MSCF TOTAL VOLUME 409 MSCF First Determination of Cause: 1. Type B Shutdown (328 MM) Depressured for water wash (MTR 618) 2. Type C Shutdown (59MM) Depressured for water wash (Mtr 618) 3. Excessive pressure while loading MI-1. (Mtr 660) 4. Excessive pressure while loading MI-1. (Mtr 660) Action Taken to Stop Flaring: 1. Oepressure completed 2. Depressure completed 3. Closed recycles. 4. Closed recycles. Monday, October 04, 2004 Page 1 of 1 STATE OF ALASKA ALASKA Oil AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 0290000008 2. Facility Name PBU CGF B Disposition 3. Field PBU - EOA Volume MCF 4. Operator 5. Month/Year of Disposition BP October-2004 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold 2,604,823 Pool Name Pool Code 640150 Percent 100.00% 7. Reinjected 11,281,581 PRUDHOE 8. Flared or vented 1 hour or less 1,116 9. Flared or vented more than 1 hour (see instr.) 328 10. Pilot and Purge 25,761 11. Used for lease operations (specify in Remarks) 3,272,378 12. Other (see instructions) o MCF 13. TOTAL VOLUME (ITEMS 6-12) 17,185,987 14. NGL Gas Equivalent 2,604,823 MCF 15. Purchased gas o Waste: 16. Transferred from: FS1, FS2, FS3, GC1, GC2, GC3 242,747,188 17. Transferred to: (Express as a negative #) FS1, FS2, FS3. CCP & GPMA Pt. Mcintyre MI 18. Remarks: Block 11: Fuel Gas = 3,219,992 msef and Assist Gas = 52,386 msef; Block 17: Includes MI Gas to Pt. McIntyre = 1,104,525 msef -225,561,203 I "":,::::: "ït;'rc=" ¡::"" Printed Name Bernard W. Ha'n Phone (907)564-5028 Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 600 F. Authorit 20 AAC25.235. Title Mana er, Production Taxes and Ro alt Form 10-422 Rev. 1/2004 Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT October 2004 Page 1 Unplanned Events less than or equal to 1 hour 10/14/2004 10/14/2004 0900-0915 0930-0945 208 Not required for unplanned events which 387 are less than or equal to 1 hour Not required for unplanned events which are less than or equal to 1 hour TOTAL 595 IUnPlann~dE~~nts greate,rtha~ 1 hour , OA,TE ",."" //, '~TlM,E;',,<, 'VOLtJ,Me.<De~CRIPTJOIIIOF~IIIÇIDeNT"PAU~IiL ' "', """>AÇTlOIIITAKeIllT()eLlMINATe:CAU~E' ",," See attachments See attachments TOTAL o Planned Events Less Than or Equal 1 Hour AND Not Exceedin 10/4/2004 10/15/2004 10/15/2004 1637-1709 0005-0023 1100-1117 59 See attachments 430 32 See attachments TOTAL 521 Iplanned Events Exceeding 1 Hour OR Exceedin~ 5000 Mcf , "DATE ,.."",' ' ""TIME ',' ",'VO ;.UME ,DESC~IPTIQNOFINCJQENT"CAtJSE< . .'. ",,' , " ,", ACTlQIIITAi<:eNT()ElIMINATECAtJSE,,' .'.' ,,' 10/4/2004 0933-1043 328 See attachments See attachments TOTAL 328 Unplanned Events < 1 Hour Unplanned Events> 1 Hour 0 Planned Events < 1 hour and not 521 exceeding 5,000 MCF Planned Events> 1 hour or 328 exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME 79,591 11/9/2004 10:58 AM REPORT NO: 04-0485 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 04 Oct 2004 SYSTEM 1. Flare/Relief Valve 2. Flare/Relief Valve TIME OF FLARING Black Start Stop Duration Intermittent Smoke Planned VOLUME 09:33 10:43 1 Hrs 10 Mins 0 0 ~ 328 MSCF 16:37 17:09 OHrs 32 Mins 0 0 ~ 59 MSCF TOTAL VOLUME 387 MSCF First Determination of Cause: 1. Type B Shutdown (328 MM) Depressured for water wash (MTR 618) 2. Type C Shutdown (59 MM) Depressured for Water Wash (Mtr 618) Action Taken to Stop Flaring: 1. Depressure completed 2. Depressure completed Friday, October 22,2004 Page 1 of 1 bp REPORT NO: 04-0502 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 15 Oct 2004 TIME OF FLARING Black SYSTEM Start Stop Duration Intermittent Smoke Planned VOLUME 1. Flare/Relief Valve 00:05 00:23 0 Hrs 18 Mins 0 0 ~ 430 MSCF TOTAL VOLUME 430 MSCF First Determination of Cause: 1. SO TIC 1884 FOR MAl NT. Action Taken to Stop Flaring: 1. COMPLETED BLOWDOWN OF TIC 1884 Friday, October 22, 2004 Page 1 of 1 REPORT NO: 04-0501 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF DATE: 15 Oct 2004 TIME OF FLARING Black SYSTEM Start Stop Duration Intermittent Smoke Planned VOLUME 1. Flare/ReliefValve 11:00 11:17 OHrs 17Mins 0 0 ~ 32 MSCF TOTAL VOLUME 32 MSCF First Determination of Cause: 1. Flared while CCP put 1878 on LTS3 since our Tandem 2 is down for Major Action Taken to Stop Flaring: 1. CCP completed swap Friday, October 22, 2004 Page 1 of 1 STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 0290000008 2. Facility Name PBU CGF B Disposition 3. Field PBU - EOA Volume MCF 6. Sold 2,731,231 7. Reinjected 11,356,326 8. Flared or vented 1 hour or less 5,669 9. Flared or vented more than 1 hour (see instr.) 15,865 10. Pilot and Purge 25,130 11. Used for lease operations (specify in Remarks) 3,402,857 12. Other (see instructions) o 13. TOTAL VOLUME (ITEMS 6-12) 17,537,078 14. NGL Gas Equivalent 2,731,231 15. Purchased gas o 16. Transferred from: FS1, FS2, FS3, GC1, GC2, GC3 253,211,713 4. Operator 5. MonthlYear of Disposition BP November-2004 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. Pool Name PRUDHOE Pool Code 640150 Percent 100.00% :Jf3!'- MCF MCF MCF /-//,Ø Date -235,674,637 17. Transferred to: (Express as a negative #) FS1, FS2, FS3. CCP & GPMA PI. Mcintyre MI 18. Remarks: Block 11: Fuel Gas = 3,356,866 roscf and Assist Gas = 45,991 roscf; Block 17: Includes MI Gas to Pt. Mcintyre = 1,012,083 roscf Signature Phone (907)564-5028 Title Mana er, Production Taxes and Ro alt Date I J -/ -:-.¿¡I./ Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 600 F. Authorit 20 AAC25.235. I hereby certify that the foregoing is true and c e best of my knowledge. Printed Name Form 10-422 Rev. 1/2004 Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT November 2004 Page 1 IUnplanned Events less than or equal to 1 hour .. . . · . DATE· . . . . . . TIME . . · · .. .... VOLUME . · DESCRIPTION OF INCIDENT &. CAU~E . . . . . . . . . . . . ACTION TAKEN TO ELIMINATE CAUSE. . . 11/3/2004 0355-0410 390 Not required for unplanned events which Not required for unplanned events which 11/3/2004 0400-0420 774 are less than or equal to 1 hour are less than or equal to 1 hour 11/3/2004 0547-0555 195 11/3/2004 1037-1045 387 11/3/2004 1314-1320 387 11/3/2004 1040-1128 3,072 11/3/2004 1320-1408 64 11/7/2004 1210-1308 400 J TOTAL 5,669 ~Unplanned Events greater than 1 hour DATE . . . . TIME· . . VOLUME DESCf:lIPTION OFINCIPENT&. CAUSE 11/3/2004 0355-0546 15,865 See attachments ..... ... ACTION TAKEN TO ELIMINATE CAUSE. See attachments TOTAL 15,865 Iplanned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Met DATE ... TIME VOLUME DESqRIPTION OF INCIDENT &. CAUSE See attachments ........... ACTION TAKEN TO EUMINATECAUSE···· See attachments TOTAL o Iplanned Events Exceeding 1 Hour OR Exceeding 5000 Met . DATE:> TIME . VOLUMEI)E~CRIPTIONOFINCIDENT&CAUSE See attachments Ac:TJON TAI<E:N TO E:LlMINATE CAUSE See attachments TOTAL o Unplanned Events < 1 Hour Unplanned Events> 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist 15,865 o o TOTAL FLARED VOLUME 92.655 12/6/2004 4:06 PM bp REPORT NO: 04-0525 BPXA FLARE REPORT PRUDHOE BAY FACILITY: CGF. DATE: 03 Nov 2004 SYSTEM 1. FlarelRelief Valve 2. FlarelRelief Valve 3. Flare/Relief Valve TIME OF FLARING Black Start Stop Duration Intermittent Smoke Planned VOLUME 03:55 05:46 1 Hrs 51 Mins ~ 0 0 15,865 MSCF 10:40 11:28 OHrs 48 Mins ~ D D 3,072 MSCF 13:20 14:08 OHrs 48 Mins ~ D 0 64 MSCF TOTAL VOLUME 19,001 MSCF First Determination of Cause: 1. MI trains shutdown due to plant upset 2. MI train shutdown due to plant upset 3. MI train shutdown due to plant upset Action Taken to Stop Flaring: 1. Restarted MI train and warmed up L TS. Volume indicated by meter 660 2. Restarted MI train. Volume indicated by meter 660 3. Restarted MI train. Volume indicated by meter 660 Monday, November 22, 2004 Page 1 of 1 STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 0290000008 2. Facility Name PBU CGF B Disposition 3. Field PBU - EOA Volume MCF 4. Operator 5. Month/Year of Disposition BP Decembe~2004 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold 2,698,464 Pool Name PRUDHOE Pool Code 640150 Percent 100.00% 7. Reinjected 13,348,094 8. Flared or vented 1 hour or less 1,082 9. Flared or vented more than 1 hour (see instr.) o 10. Pilot and Purge 26,058 11. Used for lease operations (specify in Remarks) 3,560,250 12. Other (see instructions) o Authorization >1 hr: Safety MCF 13. TOTAL VOLUME (ITEMS 6-12) 19,633,948 Lease Use MCF 14. NGL Gas Equivalent 2,698,464 Conservation MCF 15. Purchased gas o Waste: MCF 16. Transferred from: FS1, FS2, FS3, GC1, GC2, GC3 265,209,582 17. Transferred to: (Express as a negative #) FS1, FS2, FS3. CCP & GPMA PI. Mcintyre MI 18. Remarks: Block 11: Fuel Gas = 3,515,087 mscf and Assist Gas = 45,163 mscf; Block 17: Includes MI Gas to PI. McIntyre = 802,656 mscf -245,575,634 Commissioner Date Printed Name Phone (907)564-5028 Date Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 600 F. Authorit 20 AAC25.235. Form 10-422 Rev. 1/2004 Submit in Duplicate BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - CENTRAL GAS FACILITY GAS FLARING INCIDENT REPORT December 2004 Unplanned Events less than or equal to 1 hour 12/13/2004 12/15/2004 12/15/2004 12/15/2004 12/31/2004 0138-0219 0405-0410 1 023-1 028 2245-2250 1641-1704 TOTAL 1,082 97 Not required for unplanned events which 195 are less than or equal to 1 hour 195 195 400 Page 1 Not required for unplanned events which are less than or equal to 1 hour TOTAL See attachments o See attachments Planned Events Less Than or Equal 1 Hour AND Not Exceedin TOTAL See attachments o See attachments Planned Events Exceeding 1 Hour OR Exceedin TOTAL Unplanned Events < 1 Hour Unplanned Events> 1 Hour Planned Events < 1 hour and not exceeding 5,000 MCF Planned Events> 1 hour or exceeding 5,000 MCF Pilot Purge Assist TOTAL FLARED VOLUME 72,303 See attachments o o o o See attachments 1/10/2005 3: 19 PM