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HomeMy WebLinkAboutSR Swanson River LEX Gas DispositionState of Alaska AOGCC Gas Disposition Files Year: 2013 Facility: SR Swanson River LEX Operator: HILCORP STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION 6. Sold 201,569 7. Reinjected 0 8. Flared or vented 1 hour or less 140 9. Flared or vented more than 1 hour (see instr.) 781 10. Pilot and Purge 582 11. Assist Gas 0 12. Fuel gas used in lease operations 43,955 13. Other (see instructions) 0 14. TOTAL VOLUME (ITEMS 6-13) 247,027 15. NGL Gas Equivalent 0 16. Purchased gas- Rental Return Gas 129,029 17. Transferred from: (Off -lease Gas) 0 18. Transferred to: 0 Other. To Swanson Storage 121,819 Hemlock Production Sold 41,656 correct to the best of my Title >t hr. pools, Total Use ass I to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 AAC25.235. VZ -F 312-1113 OR FLARING EVENTS GREATER THAN 1 HOUR "._..' t... ..::. pm „� ,- Sia "a, „ - w ;F.Platin . f ,-.'_Cv,F r _- of;la r trent .. b ..$'- . ,op„ aken 6NliaimdeVa as ... EXCESS FLARING IN EXCESS FLARING NECESSARY ORDER TO CONDUCT UNTIL MAINTENANCE ON SCHEDULED COMPRESSOR COULD BE 01/01/2013 124250 1330000002 01/02113 07:15:OOAM 09:0O:OOAM 01102113 p PREVENTATIVE D COMPLETED AND MAINTENANCE ON COMPRESSOR COULD BE 27 COMPRESSOR K-8. RESTARTED. EXCESS FLARING DUE TO CESS FLARING NECESSARY SCHEDULED UNTIL HEAD GASKET COULD 01101/2013 124250 1330000002 01/23/13 12:30:OOPM 04:00:OOPM 01/23/13 P MAINTENANCE ON COMPRESSOR IN BE REPLACED AND LACEK�S TO REPLACE THE DEAD COMPRESSOR K-8 BROUGHT 27 GASRDER HEAD GASKET. BACK ONLINE. EXCESS VENTING NECESSARY EXCESS VENTINGDUE UNTIL OIL PRESSURE COULD 01101/2013 124250 1330000002 01/28/13 03:30:OOPM 07:0O:OOPM 01/28/13 U TO LOW OI L PRESSURE CAUSED WELL BE CORRECTED AND THE COMPRESSOR BROUGHT SPIKES. BACK ONLINE. 637 EXCESS VENTING DUE TO UNSCHEDULED EXCESS VENTING NECESSARY MAINTENANCE ON UNTIL GOVERNOR COULD BE 01/01/2013 124250 1330000002 01/30/13 03:15:OOAM 06:OO:OOAM 01/30/13 U COMPRESSOR K22 TO REPAIREDANDTHE REPAIR BROKEN COMPRESSOR BROUGHT LINKAGE ON THE BACK ONLINE. 70 GOVERNOR. EXCESS FLARING DUE TO CESS FLARING NECESSARY UNPLANNED FACILITY UNTIL POWER RESTORED AND 01/01/2013 124250 1330000002 01/31/13 07:OO:ODPM 10:30:OOPM 01/31/13 U SHUTDOWN CAUSED BY THE FACILITY COULD BE HOMER ELECTRIC BROUGHT BACK ONLINE. 7 POWER OUTAGE. EXCESS FLARING DUE TO CESS FLARING NECESSARY UNPLANNED FACILITY UNTIL POWER RESTORED AND 01/01/2013 124250 1330000002 01/31/13 07:OO:OOPM 11:59:OOPM 01/31/13 U SHUTDOWN CAUSED BY COMPRESSOR K-8 COULD BE HOMER ELECTRIC BROUGHT BACK ONLINE. 5 POWER OUTAGE EXCESS VENTING DUE EXCESS VENTING NECESSARY TO UNSCHEDULED UNTIL REPAIRS COULD BE 01/01/2013 124250 1330000002 01/31/13 07:30�OOPM 11:59:OOPM 01/31/13 U MAINTENANCE ON COMPRESSOR K-22 TO COMPLETED AND COMPRESSOR K-22 BROUGHT FIX A HOLE IN THE FIN BACK ONLINE_ 9 FAN. Facility Name STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 3. Feld 14 6. Sold 156,699 7. Reinjected 0 8. Flared or vented 1 hour or less 470 9. Fared or vented more than 1 hour (see instr.) 647 10. Pilot and Purge 4,248 11. Assist Gas 0 12. Fuel gas used in lease operations 36,366 13. Other (see instructions) 0 14. TOTAL VOLUME (ITEMS 6-13) 198,430 15. NGL Gas Equivalent 0 16. Purchased gas - Rental Return Gas 112,979 17. Transferred from: (OS -lease Gas) 0 18. Transferred to: 0 19. Remarks Other. To Swanson Storage Hemlock Production Sold my 35,399 69,062 Use ibruary 2013 pool as a pe 4--1- 13 e to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 VL -f7 31ZI13 GAS DISPOSITION IMPORT FORM FOR FLARING EVENTS GREATER THAN 1 HOUR R tDate O No FacilftyNo Date Flared Start Time Ending Time End Date Janne MCF Description of Flaring Event Action Taken to Minimize Volume EXCESS FLARING DUE TO PLANNED TESTING OF EXCESS FLARING NECESSARY DURING 2/1/2013 124250 1330000002 2/3/2013 0:01:00 23:59:00 2/3/2013 P 60 GAS WELL 12-15 FOR ADDITIONAL VOLUME. TESTING OF WELL 12-15 FOR ADDITIONAL VOLUME. EXCESS FLARING DUE TO TESTING 12-15 GAS WELL EXCESS FLARING NECESSARY UNTIL WELL 2/1/2013 124250 1330000002 2/4/2013 0:01:00 10:00:00 2/4/2013 P 53 FOR ADDITIONAL VOLUME. TESTING COMPLETED. EXCESS FLARING DUE TO TESTING 12-15 GAS WELL EXCESS FLARING NECESSARY UNTIL WELL 2/1/2013 124250 1330000002 2/4/2013 21:00:00 23:59:00 2/4/2013 P 36 FOR ADDITIONAL VOLUME. TESTING COMPLETED. EXCESS FLARING AT TANK SETTING 2-15 DUE TO EXCESS FLARING NECESSARY UNTIL LINE HIGHER THAN NORMAL GAS RATE CAUSED BY WELL SWEEPING COMPLETED. SWEEPING THAT OVERPRESSURED THE LINE IN AN 2/1/2013 124250 1330000002 2/5/2013 0:01:00 23:59:00 2/5/2013 P 56 EFFORT TO INCREASE GAS PRODUCTION AND LOWER TUBING PRESSURES. EXCESS FLARING DUE TO UNPLANNED FIELD EXCESS FLARING NECESSARY UNTIL THE 2/1/2013 124250 1330000002 2/6/2013 21:30:00 23:30:00 2/6/2013 U 109 SHUTDOWN DUE TO OIL IN THE 45 POUND FLARE FIELD RESTARTED. LINE. EXCESS FLARING DUE TO UNSCHEDULED POWER EXCESS FLARING NECESSARY UNTIL OUTAGE. HOMER ELECTRIC ASSOCIATION COULD 2/1/2013 124250 1330000002 2/10/2013 19:00:00 22:00:00 2/10/2013 U 3 RESTORE POWER AND THE FACILITY COULD BE BROUGHT BACK ONLINE. EXCESS VENTING DUE TO UNSCHEDULED EXCESS VENTING NECESSARY UNTIL 2/1/2013 124250 1330000002 2/1/2013 0:01:00 17:00:00 2/1/2013 U 17 MAINTENANCE ON COMPRESSOR K-22 TO FIX A REPAIRS COULD BE COMPLETED AND HOLE IN THE FIN FAN. COMPRESSOR K-22 BROUGHT BACK ONLINE. EXCESS VENTING DUE TO LOW COMPRESSOR OIL EXCESS VENTING NECESSARY UNTIL 2/1/2013 124250 1330000002 2/2/2013 12:00:00 19:30:00 2/2/2013 U 9 CAUSED BY WELL SPIKES INCREASING PRESSURE COMPRESSOR COULD BE BROUGHT BACK IN TANK 22. ONLINE. EXCESS VENTING DUE TO LOW COMPRESSOR OIL EXCESS VENTING NECESSARY UNTIL 2/1/2013 124250 1330000002 2/6/2013 20:00:00 23:59:00 2/6/2013 U 5 CAUSED BY WELL SPIKES INCREASING PRESSURE COMPRESSOR COULD BE BROUGHT BACK IN TANK 22. ONLINE. EXCESS VENTING DUE TO SHUTDOWN OF EXCESS VENTING NECESSARY UNTIL CLEAN COMPRESSOR K22 IN ORDER TO CONTINUE CLEAN- UP EFFORTS OF THE 45 LB LINE COULD BE 2/1/2013 124250 1330000002 2!7/2013 0:01:00 21:45:00 2/7/2013 U 25 UP EFFORTS ON THE 45 POUND FLARE LINE TO COMPLETED AND THE COMPRESSOR REMOVE THE OIL. RESTARTED. EXCESS VENTING DUE TO FLARE MAINTENANCE ON EXCESS VENTING NECESSARY UNTIL THE SMOKELESS FLARE REQUIRING MAINTENANCE ON THE SMOKELESS FLARE 2/1/2013 124250 1330000002 2/8/2013 3:30:00 23:59:00 2/12/2013 U 132 COMPRESSORS K-8 AND K-22 TO BE SHUT DOWN. COULD BE COMPLETED AND THE COMPRESSORS BROUGHT BACK ONLINE. 647 EXCESS VENTING DUE TO MAINTENANCEICLEANING EXCESS VENTING NECESSARY UNTIL 2/1/2013 124250 1330000002 2/13/2013 0:01:00 16:00:00 2/17/2013 U 127 ON VESSEL 20V2 TO REMOVE OIL THAT WENT MAINTENANCE COULD BE COMPLETED ON DOWN THE LINE. THE VESSEL. EXCESS VENTING DUE TO MAINTENANCE ON EXCESS VENTING NECESSARY UNTIL 2/1/2013 124250 1330000002 2/18/2013 9:00:00 10:30:00 2/18/2013 U 2 COMPRESSOR K-22 TO REPLACE SUCTION AND VALVES ON COMPRESSOR K-22 COULD BE DISCHARGE VALVES. REPLACED AND THE COMPRESSOR RESTARTED. EXCESS VENTING DUE TO MAINTENANCE ON EXCESS VENTING NECESSARY UNTIL 2/1/2013 124250 1330000002 2/19/2013 9:00:00 4:15:00 2/20/2013 U 8 COMPRESSOR K-22 TO REPLACE SUCTION AND VALVES ON COMPRESSOR K-22 COULD BE DISCHARGE VALVES. REPLACED AND THE COMPRESSOR RESTARTED. EXCESS VENTING DUE TO LOW COMPRESSOR OIL EXCESS VENTING NECESSARY UNTIL 2/1/2013 124250 1330000002 2/26/2013 4:30:00 9:00:00 2/26/2013 U 5 CAUSED BY WELL SPIKES INCREASING PRESSURE COMPRESSOR COULD BE BROUGHT BACK IN TANK 22. ONLINE. 647 STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 1330000002 2. Facility Name3. Swanson River Field Swanson River Unit 4. Operator I HILCORP ALASKA LLC 5. MonthNear of Disposition I March 2013 Disposition Volume MCF 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold 203,346 Pool Name Pool Code Percent 7. Reinjected 0 SWANSON RIVER, HEMLOCK 772100 68.15% SWANSON RIVER, TYONEK UNDEFINED 772500 1.06% 8. Flared or vented 1 hour or less 524 SWANSON RIVER, BELUGA UNDEFINED 772520 21.66% SWANSON RIVER, STERLING UNDEFINED 772550 9.13% 9. Flared or vented more than 1 hour (see instr.) 551 10. Pilot and Purge 568 11. Assist Gas 0 12. Fuel gas used in lease operations 43,799 I13. Other (see instructions) 0 Official Use Only Authorization>1 hr Safety S -JF'/ MCF 14. TOTAL VOLUME (ITEMS 6-13) 248,788 Lease Use MCF 15. NGL Gas Equivalent p Conservation MCF 16. Purchased gas - Rental Return Gas 147,465 Waste: MCF 17. Transferred from: (Off -lease Gas) 0 Gom iss Date 18. Transferred to: 0 Other: To Swanson Storage 172,924 Hemlock Production Sold 18,032 is true and correct to the best of my knowledge. V Note: All volumes must be comecte Signature ,�/tti Title Regulatory Analyst to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 ted Name Jamie Oli Irez Phone 713-289-2838 Date 4/18/2013 AAC25.235, VLF 41121/3 OR FLARING EVENTS GREATER THAN 1 HOUR Action Taken to Minimize R tDate O No FacifityNo Date Flared Start Time Endinq Time End Date Planned MCF Description of Flaring Event Volume EXCESS FLARING DUE TO EXCESS FLARING 03/01/2013 124250 1330000002 3/11/2013 11:30:00 AM 1:30:00 PM 3/11/13 0:00 U 356 UNPLANNED FIELD NECESSARY UNTIL HOMER SHUTDOWN CAUSED BY ELECTRIC ASSOCIATION POWER OUTAGE. COULD RESTORE POWER. EXCESS FLARING DUE TO EXCESS FLARING 03/01/2013 124250 1330000002 3/11/2013 12:00:00 PM 2:30:00 PM 3/11/2013 U 37 UNPLANNED FIELD NECESSARY UNTIL HOMER SHUTDOWN CAUSED BY ELECTRIC ASSOCIATION POWER OUTAGE. COULD RESTORE POWER. EXCESS FLARING DUE TO EXCESS FLARING UNPLANNED SHUTDOWN NECESSARY UNTIL 03/01/2013 124250 1330000002 3/30/2013 12:30:00 PM 6:30:00 PM 3/30/2013 U 106 OF COMPRESSOR K-8 COMPRESSOR K-8 COULD CAUSED BY HIGH TEMPS BE COOLED DOWN AND FROM WELL SPIKES, RESTARTED. EXCESS VENTING DUE TO UNPLANNED SHUTDOWN EXCESS VENTING OF COMPRESSOR K-22 03/01/2013 124250 1330000002 3/3/2013 12:30:00 PM 2:30:00 PM 3/3/2013 U 4 DUE TO COMMON HIGH NECESSARY UNTIL COMPRESSOR K-22 COULD TEMP CAUSED BY OVERLOADING OF BE COOLED DOWN AND BROUGHT BACK ONLINE. COMPRESSOR BY WELL SPIKES. EXCESS VENTING DUE TO UNPLANNED SHUTDOWN OF COMPRESSOR K-22 EXCESS VENTING 03/01/2013 124250 1330000002 3/6/2013 9:45:00 PM 11:15:00 PM 3/6/2013 U 3 DUE TO COMMON HIGH NECESSARY UNTIL COMPRESSOR K-22 COULD TEMP CAUSED BY OVERLOADING OF BE COOLED DOWN AND COMPRESSOR BY WELL BROUGHT BACK ONLINE. SPIKES. EXCESS VENTING DUE TO EXCESS VENTING 03/01/2013 124250 1330000002 3/11/2013 12.00:00 PM 2:30:00 PM 3/11/2013 U 5 UNPLANNED FIELD NECESSARY UNTIL HOMER SHUTDOWN CAUSED BY ELECTRIC ASSOCIATION POWER OUTAGE. COULD RESTORE POWER. EXCESS VENTING DUE TO UNPLANNED SHUTDOWN EXCESS VENTING OF COMPRESSOR K-22 NECESSARY UNTIL 03/01/2013 124250 1330000002 3/20/2013 9:45:00 PM 5:15:00 PM 3/20/2013 U 3 DUE TO COMMON HIGH COMPRESSOR COULD BE TEMP CAUSED BY COOLED DOWN, OVERLOADING OF RESTARTED, AND THE COMPRESSOR BY WELL DISCHARGE LINE SWEPT. SPIKES. EXCESS VENTING DUE TO UNPLANNED SHUTDOWN OF COMPRESSOR K-22 EXCESS VENTING 03/01/2013 124250 1330000002 3/22/2013 6:45:00 PM 9:00:00 PM 3/22/2013 U 4 DUE TO COMMON HIGH NECESSARY UNTIL COMPRESSOR K-22 COULD TEMP CAUSED BY OVERLOADING OF BE COOLED DOWN AND COMPRESSOR BY WELL BROUGHT BACK ONLINE. SPIKES. EXCESS VENTING DUE TO EXCESS VENTING UNPLANNED SHUTDOWN NECESSARY WHILE LINE 03/01/2013 124250 1330000002 3/23/2013 1:00:00 PM 9:15:00 AM 3/23/2013 U 17 OF COMPRESSOR K-22 SWEPTAND DUE TO COMMON HIGH XYLENE/METHANOL TEMP. PUMPED THROUGH. EXCESS VENTING DUE TO EXCESS VENTING UNPLANNED SHUTDOWN NECESSARY WHILE LINE 03/01/2013 124250 1330000002 3/24/2013 1:30:00 AM 2:45:00 AM 3/24/2013 U 2 OF COMPRESSOR K-22 SWEPT AND DUE TO COMMON HIGH XYLENE/METHANOL TEMP. PUMPED THROUGH. STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION Name 6. Sold 228,811 7. Reinjected 0 8. Flared or vented l hour or less 86 9. Flared or vented more than 1 hour (see instr.) 78 10. Pilot and Purge 913 11. Assist Gas 0 12. Fuel gas used in lease operations 56,483 13. Other (see instructions) 0 14. TOTAL VOLUME (ITEMS 6-13) 286,371 15. NGL Gas Equivalent 0 16. Purchased gas - Rental Return Gas 157,952 17. Transferred from: (Off -lease Gas) 0 18. Transferred to: 0 Signature Other: To Swanson Storage Hemlock Production Sold Jamie correct to the best of my knowledge. 214,375 7,962 amtor 5. MonthNear of Disposition HILCORP ALASKA LLC I April 2013 rom multiple pools, list contribution of each pool as a percent Total Volume. Jame I Pool Code Percer SWANSON RIVER, TYONEK UNDEFINED 772500 3.22% .WA SON RIVER, BELUGA UNDEFINED 772520 24.75% SWANSON RIVER. STERLING UNDEFINED 772550 1 11.58% 7U MCF nnr.F Use Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 AAC25.235. OR FLARING EVENTS GREATER THAN 1 HOUR Action Taken to Minimize R tDate 0 No Factit No Date Flared Start Time Ending Time End Date Planned MCF Description of Flaring Event Volume EXCESS VENTING DUE TO EXCESS VENTING UNSCHEDULED NECESSARY UNTIL 04/01/2013 124250 1330000002 4/4/2013 4:00:00 PM 8:00:00 PM 4/4/2013 U 11 SHUTDOWN OF COMPRESSOR COULD BE COMPRESSOR K-22 COOLED OFF AND CAUSED BY HIGH TEMP. RESTARTED. EXCESS VENTING DUE TO UNSCHEDULED EXCESS VENTING MAINTENANCE ON NECESSARY UNTIL 04/01/2013 124250 1330000002 4/15/2013 1:00:00 AM 3:00:00 AM 4/15/2013 U 6 COMPRESSOR K-22. MAINTNENANCE OPERATOR REPLACED COMPLETED AND THE SPARK PLUGS WHEN COMPRESSOR RESTARTED. COMPRESSOR STARTED RUNNING ROUGH EXCESS VENTING DUE TO EXCESS VENTING UNSCHEDULED NECESSARY UNTIL LINE 04/01/2013 124250 1330000002 4/16/2013 11:00:00 PM 12:45:00 PM 4/17/2013 U 39 SHUTDOWN OF COULD BE SWEPT AND THE COMPRESSOR K-22 COMPRESSOR BROUGHT CAUSED BY HIGH BACK ONLINE. EXCESS VENTING DUE TO EXCESS VENTING LOW OIL PRESSURE AND NECESSARY UNTIL LINE 04/01/2013 124250 1330000002 4/18/2013 1:30:00 PM 2:00:00 AM 4/19/2013 U 11 LOW OIL ALARM COULD BE SWEPT AND THE MALFUNCTION. COMPRESSOR BROUGHT BACK ONLINE. EXCESS VENTING DUE TO EXCESS VENTING UNSCHEDULED NECESSARY UNTIL 04/01/2013 124250 1330000002 4/21/2013 6:00:00 AM 9:30:00 AM 4/21/2013 U 10 SHUTDOWN OF PRESSURE STABILIZED AND COMPRESSOR K-22 COMPRESSOR COULD BE CAUSED BY FIELD WELL RESTARTED. SPIKES. STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 1330000002 2. Facility Name Swanson River 3. Field Swanson River Unit 4.Operator HL 0RP ALASKA LLC 5. Month/Year of Disposition May 2013 Disposition Volume MCF 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume. 6. Sold 226,358 Pool Name Pool Code Percent 7. Reinjected 0 SWANSON RIVER, HEMLOCK 772100 64.290% SWANSON RIVER, TVONEK UNDEFINED 772500 2.49% 8. Flared or vented 1 hour or less 111 SWANSON RIVER, BELUGA UNDEFINED 772520 20.85% SWANSON RIVER, STERLING UNDEFINED 772550 12.37% 9. Flared or vented more than 1 hour (see instr.) 325 10. Pilot and Purge 970 11. Assist Gas 0 12. Fuel gas used in lease operations 53,086 13. Other (see instructions) 0 Official Use Only Authorization>1 hr: Safety.32-5- 3z � J MCF 14. TOTAL VOLUME (ITEMS 6.13) 280,850 Lease Use MCF 15. NGL Gas Equivalent 0 Conservation MCF 16. Purchased gas - Rental Return Gas 161,317 Waste: MCF 17. Transferred from: (Off -lease Gas) 0Q4&7 /t�-_ _ I / ( / Co ssioner c�Date T 18. Transferred to: 0 19. Remarks Other: To Swanson Storage Hemlock Production Sold 193,656 18,632 certlty trial the foregoing is true and correct to the best of my knowledge. ' ^ Note: All volumes must be corrected Signature Title Regulatory Analyst to pressure of 14.65 psia and to a AUT temperature of 60o F. Authority 20 OR FLARING EVENTS GREATER THAN 1 HOUR c iona en o Minimize RptDate OpNo FacilityNo Date Flared Start Time Ending Time End Date Planned MCF Description. of Flaring Event Volume EXCESS VENTING DUE TO UNSCHEDULED SHUTDOWN EXCESS VENTING NECESSARY 05/01/2013 124250 1330000002 5/1/2013 9:00:00 PM 5/1/2013 11:00:00 PM U 20 OF COMPRESSOR K-22 UNTIL COMPRESSOR COULD BE CAUSED BY HIGH PRESSURE RESTARTED. DISCHARGE. EXCESS VENTING DUE TO UNSCHEDULED SHUTDOWN EXCESS VENTING NECESSARY 05/01/2013 124250 1330000002 5/2/2013 4:45:00 AM 5/2/2013 8:00:00 AM U 32 OF COMPRESSOR K-22 UNTIL COMPRESSOR COULD BE CAUSED BY HIGH COOLED OFF AND RESTARTED. TEMPERATURE. EXCESS VENTING DUE TO UNSCHEDULED SHUTDOWN EXCESS VENTING NECESSARY 05/01/2013 124250 1330000002 5/3/2013 5:00:00 AM 5/3/2013 6:45:00 AM U 17 OF COMPRESSOR K-22 UNTIL COMPRESSOR COULD BE CAUSED BY HIGH COOLED OFF AND RESTARTED. TEMPERATURE. EXCESS VENTING DUE TO UNSCHEDULED SHUTDOWN EXCESS VENTING NECESSARY 05/01/2013 124250 1330000002 5/5/2013 9:30:00 AM 5/5/2013 11:30:00 AM U 20 OF COMPRESSOR K-22 UNTIL COMPRESSOR COULD BE CAUSED BY LOW OIL AND RESTARTED. LUBRICATOR PRESSURES. EXCESS VENTING NECESSARY EXCESS VENTING DUE TO UNTIL COMPRESSOR REN 05/01/2013 124250 1330000002 5/9/2013 10:30:00 PM 5/9/2013 11:59:00 PM U 15 UNSCHEDULED SHUTDOWN METER SCREEN WAS CLEANED, OF COMPRESSOR K-22 SPARK PLUGS CHANGED, LINE CAUSED BY LUBE FAILURE. FLUSHED WITH XYLENE, AND THE COMPRESSOR RESTARTED. EXCESS VENTING DUE TO EXCESS VENTING NECESSARY 05/01/2013 124250 1330000002 5/10/2013 2:30:00 AM 5/10/2013 7:45:00 AM U 52 UNSCHEDULED SHUTDOWN UNTIL COMPRESSOR COULD BE OF COMPRESSOR K-22 REPAIRED AND RESTARTED. CAUSED BY LUBE FAILURE. OR FLARING EVENTS GREATER THAN 1 HOUR Action I a en to Minimize RptDate OpNo FacilityNo Date Flared Start Time Ending Time End Date Planned MCF Description of Flaring Event Volume EXCESS VENTING DUE TO UNSCHEDULED SHUTDOWN EXCESS VENTING NECESSARY 05/01/2013 124250 1330000002 5/10/2013 7:00:00 PM 5/10/2013 10:30:00 PM U 35 OF COMPRESSOR K-22 UNTILCOMPRESSOR COULD BE CAUSED BY HIGH SUCTION RESTARTED. PRESSURE. EXCESS VENTING DUE TO EXCESS VENTING NECESSARY 05/01/2013 124250 1330000002 5/11/2013 10:00:00 AM 5/11/2013 11:OO:OOAM U 50 SHUTDOWN OF UNTIL COMPRESSOR COULD BE COMPRESSOR K22 TO SWEEP RESTARTED. THE DISCHARGE LINE. EXCESS VENTING DUE TO EXCESS VENTING NECESSARY 05/01/2013 124250 1330000002 5/18/2013 12:01:00 AM 5/18/2013 1:30:00 AM U 15 UNPLANNED SHUTDOWN OF UNTIL COMPRESSOR COULD BE COMPRESSOR K22. RESTARTED. EXCESS VENTING DUE TO EXCESS VENTING NECESSARY 05/01/2013 124250 1330000002 5/20/2013 5:00:00 PM 5/20/2013 7:30:00 PM U 27 UNPLANNED SHUTDOWN OF UNTIL COMPRESSOR COULD BE COMPRESSOR K22. RESTARTED. EXCESS VENTING DUE TO EXCESS VENTING NECESSARY SHUTDOWN OF UNTIL COMPRESSOR CAN BE 05/01/2013 124250 1330000002 5/22/2013 11:00:00 AM 5/22/2013 12:25:00 PM U 12 COMPRESSOR K22 BECAUSE COOLED DOWN AND OF HIGH COMPRESSOR RESTARTED. LOAD REDUCED TEMPERATURE. TO PREVENT REOCCURENCE. EXCESS VENTING DUE TO EXCESS VENTING NECESSARY SHUTDOWN OF UNTIL COMPRESSOR CAN BE 05/01/2013 124250 1330000002 5/24/2013 12:00:00 PM 5/24/2013 15:00:00 PM U 30 COMPRESSOR K22 BECAUSE COOLED DOWN AND OF HIGH COMPRESSOR RESTARTED. LOAD REDUCED TEMPERATURE. TO PREVENT REOCCURENCE. STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 2. Facility Name 3. Field 4. Operator 5. Month(Year of Disposition 1330000002 Swanson River Swanson River Unit HILCORP ALASKA LLC June 2013 Disposition Volume MCF 1 20. For production from multiple pools, list contribution of each pool as a percent of 6. Sold 197,072 7. Reinjected 0 8. Flared or vented 1 hour or less 263 9. Flared or vented more than 1 hour (see instr.) 0 10. Pilot and Purge 717 11. Assist Gas 0 12. Fuel gas used in lease operations 46,918 13. Other (see instructions) 0 14. TOTAL VOLUME (ITEMS 6.13) 244,970 15. NGL Gas Equivalent 0 16. Purchased gas - Rental Return Gas 147,547 17. Transferred from: (Off -lease Gas) 0 18. Transferred to: 0 Other: To Swanson Storage Hemlock Production Sold is Signature my 188,554 17,360 Title Use 59.87 1.80 Date lote: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 AAC25.235. RECEIVED AUG 21 2013 STATE OF ALASKA®��� ALASKA OIL AND GAS CONSERVATION COMMISSION 1. 1-aclllty Number 1330000002 2. Facility Name Swanson River 3. Field Swanson River Unit 4, Operator HILCORP ALASKA LLC 5. MonthNear of Disposition July 2013 Disposition Volume MCF 20. For production from multiple pools, list contribution Total Volume. of each pool as a percent of 114' X113113 6. Sold 167,048 Pool Name Pool Code Percent 7. Reinjected 0 SWANSON RIVER, HEMLOCK 772100 65.76% HEMLOCK FROM STERLING UNDEF 772105 0.47% 8. Flared or vented 1 hour or less 4 SWANSON RIVER, TYONEK UNDEFINED 772500 2.15% SWANSON RIVER, BELUGA UNDEFINED 772520 20.94% 9. Flared or vented more than 1 hour (see instr.) 1,043 SWANSON RIVER, STERLING UNDEFINED 772550 10.68% 10. Pilot and Purge 840 11. Assist Gas 0 12. Fuel gas used in lease operations 49,014 13. Other (see instructions) O Official Use Only 14. TOTAL VOLUME (ITEMS 6-13) 217,949 Authorization >t hr: Safety MCF 15. NGL Gas Equivalent 0 Lease Use MCF 16. Purchased gas - Rental Return Gas 139,735 Conservation MCF 17. Transferred from: (Off -lease Gas) 0 Waste: MCF �' U �� -.3 J� n��e 18. Transferred to: 011-9 Signature Other: To Swanson Storage 171,314 Hemlock Production Sold 12,578 Jamie tote: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 AAC25.235. OR FLARING EVENTS GREATER THAN 1 HOUR Action I a en to Minimize RptDate OpNo FacilityNo Date Flared Start Time Ending Time End Date Planned MCF Description of Flaring Event Volume EXCESS FLARING AT THE EXCESS FLARING NECESSARY 45LB FLARE DUE TO UNTIL HOMER ELECTRIC 07/01/2013 124250 1330000002 7/9/2013 12:15:00 AM 5:00:00 PM 7/9/2013 U 80 UNPLANNED POWER ASSOCIATION COULD RESTORE OUTAGE CAUSING POWER AND COMPRESSOR K-8 COMPRESSOR K-8 TO COULD BE BROUGHT BACK SHUTDOWN. ONLINE. EXCESS FLARING AT THE EXCESS FLARING NECESSARY 07/01/2013 124250 1330000002 7/9/2013 12:15:00 AM 4:00:00 AM 7/9/2013 U 873 150LB FLARE DUE TO UNTIL HOMER ELECTRIC UNPLANNED POWER ASSOCIATION COULD RESTORE OUTAGE. POWER. EXCESS VENTING NECESSARY EXCESS VENTING AT DUE TO UNTIL HOMER ELECTRIC UNPLANNED POWER 07/01/2013 124250 1330000002 7/9/2013 12:15:00 AM 5:30:00 PM 7/9/2013 U 45 OUTAGE CAUSING ASSOCIATION COULD RESTORE POWER POWER AND COMPRESS OMPRESSOR K-22 TO 22 COULD BE BROUGHT BACK BACK SHUTDOWN. ONLINE. EXCESS VENTING DUE TO COMPRESSOR K-22 FAILING UNEXPECTEDLY DUE TO A EXCESS VENTING UNTIL BELT 07/01/2013 124250 1330000002 7/14/2013 6:00:00 PM 7:30:00 PM 7/14/2013 U 35 BROKEN BELT (BLEW A BELT COULD BE REPLACED AND THE OFF THE FAN DRIVE TO UNIT BROUGHT BACK ONLINE. JACKET/AUX WATER COOLER). EXCESS VENTING DUE TO EXCESS VENTING NECESSARY 07/01/2013 124250 1330000002 7/21/2013 12:30:00 PM 3:00:00 PM 7/21/2013 U 6 UNSCHEDULED UNTIL BELT COULD BE MAINTENANCE CAUSED BY REPLACED AND COMPRESSOR WORN BELT. K-22 BROUGHT BACK ONLINE. EXCESS VENTING NECESSARY EXCESS VENTING AT DUE TO UNTIL HOMER ELECTRIC UNPLANNED POWER 07/01/2013 124250 1330000002 7/25/2013 1:45:00 PM 3:00:00 PM 7/25/2013 U 4 OUTAGE CAUSING ASSOCIATION COULD RESTORE POWER AND COMPRESSOR K - COMPRESSOR K-22 TO 22 COULD BE BROUGHT BACK SHUTDOWN. ONLINE. STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION 1. Facility Number 1330000002 2. Facility Name Swanson River 3. Field Swanson River Unit 4, Operator HILCORP ALASKA LLC 5. Month/Year of Disposition August 2013 Disposition Volume MCF 20. For production from multiple pools, list contribution of each pool as a percent of Total Volume, 6. Sold 134,660 Pool Name Pool Code Percent 7. Reinjected 0 SWANSON RIVER, HEMLOCK 772100 68.52% SWANSON RIVER, HEM F/STERLING UNDEF 772105 0.00% 8. Flared or vented 1 hour or less 29 SWANSON RIVER, TYONEK UNDEFINED 772500 2.27% SWANSON RIVER, BELUGA UNDEFINED 772520 18.25% 9. Flared or vented more than 1 hour (see instr.) 579 SWANSON RIVER, STERLING UNDEFINED 772550 10.97% 10. Pilot and Purge 775 11. Assist Gas 0 12. Fuel gas used in lease operations 49,340 13. Other (see instructions) 0 Official Use Only Authorization >1 hr: Safety MCF 14. TOTAL VOLUME (ITEMS 6-13) 185,603 Lease Use MCF 15. NGL Gas Equivalent 0 Conservation MCF 16. Purchased gas - Rental Return Gas 125.634 Waste: MCF 17. Transferred from: (Off -lease Gas) 0 mmissi ner at 18. Transferred to: 0 Note: All volumes must be corrected Analyst to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 Date g/20/2013 AAC25.235. 19. Remarks: Other: To Swanson Storage 52,493 (for storage and fuel usage) Hemlock Production Sold 62,716 1 hereby certify that the foregoing is true and correct to the best of my knowledge. Signature a— Title Regulatory Printed Name Jamie OIz Phone 713-289-2838 ' re OR FLARING EVENTS GREATER THAN 1 HOUR Action I a en to Minimize RptDate OpNo FacilityNo Date Flared Start. Time Ending Time End Date Planned MCF Description of Flaring Event Volume EXCESS FLARING DUE TO EXCESS FLARING NECESSARY 08/01/2013 124250 1330000002 8/27/2013 13:05:00 PM 19:05:00 PM 8/27/2013 P 579 SCHEDULED INSTALLATION UNTIL CONSTRUCTION OF NEW SPOOL PIECES FOR ACTIVITIES COMPLETED. LEX TIE-IN PROJECT. STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION 6. Sold 166,787 7. Reinjected 0 8. Flared or vented 1 hour or less 35 9. Flared or vented more than 1 hour (see instr.) 472 10, Pilotand Purge 660 11. Assist Gas 0 12. Fuel gas used in lease operations 50,487 13. Other (see instructions) 0 14. TOTAL VOLUME (ITEMS 6-13) 218,441 15. NGL Gas Equivalent 0 16. Purchased gas- Rental Return Gas 141,105 17. Transferred from: (Off -lease Gas) 0 18. Transferred to: 0 Other hereby certify that the foregoing is To Swenson Storage (for storage: 77735 a fuel usaga: 18923) Hemlock Production Sold 96,712 55,287 61 Total Volume. as a .. utticial use. Gnly -I I I >1 hr. Safety /1 y1 MCF V'/-,l%v Lease Use MCF Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 AAC25.235. OR FLARING EVENTS GREATER THAN 1 HOUR � y:� .h .Ifdlffaa d1� .1 ., k * f + ,F8N7 1 EXCESS FLARING EXCESS FLARING DUE TO 09/01/2013 124250 1330000002 9/1/2013 9:30:00 AM 11:00:00 AM 9/1/2013 U UNSCHEDULED POWER OUTAGE NECESSARY UNTIL HOMER ELECTRIC COULD RESTORE CAUSING FACIUTY WIDE SHUTDOWN- 7unplanned POWER. Excess venting necessary until Excess venting due to unscheduled power restored by Homer 09/0172013 124250 1330000002 9/1/2013 930:00 AM 11:00:00 AM 9/1/2013 Ufacility wide shutdown caused by Electric Association and power outage. Compressor K-22 brought back online. Excess veting due to Ren Oil Level EXCESS FLARING 09/01/2013 124250 1330000002 9/10/2013 3.00:00 AM 8:00:00 AM 9/10/2013 U 11 Controller plugging up causing NECESSARY UNTIL HOMER Compressor K-22 to shutdown ELECTRIC COULD RESTORE unexpectedly. POWER. EXCESS FLARING EXCESS FLARING DUE TO 09/01/2013 124250 1330000002 9/11/2013 7:30:00 AM 10:30:00 AM 9/11/2013 U 75 UNSCHEDULED POWER OUTAGE NECESSARY UNTIL HOMER ELECTRIC COULD RESTORE CAUSING FACILITY SHUT DOWN. POWER. Excess venting necessary until Excess venting due to unscheduled power restored by Homer 09/01/2013 124250 1330000002 9/11/2013 7:30:00 AM 9:30:00 PM 9/11/2013 U 32 facility wide shutdown caused by Electric Association and unplanned power outage. Compressor K-22 brought back online - Excess venting due to unscheduled Excess venting necessary until 09/012013 124250 1330000002 9/12/2013 5:00:00 PM 6:00:00 PM 9/12/2013 U 2 shutdown of Compressor K-22 Compressor K-22 could be because of high discharge pressure. brought back online - Excess venting due to unscheduled Excess venting necessary until shutdown of Compressor K-22 due to Compressor K-22 could be 09/012013 124250 1330000002 9/13/2013 4:30:00 PM 1:4S:00 PM 9/14/2013 U 48 a faulty temperature shutdown repaired and brought back switch. online. Excess venting dueto pigging project Excess venting necessary until 09/01/2013 124250 1330000002 9/20/2013 9:00:00 AM 8:15:00 PM 9/21/2013 P 248 on the 16" SR Sales Line in order to pigging work completed. remove liquids - Excess venting due to scheduled Excess venting necessary in 09/012073 724250 1330000002 9/27!2013 7:00:00 PM 7:10:00 PM 9/27/2013 P 3 order to conduct well maintenance on Well 21-27- maintenance. Excess venting necessary until Excess venting due to scheduled 09/012013 124250 1330000002 9/30/2013 8:30:00 PM 9:00:00 PM 9/30/2013 P 1 preventative maintenance on preventative maintenance completed and Compressor K - Compressor K-22. 22 brought back online. STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION TT Field 14 6. Sold 213,633 7. Reinjected 0 B. Flared orvented 1 hourorless 479 9. Flared or vented more than 1 hour (see instr.) 0 10. Pilot and Purge 616 11. Assist Gas 0 12. Fuel gas used in lease operations 53,445 13. Other (see instructions) 14. TOTAL VOLUME (ITEMS 6.13) 268,173 15. NGL Gas Equivalent 2,739 16. Purchased gas - Rental Return Gas 246,207 17. Transferred from: (Off4ease Gas) 0 18. Transferred to: (44,393) 19. Remarks Transferred to: Swanson Storage 44,393 For storage: 61363 and fuel usage: 44393 Storage portion is inclWed in Line 6. Sold volume subject to royalty. Other: Hemlock production Sold 119,942 the foregoing is true and correct to/ the best of my knowledge. Total Use age NI[4�17A Note: All volumes must be corrected to pressure of 14.65 psis and to a temperature of 60o F. Authority 20 AAC25235. W C_ cm v c cu O c v O E L OY C U O 0 >- 6 4 4 Y Y N Y L a E O N W ID do u 3 N p N LO Z Y N C v a U N N m i.+ O O N c 0 0 ep co v w t- ° .mi o O p= Q da o 0 Sa�[ un X N 1� ti ry ^ Ya Z O ti O ECL O N — 120- .H H N E Y u m L C (UY .0 3 Y = o O O >C L O v Z Y N L Y N O m a o a 3 v E to A w o y E v Y �N Y Y ° U O a d O_ c C U L m m m E O N ° W w Q e1 -LJ- r 0_ U m U — 0 r n Q r C Y o c C c (dJ 0 i 3 � m o� p c n m m N T N '6 O N O r o y Wi+ N V_I J J m Ql E C O > > C7 C7 T Q w 01 Z Z M w w C C -o V o .'. v Q w U m eco o C 0 c m 3 o 03:0 n m°' Y V H Q V7 eo L := ICL O J Z Y e O T+ O v O Y V O Y N 3 wo m v v > E � a 0 L o — O m C Z Y C m W 3 Z T o — oo w o a w O O> Cm in >• mvi L C N Y L v 0 0 N° y v Y p O m N o 3 y Y W W L 3 y L Obo N w w 30 C Y E c v O> ''' > O OL O L C C v c G l VI H Ln 2 � w m Y Q 0 O L cm v N 0 IN a C 6 Y O N W ID W O N p N LO Z 01 C U N N Q i.+ L N c .�„i ep .mi o O p= Q da o Sa�[ un X Q 1� ti N 0 IN STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION 6. Sold 234,478 7. Reinjected 0 8. Flared or vented 1 hour or less 1,358 9. Flared or vented more than 1 hour (see instr.) 0 10. Pilot and Purge 585 11. Assist Gas 0 12. Fuel gas used in lease operations 55,093 13. Other (see instructions) 14. TOTAL VOLUME (ITEMS 6-13) 291,514 15. NGL Gas Equivalent 1,546 - 16. Purchased gas - Rental Return Gas 238,328 17. Transferred from: (Off -lease Gas) 0 18. Transferred to: (20,556) Transferred to: Swanson Storage 20,556 For storage: 20,569 Storage porton Is Induded In Lim 6. Sale volume subled to royalty. Other: Hemlock Production Sold 174,891 Lease Use - REVISED as a certify that the foregoing is true and correct to the best of my knowledge. Note: All volumes must be correcte Signature 6 ' 100" Title Production Analyst to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 led Name Codnev Over Phone 713-289-2881 Dale 6/22/2017 AAC25.235. G 12gI,1- STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION ursposltlon Volume MCF 6. Sold 234,478 7. Reinjected 0 8. Flared or vented 1 hour or less 1,358 9. Flared or vented more than 1 hour (see instr.) 0 10. Pilot and Purge 585 11. Assist Gas 0 12. Fuel gas used in lease operations 55,093 13. Other (see instructions) 14. TOTAL ( - .. 291,514 15. NGL Ga i 1,227 16. Purchased gas - Rental Return Gas 238,328 17. Transferred from: (Off -lease Gas) 0 18. Transferred to: (20,556) 19. Remarks: Transferred to: Swanson Storage 20,556 For storage: 20.569 Storage portion is ineluded in Line 6. Sold volume subject to royalty. Other: Hemlock Production Sold 174,891 I hereby certify that the foregoing is true and correct to the best of my knowledge 20. 4SKA LLC ools, list C( Total Volu Lease Use of each pool as a 772100 Note: All volumes must be corrected Signature Title R ulato Anal st to pressure of 14.65 Pala and to a temperature of 60o F. Authority 20 ted Name Jamie Oliva z Phone 713-289-2838 Date tv2m2m3 AAC25.235_ 1330000002 S. Sold 7. Reinjected B. Flared or vented 1 hour or less 9. Flared or vented more than 1 hour (see instr.) 10. Pilot and Purge 11. Assist Gas 2. Fuel gas used in lease operations 3. Other (see instructions) 4. TOTAL VOLUME (ITEMS 6-13) 5. NGL Gas Equivalent 6. Purchased gas - Rental Return Gas 7. Transferred from: (Off -lease Gas) B. Transferred to: STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Swanson River I Swanson River Unit I HILCORP ALASKA LLC 195,275 0 1,1261 204 713 0 56,703 Transferred to: Swanson Storage 16,986 To storage for reel usage: e To storage for iNection Is Ircluded In Llne 6 as abject to royalty. Other: Hemlock Production Sold 148,948 Signature ,V 4" Cc✓ December 2013 each Dool as a c � . F12e (7 vs k. Wrj2r0Vt), e., ov-Ir-a1. 6/22/201 (o/71/I-� Iota: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 Authorization >1 hr: Safety 264,021 Lease Use 2,189 ' Conservati 212,217 Waste: 0 Commissioner (16,986) Transferred to: Swanson Storage 16,986 To storage for reel usage: e To storage for iNection Is Ircluded In Llne 6 as abject to royalty. Other: Hemlock Production Sold 148,948 Signature ,V 4" Cc✓ December 2013 each Dool as a c � . F12e (7 vs k. Wrj2r0Vt), e., ov-Ir-a1. 6/22/201 (o/71/I-� Iota: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 Facility Name 1330000002 STATE OF ALASKA ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION River 6. Sold 195,275 7. Reinjected 0 6. Flared or vented 1 hour or less 1,126 9. Flared or vented more than 1 hour (see instr.) 204 10. Pilot and Purge 713 11. Assist Gas 0 12. Fuel gas used in lease operations 56,703 13. Other (see instructions) .I 14. TOTAL VOLUME (ITEMS 6.13) 254,021 15. NGL Gas n - r- 1,737 16. Purchaseg e etudg, 4i y 212,217 .I 17. Transferred from: (Off -lease Gas) 0 18. Transferred to: (16,986) 19. Remarks: Transferred to: Swanson Storage 16,986 To storage for fuel usage 0 To storage for injection is included in Line 6 as subject to royalty. Other: Hemlock Production Sold 148,948 I hereby certify that the foregoing is true and correct to the best of my knowledge HILCORP ALASKA Ll from multiple pools, list Total Vc Name Use zU as a 6-9 Date 0.00% 2.41% 6.30% 3,51% to pressure of 14.65 psia and to a temperature of 60o F. Authority 20 �OR FLARI�N;.G EVENTS GREATER THAN I HOUR ';t -we , " " , ,, i ,I Al, ", l, orifi„ "k ORT inimin glVakento.M , 3l, Excess flaring due to losing Excess flaring necessary until 12/01/2013 124250 1330000002 12/05/13 2:30:00 PM 4:30:00 PM 12/05/13 u 11 compressor K-13 which caused high the plant could be restarted 150 that lead to the shutdown of K -S, and compressors brought back the smokeless Flare. online. Excess flaring neciessa ry until Excess flailing necessary due to issues repairs could be done on K-22. 12101/2013 124250 1330000002 12/14/13 530:00 PM 9:30:00 PM 12/14/13 U 1 with the govenor control rod on A new u joint was put on and compressor K-22- the compressor was brought back online. Excess flaring due to a plant wide Excess flaring necessary until 12101/2013 124250 1330000002 12/18/13 9:00:00 AM 10:30:00 AM 12/19/13 U 121 shutdown because of a power Homer Electric power could be outage. restored to all units. Excess venting necessary until Excess venting due to shutdown of K- the mechanic could look at 1210112013 124250 1330000002 12/21/13 1:00:00 AM 8:30.-00 AM 12/21/13 U 3 22 Compressorfor unscheduled compressor, maintenance could be done, and maintenance. compressor brought back online. Excessventing due to shutdown of K- Excess venting necessary until 12t0112013 124250 1330000002 12/23/13 10'00:00 AM 11:59:00 PM 12/23/13 U 2 22 Compressorfor unscheduled methanal could be pumped into the discharge tire. Line maintenance due to a frozend discharge line. will be sweep regularly with methanal in the future. Excess ventingdue to the Excess venting necessary until 12/0112013 124250 1330000002 12/24/13 12:00:00 AM 10:00:00 PM 12I24/13 U 8 unscheduled shutdown of line could be depressurized Compressor K-22 caused by a and cleared with plugged discharge line. methanol/xylene. Excess flaring of the smokeless flare Excess flaring necessary until 1210112013 124250 1330000002 12/27/13 11:15;00 PM 1:15:00 AM 12/28/13 U I due to a power outage causing a Homer Electric could restore facility wide shutdown. power and all units could be brought back online. Excess flaring of flare 150 due to a Excess flaring necessary until 12/OZ'2013 124250 1330000002 12/27/13 11:15:00 PM 1:15:00 AM 12,/28/13 U 57 power outage causing a facility wide Homer E'ectric could restore shutdown. power and all units could be brought back online.