Department of Commerce, Community, and Economic Development
Alaska Oil and Gas Conservation Commission
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HomeMy WebLinkAboutNinilchik G Oskolkoff / MarathonSTATE OF ALASKA
AOGCC
GAS DISPOSITION FILES
YEAR: 2007
FACILITY: Ninilchik G Oskolkoff
OPERATOR: MARATHON OIL CO
1. Facility Number
1330000032
Name
�CitASSIM OSKOLKOFF
3. Field
NNRLNIIC
Operator 15.
['Marathon Oil Company
Month/Year of Disposition
Jan -07
Disposition
Volume MCF
20. For production from multiple pools, dirt contribution of each pool as a percent of
Total Volume.
6. Sold
428666
./'
✓��
Pool Name
Pool Code
Percent
GO TYONEK UNDEFINED35
562540
100.00
7. Reinjected
0
8. Flared or vented 1 hour or las
77
9. Flared or vented more than 1 hour (sec instr.)
906
10. Pilot and Purge
0
11. Used for lease operations (specify in Remarks)
324
Authorization >I hr.
Safety
MCF
12. Other (see instructions)
0
13. TOTAL VOLUME (ITEMS 6.12)
429973
Lease Use
MCP
14. NGL Gas Equivalent
0
Conservation
q0(�
MCF
15. Purchased gas
0
Wane_
MCF
/ Y' 3 -2-7-07
Commissioner Date
16. Translated flan:
0
17. Transferred to: (Express as a negative #)
0
18. Remarks:
I hereby certify that the foregoing is true and correct to the bat of my knowledge.
signatures Rivas 4t to Tick Accountant
Note All volumes must be corrected
to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
AAC15.135.
Printed Name: Randy Jirdra Phone•. 918-925-7098 Date•. February 15, 2007
Form 10.422
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Date
Time
Total
Well # or
Facility
Planned
Y/N
Reason
Mitigation
Start
Stop
Duration
Flare /
Vent
MCF
1/3/2007
910
1120
2hr10min
270
GO -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
1/11/2007
1605
1725
1 hr2Omin
206
GO -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
1/20/2007
1700
1830
1 hr30min
230
GO -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
1/26/2007
1000
1140
1hr4Omin
200
GO - 3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
Facility Name:
Grassium Oskolkoff
Total:
906
2007 Jan - Grasium Oskolkoff - Vent Incident Report. xis
Marathon Oil Company
Gas Flare I Vent Incident Report
January 2007
Originator Jaci Stasak, MOC
1. Facili 1330000032 I2.
GRASS OSO Ks OI3COFF
3. Field
NENILC
14. ro Oil Company
15. Month/Year o Feb -0 7 con
Disposition
Volume MCF
20. For production from multiple pools, lift contribution of each pool as a percent of
Total Volume.
6. Sold
345371
\ N
Pool Name
Pool Code
Patent
7. Reinjected
0
GO TYONEK UNDEFMED35
562540
100.00
8. Flared or veined 1 hour or leas
0
9. Flared or vented more than 1 hour (see instr.)
699
10. Pilot and Purge
0
11. Used for lease operations (specify in Remarks)
263
Authorization >1 hr.
Safety
MCF
12. Other (see instructions)
0
13. TOTAL VOLUME (ITEMS 6-12)
346333
Lase Use
MCF
14. NGL Gas Equivalent
0
Conservation
Gq
/ I
MCF
15. Purchased gas
0
Waste:
MCF
O (/ -
a / T' 4---
Commissions Date
16. Tracts &rfed from:
0
17. Transferred to: (Express as a negative #)
0
18. Remarks:
1 hereby certify that the forgoing is true and conect to the bat of my knowledge.
signature Rada Oladdta. Title: Accountant
Note All volumes must be corrected
to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
AAC25.235.
Printed Name: Randy lindn Plane. 918-925-7098 Date: Match 16, 2007
Form 10-422
STATE OF ALASKA
ALASKA OIL AND CAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Date
Time
Total
Well # or
Facility
Planned
Y/N
Reason
Mitigation
Start
Stop
Duration
Flare /
Vent
MCF
2/9/2007
1345
1600
2hr15min
290
GO -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
2/18/2007
1515
1630
1 hrl5min
168
GO -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
2/26/2007
1045
1235
1 hr50min
241
GO -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production,
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
1
Facility Name:
Grassium Oskolkoff
Total:
699
2007 Feb - Grasium Oskolkoff - Vent Incident Report . xis
Marathon Oil Company
Gas Flare / Vent Incident Report
February 2007
Originator. Jaci Stasak, MOC
1. Facility Number
1330000032
2. Facility Name
GRASSIM OSKOLKOFF
3. Field
NINILCHIK
4. Operator
IMsrathort Oil Company
mr of Disposition
15. Manth/Y Mar -07
Disposition
Volume MCF
20. For production from multiple pool5 list contnbution ofeach pool as a percent of
Total Volume.
6. Sold
354176
Pool Name
Pool Code
Percent
7. Reinjected
0
GO TYONEK UNDEFINED35
562540
100.00
8. Flared or vented 1 hour or less
0
9. Flared or vented more than 1 hour (see itistr.)
423
10. Pilot and Purge
0
11. Used for lease operations (specify in Remarks)
335
Authorization >1 hr.
Safety
MCF
12. Other (see instructions)
0
13. TOTAL % OLUME (ITEMS 6-12)
354934
(rase Use
MCF
14. NGL Gas Equivalent
0
Conservation
K `423
MCF
15. Purchased gas
0
Waste:
MCF
I6. Transferred
Transferred from:
0
(!N+''L"n
{ ommissioner
may( /. /�
„
tom/ >/ J MCFF
[ _ Cam' - v
Date
f
17. Translated to: (Express as a negative a)
0
' l
I S. Remarks:
I hereby certify that the foregoing is true and correct to the best of my knowledge.
01401.44 Signature' Zanda Title Accountant
Note All volumes must be corrected
(0 pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
AAC25.235.
Printed Name! Randy )indra Phone: 918 - 925 -7098 Date•. April 16, 2007
Form 10-422
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Date
Time
Total
Well # or
Facility
Planned
Y/N
Reason
Mitigation
Start
Stop
Duration
Flare /
Vent
MCF
3/9/2007
830
1015
1h r45min
240
GO -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
3/17/2007
1315
1445
1 hr3Omin
183
GO -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
Facility Name:
Grassium Oskolkoff
Total: 423
2007 Mar - Grasium Oskolkoff - Vent Incident Report. Os
Marathon 00 Company
Gas Flare / Vent Incident Report
Originator. Jaci Stasak, MOC
March 2007
I. Facility Number
1330000032
2. Facility Name
GRASSIM OSKOLKOFP
3. Field
NINILCHIK
Operator
Marathon Oil Company
5. Month/Year of Disposition
Aor -07
Disposition
Volume MCF
20. For production from multiple pools, list contribution of each pool as a percent of
Total Volume.
6. Sold
307650
Pool Name
Pool Code
Percent
7. Reinjected
0
GO TYONEK UNDEFINED35
562540
100.00
8. Flared or vatted 1 house or less
) 38
9. Flared or vented mom than I hour (see imtr.)
a.0 Q
10. Pilot and Purgc
0
.
11. Used for lease operations (specify in Remarks)
219
Authonration>1 hr.
Safety
MCF
12. Other (see instructions)
0
13. TOTAL VOLUME (ITEMS 6-12)
308207
Lease Use
MCF
14. NGL Gas Equivalent
0
Conservation
2 p
MCF
15. Purchased gas
0
Waste:
MCF
16. Transferred from:
0
Commissioner Due
17. Transferred to: (Express as a negative 1)
0
18. Remarks:
I hereby certify that the foregoing is true and correct to the best of my knowledge.
Signature: Raabe Co Title Accountant
Note All volumes must be corrected
to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
AAC25.235.
Printed Name - Randy Jirdra Phone- 918-925.7098 Date: May 16, 2007
Form 10422
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Date
Time
Total
Well # or
Facility
Planned
Y/N
Reason
Mitigation
Start
Stop
Duration
Flare /
Vent
MCF
4/3/2007
1540
1710
1 hr30min
200
GO -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
Facility Name:
Grassium Oskolkoff
Total:
200
F:t1 A e Steve\2007 Apr - Grasium Oskolkoff - Vent Incident Report. xis
Marathon Oil Company
Gas Flare / Vent Incident Report
Originator: Jaci Stasak, MOC
April 2007
1. Facility Number
1330000032
Fsoility Name
GSUI OS
12o.
3. Field
NINILCHIK
Opastor
!Marathon 0i1 Company
5. Month/Year of Disoosition
May
Disposition
Volume MCF
20. For production from multiple pools, Urt contribution of each pool as a percent of
Total Volume.
6. Sold
297629
/
✓
i
Pool Name
Pool Code
Percent
GO TYONEK UNDEFINED35
562540
100.00
7. Reinjected
0
8. Flared or vented 1 boor or less
559
9. Flared or vented more than 1 hour (see imtr.)
167
10. Pilot and Rage
0
11. Used for lease operations (specify in Remarks)
204
ryyajmNoo >I hr.
Safety
CF
12. Giber (see instructions) /1 r /1
Rr C
` ,� D
I v
°
13. TOTAL VOLUME (ITEMS 6
298559
Lease Use
MCF
JUN 8 E 2eol
14. NGL Gas Equivalent
0
Comavatioo
(6, -1
MCF
Asa Os a an bons. tannislisn
15. Purchased gas Anthony
0
lye
$CF
C� 16.
L /990441"24"."----- 7-z‘-0-7
Commissioner Date
Transferred from:
0
17. Transferred m: (Express as a negative a)
0
18. Remarks:
foregoing is true and correct to the bat of my knowledge.
thereby certify that the
Signsmmt an 06geoset Title. Accountant
Note All volumes must be corrected
to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
AAC2S.135.
Primed Name: Randy lindn Phone: 918- 925 -7098 Data June 18, 2007
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Form 10-422
Date
Time
Total
Well # or
Facility
Planned
Y/N
Reason
Mitigation
Start
Stop
Duration
Flare /
Vent
MCF
5/20/2007
1000
1138
1 hr38min
167
GO -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
Facility Name:
Grassium Oskolkoff
Total:
167
C: \TEMP\2007 May- Grasium Oskolkoff - Vent Incident Report.xls
Marathon Oil Company
Gas Flare / Vent Incident Report
Originator: Jaci Stasak, MOC
May 2007
L Facility Number
1330000032
2. Facility Name
i GRASSIM OSKOLKOFF
3. Field
Field
Operator
Marathon OiI Company
S. MonrNYwrof Disposition
Jun -07
Disposition
Volume MCF
20. For production from multiple pool . eat contribution of each pool as a percent of
T otal Volume.
6. Sold
250126
Pool Name
Pool Code
Percent
GO TYONEK UNDEFINED35
562540
100.00
7. Reinjected
0
8. Flared or vented 1 hour or less
0
9. Flared or vented mom than 1 hour (sec instr.)
7(r )6'C
10. Pilot and Purge
0
11. Used for lease operation (specify in Remarks)
193
Attthoritation>I hr.
Safety
MCF
12. Other (see instructions) RECEIVED
0
13. TOTAL VOLUME (ITEMS 6-12) JUL 2 3 2007
251083
Lease Use
MCF
14. NGL Gas Equivalent Alaska Oil a Gas Cons. Commission
Afrtinca a
0
Conservation
763
MCF
15. Purchased gas
0
Waste:
MCF
/� /( //, /� ,., G, , (G_
lJ�—r V-� / rtr"r
Commissi Date
16. TranstertM from:
0
17. Transferred to: (Express as a negative #)
0
18. Remarks:
I hereby certify that the foregoing S Itue and correct to the best of my kmwlalge.
n������ Title Accountant
Signature: Rands t�caa
Note A11 volumes must be corrected
10 pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
AAC2S.135.
Printed Name Randy Jindra Phone 918- 925 -7098 Date: July 16, 2007
Form 10422
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Date
Time
Total
Well # or
Facility
Planned
YIN
Reason
Mitigation
Start
Stop
Duration
Flare /
Vent
MCF
6/4/2007
100
300
2 hrs.
229
Go-3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
6/17/2007
330
530
2hrs.
260
Go-3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
6/28/2007
130
350
2h20min
274
Go -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
Facility Name:
Grassium Oskolkoff
Total:
763 V
Marathon Oil Company
Gas Flare I Vent Incident Report
C: \temp\Temporary Internet Files\OLK489\2007 Jun - Grasium Oskolkoff - Vent Incident Report.xls Originator: Jac' Stasak, MOC
June 2007
I. Facility 1330000032
1 OS KOIK OFF
3 NINILCHIK (Ma er n oil Company
I3. Month/Year I)it7aaioo
MI-07
DapsUWa
VName MCF
20. For podumlonfrom multiple pools. Nat conmib,noa o/tack pool as a percent of
Total Volume.
6. Sold
191773
✓
A
-
Pool Name
Pool Code
Percent
7. Reinjected
0
GO TYONEI( UNDEFINED35
362540
100.00
8. Fond or vented t has of las
255
9. Flared or weed mote than 1 Inn (see instr.)
2874
10. Pilot and Purge
0
11. Used for In operations (specify in Remarks)
203
. >l m:
Safety
AS
MCF
12. Other (see ructions)
0
13. TOTAL VOLUME (ITEMS 6-12)
195105
Lan Use
MCF
14. NGL Gas Equivalent
0
Comwatim
Z8/4
MCF
15. Purchased pa
0
Waver.
MCF
J It
9 7l -v 7
Dale
16. Tnmfared from:
0
17. Trarafined b: (Express as a negative #)
0
18. Remarks.
1 hereby certify that the foregoing is rue and correct to the bat of my knowledge.
-�� ^.,
SigWUre: *ands &!14il4a Tide: Accountant
Note AN Volumes must be corrected
to pressure of 14.65 psla and to a
temperature of 60o F. Authority 20
AAC25.235.
Printed Name. Raady liffia Phone: 918- 925 -7098 Date: Augur 17, 2007
Form 10-422
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Date
Time
Total
Well # or
Facility
Planned
Y/N
Reason
Mitigation
Start
Stop
Duration
Flare /
Vent
MCF
7/13/2007
1140
1330
1 hr5gmin
317
GO -1
Y
Vent - water build up in the production string
causing reduced production, Requires
unloading of the well to resume production-
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
7/14/2007
1445
1645
2hr
499
GO -1
y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for welt to
achieve minimum unloading velocities
without requiring vent.
7/14/2007
1000
1150
1hr50min
217
GO -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the wail, hoping to
increase production enough for well to
achieve minimum unloading velocities
wilhout requiring vent.
7/24/2007
955
1130
1 hr35min
480
GO -1
Y
Vent - water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
7/27/2007
1910
2050
1 hr40min
509
GO -1
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
7/27/2007
610
810
2hrs
252
GO-3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
7/29/2007
1000
1130
1 hr30min
600
GOA
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
Facility Name:
Grassium Oskolkoff
Total:
2874
Marathon Oil Company
Gas Flare / Vent Incident Report
C:\temp \Temporary Internet Files \OLK489\2007 Jul_Revl - Grasium Oskolkoff - Vent Incident Report.xIs
Originator. Jaci Stasak, MOC
July 2007
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
1. Facdnv Numba 2. Facility Name
1330000032 GRASSIM OSKOLKOFT
Disposition
6. Sold
7. Reinjated
8. Fold or vented 1 hour or leas
9. Flared or vented more than 1 hour (see instr.)
10. Pilot and Purge
11. Used for lone operations (spairy in Remarks)
12. Other (sot irrtmctions)
13. TOTAL VOLUME (ITEMS 612)
17. Transfaad to: (Express as a negative N)
3. Field ()pastor nth pastor Is. Mont /la of Disposition
NINILCHIX 1 Oil Company I Aua -07
Volume MCF
186824
0
143
2418
0
193
0
189578
14. NOL Gas Equivalent
15. Purchased pa
16. Transferred from
0
0
0
0
20. For production from mdtiple pools. list contribution of each pool as a potent of
Total Volume.
Pool Name
Pool Code Percent
GO TYONEK UNDFFINED35
Authorization >I hr. Safety _ MCF
Lease Use MCF
Conservation
Z r IS MCF
waste:
562540
100.00
MCF
( 4 -'
/0 -17 -0
Dare
18. Ranada:
1 haeby catty tart the foregoing is true and correct to the bat of my knowledge.
Si Z • gueuz
Printed Name: Radyiinda
Title Accauntam
Phone: 918-925-7098 Date. September 17, 2007
Note All volumes must be corrected
to pressure of 14.65 psis and to a
temperature of 60o F. Authority 20
AAC25.235.
Sgt
Form 10422
Date
Time
Total
Planned
Y/N
Reason
Mitigation
Start
Stop
Duration
Flare /
Vent
MCF
Well # or
Facility
`
8/4/2007
1415
1535
1 hr 20min
513
GO -1
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities,
without requiring vent.
8/11/2007
1255
1420
1 hr25min
526
GO -1
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
8111/2007
1000
1157
1hr57min
245
GO -3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
8/20/2007
745
850
1hr5min
441
GO -1
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
8/26/2007
1450
1620
1hr30min
181
GO-3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
8/29/2007
1924
2046
1 hr22min
512
GO-1
Y
Vent - water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
Facility Name:
Grassium Oskolkoff
otal:
Marathon Oil Company
Gas Flare / Vent Incident Report
C: \temp\Temporary Internet Files \OLK489\2007 Aug - Grasium Oskolkoff - Vent Incident Report.xls
Originator: Jaci Stasak, MOC
August 2007
1330000032 I 1. Facility NNumber
2. Facility Name
GRASSIM OSKOLKOFF
3 F
Nt :HD(
. Operator
'Marathon Oil Company
5. Month/Year Of Diaoaition
Sc0 -07
Disposition
Velem MCF
20. Forproduciion from multiple pools, list contribution of each pmt as a pecan of
Toter! Ya(umr
6 Sold
157964
� � �
Pool Name
Pool Code
Parcae
GO TYONEK UNDEFINED55
562540
100.00
7. Reinjected
o
8. Flared or vented 1 hour or less
257
9. Flared or vented more than 1 hour (see Instr.)
2539
I0. Pilo* and Purge
0
1 I. Used for lease operations (specify in Remarks)
162
Auhonzalion>I hr.
Safety
MCF
12. Other (see uattuctions)
0
13. TOTAL VOLUME (ITEMS 6-12)
160922
Lease Use
MCF
14 NGL Gas Equivalent
0
Conservation
z
MCF
15. Purchased gas
0
Waste:
MCF
��
16. Transferred from:
0
C tnntissiotwr Dan
17. Transferred to: (Express as a negative
ve al
p
18. Remarks:
1 hereby certify that the foregoing is we and correct to the beat of my knowledge.
Signature. Rands eiselaa Tide Accountant
Note AtI vollanes must be corrected
to pressure of 14.65 psis and to a
temperature of 60o F. Authority 20
AAC25.235.
Printed Name: Randy fitdra Phone. 918- 925 -7098 Dab October 16, 2007
Form 10-422
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Date
Time
Tut
Well # or
Facility
Planned
YIN
Reason
Mitigation
Start
Stop
Duration
flare /
Vent
MCF
9/5/2007
1838
1958
t hr2Omin
539
GO
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to increase production
enough for well to achieve minimum unloading velocities without
requiring vent.
9/7/2007
1300
1503
2hr3min
239
GO-3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to increase production
enough for well to achieve minimum unloading velocities without
requiring vent.
9/9/2007
1957
2112
l hrl5n1in
461
GO - 1
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to increase production
enough for well to achieve minimum unloading velocities without
requiting vent.
9/16/2007
1730
2100
3hr30min
153.9
GO-3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to increase production
enough for well to achieve minimum unloading velocities without
requiring vent.
9/19/2007
1103
1213
1 hrlOnpn
101.3
GO-3
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well t0 resume production.
Unloaded water from the well, hoping to increase production
enough for well to achieve minimum unloading velocities without
requiring vent.
9/23/2007
1315
1500
lhrl5min
528
GO -1
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to increase production
enough for well to achieve minimum unloading velocities without
requiring vent.
9/28/2007
1840
1955
1 hrl5min
517
1
GO-1
Y
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to increase production
enough for well to achieve minimum unloading velocities without
requiring vent.
Facility Name:
Grassium Oskolkoff
Total: 2539.2
Cttemp\Temporary Internet Files10LK48912007 Sep -Grave Oskalkdf - Vent Incident Report xls
Marathon Oil Company
Gas Flare / Vent Incident Report
September 2007
Originator. Jaci Stasak, MOC
1. Facility Number
1330000032
Facility Name
IaGRASSIM OSKOIXOFF
3. Field
Nil :HIK
4. Operator
IMarat on Oil Company
S. Month/Year o(Disoosilion
Oct -07
Disposition
VoitION MCF
20. For production from multiple pool,. list contribution of each pool as a percent of
Total Volume
6 Sold
161594
1 8 8
Pool Name
Pool Code
Percent
GO TYONEK UNDEFINFD35
562540
100.00
7. Reinjected
0
8. Flared or vented 1 Item or las
2488
9. Flared or vented more than 1 tour (s� Instr.)
447
10. Pilot and Purge
0
11. Used for lease operations (spaify in Remarks)
179
Authorization >1 M:
-.
Safety
(554-445L---
MCF
12. Otha (see instruction)
0
13. TOTAL VOLUME (ITEMS 6-12)
164708
Iran Use
MCF
14. NGL Gas Equivalent
0
Comavuion
4 -7
°�`F f
MCF
15. Purchased gas
0
Waste:
MCF
/z 7? — o7
usaio,mr Date
16. Transferred from:
0
17. Transferred to: (Express as • oeghtive II)
0
18. Remarks:
1 hereby certify that the foregoing is true and correct to the Dat of my knowledge.
signature ZUNIS Title Accountant
Note All volumes must be corrected
to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
AAC2S.235.
Primed Name: Randy Jindra Phone 918 - 925 - 7098 Date: November 16, 2007
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPOR'f OF PRODUCED GAS DISPOSITION
Form 10.422
Date
Time
Total
Well # or
Facility
Planned
V/N
Reason
Mitigation
Start
Stop
Duration
Flare /
Vent
MCF
10/7/2007
16:45
17:55
1 hrl0min
447
4
GO -1
Vent -water build up in the production string
causing reduced production. Requires
unloading of the well to resume production.
Unloaded water from the well, hoping to
increase production enough for well to
achieve minimum unloading velocities
without requiring vent.
Facility Name:
Grassium Oskolkoff
Total:
Marathon Oil Company
Gas Flare / Vent Incident Report
C:Uemp \Temporary Internet Flies\OLK489■2007 Oet - Grasium Oskolkoff - Vent Incident Report (2).xls Originator: Jaci Stasak, MOC
Date
Time
Total
BBLS
Unloaded
Well # or
Facility
Lowest FTP
Attained
Unload Gas
Rate
MMCF
MMCFD
Start Rate
MMCFD
End Rate (1
hour after
B/D)
Psi
Start Tbg
Psi
End Tbg
Start
Stop
Duration hr.
min
Flare /
Vent
MCF
10/3/2007
19:10
20:09
59min
463.8
5.28
GO-1
569
10
3.7
5.9
776
791
10/7/2007
12:20
12:55
35min
40.2
0
NS -2
185
rVa
0
0
800
building
10/7/2007
16:45
17:55
lhr10min
447
4
GO-1
565
10
4.3
6
779
788
10/13/2007
9:37
10:32
55min
406.2
4.6
GO -1
530
10
3.6
5.7
764
791
10/18/2007
13:45
15:00
1hr15min
30.9
1
NS -2
8
3.5
0
0
975
8
10/21/2007
15:00
15:58
58min
433.4
3.38
GO-1
555
10
3.7
6
784
782
10/25/2007
11:25
12:20
55min
352.8
2.9
GO -1
448
9.2
2.2
5
773
790
10/28/2007
12:20
13:18
58min
414.4
2.8
GO-1
540
10
4.3
5.7
777
786
Facility Name:
Ninilchik Gas Field
Marathon Oil Company
NGF Well Blowdown Report
Oct -07
'•` Note: These blowdowns were kep under 1 hour in duration because it was determined that a 55 minute blowdown time was ideal for this well. No additional
water was being unloaded after this timeframe.
..
•••
...
..•
1. Facility Number
1330000032
2. Facility Name
GRASSLM OSKOLKOFF
3. Field
NINR.CNIK
4. Operator
lManthnn Oil Company I
S. Month/Year of Disposition
Nov -07
Disposition
Volume MCF
20. for roduaion from multiple p f ip pools, list contribution of each popl as a percent of
regal Volume.
6. Sold
156037
Pool Name
Pool Code
Percent
7 Reinjected
0
GOTYONEKUNDEFOVED35
562540
100.00
8. Flared or vented I hour or less
1899
9. Flared or vented more than 1 hour (see Instr.)
0
10. Pilot and Purge
0
I I. Used for lease opmticros (specify in Remarks)
270
12. Other (see instructions)
0
Authorization >I hr:
Safety
MCF
13. TOTAL VOLUME (ITEMS 6-12)
158206
Lease Use
MCF
14. NGL Gas Equivalent
0
Conservation
MCF
1 S. Purchased gas
0
waste'.
MCF
16. Transferred from:
0
Commissioner Date
17. Transferred to: (Express as a negative g)
0
18. Remarks:
I hereby certify that the foregoing is we and correct to the bat of my knowledge.
p
Signature Rtak 4:44142
Title
Phone-
Arenuntant
Note All volumes must be corrected
to pressure of 14.65 psia and to a
temperature of 60o F. Authority 20
AAC2S.235.
Printed Name Randy linden
918 - 925 -7098 Date December 19, 2007
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
From 10-422
I Fertility Number
1330000032
2. Facility None
GRASSIM OSKOLKOFF
3 Field
NINILCHIK
Operator
'Marathon Oil Company
I5. Month/Year of Dlaooaitlon
! Dec-07
Dtspasitlea
Volume MCF
20. For production from multiple pods. hart contribution of each pool as a percent of
Tenet Volume
6. Sold
1
Pool Name
Pool Code
Percent
7 Reinjected
0
GOTYONEKUNDEFMED35
562540
100.00
8. Flared or vatted 1 (lour or less
0
9. Flared or vaned more then 1 lour (sec tnstr.)
0
10 Pilot and Purge
0
II Used for lease operations (specify in Remarks)
2000
12. Otha(see inauctumxl
0
Authonrauon >1 hr:
Safety
MCF
13. TOTAL VOLUME (ITEMS 6-12)
302676
Lease Use
MCF
14 NGL Gas Equivalent
0
Conservation
MCF
15. Purchased ps
0
Waste
MCF
16. Transferred from:
0
Commissions Date
17. Transferred lo: (Express as a negative 11)
0
18. Remarks.
1 hereby certify that the foregoing is true and correct to the bear of my knowledge.
Signature R ader & &stota.
Titk'
Phone:
Accountant
Note All volumes must be corrected
to pressure of 14.65 psia and to 0
temperature of 60o F Authority 20
4.405.235.
Printed Name Randy lindra
918- 925 -7098 Date January 16, 2008
Form 10-422
STATE OF ALASKA
ALASKA OIL AND GAS CONSERVATION COMMISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
j
FW: Ninilchik Venting Update 1/21/2008 Page 1 of 2
McMains, Stephen E (DOA)
From: Regg, James 8 (DOA)
Sent: Tuesday, January 22, 2008 9:39 AM
To: McMains, Stephen E (DOA)
Cc: Williamson, Mary J (DOA)
Subject: FW: Ninilchik Venting Update 1/21/2008
Steve —
Copies should probably be placed with gas disposition files for these Ninilchik Unit pads. Thank you.
Jim Regg
AOGCC
333 W.7th Avenue, Suite 100
Anchorage, AK 99501
phone: 907-793-1236
fax: 907 - 276 -7542
From: Walsh, Ken [ mailto:kdwatsh @marathonoil.com)
Sent: Monday, January 21, 2008 11:51 AM
To: Regg, James B (DOA)
Cc: Zeman, Kaynell J.; Laughlin, Gary A.; Gay, Chris; Cissell, Wayne E.; Donovan Jr, Dennis M.; Grant, Patrick;
Ibele, Lyndon; Mullin, Mickey; Rang, Craig L.; Skiba, Kevin 1; Sulley, Michael
Subject: FW: Ninilchik Venting Update 1/21/2008
Jim,
This email is meant to serve as an update to the summary of Ninilchik gas venting that I
described in my email to you on March 14, 2007. Below please find an explanation of changes
and future plans.
Falls Creek (FC) Pad
Pad -based compression and the initiation of foamer injection into the wellbore to lift produced
water has essentially eliminated gas venting to keep the FC #1 rd, FC #3, and FC #4 wells
flowing to sales.
Grassim Oskolkoff (GO) Pad
No gas venting to keep the wells unloaded has been necessary since mid - November 2007.
Marathon installed pad -based compression and began gas compression on December 3,
2007. Due to compression, GO #1 is producing to sales without the need to vent to
atmosphere. GO #2 remains shut in for evaluation to shut off excessive water and re- establish
economic gas production. A coiled tubing velocity string was installed in the GO #3 well in
mid - November 2007 to eliminate the necessity for venting. The well is currently shut in
waiting on stickline work to clear debris from the velocity string and reinstate gas sales. GO #5
is waiting on adding perforations to achieve an economic gas rate. The GO #6 well is
1/22/2008
FW: Ninilchik Venting Update 1/21/2008 Page 2 of 2
producing to sales and is being considered for foamer or velocity string installation to prevent
liquid loading. Marathon anticipates adding the new well, GO #7, in the first quarter of 2008.
Ninilchik State (NS) Pad
NS #1 and NS #3 are flowing to sales line pressure at sufficient gas rates to prevent liquid
loading.
Paxton Pad
Marathon installed a coiled tubing velocity string in the Paxton #1 wellbore on 1/26/2007.
Since the installation, Marathon has eliminated the periodic venting of this well to unload
produced water and maintain gas production. Marathon has spudded and is currently drilling
the Paxton #2 Tyonek well at this writing.
Susan Dionne (SD) Pad
SD #3 and SD #4 are producing at sufficiently high enough gas sales rates from each well to
unload produced water without venting.
It should be pointed out that Marathon has been successful in limiting or eliminating gas
venting by installing coiled tubing velocity strings in some of these wells. If the SCSSV
regulations are implemented and this equipment is installed, it will prevent the deployment of
these coiled tubing velocity strings or capillary foamer strings in the future. If you have
questions or comments that you would like addressed, please feel free to call me at 907 -394-
3060 or email me at kdwalsh @marathonoil.com.
Best Regards,
flat
Ken D. Walsh
Senior Production Engineer
Marathon Oil Company - Alaska Asset Team
907 - 283 -1311 (office)
907.394 -3060 (cell)
1/22/2008