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HomeMy WebLinkAboutBPX - MILNE POINT- ,.: u~n man•<~rrrw~irisewir..®i..~iac~r®i+Srieww:r~risio.irrer~w~wirm~awi..~rrri~rar~rra~i..rierir+cav®r~.reirriarerivzs~risir~srriinwrrrrrsirriri~carrr~iriirsrir~r~ri~~s~sisisrrrwioi~:a..rir^.x~eie qe - ~ AGOCC GAS Disposition Files .BPX 1997 M/ LN6 PO%ivT 3 : °P0',~{r;'~%~;&%1Y%dr/~8:'ar'/~/~'/~Y%c4~/a~/.®Y%~/~/~Y~/B"///EV/~~/~~/fi1/®'/~@/~'/.~Y.~/~/~//~/~/~/4/p"/,~/i'Y.~/•Y/~iY/~/.O/M/~/A~/~/.Y%O/O/®/~B/Y/1//~/M//VB'/.IV/wtl>/~/B"/J~/~/.~/O/B//O/~/A/~/O'/A/41D/.~/~'/.6%aW:'9 /® ' ALASKA OIL AND GAS CONSERVATION CONII~lISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition Milne Point BP Exploration (Alaska) Inc. Milne Point Dec-97 Disposition ~~ ~~ ~ Z ~ Cs-; ~ ~ t"g cf~ ~a an" :~ ;~" x Volume MCF* 1. Sold Fuel 16,844 2. Reinjected 657,338 3. Flared or vented less than 1 hour 4,073 4. Flared or vented greater than 1 hour (Supplemental report required--See 20 AAC 25.235) 11,170 5. Pilot and Purge 2,077 6. Used for lease operations Fuel Assist 276,539 24,999 7. Other TOTAL items 1-7 993,040 8. NGL gas equivalent produced Purchased gas 0. Transferred from: ~1. Transferred to: Remarks: I hereby certify that the foregoing is true and correct to the best of my knowledge. M6~.. dU~~ ~~t Signature ~ Title Date ~•~2~~7J *Indicate contribution of each pool to total. Pool Name Code Percent KUPARUK 525100 94.7 SCH. BLUFF 525140 5.3 Official Use Only-Flaring AutYiorization>1 kir; 1. Safety MCF 2. Lease MCF 3. Conserv. Purposes MCF Commissioner Date Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month folowing the month of disposition. Authority 20 AAC 25.235. Form 10-422 Rev. 4/95 01/01/98 09:23 Milne Point Unit mthly Gas Flaring Incident Report For: Dec /1997 Flare Name: Flare 1 np anne vents greater t an our Duration -Volume (MSCF) Start Time (hh:mm) Flare Assist Cause Comment 12/05/97 13:26:00 01:19 190.5 263.9 Unplanned shutdown of C pad IWAG SI high GOR wells C03, C09, E06, injection compressor. Shutdown E11, E13, L06 for flare relief during initiated for repair of fire/gas sensing repairs. Wells BOL after repairs device. complete. 12/06/97 07:05:00 02:10 624.1 887.4 Unplanned flare events due to shutdown Dispatched maintenance crews several of C pad IWAG compressor. times to C pad to repair tube oil system. Shutdowns all triggered by problems SI high GOR wells B09, B22, C03, with Trabon tube oil system. C07, C09, E06, E13, L06 for flare relief during upsets. 12/06/97 09:46:00 01:44 210.8 498.9 See above. ~ Wells BOL after repairs complete. 12/07/97 17:46:00 01:14 208.5 347.8 See above. Trabon Tube oil problems High GOR wells remained SI until persisted throughout day. Trabon problems remedied. 12/15/97 16:44:00 09:31 5,982.0 2,525.1 Unplanned flaring event due to Root cause of shutdown is still unplanned emergency shutdown of unknown but strongly believed to be MPU Central Processing Facility (CFP). PLC related. Extended flaring duration S/D was initiated from a unit alarm in was due to extensive safety-related Mod 58. troubleshooting before & during restart of facility. A complete investigation is pending. 12/22/97 15:51:00 01:39 469.4 524.0 Unplanned flaring event related to Prepared contingency high GOR SI list unplanned IWAG shutdown due to low but did not implement due to perceived tube oil pressure. quick fix. 12/22/97 19:15:00 02:00 613.3 741.9 2nd unplanned IWAG shutdown due to Identified fouled spark plugs & several misfires on engine. replaced. Returned to service. All 12/22 field maintenance operations were impacted by extreme cold NS ambient temps (<-45F). 12/23/97 21:21:00 02:09 679.9 792.5 Unplanned flaring due to stepper valve Prepared contingency high GOR SI list malfunction on IWAG compressor. but did not implement due to perceived quick fix. 12/24/97 15:51:00 02:54 722.2 948.8 Unplanned IWAG S/D, adjusted & High GOR wells were SI to mitigate repaired fine system, made numerous flare. start attempts. 12/24/97 18:46:00 01:14 252.5 341.0 See above See above 12/25/97 00:34:00 03:26 816.5. 1,067.6 Unplanned IWAG S/D due to PLC card Shut in high GOR wells to mitigate failure. After repair the tube oil and flare. fuel control systems required repair. 12/25/97 04:02:00 01:58 266.4 395.8 See above. SI additional wells. 12/26/97 14:38:00 01:07 73.2 109.3 Unplanned event due to a process upset . A contingency plan was prepared but A PSV did not properly re-seat and it not implemented as the problem was took a while to find the problem. fmally solved. ~, ~~~ Jt~N 1:~ 199 '~kc"~~~ >~?~ +~ ~B~ (GP9~. (eC9t:'?9TliS~!'rrrr ?'~.?3C~'id3,'?~ BP Exploration Page 6 of 7 ® Milne Point, Alaska otioti9s 0923 Milne Point Unit • onthly Gas Flaring Incident Report For: Dec /1997 Flare Name: Flare 1 Planned Events Exceeding 1 hour OR Volumne Exceeding SUUU M5(:1•' Duration -Volume (MSCF) Start Time (hh:mm) Flare Assist Cause Comment 12/09/97 12:52:00 01:08 60.8 91.1 Planned flaring event during repair of Staged equipment & expedited repairs. leaking discharge valve gasket on Contingency high GOR SI list was C-5531B injection compressor. prepared but not implemented due to short repair duration. Flare Assist Unplanned Events <= 1 hoar 4,072.6 6,163.9 Unplanned Events > 1 hour 11,109.1 9,444.1 Planned Events <= 1 hour and not exceeding 5,000 MCF 0.0 0.0 Planned Events > 1 hour or exceeding 5,000 MCF 60,8 91.1 Unmetered Assist Gas 11,377.0 TOTAL FLARED VOLUME 15,242.5 27,076.1 MSCF 4=:~.~~ ~ ., 1998 BP Exploration Page 7 of 7 Milne Point, Alaska • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point December 5, 1997 Time and duration of incidents: 13:26 hrs - 1:19 min Flare Volume: 191 Assist Gas Volume: 264 • This event was an unplanned flaring event that occurred after the IWAG Injection Compressor was shutdown for repair of a fire and gas sensing device. High GOR production wells were shut-in in order to mitigate flaring. Once repairs were completed the IWAG injection compressor was returned to service and the flare was eliminated. • . Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point December 6, 1997 Time and duration of incidents: 07:05 hrs - 2:10 min Flare Volume: 624 Assist Gas Volume: 887 Time and duration of incidents: 09:46 hrs - 1:44 min Flare Volume: 211 Assist Gas Volume: 499 These unplanned flaring events occurred when the IWAG Injection Compressor shutdown several times as a result of a trabon lubrication failure. Maintenance crews were dispatched numerous times to correct the problem. High GOR production wells were shut-in in order to mitigate flaring. Once repairs were completed the IWAG injection compressor was returned to service and the flare was eliminated. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point December 7, 1997 Time and duration of incidents: 17:46 hrs - 1:14 min Flare Volume: 208 Assist Gas Volume: 348 This was an unplanned flaring event which occurred when the IWAG Injection Compressor shutdown as a result of a trabon lubrication failure. Maintenance crews were dispatched to correct the problem. High GOR production wells were shut-in in order to mitigate flaring. Once repairs were completed the IWAG injection compressor was returned to service and the flare was eliminated. • • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point December 9, 1997 Time and duration of incidents: 12:52 hrs - 1:08 min Flare Volume: 61 Assist Gas Volume: 91 This was a planned flaring event which occurred when we shut-down the C-5531-B injection compressor in order to repair a leaking discharge valve gasket. Maintenance crews were dispatched to correct the problem. Once repairs were completed the injection compressor was returned to service and the flare was eliminated. • Flaring Incident Report (exceeding i hour) BP Exploration -Milne Point December 16, 1997 Time and duration of incidents: 16:44 hrs - 9:31 min Flare Volume: 5982 Assist Gas Volume: 2525 • This was an unplanned flaring event which occurred when a CFP emergency shut down and power failure occurred. The shut down was initiated from a unit alarm in Module 58. The extended flaring duration occurred because of extensive safety related troubleshooting before and during the restart of the facility. Once the facility was restarted, the flaring was eliminated. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point December 23, 1997 Time and duration of incidents 21:21 hrs - 2:09 min Flare Volume: 680 Assist Gas Volume: 793 This event was an unplanned flaring event that occurred after the IWAG Injection Compressor shutdown due to stepper valve failure (engine fuel flow control). Maintenance made adjustments and repairs to get the engine /compressor back on line, however stepper valves will require additional attention in the future for reliable operation. Once repairs were completed the IWAG injection compressor was returned to service and the flare was eliminated. `'~„'~ i ,iAN ~ ,~; 1998 ~! ~ has ~~n~. ~cm~~i~ ch~~Q • • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point December 24, 1997 Time and duration of incidents 15:15 hrs - 4:hrs 8 min Flare Volume: 975 Assist Gas Volume: 1290 This event was an unplanned flaring event that occurred after the 1WAG Injection Compressor shutdown due to engine' fuel flow /speed control problems. Maintenance made adjustments and repairs to the engine fuel system, numerous start attempts were conducted, first start attempts-were conducted within an hour of the unit failure. High FGOR wells were shut in mitigate flaring. Once repairs were completed the IWAG injection compressor was returned to service and the flare was eliminated. ;~ 1 19~~ ,, ..~, e ~~;~~ • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point December 25, 1997 Time and duration of incidents 00:36 hrs - 7:hrs 13 min Flare Volume: 1297 Assist Gas Volume: 1777 • This event was an unplanned flaring event that occurred after the IWAG Injection Compressor shutdown due to a PLC processor card failure. The card was repaired and we then experienced problems re-starting the compressor unit. The Tube oil system caused problems and the electronic fuel controller system caused problems. Several (4) high FGOR wells were immediately shut in to mitigate flaring. As these wells worked out of the system and lowered the header pressure other wells picked up gas flow. Additional wells wire then shut in to mitigate flaring. Flaring was reduced to a minimum but required even more wells to be shut in to get completely off the flare. A total of 11 wells were shut in for this event. n Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point December 26, 1997 Time and duration of incidents 14:38 hrs - l :hrs 7 min Flare Volume: 73 Assist Gas Volume: 109 • This event was an unplanned flaring event that occurred when a flow surge from- the field caused a process plant upset and pressure spike. The pressure spike lifted ±he fuel gas separator safety valve and when the pressure returned to normal the safety valve did not re-seat. Personnel were busy re-setting and re-starting process equipment after the upset and there was a delay in finding this valve that had not re-seated properly. _ __ r ~ • • BP EXPLORATION BP Exploration (Alaska) Inc. 900 East Benson Boulevard P.O. Box 196612 Anchorage, Alaska 99519-6612 (907) 561-5111 December 15, 1997 State of Alaska Alaska Oil and Gas Conservation Commission 3001 Porcupine Drive Anchorage, AK 99501 Attn. Wendy Mahan: Attached are the Monthly Producer's Report of Gas Disposition for the month of November 1997 . Should you have any questions, please contact Bob Wilks at (907) 564-5670. Sincerely, ~~~ Paul D. Bly Manager, Volume, Royalty & Severance ~~ ,'~r ;~,< ~, Ck~~' ALASKA OIL AND GAS CONSERVATION CONII~lISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition Milne Point BP Exploration (Alaska) Inc. Milne Point Nov-97 Disposition Volume MCF* 1. Sold Fuel 15,459 2. Reinjected 610,910 3. Flared or vented less than 1 hour 4,800 4. Flared or vented greater than 1 hour 10,334 (Supplemental report required--See 20 AAC 25.235) 5. Pilot and Purge 2,010 6. Used for lease operations Fuel 247,824 Assist 30,327 7. Other TOTAL items 1-7 ~ 7C 921,664 Q 8. NGL gas equivalent produced ~' ~ ~""r1 ~ ~ 9. Purchased gas 0 0 ~ c~•a t.G 10. Transferred from: o GCS ~ ~'`.~ 11. Transferred to: Remarks: I hereby cert'fy Signature C~ that the /! • /~ foregoing is true and ~ Title correct to the Joy best of my knowledge. Date ~ Z/s/~ *Indicate contribution of each pool to total. Pool Name Code Percent KUPARUK 525100 94.9 SCH. BLUFF 525140 5.1 Official Use Only-Flaring Authorization>lhr. 1. Safety MCF 2. Lease MCF 3. Conserv. Purposes MCF Commissioner Date Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month folowing the month of disposition. Authority 20 AAC 25.235. • • Form 10-422 Rev. 4/95 ,. 12/04J97 1422 Flare Name: Flare 1 Milne Point Unit mthly Gas Flaring Incident Report • For: Nov /1997 ', np anne~c Events greater t an 1 )lour Duration -Volume (MSCF) StarYTime (hh:mm) Flare Assist Cause Comment 11/11/97 16:47:00 06:58 4,596.0 2,188.2 Unplanned flaring event occurred with Dispatched maintenance crews for l~, 9 ~ - Z3~•`f~S LSHH in CFP 1st stage suction emergency repairs. SI high GOR wells scrubber. Caused emergency shutdown B6, B9, B 10, B22, C4, C7, L6, E 11 for of mod 55 gas processing plant. Also flare relief. experienced unplanned 08 turbine s/d on low fuel that triggered load shed & slowed BOL efforts. 11/18/97 20:53:00 01:07 ~~•~..~ - 2Z~ 00 11/23/97 21:45:00 01:45 zl'.~S - z3' 3~ 11/23!97 23:32:00 01:58 23'32- Off' 30 11/24/97 04:49:00 01:11 ~~q'q~ - ob'.o~ 11 /24/97 06:01:00 02:44 11/24/97 09:17:00 0 ~28 aq~-~- EO`4~ 1 I /24/97 i 8:18:00 01:42 13'.1- Zo-~~ 116.7 228.8 Unplanned flaring event occurred in 12 high GOR wells were SI during conjunction with IWAG restart after prolonged IWAG s/d. Flaring occurred prolonged shutdown for repairs. while bringing wells BOL. Corrective action was to slow down well restarts until flaring ceased. 473.1 670.9 Unplanned flare event due to unplanne d Operator & critical maintenance shutdown of IWAG compressor on hig h personnel dispatched to IWAG module gas alarm in module. for inspection. Checked for leaks with gas sniffer & found leak on 1-1/2" neutron PSV isolation valve on 3rd stage. SI high GOR wells E06, E11, C09 for flare relief. 339.4 583.9 See above event. SI additional high GOR wells L06 and C03. 148.9 275.7 See above. Still working on IWAG SI high GOR wells B09 and B10 for repair. additional flare relief. 311.9 597.2 See above. See above. Convened MPU on-site supervisors for opportunistic planned maintenance during prolonged IWAG shutdown. 164.7 319.7 See above. See above. 235.3 211.6 BP Exploration Page 8 of 9 Milne Point, Alaska 12/04197 14:22 Milne Point Unit ~thly Gas Flaring Incident Report • For: Nov /1997 Flare Name: Flare 1 !P annl ed Events xceE euing r our OR Dolumne xcee mg 30~OZVISCF --- Duration. -Volume (MSCF) Start Time (hh:mm) Flare Assist Cause Comment 11/13/97 09:20:00 02:55 09', Zc ' /Z•, i5 11/13/9712:31:00 03.14 Iz~ 31 - l S' 45' 11/13/97 1 5:46 00/7` 01:29 11/23/97 09:27:00 02:18 ~~'2~ - 11:45 11/23/9711:46:00 02:59 I1'~~tb- 14.x+5 I 1 /24/97 ~ i .:~4~6:00 0~ 1:14 11/24/9713:02:00 05:13 13'.oa- i8'~Is 606.3 1,025.0 Planned flaring event to repair #2 Initiated shutdown for safeout & cylinder knocking. Also performed repairs. rnisc opportunity maintenance on ' compressor unit during this shutdown. 630.4 1,146.8 See above. SI high GOR wells B10, C26, E06, E11 for flare control during repairs. 313.4 481.6 369.9 822.2 Planned flaring event associated with Operator observed misfiring in #8 shutdown of C pad IWAG compressor. cylinder on IWAG engine. SD for Initiated shutdown for quick turnaround inspection & repair. repairs. 445.0 894.9 See above. SI high GOR wells E06, E11 and C09 for flare relief during upset. Repaired compressor &RTS. Well BOL after compressor RTS. 150.8 289.1 Planned event for Big A/B repairs. 1,432.3 1,647.9 Flare Assist Unplanned Events <= 1 hour 4,799.5 9,943.9 Unplanned Events > 1 hour 6,386.0 5,076.0 Planned Events <= 1 hour and not exceeding 5,000 MCF 0.0 0.0 Planned Events > 1 hour or exceeding 5,000 MCF 3,948.1 6,307.5 Unmetered Assist Gas 11,010.0 TOTAL FLARED VOLUME 15,133.6 32,337.5 MSCF BP Exploration Page 9 of 9 Milne Point, Alaska • BPX BLACK SMOKE REPORT MILNE POINT Facility: MILNE POINT Report # 97-16 BLACK SMOKE FLARING Date and Time of Flaring: Date: November 3, 1997 Time: 15:12 hrs Duration of Black Smoke Produced: hrs 16 min Was the Black Smoke Intermittent?: Yes X No Initial Cause for Black Smoke Event: (identify any AOCP permitted equipment, if involved) Shutdown C-5501-A gas lift compressor due to emergency compressor maintenance. Glycol leak was discovered on the cooling system of the #3 cylinder. Flared gas off the Slugcatcher while repairs were completed. Action Taken to Stop Black Smoke Flaring: Completed Glycol leak repair on cooling system of #3 cylinder. Once repairs were completed,`the Gas Lift Compressor was returned to service and the flare was eliminated. Type of Material Burned: (Check One) Gas: X Other: Approximate Volume Flared which Created Black Smoke: 297 Black Smoke was Result of: (Check One) Flare Relief Valve: Controlled Slowdown: X MSCF Ambient Air Temperature: 21 F Wind Velocity : 36-41 mph Dir: E Other: Time Taken: 16:20 hrs When black smoke is produced for more than three (3) minutes, notification must be made within 24 hours to the Alaska Department of Environmental Conservation. NOTIFICATION: By direction of BPX Milne Production Supervisor, notification was made to ADEC by: ^ Phone: (907) 465-5100 ADEC ^ Phone: (907) 271-4336 (answering machine after hours/weekends) X FAX: (907) 465-5129 (confirmation report must be attached) Notification Made By Henry Harrington 11/3/97 16:30 (Name) (Date) (Time) Milne Point Production Supervisor Date FAX To: Allison Cooke, Environmental Compliance, 564-5020 • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point November 11, 1997 Time and duration of incidents: 16:47 hrs - 6:58 min Flare Volume: 4,596 Assist Gas Volume: 2,188 An unplanned flaring event occurred when a LSHH in the ls` stage Suction Scrubber tripped and caused an emergency shutdown of the gas compression system in Module 55: Maintenance crews were dispatched to correct problem with high level in Suction Scrubber. Level Control Valve on the ls` stage Suction Scrubber failed, and was unable to dump liquid level in vessel. During this same period the 08 turbine shutdown on a low pressure liquid fuel alarm which resulted in a load shed condition. Maintenance crews were dispatched to resolve problem with 08 turbine. High GOR Production wells (B6, B- 9, B-10, B-22, C-4, C-7, L-6, and E-11) were shut-in to mitigate flaring. Once the problem with the turbine was resolved, gas compressor's were returned to service and the flare was eliminated. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point November 13, 1997 Time and duration of incidents: 09:20 hrs - 2:55 min Flare Volume: 606 Assist Gas Volume: 1,025 • Time and duration of incidents: 12:31 hrs - 3:14 min Flare Volume: 630 Assist Gas Volume: 1,147 Time and duration of incidents: 15:46 hrs - 1:29 min Flare Volume: 313 Assist Gas Volume: 482 Three planned flaring events occurred when the 1WAG Injection Compressor was shutdown due to a knock in the #2 cylinder of the compressor. Maintenance crews organized and completed repair of the compressor in an orderly fashion. High GOR wells were shut-down to mitigate flaring. Once the problem with the compressor cylinder was corrected the compressor was returned to service and the flare was eliminated with no further incident. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point November 18, 1997 Time and duration of incidents: 20:53 hrs - 1:07 min Flare Volume: 117 Assist Gas Volume: 229 • This event was an unplanned flaring event that occurred after the IWAG Injection Compressor was restarted after planned maintenance. The production wells were brought on slightly too fast and the Central facilities incoming gas volume temporarily exceeded capacity. Start up of additional high GOR wells was deferred until gas volumes subsided so that the flaring could be mitigated. Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point November 23, 1997 Time and duration of incidents: 09:27 hrs - 2:18 min Flare Volume: 370 Assist Gas Volume: 822 Time and duration of incidents: 11.:46 hrs - 2:59- min Flare Volume: 445 .Assist Gas Volume: 895 • Two planned flaring~events occurred when the IWAG Injection Compressor was shutdown due. to a knock in the #2 cylinder of the compressor. Maintenance crews organized and completed repair of the compressor in an orderly fashion. High GOR wells were shut-down to mitigate flaring. Once the problem with the compressor cylinder was corrected the compressor was returned to service and the flare was eliminated with no further incident. Time and duration of incidents: 21:45 hrs - 1:45 min Flare Volume: 473 Assist Gas Volume: 671 This was an unplanned flaring event that occurred due to a gas leak inside the module that houses the IWAG Injection Compressor. The machine was immediately shut down to repair the leak. High GOR wells were shut in to mitigate flaring. SENT BY~BPX-MPOC ;11- 7-97 742 BPX-MILNE POINT 907 276 7542;# 1/ 1 ~ • • I B,PX 1V~itne Point Linit Event N~tificahan a_ Fire, Stipulation 1.14.1 ___ . d, Uil or Ytatardous Substance Stipulation a.t0.i _h_ Serious Accidents, Stipulatlai 1.'1').t _ _ dis;ckwrge > 5~ gak c Threats M Pipekine Ihtegrity 1.3.3 _ ,~ dischrr};e ~ 55 gal > 1 gal uru,cheduled ~luw down diycfiar+e to sect ary > 55 ~I (:~ 2U% zeduttion) .X ._ Aarceou~ emi~.gi~5 _ unsclicd~drd Shut Down other 2. Report No. 001 3. Notification by: 659-(i3fi1 4. Tune of Notification: 11-2-97 Sinor, Jocl 11 /7197 08(X) 5. Fax To: (~. SIG ATUILE: AOC:CC (907) .276-7542 7. tvent Location: :vent Date anal Time: iV1TLNE PU1NT K-Pf1D 11 /2/97 0600 9. Evectt Description (Attach Additional Pages if Needed) ' Who, What, Why: 2" valve body gasket failed on pil; launcher bypaws ran pipeline from K-Pad to'11+Iilne Point CFP Facility_ Approximately 2t)O,OOi) cubic fta~et of has wc+re' r+tic~aed. to abnns~phere. Y+t>lume is based. on dimensions of the paint of leakrbe (1" x 0-125") over an estimated R hour time rwriod_ No oil or produced water spill occurred. 10. Action Taken Attach Additicutal Pa e:+ if Needed Well ad shut down. Pi line isolated and depressurized. Defective valve rr. laced with value from different manufa~^turer. Put pipeline back into service. Failed valve .is bein set to manufacturer for failure analysis. ~ For Receiving Office Use ~ }~ ~ ... 'iti` f su ~, ~' `<~~ ' , ~x s..;~ ;t)1?5. uJ('3il;SSIUI"i • BP EXPLORATION November 14, 1997 State of Alaska Alaska Oil and Gas Conservation Commission 3001 Porcupine Drive Anchorage, AK 99501 Attn. Wendy Mahan: • BP Exploration (Alaska) Inc. 900 East Benson Boulevard P.O. Box 196612 Anchorage, Alaska 99519-6612 (907) 561-5111 Attached are the Monthly Producer's Report of Gas Disposition for the month of October 1997 . Should you have any questions, please contact Bob Wilks at (907) 564-5670. Sincerely, ~~ Paul D. Bly Manager, Volume, Royalty & Severance ,. '; ,_:r !~ J,~,' o_ ~ s~ ~ ~ ~~ ~ h ...~ C tQ = 'V ALASKA OIL AND GAS CONSERVATION CONIl~lISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION lity e Point Operator Field(s) BP Exploration (Alaska) Inc. Milne Point Disposition Volume MCF* 1. Sold Fuel 15,859 2. Reinjected 649,235 3. Flared or vented less than 1 hour 2,561 4. Flared or vented greater than 1 hour (Supplemental report required--See 20 AAC 25.235) 6,156 5. Pilot and Purge 2,077 6. Used for lease operations Fuel Assist 250,658 24,381 7. Other TOTAL items 1-7 950,927 8. NGL gas equivalent produced 9. Purchased gas 10. Transferred from: 11. Transferred to: Remarks: I hereby certify that the foregoing is true and Signature //. Title '~"C7~• correct to the best of my knowledge. V(!r~ ic(Jr Q J~~ Date ~,~ ~ (Month/Year of Disposition Oct-97 *Indicate contribution of each pool to total. Pool Name Code Percent KUPARUK 525100 94.7 SCH. BLUFF 525140 5.3 Official LTSe Only-Flarzng Authorization>1 hr; 1. Safety MCF 2. Lease MCF 3. Conserv. Purposes MCF Commissioner Date Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month folowing the month of disposition. Authority 20 AAC 25.235. • • Form 10-422 Rev. 4/95 nio4i9i t9a2 Milne Point Unit mthly Gas Flaring Incident Report For: Oct /1997 Flare Name: Flare 1 ITn~anne vents greater t an our Duration -Volume (MSCF) Start Time (hh:mm) Flare Assist Cause Comment 10/06/97 ] 3:08:00 01:22 392.0 560.1 Unplanned flaring event occurred when l~ ~g _ ~~3~ C-2605 compressor (C pad IWAG) shutdown. Shutdown was triggered by H-2601 heater s/d on fire eye failure. The heater heats fuel gas for feed to WAG compressor. 10/21/97 17:37:00 03:23 1,761.0 1,368.7 Unplanned flaring event due to }~ 3~ ,. ZI oC~ unplanned shutdown on PU-0801 turbine on flame-out detection. Flaring occurred as part of load shed scheme that s/d C-5501/11A compressors. 10/23/97 15:47:00 01:13 89.5 508.4 Unplanned flaring event in conjunction 1 ~~~ _ t~ ~ o with restart of C-2610 compressor. A gas leak was discovered during restart & req'd s/d for repair. Automation & electrical problems were also encountered during restart. 10/23/97 17:19:00 05:26 721.2 1,607.6 See above. l~ i~j- 2z45' 10/24/97 05:16:00 01:14 167.1 393.7 Unplanned event occurred when C pad r,~ IlO " ~ b3 O IWAG compressor (C-2610) shutdown on high vibration. Occurred about 3 hours after post-maintenance restart. Promptly repaired heater & returned compressor to service. Left high GOR wells B15 & C04 SI during upset. Made contingency SI list. Production was not SI because it was believed to be a quick turnaround. Troubleshooting took longer that first projected & turbine was allowed to run w/out load for awhile before restarting compressors. Deternmined that flaring had become "unplanned" after compressor restart problems were encountered. B 10, B22, E 11 remained SI. Maintenance crews remained on location until compressor was RTS. High GOR wells C04, C07, E06, E22 were SI at 18:00 hrs for add'I flare relief during "un lanned" hase of this event. `Dispatched crew to C pad & w out incident. Re-shutin high GOR wells that were down for flare control during previous IWAG activity. Did not bring any add'1 wells on until flare out. BP Exploration Page 6 of 7 Milne Point, Alaska 11/04/7 1'x:52 Milne Point Unit • mthly Gas Flaring Incident Report For: Oct /1997 Flare Name: Flare 1 anne vents xcee mg our o umne xcee mg Duration -Volume (MSCF) Start Time (hh:mm) Flare Assist Cause 10/15/97 08:27:00 08:33 o P~~,~ -- ~ ~ o 0 10/21/9714:03:00 01:27 1-03 - ~S3 0 10/23/97 07:27:00 03:33 d~ 2 ~ -- >< a-e O 10/23/97 li ~002001~~0~:58 10/23/9713:01:00 01:29 i3ol - l't3fl Comment 1,558.6 3,283.8 This was a planned flaring event due to Repaired valves & returned compressor planned maintenance/repairs on to service. SI following wells for flare cylinder #1 valves. Modelling relief: B03, 04, 06, 09 ,10, 15, 20, 21, indicated that compressor was C03, 04, O5, 07, 09, 14, L06. Saw performing at low efficiency & bad significant increase in compressor valves were believed to be cause. effienciecy after RTS. 77.8 116.2 Brief planned flaring event that Repaired leak &RTS. occurred when C-5531B was s/d to repair cylinder #4 glycol leak. 759.8 1,073.8 Following events occurred in Initiated shutdown of C-2610 for conjunction with C-2610 compressor preventative maintenance. SI high planned maintenance/repair on GOR wells B10, B22 & E11 for flare discharge valve of 2nd stage. Operating relief during this activity. temps were running a bit high & impacting operating efficiency. 390.2 528.7 See above. 238.6 574.4 See above. • Flare Assist Unplanned Events <= 1 hour 2,561.5 5,065.3 Unplanned Events > 1 hour 3,131.0 4,438.6 Planned Events <= 1 hour and not exceeding 5,000 MCF 0.0 0.0 Planned Events > 1 hour or exceeding 5,000 MCF 3,025.0 5,577.0 Unmetered Assist Gas 11,377.0 TOTAL FLARED VOLUME 8,717.4 26,457.9 MSCF BP Exploration Page 7 of 7 Milne Point. Alaska U BP EXPLORATION October 15, 1997 State of Alaska Alaska Oil and Gas Conservation Commission 3001 Porcupine Drive Anchorage, AK 99501 Attn. Wendy Mahan: • BP Exploration (Alaska) Inc. 900 East Benson Boulevard P.O. Box 196612 Anchorage, Alaska 99519-6612 (907) 561-5111 Attached are the Monthly Producer's Report of Gas Disposition for the month of September 1997 . Should you have any questions, please contact Bob Wilks at (907) 564-5670. Sincerely, ~~ //" Paul D. Bly Manager, Volume, Royalty & Severance ALASKA OIL AND GAS CONSERVATION CONII~RISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition Milne Point BP Exploration (Alaska) Inc. Milne Point Sep-97 • • Disposition Volume MCF* 1. Sold Fuel 14,777 2. Reinjected 647,990 3. Flared or vented less than 1 hour 3,872 4. Flared or vented greater than 1 hour (Supplemental report required--See 20 AAC 25.235) 7,552 5. Pilot and Purge 2,016 6. Used for lease operations Fuel Assist 230,766 29,440 7. Other TOTAL items 1-7 '~''' ~-,._, 936,413 8. NGL gas equivalent produced ~;~"` ~ w. ' :~ '.~"a`.. 9. Purchased gas ~~- _ „~ 10. ~,.,,~ Transferred from: _ e k i, 11. Transferred to: Remarks: I hereby certify that the foregoing is true and correct to the best of my knowledge. J M~K. /GL., 1Z0~( d~, Signature ~~ ~(~ Title d ~/. Date ~~ /3 ~ *Indicate contribution of each pool to total. Pool Name Code Percent KUPARUK 525100 94.5 SCH. BLUFF 525140 5.5 Official Use Only-Flaring Authorization>1 hr: 1. Safety MCF 2. Lease MCF 3. Conserv. Purposes MCF Commissioner Date Note: All volumes must be corrected to pressure of 14.65 Asia and to a temperature of 60 degrees F. Report due by the 20th of the month folowing the month of disposition. Authority 20 AAC 25.235. Form 10-422 Rev. 4/95 10/03/97 1x:51 Milne Point Unit . l~thly Gas Flaring Incident Report For: Sep /1997 Flare Name: Flare 1 np anne vents greater t an our ----- Duration =Volume (MSCF) Start Time (hh:mm) Flare Assist Cause 237.7 542.7 Unplanned shutdown on C pad IWAG compressor due to gas leak in compressor building. 683.0 1,589.3 Unplanned shutdown on C pad IWAG compressor due to low flow problems with Trabon Tube oil pump system. 09/11/9712:54:00 01:21 X254 - I1{ 1 S 09/17/97 08:23:00 03:52 Q~Z3 - I L 15 09/17/9718:18:00 03:57 113- ~z~S 09/ 18/97 00:07:00 01:23 ooo~ ^ a13c~ 09/18/97 03:51:00 01:24 o?~~ ~ ~ oSIS 09/18/97 08:43:00 01:02 C$q3 -O~i-¢S.. 09/18/9712:07:00 03:23 Izo~7- IS3~ 09/18/97 22:16:00 01:59 z z lb - c7a l.'j- 09/19/97 00:36:00 01:09 oo3b - o--tS 09/19/97 04:06:00 03:54 155.7 312.3 Unplanned flaring believed to be due to excessive gas flashing off 2nd and 3rd stage separators. 59.4 118.5 Continued flaring off 2nd & 3rd stage separators. Believed to be due to excessive flash gas. 50.7 101.4 Flaring persisted off 2nd & 3rd stage. 37.6 74.9 138.3 276.2 See above. 63.0 125.9 Unplanned flaring (low volumes) off 2nd & 3rd stage. 41.6 83.0 Unplanned flaring (low volumes) off 2nd & 3rd stage. 158.1 315.8 Three unplanned shutdowns on C pad IWAG compressor due to low-flow problems with Trablon lube oil system. ..731.6 See above. 583.6 See above. 444.3 Unplanned shutdown on C pad IWAG compressor due to bad 02 sensor. 09/19/97 09:43:00 02:32 o~,~t3 -I vS620.3 09/19/9712:39:00 01:36iz39-iaiS 621.2 09/21 /97 22:24:00 01:06 348.6 za24 - z33 0 09/24/97 09:43:00 01:32 vg~w ~ ,. ~ 115 09/24/9711:31:00 01:29 1~3r-t3oo 09/25/97 09:21:00 02:39 09/26/97 00:16:00 03:14 oolE, -033 509.5 623.5 Unplanned shutdown on C pad IWAG compressor due to a fin fan bearing failure that initially shutdown the compressor on high vibration. 208.7 553.6 (See above) Comment Inspected & tightened fittings and returned compressor to service. SI high GOR wells E11, E22 & C14 for flare relief. Trabon Tube oil problems were corrected; however, compressor was left shut-in to perform planned shutdown work related to the commissioning of the new gas injection pipeline to L/F pads. Flaring appeared to be insensitive to gas cutbacks in system. Had to troubleshoot problem. SI high GOR wells B10, B15, C13, C 14. Expedited C-5531 repairs. This is not a normal flaring occurence at MPU and was believed to be due to unusually low processing temps on 1st stage slug catcher (110 vs normal 130 F) causing add'1 carryover to 2nd & 3rd stage. Postponed H-2603 heater repairs. Refilled glycol into vessel and returned heater to service. Brought up processing temps throughout the day. Flare mitigation throughout day as 1st stage processing temps increased. Minor flaring while H-2603 building up to temperature. Flaring ceased after H-2603 and C-5531 RTS. High GOR wells B10, B15, B22; E11, C13, C14 remained SI for flare control. High GOR wells B10, B15, B22, E11, C 13, C T4 remained SI throughout day for flare control. See above See above. Repaired 02 sensor & returned to service. High GOR well CI4 SI for flare control. Dispatched maintenance crew to expedite repair. SI 11 high GOR wells (B09, 10, 22, C03, 09, 13, 14, K33, E11, E22) for flare relief. Returned wells to production after compressor RTS. 499.4 1,097.7 Unplanned shutdown on C pad IWAG Completed repairs &RTS. High GOR compressor. Due to fin fan cooler well C14 remained SI for flare control. vibration alarm while repair work was being performed in the associated cooler to repair the bearing. 1,124.2 1,300.7 Two unplanned flaring events due to C Still troubleshooting tube oil pressure pad IWAG compressor due to low tube problems. High GOR well C 141eft SI oil pressure switch failure. until IWAG stabilizes. BP Exploration Page 7 of 9 Milne Point, Alaska 10!03/97 i4al Milne Point Unit l~thly Gas Flaring Incident Report • For: Sep /1997 Flare Name: Flare 1 np anne ~ vents greater t an our ~ ~. Duration -Volume (MSCF) Start Time (hh:mm) Flare Assist Cause Comment 09/26/97 17:07:00 02:08 293.8 838.1 Unplanned pad ESD at E pad triggered SI high GOR wells B09, B 10, B22, I~o7 , ~ 9,S E pad injection compressors Cl4 during pad s/d. High GOR wells (C-5531AB) to SI pending pad BOL. E11 & E22 were SI during S/D for add'1 flare relief. Took opportunity while S/D to perform planned repairs on C-5531A compressor. RTS after pad BOL. 09/26/97 19:57:00 01:03 37.1 92.1 Unplanned IWAG shutdown (see High GOR wells B09, B10, B22, C14 i q s ~ - zl o o above). remained SI until IWAG RTS. 09/27/97 06:08:00 01:22 291.4 558.7 Three unplanned flaring events due to High GOR well C 14 remains SI until ob o 8 - 07 3 o unplanned shutdowns on C pad IWAG IWAG stabilizes. Still troubleshooting compressor. recurring IWAG problems. 09/27/97 15:14:00 01:01 256.1 413.5 (See above) Programmed PLC "trap" to detect i S ~ 4- 1 {,1 S shutdown source. 09/27/97 20:29:00 01:16 371.7 486.2 (See above) Found compressor vent valve V-2601 2A 2..9 - Z i 4~ limit switch intermittently in fault sending false signal to Trabon Tube oil system to shutdown. Repaired fault & RTS. 09/29/97 17:29:00 03:01 250.4 624.7 Emergency repairs required on Maintenance crews were dispatched to l~ 2q ,, ~®~~ C-5531A injection compressor to fix correct problem. High GOR wells were knock in #4 cylinder. shut in. BP Exploration Page 8 of 9 Milne Point, Alaska loia3i9~ 14at Milne Point Unit l~thly Gas Flaring Incident Report • For: Sep /1997 Flare Name: Flare 1 anne vents xcee mg our o umne xcee mg - --- Duration -Volume (MSCF) Start Time (hh:mm) Flare Assist Cause Comment 09/17/97 12:17:00 03:43 382.4 1,007.4 Planned shutdown on C pad IWAG SI high GOR wells B10, B15, C13, compressor for F/L gas injection C14 for flare relief during SI. pipeline commissioning. 09/17/97 16:10:00 02:05 112.2 224.8 See above See above Flare Assist Unplanned Events <= 1 hour Unplanned Events > 1 hour Planned Events <=1 hour and not exceeding 5,000 MCF Planned Events > 1 hour or exceeding 5,000 MCF Unmetered Assist Gas TOTAL FLARED VOLUME 3,872.0 7,325.4 7,057.5 11,888.4 0.0 0.0 494.6 1,232.3 11,010.0 11,424.1 31,456.1 MSCF BP Exploration Page 9 of 9 Milne Point, Alaska • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point September 29, 1997 Time and duration of incidents: 17:29 hrs - 3 hrs O1 min Flare Volume: 250 Assist Gas Volume: 625 • An unplanned flaring event occurred when the C-5531-A injection compressor experienced a knock in the #4 cylinder. Compressor was shut-down and maintenance crews were immediately dispatched to correct problem. High GOR wells were shut-in to mitigate flaring. Once the injection compressor was returned to service, the flare was eliminated with no further incident. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point September 19, 1997 Time and duration of incidents: 00:36 hrs - 1 hrs 9 mins Flare Volume: 42 Assist Gas Volume: 83 Time and duration of incidents: 04:06 hrs - 3 hrs 54 mins Flare Volume: 158 Assist Gas Volume: 316 Time and duration of incidents: 09:43 hrs - 2 hrs 32 mins Flare Volume: 620 Assist Gas Volume: 732 Time and duration of incidents: 12:39 hrs - 1 hrs 36 mins Flare Volume: 621 Assist Gas Volume: 584 • One brief unplanned shutdown due to C-5531 out of service for repair. Three unplanned shutdowns on C pad IWAG compressor (C-2605). All IWAG shutdowns were due to problems with the Trabon Tube oil system. Emergency IWAG repairs were performed throughout the day and flaring ceased. High GOR wells B 10, B 15, C 13, C 14 and E 11 remained shutin throughout the day to mitigate excessive flaring. u Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point September 18, 1997 Time and duration of incidents: 00:07 hrs - 1 hr 24 mins Flare Volume: S9 Assist Gas Volume: 118 Time and duration of incidents: 03:51 hrs - 1 hrs 24 mins Flare Volume: 51 Assist Gas Volume: 101 Time and duration of incidents: 08:43 hrs - 1 hrs 2 mins Flare Volume: 112 Assist Gas Volume: 225 Time and duration of incidents: 12:07 hrs - 3 hrs 23 mins Flare Volume: 138 Assist Gas Volume: 276 Time and duration of incidents: 22:16 hrs - 1 hrs 59 mins Flare Volume: 63 Assist Gas Volume: 126 • Unplanned flaring events persisted from previous day. Repairs were ongoing throughout the day on C-5531 compressor. Problems were still attributed to low processing temps on 1st stage slug catcher & subsequent gas carryover to 2nd and 3rd stage separators. High GOR wells B 10, B 15, C 13, C 14 were left SI from previous day. In addition, high GOR wells B22 and El l were also SI. Intermittent flaring persisted until the front end processing temps were restored during the afternoon. H-2603 heater was restarted at 03:30 hours and gradually brought up to temperature during the day. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point September 17, 1997 Time and duration of incidents: 08:23 hrs - 3 hrs 52 mins Flare Volume: 683 Assist Gas Volume: 1,589 Time and duration of incidents: 12:17 hrs - 3 hrs 43 mins Flare Volume: 382 Assist Gas Volume: 1,007 Time and duration of incidents: 16:10 hrs - 2 hrs 5 mins Flare Volume: 112 Assist Gas Volume: 225 Time and duration of incidents: 18:18 hrs - 3 hrs 57 mins Flare Volume: 156 Assist Gas Volume: 312 Four events during the day. An unplanned shutdown occurred on the C pad IWAG compressor due to problems with the Trabon lube oil pump system. Repairs were performed and the shutdown was extended to perform lap nned commissioning work on the new gas injection pipeline to L/F pads. The second two flare events were unplanned and due to excessive gas flashing off the 2na and 3ra stage separators in conjunction with an unplanned shutdown on the C-5531 compressor. Flaring was in low volumes & seemed to be insensitive to cutting high GOR production. This is an unusual occurrence at MPU and hence did not fit into any of our customary optimization schemes for reducing flare volumes. After a bit of troubleshooting, it was determined that the carryover problems were due to unusually low processing temps on the 1St stage slug catcher. Low processing temps were caused by a planned H-2603 heater shutdown for repair. The heater was returned to service pending C-5531 repairs and the flaring subsided. High GOR wells B 10, B 15, C 13, C 14 remained shutin throughout the day to mitigate excessive flaring. Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point September 24, 1997 Time and duration of incidents: 09:43 hrs - 1 hrs 32 min Flare Volume: 509 Assist Gas Volume: 623 Time and duration of incidents: 11:31 hrs - 1 hrs 29 min Flare Volume: 209 Assist Gas Volume: 554 Two unplanned flaring events occurred when the C-Pad IWAG injection shut-down due to a fin fan bearing failure which initially shut-down the compressor on high vibration. Repairs were performed by maintenance crews to return the injection compressor to service as soon as possible. Nine high GOR production wells were shutdown in order to mitigate flaring. Once the IWAG injection compressor was returned to service, the flare was eliminated with no further incident. Production wells were returned to service after the compressor was checked out and back to normal operation. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point September 25, 1997 Time and duration of incidents: 09:21 hrs - 2 hrs 39 min Flare Volume: 499 Assist Gas Volume: 1,098 • An unplanned flaring event occurred when the C-Pad IWAG injection compressor shut- down due to a fin fan cooler vibration shut-down alarm which occurred while repair work was being performed in the associated cooler to repair the bearing . Once the IWAG injection compressor was returned to service, the flare was eliminated with no further incident. Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point September 21, 1997 Time and duration of incidents: 22:24 hrs - 1 hrs 6 rains Flare Volume: 349 Assist Gas Volume: 444 • Unplanned shutdown on C pad IWAG compressor (C-2605). Problems with the Trabon Tube oil system persist. High GOR well C 14 remained SI until flaring stopped. Flaring Incident Report (exceeding 1 hour} BP Exploration -Milne Point September 11, 1997 Time and duration of incident: 12:54 hrs - 1 hrs 21 mins Flare Volume: 238 Assist Gas Volume: 543 • This was an unplanned flaring event as a result of an unknown immediate need ~o shut down the gas re-injection compressor on C-pad for repairs. A gas leak was discovered in the compressor building that required inspection/tightening of fittings. It was necessary to shut down the compressor to safely work on the'associated piping and fittings. The work was expedited and the compressor returned to service as soon as possible. To mitigate flaring, high GOR wells were shut in. n Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point September 27, 1997 Time and duration of incidents: 06:08 hrs - 1 hrs 22 min Flare Volume: 291 Assist Gas Volume: 559 Time and duration of incidents: 15:14 hrs - 1 hrs O1 min Flare Volume: 256 Assist Gas Volume: 414 Time and duration of incidents: 20:29 hrs - 1 hrs 16 min Flare Volume: 372 Assist Gas Volume: 486 Three unplanned flaring events occurred when the C-Pad IWAG injection compressor shut-down due to trabon lubricating system failure. High GOR wells were shut-in to mitigate flaring. Once the IWAG injection compressor was returned to service, the flare was eliminated with no further incident. • BP EXPLORATION September 15, 1997 State of Alaska Alaska Oil and Gas Conservation Commission 3001 Porcupine Drive Anchorage, AK 99501 Attn. Wendy Mahan: • BP Exploration (Alaska) Inc. 900 East Benson Boulevard P.O. Box 196612 Anchorage, Alaska 99519-6612 (907) 561-5111 Attached are the Monthly Producer's Report of Gas Disposition for the month of August 1997 . Should you have any questions, please contact Bob Wilks at (907) 564-5670. Sincerely, G%G~ Paul D. Biy Manager, Volume, Royalty & Severance ALASKA OIL AND GAS CONSERVATION CONIl~lISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition Milne Point BP Exploration (Alaska) Inc. Milne Point August, 1997 "s c.~ Disposition Volume MCF* *Indicate contribution of each pool to total. Pool Name Code Percent KUPARUK 525100 93.4 SCH. BLUFF 525140 6.6 • 1 ~J ~~ ,~ 'c> .-4 ,> 4r ,4:.e s w [::- r,7 1. Sold Fuel 13,378 2. Reinjected 566,829 3. Flared or vented less than 1 hour 9,738 4. Flared or vented greater than 1 hour (Supplemental report required--See 20 AAC 25.235) 26,561 5. Pilot and Purge 2,077 6. Used for lease operations Fuel Assist 201,948 63,050 7. Other TOTAL items 1-7 883,581 8. NGL gas equivalent produced 9. Purchased gas 10. Transferred from: a~"^ ~.~: ~~1. Transferred to: : emarks: d I hereby cert++i/nf~y that theuuf//oregoing is true and correct to the best of my knowledge. .. 1`~~ 1, Cam/ M~ /o~~ ~~ ~~.~. 9 ~~•~'~ ~~ignature Title Date Form 10-422 Rev. 4/95 Of facial LTse Only-Flaring Authorization>1 hr: 1. Safety MCF 2. Lease MCF 3. Conserv. Purposes MCF Commissioner Date Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month folowing the month of disposition. Authority 20 AAC 25.235. o9inv9~ lo:t6 Milne Point Unit • ~ nthly Gas Flaring Incident Report For: Aug /1997 Flare Name: Flare 1 np anne vents greater t an our Duration -Volume (MSCF) Start Time (hh:mm) Flare Assist Cause Comment 08/07/9710:50:00 02:25 274.7 748.6 08/09/97 01:17:00 02:13 271.4 162.4 Unplanned flaring event while bringing Problems restarting IWAG compressor. field BOL after TAPS slowdown & High GOR production remained SI for IWAG maintenance/construction. flare relief. 08/09/97 03:31:00 04:44 1,015.8 1,365.5 08/20/97 17:12:00 O l :18 633.6 504.4 Unplanned flaring event due to F pad High GOR wells B 10 and E 11 shutdown. Received pressure surge in remained SI for flare relief. Flaring plant during pad restart. subsided after pad BOL & stabilized. 08/24/97 14:01:00 01:14 80.4 160.8 Unplanned flaring during several restart Several high GOR wells at B, C & E attempts on C pad IWAG compressor. pads remained SI until IWAG compressor was RTS and stabilized. 08/25/97 01:17:00 02:58 198.2 296.8 Unplanned flare event due to Flare event started after unplanned s/d unexpected increase in formation gas to on IWAG compressor. However, process in CFP. flaring unexpectedly continued after all gas processing equipment was RTS. Ordered calibrations of critical gas equipment & cycling of wells thru-test separator. 08/25/97 04:31:00 01:29 99.0 148.6 See above. Discovered anomalous increase in E22 produced gas, believed. to be due to gas breakthrough from IWAG injection. Following other wells were SI during flare events: B 10, C02, E 11, E09. 08/25/97 07:32:00 01:43 109.8 164.3 See above. SI E22 and flaring ceased. 08/29/97 16:01:00 01:14 97.0 514.8 Unplanned flaring event due to Replaced defective 02 sensor & 3 emergency shutdown of C pad IWAG fouled spark plugs. SI high GOR wells compressor. B09, 10, 22, C 13, C 14, E22 for flare relief. BP Exploration Page 1 i of 17 Milne Point. Alaska 09iQ1/97 I,o:lb Milne Point Unit • l~thly Gas Flaring Incident Report For: Aug /1997 Flare Name: Flare 1 anne vents xcee ing our o umne xcee ling Duration -Volume (MSCF) Start Time (hh:mm) Flare Assist Cause 08/01/97 21:55:00 04:20 370.2 274.2 Planned flaring event for maintenance ~ 55 .d ~- I ~ and expansion tieins on C pad IWAG compressor. 08/02/97 02:21:00 2:24 oa~l' ®44, 08/02/97 OS~:~~~O~o, 3004:58 08/02/9712:01:00 54:44 ~~ 12' ~1- ~'~1~ 08/08/97 04:34:00 01:26 c~~',3q-, a6' 0O a~'. S-t - to ~ I S 08/08/97 08:54:00 01:21 08/22/97 08:39:00 09:51 08'. ~q ., i 3' 3 0 08/23/97 07:16:00 03:29 ~7' I b - 1~' q5 08/23/9712:42:00 07:33 I Z ", 9 Z- ~o', I S v3:"~3 ~ao`'~e1 08/23/97 23:33:00 01:57 08/30/97 06:01:00 01:44 ob'. ~ f ,~ ~-~ : ~'~ 08/30/9714:46:00 01:14 }~,'~~, 3r~ ' C> v 342.1 609.5 See above. Comment Work was performed in conjunction with TAPS slowdown to mitigate flare volumes. Left high GOR C pad production SI during post-TAPS rampup for add'1 flare relief. Assist gas utilized on all planned flaring to prevent black smoke. 1,089.2 1,029.9 See above. 13,825.1 17,969.1 Planned flaring event during planned Two day flare event. Field was maintenance and new construction on C returned to production after TAPS pad IWAG injection compressor. shutdown at 01:00 hrs on Aug 2. High IWAG compressor was returned to GOR wells at C pad remained shut-in service at 23:30 hours on Aug 4 and throughout IWAG work. Add'1 high flare was eliminated. GOR wells at B pad were SI when IWAG experienced problems (BDV) with restart. 215.1 255.9 Planned flaring event for full field A planned full field shutdown was shutdown during TAPS proration. taken to perform maintenanceand Dean Warnken phoned Wendy Mahan construction in CFP & C pad IWAG (AOGCC) on Aug 11 for notification of compressor. Work was perfomed in planned events during the two TAPS conjunction with TAPS slowdown to slowdowns. minimize flare. 80.1 0.0 See above. 1,399.9 2,705.3 Planned flaring event in conjunction High GOR wells B10, E09 and E11 with annual PSV certification (ASME remained SI for flare relief. Code Sec 1,4,8) on C-5502/03/31 compressor package. Compressor was RTS at 21:45 hrs & flare eliminated. 351.6 662.4 Planned flaring in conjunction with SI following high GOR wells during annual certification (ASME Code compressor repatrs & testing: B09, Section 1, 4, 8) of Pressure Safety B 10, C 13, C 14,E 11. Valves (PSV's) on C-5502/03/31 & C-5501/11 B compressor packages. 4,846.0 3,109.2 See above. Experienced unplanned gas SI add'1 high GOR wells at B, C pads to plant shutdown during C-5501/11B eliminate black smoke & mitigate flare restart due to exceeding power factor. volumes. Also performed emergency repair on broken nipple & vent line while down. 347.3 562.5 See above. 194.9 630.5 Planned flaring event in conjunction SI following wells for flare relief with annual compliance recertification during testing: B03, 04, 06, 09, 10, 20, of PSV's on C-5511 and C-2605 (C 21, 22, C04, 07, 13, 14, El I. pad IWAG) compressors. Opportunity maintenance/repairs were performed on both machines during this shutdown. 176.4 246.4 See above. BP Exploration Page I6 of U Milne Point. Alaska os~ov9~ .lo:lb Milne Point Unit • 1Qlonthly Gas Flaring Incident Report For: Aug /1997 Flare Name: Flare 1 anne vents xcee ing our ~ o umne xcee mg Duration -Volume (MSCF) Start Time (hh:mm) Flare Assist Cause Comment 08/30/97 19:17:00 01:43 542.7 633.2 See above. Unplanned Events <=1 hour Unplanned Events > 1 hour Planned Events <= 1 hour and not exceeding 5,000 MCF Planned Events > 1 hour or exceeding 5,000 MCF Unmetered Assist Gas TOTAL FLARED VOLUME Flare Assist 9,737.7 20,995.5 2,780.0 4,066.2 0.0 0:0 23,780.8 28,688.3 11,377.0 36,298.5 65,126.9 MSCF BP Exploration Page 17 of l7 Milne Point, Alaska s Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point August 30, 1997 Time and duration of incident: 06:01 hrs - 1 hrs 44 mins Flare Volume: 195 Assist Gas Volume: 631 This was a planned flaring event that occurred in conjunction with annual pressure safety valve (PSV) certification on C-5511-A and C-2605 compressors. Misc maintenance was performed on both compressors in conjunction with this testing to shelter production impact & minimize future flaring. Following high GOR wells were shut in to mitigate the flaring: B03, 04, 06, 09, 10, 20, 21, 22, C04, 07, 13, 14, E11. When repairs were ~~ ~~ completed both compressors & wells were returned to service and the flare was eliminated with no further incident. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point August 29, 1997 Time and duration of incident: 16:01 hrs - 1 hrs 14 mins Flare Volume: 97 Assist Gas Volume: 515 • This was an unplanned flaring event that occurred due to an unexpected emergency shut down of the IWAG compressor. The compressor S/D due to problems with the engine driver. High gas production wells were shut in to mitigate the flaring. Repairs were made to the engine and the compressor was restarted. S~ (,~.~//5 ~I~~ CZz~CI;,C;~ ~~g ~2z F~ IG.~~~ • • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point August 25, 1997 Time and duration of incident: 01:17 hrs - 2 hrs 58 mins Flare Volume: 198 Assist Gas Volume: 297 Time and duration of incident: 04:31 hrs - 1 hrs 29 mins Flare Volume: 99 Assist Gas Volume: 149 Time and duration of incident: 07:32 hrs - 1 hrs 43 mins Flare Volume: 110 Assist Gas Volume: 164 These were unplanned flaring events that occurred due to an E-Pad well that suddenly developed gas break through. The E-22 well went from producing less than 1000 mscf to over 4000 mscf virtually overnight. Production wells were S/I to mitigate the flaring until the problem well could be identified. Once the well was identified and actions taken to reduce gas production, the process returned to normal and the flaring subsided. .~ ~, • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne-Point August 24, 1997 Time and duration of incident: 14:01 hrs - 1 hrs 14 mins Flare Volume: 80 Assist Gas Volume: 161 • This was an unplanned flaring event that occurred due to blowing down several wells that had been shut in. Production wells were choked back to help mitigate the flare rate. S • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point August 23, 1997 Time and duration of incident: 07:16 hrs - 3 hrs 29 mins Flare Volume: 352 Assist Gas Volume: 662 Time and duration of incident: 12:42 hrs - 7 hrs 33 mins Flare Volume: 4846 Assist Gas Volume: 3109 Time and duration of incident: 23:33 hrs - 1 hrs 57 mins Flare Volume: 347 Assist Gas Volume: 562 This was a planned flaring events that occurred during planned maintenance on the 0- 5502/03/31 and C-5501/11B compressor packages for required annual certification of pressure safety valves (PSV). Production wells were S/I to help mitigate the flare rate. The compressors were returned to service upon completion of repairs and certifications thus eliminating the flaring. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point August 22, 1997 Time and duration of incident: 08:39 hrs - 9 hrs 51 mins Flare Volume: 1400 Assist Gas Volume: 2705 • This was a planned flaring event that occurred during planned maintenance on the 0- 5502/03/31 compressor package for required annual certification of pressure safety valves (PSV). The compressor was returned to service at 0945 hrs which eliminated the flaring. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point August 20, 1997 Time and duration of incident: 17:12 hrs - 1 hrs 18 mins Flare Volume: 634 Assist Gas Volume: 504 This was an unplanned flaring event that occurred due to an F-Pad shut down. F-Pad S/D when an ESD occurred in the test separator module. Upon start up the pad, the initial gas production volume exceeded the facility compressor capacity and flaring occurred. Once the pressure surge subsided, the process returned to normal and the flaring subsided. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point August 9, 1997 Time and duration of incident: 00:29 hrs - 7 hrs 43 mins Flare Volume: 1,329 Assist Gas Volume: 1,617 n U This was an un-planned flaring event that occurred when the field was brought up from the TAPS shutdown due to construction and maintenance activities. The IWAG injection compressor was started several times with-out success, and maintenance crews were called out to trouble shoot the problem. Also, an annual PM was being performed on C- 5531-A injection compressor and asafe-in of equipment was required prior to start-up. High GOR wells were shut-down in order to eliminate additional flaring. The IWAG compressor is still down for maintenance and PM work, and we are no longer venting gas to the flare header. C~ Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point August 8, 1997 Time and duration of incident: 04:34 hrs - 1 hrs 26 mins Flare Volume: 215 Assist Gas Volume: 256 • This was a planned flaring event that occurred when the field was shutdown for construction and maintenance activities in conjunction with a TAPS slowdown. The process of de-pressuring the production equipment and purging of lines in the facility was the cause of this event. Once the field was shut-down and isolated the flare eliminated, and maintenance crews proceeded to work. • • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point August ;6; 1997 7 Time and duration of incident: 10:50 hrs - 2 hrs 25 mins Flare Volume: 275 Assist Gas Volume: 749 This was a un-planned flaring event that occurred when C-5511-A gas lift compressor shut-down due to a faulty wire in a temperature transmitter. Maintenance crews repaired wiring in transmitter and compressor was returned to service. The gas lift compressor was returned to service and the flare was eliminated. Assist gas was utilized to prevent Black Smoke.- L • • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point August 2 - 4, 1997 Time and duration of incident: 12:01 hrs - 54 hrs 44 mins Flare Volume: 13,825 Assist Gas Volume: 17,969 This was a planned flaring event that occurred during planned maintenance and new ____ __ _ construction on the IWAG injection compressor during TAPS ramp-up of the field. This ___ ____..___~_~__,.~-was a two day flare event, which high GOR wells were shut in to mitigate additional flaring during start-up of the field. The IWAG injection compressor experienced -- - oblems with start-up due to maintenance problems with a blow down valve. The field .._ _ - ~` was returned to production at 0100 hrs on 8/2/97. The IWAG injection compressor was returned to service at 2330 hrs on 8/4/97 and the flare was eliminated. . ,. Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point August 2, 1997 Time and duration of incident: 0221 hrs - 2 hrs 24 mins Flare Volume: 342 Assist Gas Volume: 609 Time and duration of incident: 0532 hrs - 4 hrs 58 mins Flare Volume: 1,089 Assist Gas Volume: 1,030 • This was a planned flaring event that occurred during planned maintenance and new construction on the IWAG injection compressor during TAPS shutdown. High GOR wells were shut in to mitigate additional flaring. The IWAG injection compressor is expected to be down until all planned shut-down work is complete. The field was returned to production at 0100 hrs on 8/2/97. Expected return to service of the IWAG injection compressor is 8/3/97 @ 1800 hrs. "~~, • • MPU, Production Coordinator From: Warnken, Dean K. Sent: Wednesday, August 06, 1997 10:11 AM To: MPU, Field Production Supr; MPU, Maint Proj Cntrl Eng; MPU, Operations Superintendent; MPU, Facilities Supervisor; Wilks, Bob J. Cc: MPU, Production Coordinator Subject: MPU >1 hr flaring events 7/31-8/4. Note to MPU AOGCC compliance file. Note to File: Re: MPU > 1 hr flaring events July 31 thru August 4, 1997 Planned >1 hr flaring events occurred at Milne Point from July 31 -August 4, 1997. Flaring occurred in during preventative maintenance and repair on the C pad IWAG gas compressor and annual preventative maintenance on gas compressors in the CFP. Work was performed in conjunction with an August 1 20% TAPS proration to minimize overall flare volumes during these activities. High GOR wells at B and C pads remained shut-in during this time to maintain reasonable flare volumes. Maintenance records are on file at Milne Point and available for inspection upon request. Page 1 •, .. • • MPU, Production Coordinator From: MPU, Production Coordinator Sent: Thursday, August 28, 1997 5:34 PM To: MPU, Production Coordinator Cc: MPU, Operations Superintendent; MPU, Facilities Supervisor Subject: AOGCC Flare Notification during TAPS Note to File: A note of confirmation that Dean Warnken phoned Wendy Mahan with AOGCC on August 11 to notify her of MPU flaring events sustained during recent planned maintenance and construction activity that was performed during TAPS slowdowns on Aug 1 & 8. Flare events are documented & will be submitted with monthly AOGCC flaring report. Page 1 • BP EXPLORATION August 15, 1997 State of Alaska Alaska Oil and Gas Conservation Commission 3001 Porcupine Drive Anchorage, AK 99501 Attn. Wendy Mahan: • BP Exploration (Alaska) Inc. 900 East Benson Boulevard P.O. Box 196612 Anchorage, Alaska 99519-6612 (907) 561-5111 Attached are the Monthly Producer's Report of Gas Disposition for the month of July 1997 . Should you have any questions, please contact Bob Wilks at (907) 564-5670. Sincerely, ~~ ~~ Paul D. Bly Manager, Volume, Royalty & Severance ALASKA OIL AND GAS CONSERVATION CONII~lISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition Milne Point BP Exploration (Alaska) Inc. Milne Point July, 1997 Disposition Volume MCF* 1. Sold Fuel 14,606 2. Reinjected 595,689 3. Flared or vented less than 1 hour 769 4. Flared or vented greater than 1 hour (Supplemental report required--See 20 AAC 25.235) 472 5. Pilot and Purge 2,077 6. Used for lease operations Fuel Assist 226,301 17,729 7. Other TOTAL items 1-7 857,643 8. NGL gas equivalent produced 9. Purchased gas 10. Transferred from: 11. Transferred to: Remarks: I hereby cer~tQify th~a~t the foregoing is true and correct to the best of my knowledge. I g l ~.1~ /C~ /fit.. fkX.~ ~'C1f ~Sr~/. fi ~9~ Si nature Title Date 8 L *Indicate contribution of each pool to total. Pool Name Code Percent KUPARUK 525100 92.1 SCH. BLUFF 525140 7.9 Official Use Only-Flaring Ailthozizataon>l hr: 1. Safety MCF 2. Lease MCF 3. Conserv. Purposes MCF Commissioner Date (Note: All volumes must be corrected 'to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month folowing the month of disposition. Authority 20 AAC 25.235. • • Form 10-422 Rev. 4/95 SENT BY=BPX-MPOC ; 8- 5-97 ; 754 BPX-MILIVE POINT-' 9075644094;#10/15 ---- ~ moue roint ua~t ... V ly Gan Flaring Incident Rclwrt • >For: JuI f ] 997 Flaire Name: Marty 1 nTried Events~greatelr than pour Durutiou ~Volumc (MSCF~ Start Timc (hh:mm) Flare Assist Gause Comment 07/18/97 13:S4:OU O l :OG 46.9 450.0 Unplanned flaring event during SI high GOR wells for flare relief unplanned maintenance on C pad during repairs. Repaired stepper valves 1WAG compressor. Identified & RTS. problems write stepper valves that req'd immediate repair. 07/23151712:03:00 02:12 113.5. 616.9 Unplanned event due to compressor SI hifh GOR wells for gas handling shutdowns in CNP. Shutdowns caused relief. by high processing temps in .conjunction with warm ambient temps (BU+F). 0727/97 07:53:00 02:37 174.9 37C.$ Unplanned event due to compressor Shut-in high GOR wells for plant shutdowns in GFP. Unplanned field stability dosing r~hart. shutdowns occurri:d followuig a partial field power outage &-the subsequent field restart. I, BP F.zpbruwn Page G of 7 Milne Noint, Alaska SENT BY~BPX-MPOC 8- 5-9? 754 13PX-MIL]VE POINT-' 9075644094;#11/15 -~--- Ivx~tne rutn>< un><c - ' . . ,,. V Nl~ly Gas Flaring Incident Report , For: Tul /1997 .Flare Name: Flare 1 ~'lanned'Evco Fa<ceeding Y'6ourZjA'"volutane Eic`eeding SOOO~MS-CF -'"-"'- ---"--"" '- '--" Daration Volume (M.SC;~ Start Time (hh:mm) Flare Aswist Cause Comment 07!31 /97 19:01:00 02:59 136.5 936.8 Planned flaring event occurred during. Nigh GUR wells were Sl at B & C blowdown of C: pad 1WAG compressor. pads. Preventative compressor maintznanee performed in conjunction with '1'Al'S proration to minimlu~ gas flaring during ilnwntime. Flare Assist .Unplanned Events ~ 1 Lour 768.7 6,048.6 Unplanned Events> 1 hour 335.3 1,443.7 Planned Events ~ 1 hour and. not exceeding 5,000 MCF 0.0 0.0 Planned Events > 1 Lour or ..exceeding 5,000 MCF 136.5 936.8 Unmetered Assist'Gas 11,377.E TOTAL FLARED VOLUME. 1,240.5 19,806.1 MSCF a; °~~ " B ,t G,: :. 1 ~i,~~` `j" '~J ~ - :Qi1 qq R`' r CY UGI.~' ~6in4 i;:, ~ , BP Explcuatinn Pape 7 0!~ Milne Yoinc, Alaska a.5 '~ SFNT BY~BPX-MPOC 8- 5-97 7=54 BPX-MILIVE POINT 9075644094;#12/15 I • . ~ Flaring ~neident Report (~zc:c;e:ding 1 hour} BF Exploration -Milne Point July l8, 1997 Time and duration of incident:. 1354 hrs - 1 hrs. b wins Flare Volume:. 47 Assist Gas Volume: 45U -This. was unplanned flaring caused by unplanned,maintenance on the C-find gas compressor. The compressor developed problems with it's stepper valves an had to be shut down immediately. High GOR wells were shut in to reduce gas rates. far enabling more efficient compressor relative capacity handling. Repairs were made and the compressor returned to service. ~~ ~°"' 1~9f ' ~a'~a~ } ions. ;~,.- ..~ ~~~ SENT BY~BPX-MPOC 8- 5-9? 7=55 SPX-MILIVE POINT 9075644094;#13/15 • • Flaring Incident. Report (exceeding. l hour] BP Exploration -Milne Point July 27, 1997 Time and duration of incident: O7531us - 2 hrs 37 rains Flare Volume: 175 :Assist Gas Volume:- 377 This was unplanned flaring following unexpected gas compressor shut downs. The event occurred when a high voltage power line. connector shat attached to transformer blew out. The central facility'. experienced multiple gas compressor shut downs while attempting to restart. High GUR wells were shut in io reduce gas rates for enabling more efficient compressor rclativ~ capacity handling. SENT BY ~ BPX-1~iPOC ^ 8- 5-97 7=55 SPX-MIISIE POINT-' 9075644094;#14/15 Flaring Incident Keport (exccA:ding t hour] BP Exploration -Milne Point July 23, 'I 997 Time and duration of incident: 1203 hrs - 2 hrs 12 minx Flare Volume: 113 A.~iyt Gas Volume:.. 6l7 This was unplanned flaring following unexpected g~~s compressor shut downy. Resulting from the extreme high ambient temperatures (>8U° F), the central facility experienced multiple gas compressor shut downs. High GUR wells were shut` in to reduce gas rater for enabling more efficient compressor relative capacity handling. Ancillary process was altered, glycol heaters swapped, for. the period of higher than normal ambient temperatures to optimi:~e compressor of#iciency. f SENT BY~BPX-MPOC 8- 5-97 755 ; BPX-MILNE POINT-~ 9075644094;#15/15 . . Flaring Incident Report (cacxeding l hour) BP Exploration - Milnc Point July 31, :1997 Time and duration of incident: 1901 hrs - 2 hrs 59 minx Flt~re Volume: 137 .Assist Gas Volume: 937 This was a platu~ed flaring event that occurred when the IWAG compressor was shut- ciawn for maintenance in conjunction with the TAPS slowdown. High GOR wells were .shut in to mitigate .flaring. Compressor is expected ro he down until all planned shut- dawn work is complete. The field is prescntly down, and all flaring has peen eliminated. ..Expected return to service is on 8/2/97 @ 2300 hrs. BP EXPLORATION July 17, 1997 State of Alaska Alaska Oil and Gas Conservation Commission 3001 Porcupine Drive Anchorage, AK 99501 Attn. Wendy Mahan: • BP Exploration (Alaska) Inc. 900 East Benson Boulevard P.O. Box 196612 Anchorage, Alaska 99519-6612 (907) 561-5111 Attached are the Monthly Producer's Report of Gas Disposition for the month of June 1997 . Should you have any questions, please contact Bob Wilks at (907) 564-5670. Sincerely, ~~~ Paul D. Bly Manager, Volume, Royalty & Severance :. ~ ~~ ~ ~` t~s ~~rnc~~~s~~~a Aias~a ~tl & ~~~ ~'~.. . ~,r~chQr~~3~: ALASKA OIL AND GAS CONSERVATION CONIl~lISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition Milne Point BP Exploration (Alaska) Inc. Milne Point June, 1997 C._ ~:; t'"° ~' CC7 CQ --~E Disposition Volume MCF* 1. Sold Fuel 11,225 2. Reinjected 539,751 3. Flared or vented less than 1 hour 1,112 4. Flared or vented greater than 1 hour (Supplemental report required--See 20 AAC 25.235) 3,092 5. Pilot and Purge 2,010 6. Used for lease operations Fuel Assist 186,708 29,590 7. Other TOTAL items 1-7 773,488 .+~ 8. NGL gas equivalent produced •• 9. Purchased gas ~_~ ~N, ~ 0. Transferred from: 11. Transferred to: Remarks: I hereby certif that the foregoing Signature ~ ~ ~l is true and correct to the best Title of my knowledge. Date // •~~ *Indicate contribution of each pool to total. Pool Name Code Percent KUPARUK 525100 91.8 SCH. BLUFF 525140 8.2 Official Use Only-Flaring Authorazatkon>J hr: 1. Safety MCF 2. Lease MCF 3. Conserv. Purposes MCF Commissioner Date Note: All volumes must be corrected to pressure of 14.65 psia and to a ,temperature of 60 degrees F. Report due by the 20th of the month folowing the month of disposition. Authority 20 AAC 25.235. • u Form 10-422 Rev. 4/95 o~io2i97 t~:os Milne Point Unit • ~ thly Gas Flaring Incident Report For: Jun /1997 Flare Name: Flare 1 Unplanned Events greater than 1 hour Duration =Volume (MSCF) _ Start Time (hh:mm) Flare Assist Cause Comment 06/01/97 20:01:00 02:14 231.4 513.0 Unplanned shutdown due to halon Repaired fault and returned facility to discharge in 07 turbine enclosure. service. Entire gas compression facility shutdown. 06/11/97 23:02:00 02:28 201.9 317.1 Unplanned flaring events June 11-12. Further complications when coming Occurred when 08 turbine shutdown on back on line. LSHH in gas lift scrubber high exhaust temp. Caused fieldwide shutdown gas compression module & shutdown. hampered restart attempts. Repaired problems and returned field to production. 06/12/97 03:35:00 04:10 296.8 1,s00.3 06/12/97 08:38:00 05:37 463.9 2,144.7 06/16/97 16:41:00 06:04 s6s.4 2,409.4 Unplanned event occurred when Extensive troubleshooting to identify & C-5501/11-A gas lift compressor lost correct problem. Installed 24V breaker power to local alarm panel in mod s5. & returned to service. 06/23/97 19:s8:00 04:47 379.7 1,832.0 Unplanned flare event due to unplanned Extensive troubleshooting requ'd to shutdown of generator. Field was identify & repair automatic control operating on single turbine. system malfunction. Repaired &RTS. 06/24/97 07:48:00 05:27 381.3 2,143.s Unplanned flaring from two separate Restarted compressors in CFP &RTS. events. One main compressor s/d on a Dispatched crew to C pad IWAG & lubricator low flow alarm & other repaired &RTS. compressors s/d on high pressure safety switch. 2nd event due to IWAG s/d on engine cooling malfunction. 06/29/97 1 s:16:00 02:29 248.9 799.4 Three unplanned flaring events due to Curtailed production rates until mod Ss unplanned shutdown of gas compression main gas compression & C pad IWAG facility. Believed to be related to high could be restarted. ambient temps. 06/29/9718:20:00 O1:SS 91.9 .834.6 06/29/97 22:18:00 02:27 230.6 562.2 Flare Assist Unplanned Events <=1 hour 1,112.3 7,533.5 Unplanned Events > 1 hour 3,091.8 13,056.1 Planned Events <= 1 hour and not exceeding 5,000 MCF 0.0 0.0 Planned Events > 1 hour or exceeding 5,000 MCF 0.0 0.0 Unmetered Assist Gas 11,010.0 TOTAL FLARED VOLUME 4,204.1 31,599.6 MSCF BP Exploration Page 9 of 9 Milne Point, Alaska • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point June 1, 1997 Time and duration of incident: 2001hrs - 2 hrs 14 mins Flare Volume: 231 Assist Gas Volume: 513 • This was an unplanned emergency shut-down due to a Halon discharge that occurred in the 07 turbine enclosure. The turbine S/D and activated the load shed command which created a pressure spike and S/D the entire Gas Compression Facility. Once the fault was repaired on the turbine, gas compression was returned to service and the flare was eliminated. Black Smoke was reported with this incident, and all reports completed and sent to the ADEC. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point June 12„ 1997 • Time and duration of incident: 23:02 hrs -13 hrs 1 min (June 11 to the 12`h) Flare Volume: 999 MCF Assist Gas Volume: 4274 MCF This was an unplanned flaring event which occurred when the 08 turbine shut-down due to a high temperature on the turbine exhaust, causing a field wide production shutdown. While attempting to bring gas compression back on line, we experienced a LSHH in the gas lift scrubber which tripped and shut-down the gas compression module again. Once the problems with the turbine and the gas lift scrubber were repaired the field was returned to full production and the flare was eliminated. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point June 16, 1997 Time and duration of incident: 16:41 hrs - 6 hrs - 4 min Flare Volume: 565 MCF Assist Gas Volume: 2409 MCF This was an unplanned flaring event which occurred when the C-5501/11-A gas lift. compressor lost power to the local alarm panel in Mod. 55. Maintenance crews had problems identifying the problem. Once the problem was corrected with a 24 V breaker the Compressor was returned to service and the flare was eliminated with no further incident. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point June 23 & 24, 1997 • Time and duration of incident: 1958 hrs (6/23) - 4 hrs 48 rains Flare Volume: 426 Assist Gas Volume: 2147 (carry over past midnight from 6/23 to 6/24) This was unplanned flaring following a main power generator unexpected shut down. The power generation package, singularly carrying full field load, shut down on an automatic control system malfunction. Extensive trouble shooting was required prior to returning the power generator to service. The other main power generator was out of service for a gas turbine engine exchange and governor control system upgrade. Start-up conditions were achieved and main power restored Time and duration of incident: 0727 hrs (6/24) - 5 hrs 52 rains Flare Volume: 402 Assist Gas Volume: 2244 This was unplanned flaring from two separate events. The gas compression module in the CFP shut down. One main compressor shut down on a lubricator low flow alarm and the other compressors consequently shut down from a transient pressure spike tripping a high pressure safety switch. The condition was verified safe and the compressors restarted as soon as possible. The C-pad gas reinjection compressor (1WAG) required unplanned repairs when the engine cooling system malfunctioned, causing the compressor to shut down. Repairs were expedited and the compressor returned to service as soon as possible. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point June 29, 1997 Time and duration of incident: 1516 hrs 5 hrs 55 mins Flare Volume: 392 Assist Gas Volume: 2258 Time and duration of incident: 2218 hrs 2 hrs 27 mins Flare Volume: 231 Assist Gas Volume: 562 • Both of these events were unplanned flaring following unexpected gas compression module shut downs. The C-pad gas injection compressor shut down along with the main facility compressors. Production rates were reduced until the compressors could be restarted. • BP Exploration (Alaska) Inc. 900 East Benson Boulevard P.O. Box 196612 Anchorage, Alaska 99519-6612 (907) 561-5111 June 13, 1997 State of Alaska Alaska Oil and Gas Conservation Commission 3001 Porcupine Drive Anchorage, AK 99501 Attn. Wendy Mahan: Attached are the Monthly Producer's Report of Gas Disposition for the month of May 1997 . Should you have any questions, please contact Bob Wilks at (907) 564-5670. Sincerely, /~~,~ ~" Paul D. Bly Manager, Volume, Royalty & Severance ~~~_.~ -- ,. j _. ~. ~, ~;~~ ALASKA OIL AND GAS CONSERVATION CONII+~lISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition Milne Point BP Exploration (Alaska) Inc. Milne Point May, 1997 Disposition 1. Sold Fuel 15,273 2. Reinjected 597,831 3. Flared or vented less than 1 hour 605 4. Flared or vented greater than 1 hour (Supplemental report required--See 20 AAC 25.235) 706 5. Pilot and Purge 2,077 6. Used for lease operations Fuel Assist 240,060 17,367 7. Other TOTAL items 1-7 873,919 8. NGL gas equivalent produced 9. Purchased gas 10. Transferred from: ~~° r-~ -~ •~. Transferred to: 3emarks : 3 hereby certify that the foregoing is true and correct to the best of my knowledge. Signature Title~,~~~ ~ Date ~ ~~ Volume MCF* *Indicate contribution of each pool to total. Pool Name Code. Percent KUPARUK 525100 92.8 SCH. BLUFF 525140 7.2 Official Use Only-Flaring Authorizatzon>1 hr. 1. Safety MCF 2. Lease MCF 3. Conserv. Purposes MCF Commissioner Date Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month folowing the month of disposition. Authority 20 AAC 25.235. i • Form 10-422 Rev. 4/95 or~o9~9~ 09:30 Milne Point Unit l~thly Gas Flaring Incident Report • For: May /1997 Flare Name: Flare 1 nplanned Events greater than 1 hour i Duration =Volume (MSCF) _ Start Time (hh:mm) Flare Assist Cause Comment 05/08/9710:37:00 04:23 l~'~3~- I~~.oo 05/19/9715:43:00 02:17 i s' 43 -B' e~ ~ 05/22/97 22:10:00 01:05 y2~,~o - z3~i~ 05/23/97 01:46:00 02:14 of 46 - ~'.o d 05/23/97 04:02:00 01:13 o ~4 '. o z. - dS`~. I S 367.9 905.2 Unplanned emergency shutdown of gas PLC processor in 08 turbine had a fault. compression module during load shed Triggered load shed scheme to shift all from 08 to 07 turbine. power load to 07 turbine. Repaired fault and RTS. 172.4 942.6 Unplanned flaring caused when C pad Made adjustments on stepper valves IWAG injection compressor backfired and timing of compressor engine & several times and eventually shutdown. RTS. 50.4 440.8 Unplanned shutdown of C pad IWAG Repaired and returned to service. compressor. 82.3 601.9 Unplanned event due to prolonged Had to replace #1 cylinder head and repairs on C pad IWAG compressor. repair carburetor. Shut-in 18 high GOR wells to mitigate flare during repairs. 33.0 232.2 Flare Assist Unplanned Events <=1 hour Unplanned Events > 1 hour Planned Events <= 1 hour and not exceeding 5,000 MCF Planned Events > 1 hour or exceeding 5,000 MCF Unmetered Assist Gas TOTAL FLARED VOLUME 605.1 4,944.5 706.1 3,122.6 0.0 0.0 0.0 0.0 11,377.0 1,311.2 19,444.1 MSCF BP Exploration Page 6 of 6 Milne Point, Alaska SFNT BY=JDO ; 6- 6-97 1634 JDO-- 9075644094;# 3/ 9 • . • Flaring lrldderrt Report (exceeding 1 hour) BP Exploration -Milne Point May 22 & May 23, 1997 Time .and duration of incident: 2210 hrs - 1 hr 5 min (May 22.1997} Flare Volume: 50 MCF Assist Gas Volume: 441 MCF: ; This was unplanned flaring as a result of the C-pad gas injection compressor (IWAG). The IWAG compressor shut down unexpectedly and required repairs. The- mechanical repairs were expedited and the .compressor returned to service as soon as possible. Time and duration of incident: 2352 hrs - 5 hr 23 min (May 23, 1997) Flare Volume: 162 MCF Assist Gas Volume: 1293 MCF This was unplanned flaring resulting from an unexpected. prolonged. shut down of the C-pad IWAG gas compressor. Extensive repairs were made to the compressor while production was curtailed until the machine was returned to service. Production rates were not .returned to normal. until the gas compressor was back on Fine. -. ~ , r ... . _ , SFNT BY~JDO ; 6- 6-97 1635 ; JDO-+ 9075644094;# 4/ 9 . , Flaring Yncident Report (exc:eeding 1 huurj BP )/xploration -Milne Point May 8, 1997 ~ Time and duration of incident: 1037 hrs - 4 hrs 23 nuns Flare Volume: 368 Assist Gus Volume: 905 This was an unplanned emergency shut-down of the gas compression module, which cx;curred when the O8 turbine S/D enabling the load shed scheme. The l'LC prtacecc~r in the A$ turbine had a fault causing the generator t~ shin-down and attempt to shift full load to the 07 turbine. The load shed system tripped the excessive power loads and worked as designed. Once. the fault was repaired on the turbine, gas compression was returned to service and the flats was eliminated. Black Smoke was reported with this incident, and all reports completed and sent to the ADEC. SF_NT SY = JDO ; 6- 6-97 16 ~ 35 JI)0-+ 9075644094 ; # 5/ 9 .~ , ~ • . , Flaring Incident Report (exceeding ]hour) BP Exploration -Milne Point May 19, 1997 Time and duration of incident: 1543 hrs - 2 hrs 17 min.4 Flare Volume: 172 MSCF Assist Gas Volume: 943 MSCF This wa.s an unplanned emergency flaring event which occurred when. the IWAG gas .injection compressor at C-pad backfired several tiuycs and shut-down. Maintenance ' crews worked can making several adjustments on the stepper valves and timing of compressor engine. Once the repairs were completed the 1WAG compressor wa4 returned to service and the tlazc was eliminated. SENT 13Y = JI)0 ; 6- 6-97 ; 16 = 35 ; Jl)0--~ 9075644094 ; # 6/ 9 • • Milne Polnt Gas Allocution System Estimated Gas Volume variables May-97 ; CFP Heaters 24.354.. CFP Power Generation 193,325 B Pad Fuel • 4.549 C Pad Fuel 25 747 f Pad Fuel 6.862 Flare -metered 257 Flare Assist Gas - metered 616 Flare Pllot - unmetered 2,015 , Fk~re Assist - unmetered 9,300 Flar® Purge - unmetered ~ vent system G96 C-61 InjeCllon 94,182 C-81 Injection 64,489 C-1011njectbn 80.984 C-151 Injection - C-171 Injection - . C-191 Injection - C-251 injection 204.464 C-28i injection - E-3i Inlectlon 65,285 E-5i Injection 88,427 . E-7i Injoetlon - E-161 Injection E-171 Injection - E-231 Injection - TOTAL 841,060 E-316as flowed bock for CFP fuel 0 mct SFNT BY~JDO ; 6- 6-97 ; 1636 JDO-~ 9075644094;# 7/ 9 ^ • • MPtI Load Diesel Summary - May f 997 . )ate Pumr~e~ 9l~1~ AcHvlt,r_ bate 80L . 807. 07!91 /96 26 Pump open scssv Still SI ' B07 08/02/96 15 WL - (ACk Out Flapper StUI SI D2A 04/ 13/97 86 FP tubing & flowlines Still Sl L32 05/ 16/97 9 Pump down tubing Sflll SI L32 05/17/97 81 FP fi•~hing & flowllnes Still SI L29 05121 /97 70 FP after RWO 05/31!97 ' l29 05/29!97 2 PT flowlines 05/31 /91 C05A 05/30/97 51 plot Oil Treatmerri 05/30/97 E14 05/09/97 7Q FP aftr~r RWO 05/26/9) E14 05/23/97 2 PTflowllnes 05/26/97 E18 05/06/97 70 FP affor RWO 05/23/97 C23 05/21 /97 2~ Diesel/Xylene Flush 05/21/97 820 f).5/Ob197 25 FP tubing 8c flowllnes 05/20/97 B03 05/06!97 Imes 24 FP tubing 8c now 05 20 97 / / 04 1 97 05/ 3/ RWO 110 FP after 05 7 /20/9 EOd 05/19/97 2 PT flowfines 05/20/97 C23 05/19/97 95 niwcF,l/Xylene Flush 05/19/97 . . E19 05!04/97 70 FP after RWO 05/17/97 K02 Od/28/97 16 FPtubing & flowllnes 05/11/97 H07 05/10/97 20 Pressure Test Separator .05/10/97 815 0.5/10/97 d0 Hot OII Treatment 05/10/97 H07 05/02/97 83 FP tubing & flowllnes 05/10/97 105 05/08/97 30 Hot Oil Treatment 05/08/97 J09 04/20/97 70 FP afterRWO 05/06/97 E08 04/27/97 30 SI 8c FP tbg for spil cleanup 05/04/97 ' E08 04/27/97 1 PT fbwllnes 0510x/97 C05A 05/04/97 35 Hot Oll Treatment 05/D4/97 Total 1.088 Toto>f for 871 ~ Royally Exclusion BP EXPLORATION May 13, 1997 State of Alaska Alaska Oil and Gas Conservation Commission 3001 Porcupine Drive Anchorage, AK 99501 Attn. Wendy Mahan: BP Exploration (Alaska) Inc. 900 East Benson Boulevard P.O. Box 196612 Anchorage, Alaska 99519-6612 (907) 561-5111 Attached are the Monthly Producer's Report of Gas Disposition for the month of April 1997 . Should you have any questions, please contact Bob Wilks at (907) 564-5670. Sincerely, ~~ ~. Paul D. Bly Manager, Volume, Royalty & Severance ALASKA OIL AND GAS CONSERVATION CONII~lISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition Milne Point BP Exploration (Alaska) Inc. Milne Point April, 1997 Disposition Volume MCF* 1. Sold Fuel 15,785 2. Reinjected 597,366 3. Flared or vented less than 1 hour 1,118 4. Flared or vented greater than 1 hour (Supplemental report required--See 20 AAC 25.235) 4,560 5. Pilot and Purge 2,010 6. Used for lease operations Fuel Assist 257,140 27,791 7. Other TOTAL items 1-7 a ~:~ 905,770 C'. 8. NGL gas equivalent produced ` 9. Purchased gas _ 10. Transferred from: 11. Transferred to: r ,_ ks: I hereby certify that ithe foregoing is true and correct to the best of my knowl/edge. Si nature Title Date 5 ~~ CIA ~~• ~r ~ ~~, ~l v~ *Indicate contribution of each pool to total. Pool Name Code Percent KUPARUK 525100 93.6 SCH. BLUFF 525140 6.4 Official Use Only-Flaring Authorization>1 hr: 1. Safety MCF 2. Lease MCF 3. Conserv. Purposes MCF Commissioner Date Note: All volumes must be corrected to pressure of 14.65 Asia and to a temperature of 60 degrees F. Report due by the 20th of the month folowing the month of disposition. Authority 20 AAC 25.235. • Form 10-422 Rev. 4/95 05/61/97 0~:3o Milne Point Unit l~thly Gas Flaring Incident Report • For: Apr /1997 Flare Name: Flare 1 Unplanned Events less than or equal to 1 hour Duration =Volume (MSCF) _ Start Time (hh:mm) Flare Assist Cause Comment 04/01/9717:19:00 00:26 15.7 207.8 04/01/9717:53:00 00:07 5.1 73.0 04/01/9718:03:00 00:12 5.3 37.9 04/01/9718:28:00 00:02 0.9 7.0 04/01/9719:10:00 00:05 1.6 12.0 04/01/9719:28:00 00:02 0.6 5.6 04/01/97 21:42:00 00:03 0.7 5.9 04/01/97 21:58:00 00:02 0.7 5.0 04/01; 97 21:58:00 00:17 0.7 5.0 04/01/97 22:42:00 -00:57 1.0 7.2 04/01 /97 22:42:00 00:03 1.0 7.2 04/01/97 22:42:00 00:18 1.0 7.2 04/01/97 22:42:00 00:48 1.0 7.2 04/01/97 22:55:00 00:35 1.3 8.9 Negative time readings until 4/6/97 are Software bug was fixed & negative believed to be due to a daylight savings readings ceased after moving clocks time related software glitch. ahead on 4/6/97. 04/01/97 22:55:00 00:05 1.3 8.9 Negative time readings until 4/6/97 are Software bug was fixed & negative believed to be due to a daylight savings readings ceased after moving clocks time related software glitch. ahead on 4/6/97. 04/01/97 22:55:00 -00:55 1.3 8.9 Negative time readings until 4/6/97 are Software bug was fixed & negative believed to be due to a daylight savings readings ceased after moving clocks time related software glitch. ahead on 4/6/97. 04/01/97 23:14:00 00:46 0.8 7.2 04/01 /97 23:14:00 00:01 0.8 7.2 04/01/97 23:14:00 00:16 0.8 7.2 04/01 /97 23:40:00 00:20 1.5 11.0 04/01/97 23:40:00 00:05 1.5 11.0 04/01/97 23:40:00 00:50 1.5 11.0 04/02/97 00:14:00 00:01 0.2 1.8 04/02/97 00:14:00 00:16 0.2 1.8 04/02/97 00:14:00 00:31 0.2 1.8 04/02/97 01:13:00 00:02 0.8 4.3 04/02/97 01:25:00 00:05 2.5 18.8 04/02/97 01:43:00 00:02 0.5 3.5 04/02/97 01:43:00 00:17 0.5 3.5 04/02/97 02:27:00 -00:57 1.0 5.8 04/02/97 02:27:00 00:33 1.0 5.8 04/02/97 02:27:00 00:03 1.0 5.8 04/02/97 02:43:00 00:32 1.1 8.6 04/02/97 02:43:00 00:17 1.1 8.6 04/02/97 02:43:00 00:02 1.1 8.6 04/02/97 03:28:00 00:02 0.6 4.6 04/02/97 03:28:00 -00:58 0.6 4.6 04/02/97 03:28:00 00:17 0.6 4.6 04/02/97 15:28:00 -00: I3 30.4 109.7 Unplanned shutdown of C pad IWAG Cause of shutdown not identified. compressor. Repaired & RTS. BP Exploration Page 1 of 8 Milne Point, Alaska 05/01/97 07:30 m Milne Point Unit • thly Gas Flaring Incident Report For: Apr /1997 Flare Name: Flare 1 'Unplanned Events less than or equal to 1 hour , Duration =Volume (MSCF) _ Start Time (hh:mm) Flare Assist Cause Comment 04/02/9717:19:00 00:11 9.9 62.9 04/04/9719:28:00 00:02 0.6 3.8 04/04/9719:35:00 00:10 4.4 31.9 04/05/97 14:13:00 -00:43 29.4 108.2 Unplanned shutdown of C pad IWAG Shutdown caused by Trabon Tube oil compressor. system problems. Repaired &RTS. SI four high GOR wells during repairs for flare relief. 04/05/97 14:13:00 -00:13 70.6 316.2 Unplanned shutdown of C pad IWAG Shutdown caused by Trabon Tube oil compressor. system problems. Repaired &RTS. SI four high GOR wells during repairs for flare relief. 04/05/97 18:17:00 -00:02 35.9 267.1 Unplanned shutdown of C pad IWAG Shutdown to repair leak on 3rd stage compressor. cylinder. Repaired &RTS. 04/05/97 18:17:00 -00:02 37.1 254.9 Unplanned shutdown of C pad IWAG Shutdown to repair leak on 3rd stage compressor. cylinder. Repaired &RTS. 04/05/9719:47:00 -00:02 40.2 274.3 04/05/9719:47:00 00:58 40.7 275.9 04/05/9719:47:00 -00:02 41.4 280.8 04/05/97 20:49:00 00:11 5.6 41.4 04/05/97 20:49:00 -00:04 36.4 255.8 04/06/97 01:43:00 01:17 0.5 2.5 04/06/97 03:04:00 00:11 4.4 32.0 04/06/97 03:25:00 00:05 1.9 14.7 04/08/97 00:28:00 00:02 0.8 6.0 04/08/97 01:14:00 00:01 0.3 1.6 04/08/97 01:26:00 00:04 1.6 11.4 04/08/97 01:42:00 00:03 0.9 7.9 04/08/97 02:25:00 00:05 1.8 12.7 04/08/97 03:23:00 00:07 3.4 24.3 04/08/97 05:13:00 00:02 0.6 3.3 04/08/97 05:29:00 00:01 0.4 4.0 04/12/9714:06:00 00:09 4.3 30.6 04/12/9717:50:00 00:10 11.4 65.1 04/12/9719:49:00 00:11 7.5 53.7 04/12/97 20:13:00 00:02 1.3 10.1 04/12/97 21:40:00 00:05 2.2 15.5 ~ _~ 04/12/97 22:03:00 00:12 5.0 35.4 04/12/97 22:29:00 00:01 0.5 4.1 04/13/97 00:53:00 00:07 3.8 25.8 04/13/97 01:01:00 00:14 6.0 43.4 04/13/97 01:16:00 00:14 6.5 45.8 04/13/97 01:36:00 00:09 4.2 31.0 04/13/97 01:54:00 00:06 2.2 15.1 04/13/97 02:10:00 00:05 1.9 14.7 04/13/97 02:23:00 00:07 2.7 19.4 04/13/97 03:13:00 00:02 0.9 6.9 BP Exploration Page 2 of 8 Milne Point, Alaska osiav9~ 0'~:3o Milne Point Unit ~thly Gas Flaring Incident Report • k'or: Apr /1997 Flare Name: Flare 1 Unplanned Events greater than 1 hour Duration =Volume (MSCF) _ Start Time (hh:mm) Flare Assist Cause Comment 04/01/9713:37:00 03:38 13;3 I~~IS 04/02/9715:28:00 01:47 1S'z8 -- a~=tS 04/08/9714:13:00 04:02 I.4~13- 18:1$ 04/05/9718:17:00 01:28 18' ~ ~ - 19 '. ~-S 04/12/97 18:06:00 01:39 18'06 - 19'95 04/13/9710:24:00 01:06 lo', 2h - II' 3® 11'39 - 16',00 04/13/9711:39:00 04:21 04/16/97 07:29:00 06:4 o~ ' 2q - J ~ '~. I-~ 04/20/9712:19:00 02:56 04/21 /97 20:03:00 01:12 ~',D~ - ZI', ! 5` 04/26/97 22:33:00 01:12 ~~; 3 3 - 2.~', ,4~ 2s8.9 1,501.8 Unplanned flaring event due to shutdown of C pad IWAG compressor 130.2 735.9 Unplanned shutdown of C pad IWAG compressor. 667.9 4,015.9 Unplanned shutdown of C pad IWAG compressor. 98.s 681.1 Unplanned shutdown of C pad IWAG compressor. 66.4 478.9 Unplanned shutdown of C pad IWAG compressor. 85.9 449.0 Unplanned shutdown of C pad IWAG compressor. 208.1 1,444.7 Same event as above. 2,767.0 855.8 Gas lift compressors both went off-line while shutting in A compr. for repair 148.6 881.3 Unplanned shutdown of C pad IWAG compressor. 93.9 474.4 Unplanned shutdown of C pad IWAG compressor. 45.2 174.9 Unplanned flaring during ESD at E pad for E-08 leak. Shutdown due to Tube oil leak. Repaired &RTS. SI four wells to mitigate flare during repairs. Cause of shutdown not identified. Repaired &RTS. Shutdown caused by Trabon lube oil system problems. Repaired &RTS. SI four high GOR wells during repairs for flare relief. Shutdown to repair leak on 3rd stage cylinder. Repaired &RTS. Shutdown due to broken fittings on Trabon Tube oil system. Repaired & RTS. SI five high GOR wells during repairs for flare relief. Shutdown caused by loose PLC card. Repaired &RTS. SI four high GOR wells for flare relief during repairs. Shut in 14 wells to mitigate flare Shutdown due to backfiring/carburetor & 02 sensor repair. Repaired &RTS. SI 7 high GOR wells for flare relief dueing repairs. S/D IWAG compressor to repair diaphragm on carburator air inlet & replace fouled spark plugs. No proudction impact. Manually initiated ESD at E pad after discovering leak at E08 wellhead. Pad s/d req'd for emergency personnel to access pad. Flare Assist Unplanned Events <= 1 hour 1,117.9 7,097.1 Unplanned Events > 1 hour 4,560.4 11,693.7 Planned Events <= 1 hour and not exceeding 5,000 MCF 0.0 0.0 Planned Events > 1 hour or exceeding 5,000 MCF 0.0 0.0 Unmetered Assist Gas 11,010.0 TOTAL FLARED VOLUME 5,678.3 29,800.8 MSCF 30 BP Exploration Page 8 of 8 Milne Point, Alaska • • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point April 1, 1997 Time and duration of incident: 1337 hrs - 3 hr 38 min Flare Volume: 259 MCF Assist Gas Volume: 1502 MCF This was unplanned flaring as a result of an unexpected shut down of the C-pad gas injection compressor (IWAG). Some of the gas lift producers were shut in to mitigate flaring. The circumstances of the compressor shut down were determined and conditions restored to normal. The IWAG compressor was re- started as soon as possible and flaring stopped. i • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point April 2, 1997 Time and duration of incident: 1528 hrs - 1 hr 47 min Flare Volume: 130 MCF Assist Gas Volume: 736 MCF This was unplanned flaring as a result of an unexpected shut down of the C-pad gas injection compressor (IWAG). The circumstances of the shut down were determined and conditions restored to normal. The IWAG compressor was re- started as soon as possible and flaring stopped. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point April 5, 1997 Time and duration of incident: 1413 hrs - 4 hr 2 min Flare Volume: 668 MCF Assist Gas Volume: 4016 MCF Time and duration of incident: 1817 hrs - 1 hr 47 min Flare Volume: 98 MCF Assist Gas Volume: 681 MCF These were unplanned flaring events from the same cause. The C-pad gas re- injection compressor shut down unexpectedly when the lubrication system detected no flow and automatically s/d the compressor. Maintenance personnel were immediately dispatched to begin trouble shooting to make repairs. Production rates were reduced in the field to mitigate flaring. The compressor was returned to service as quickly as possible. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point April 12, 1997 Time and duration of incident: 1806 hrs - 1 hr 39 min Flare Volume: 66 MCF Assist Gas Volume: 479 MCF This was an unplanned flaring event. The C-pad gas re-injection compressor was shut down due to a tube oil and gas leak inside the compressor module. Maintenance personnel were immediately dispatched to begin making repairs. Production rates were reduced in the field to mitigate flaring. The compressor was returned to service as quickly as possible. s • Flaring Incident R®port (exceeding 1 hour) BP Exploration -Milne Point April 13, 1997 Time and duration of incident: 1024 hrs - 1 hr 6 min Flare Volume: 86 MCF Assist Gas Volume: 449 MCF Time and duration of incident: 1139 hrs - 4 hr 21 min Flare Volume: 208 MCF Assist Gas Volume: 1445 MCF These were unplanned flaring events from the same cause. The C-pad gas re- injection compressor shut down unexpectedly when a PLC (programmable Logic Control) card vibrated loose. Maintenance personnel were immediately dispatched to begin trouble shooting to make repairs. Production rates were reduced in the field to mitigate flaring. The compressor was returned to service as quickly as possible. • • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point 16 April 1997 Time and duration of incident: 07:29 hrs - 6 hr 46 min Flare Volume: 2763 MCF Assist Gas Volume: 885 MCF This flaring event occurred as the result of a unplanned gas plant shut down. One gas lift compressor was scheduled for maintenance repairs and a number of wells had been shut in to reduce gas plant throughput. However when the stop button was pushed to shut down one compressor all gas lift compressors shut down. This resulted in a cascade effect that also shut down all plant re-injection compressors and the field re-injection compressor for a total gas handling shut down. Additional wells were shut in at this time. Purge cycles would not initiate for a re-start until automation was able to trouble shoot the cause and resolve the situation. An automated valve signal failed on one start up attempt, E-pad gas handling re-set held out re-start attempts, gas plant pressure switch setting stopped several re-start attempts. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point Apri120, 1997 Time and duration of incident: 1112 hrs - 5 hr 20 min Flare Volume: 279 MCF Assist Gas Volume: 1612 MCF • This was an unplanned flaring event when the IWAG injection at C-pad shutdown due to an oxygen analyzer wiring problem. Additional adjustments were made on the carburetor controls. Production wells were shut-in to mitigate flaring. Once maintenance was completed on the injection compressor, it was returned to service without incident. • • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point April 21, 1997 Time and duration of incident: 2003 hrs - 1 hr 12 min Flare Volume: 94 MCF Assist Gas Volume: 474 MCF This was unplanned flaring as a result of an unexpected shut down of the C-pad gas injection compressor (IWAG). The compressor required repairs before it could be brought back on line. The repairs were expedited and the compressor returned to service as soon as possible. • • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point April 26, 1997 Time and duration of incident: 2230 hrs - 1 hr 12 min Flare Volume: 45 MCF Assist Gas Volume: 175 MCF This was unplanned emergency flaring as a result of an emergency shut down on E-pad. The ESD was manually initiated after a mechanical equipment failure of a producing well component. The ESD was necessary for emergency response personnel to safely enter the immediate area. Safe conditions were restored and the well pad returned to normal service as soon as possible, at which time facility gas compressors were restarted. C~ BP EXPLORATION April 11, 1997 ~~..~F.~ ~ ~ State of Alaska Alaska Oil and Gas Conservation Commission 3001 Porcupine Drive Anchorage, AK 99501 Attn. Wendy Mahan: • BP Exploration (Alaska) Inc. 900 East Benson Boulevard P.O. Box 196612 Anchorage, Alaska 99519-6612 (907) 561-5111 Attached are the Monthly Producer's Report of Gas Disposition for the month of March 1997 . Should you have any questions, please contact Bob Wilks at (907) 564-5670. Sincerely, ~~~ Paul D. Bly Manager, Volume, Royalty & Severance ~~ ~ ~ ~~ a,~R 1 ~ ~'" ~ s' c'2~4` $E iU~S ~~~Iti~~ ;,~f~ki~~~'~ Alaslci~ ~~I~ ~~~~c~ ~~ ALASKA OIL AND GAS CONSERVATION CONII~lISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition Milne Point BP Exploration (Alaska) Inc. Milne Point March, 1997 • u Disposition Volume MCF* 1. Sold Fuel 16,464 2. Reinjected 519,279 3. Flared or vented less than 1 hour 826 4. Flared or vented greater than 1 hour 2,432 (Supplemental report required--See 20 AAC 25.235) 5. Pilot and Purge 2,077 6. Used for lease operations Fuel 281,760 Assist 26,311 7. Other » TOTAL items 1-7 ~ 849,149 8. NGL gas equivalent produced t Q° ' s G t F N -' ~"~"~ 9. Purchased gas ' ~ -P ~.~-~ ~ ~ 10. Transferred from: .'yo t.fl -d ~~ 11. Transferred to: ', Remarks: I hereby cert'fy that Signature ~~,~ ~ the foregoing C1y/ is true and correct to the Title ~F' ~~ best of my knowledge. Date ~jf~~~'J *Indicate contribution of each pool to total. Pool Name Code Percent KUPARUK 525100 93.8 SCH. BLUFF 525140 6.2 Official IIse Only'-Flaring Authorization>l hr. 1. Safety MCF 2. Lease MCF 3. Conserv. Purposes MCF Commissioner Date (Note: All volumes must be corrected 'to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month folowing the month of disposition. Authority 20 AAC 25.235. Form 10-422 Rev. 4/95 04/04/97 oszs ~ Milne Point Unit • mthly Gas Flaring Incident Report For: Mar /1997 Flare Name: Flare 1 (Unplanned Events greater than 1 hour ~~ Duration =Volume (MSCF) _ Start Time (hh:mm) Flare Assist Cause 43.3 259.8 (see above comment) 03/07/97 06:14:00 01:16 83.0 360.1 6 ' 14 - ~ ~ 3 0 03/15/97 04:34:00 06:56 298.9 1,673.3 ~i-"3't - 1 ~ ~ 3 O 03/15/97 12:16:00 02:14 74.4 371.7 ~Z~ 16 - I'}~ 3d 03/15/97 14:32:00 02:28 82.4 413.0 I <} ' 3 Z ' ~ ~' ° ~ 03/15/97 17:01:00 02:44 87.1- 445.0 1~' o t ' 19 '~'hS 03/15/97 19:51:00 02:54 91.6 480.0 19' SI ' ZZ, 46 03/15/97 23:7:00 01:28 47.0 235.3 Z3' ~{ ~ ' o I ', IS 03/16/97 03:04:00 02:11 67.7 337.7 03'.04 - oS'.i S __w'._.. 03/16/97 05:16:00 02:14 66.8 333.$ 05 ~ I b - o~'3c~ 03/16/97 08:01:00 03:44 109.4 547.1 08'. o I - It'~`l S 03/16/97 12:01:00 01:59 59.9 299.4 1 y~ 0 1 - I't'. 0 0 03/16/97 15:02:00 02:58 89.4 447.3 1 S : 0 2 -- 18'. o 0 03/16/97 18:01:00 01:4_4 49.2__ _ 246.0 18'. o t ~' -°I ; ~f S ._._____ 03/1.7/9702:45:00 04:15 163.7 816.5 oz:-tS - O'~soo.'____ 03/21/9713:45:00 01:30 569.6 13~ :I 03/21/97 15:39 00 06:36 393.6 2,101.6 15:39 - ~~ IS' 03/25/97 15:48:00 02:12 182.7 870.4 I S'. `F~~"'-~rB~O~`~` """"'a~ 03/25/97 18:16:00 O 1 29 „~.. ~.a_.. 111 9 _._,~.. ~ vm~~ 609 8 ,~. .~~ r.. ~~ . . 1 ~ , I b ~_ 19 ' ~! S ..~ w~..,,.~..,~...~-._.., ~ ,.~..~. - ,., h.„2. ~...,. ~ 03/28/97 14:43:00 03:02 187.6 . ~. 1,027.2 Unplanned shutdown of C pad IWAG ~9' A3 ^ -~'.4S compressor. 03/29/97 22:33:00 01:27 44.8 268.3 Flared in conjunction with Tract 14 'Z2 ; 33 - oO', o o electrical upgrade/tiein. 03/30/97 00:01:00 01:29 ~~.o~ - ol; 30 Comment Immediately dispatched maintenance crew. Repaired & RTS. Flaring believed to be due to change in field dynamics after T14 s/d. SI some GL wells & reduced lift rates on others to mitigate flare. Flare Assist Unplanned Events <=1 hour 826.1 4,297.8 31 Unplanned Events > 1 hour 2,432.1 12,713.0 Planned Events <= 1 hour and not exceeding 5,000 MCF 0.0 0.0 Planned Events > 1 hour or exceeding 5,000 MCF 0.0 0.0 Unmetered Assist Gas 11,377.0 TOTAL FLARED VOLUME 3,258.2 28,387.8 MSCF y r~ 0 e-s ,~ ~ :~ n 3 V1 ~. ._ ~" -' 1`-'~~ -~ ~.~~ c.so -oa 1°"~` BP Exploration Page 5 of 5 Milne Point, Alaska • • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point March 30, 1997 Time and. duration of incident: See 3/30/97 flare log report Flare Volume: 159 MCF Assist Gas Volume: 983 MCF This was unplanned flaring when Tract 14, G,H,I & J- pads, were all shut down for electrical upgrade/tie-in work. Power line feeder upgrades were made which required production ESP's to be shut down. Some gas lift wells were shut in and gas lift rates on other producers reduced to mitigate flaring. • • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point March 28, 1997 Time and duration of incident: 1443 hrs - 3 hr 2 min Flare Volume: 188 MCF Assist Gas Volume: 1027 MCF This was unplanned flaring as a result of an unexpected shut down of the C-pad gas injection compressor (IWAG). The circumstances of the shut down were determined and conditions restored to normal. The IWAG compressor was re- started as soon as possible and flaring stopped. Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point March 25, 1997 Time and duration of incident: 1548 hrs - 3 hr 54 min Flare Volume: 318 MCF Assist Gas Volume: 1637 MCF This was unplanned flaring as a result of an unexpected shut down of the C-pad gas injection compressor (IWAG). The circumstances of the shut down were determined and conditions restored to normal. The IWAG compressor was re- started as soon as possible and flaring stopped. *w :~ d, g ~ " "`; s ~+ 1597 Alaska Cil & Cos Cons. Com~s~"~ Anchorage • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point March 21, 1997 Time and duration of incident: 13:45 hrs - 8 hrs 14 rains Flare Volume: 522 MCF Assist Gas Volume: 2840 MCF i This was an unplanned intermitting flaring event which occurred when the 1WAG injection compressor was shut-down to make repairs on a glycol leak to the engine coolant header. Maintenance repairs required welding to the glycol header. Production wells were shut-in to mitigate excessive flaring. Once repairs were made, the compressor was returned to service with no further incident. ~~~ a,~;*" ~a ~~, ~~ ~ r ;.., ~ c} ~~~V s, ; ~ ~~,; '~ ' ~ i~i~Ct~~?'°~~~, ~9asiea ~i1 R~ des i~~ra~• pt~ck°s~~a~s U Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point March 17, 1997 Time and duration of incident: 02:45 hrs - 4 hrs 15 min Flare Volume: 164 MCF Assist Gas Volume: 817 MCF • This was an unplanned flaring event which occurred when the IWAG injection compressor shut-down due to loss of fuel gas, caused by a Process Heater shut-down at Cpad. Once repairs were made on (H-2601), the Process Heater was returned to service and IWAG put back on injection. Maintenance crews continue to work on problem with H-5303 (New Process Heater) which appears to have a leak in the fire tube. Once the IWAG injection compressor was returned to service, the flare was eliminated. U Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point March 16, 1997 Time and duration of incident: 00:01 hrs - 16 hrs 20 min Flare Volume: 489 MCF Assist Gas Volume: 3080 MCF • This was a continuation of an unplanned intermitting flaring event from the previous day, which was a result of a gas leak on the 3`d stage suction of the IWAG injection compressor. Maintenance crews had to make repairs several times due to leaking gaskets on the valve cover gaskets of the 3`d stage cylinder of compressor. Additional production was shut-in to mitigate excessive flaring and assist gas was utilized to eliminate any black smoke from the flare tip. Once repairs were successfully made on the IWAG injection compressor around 1800 hrs, there was another problem with accessing fuel gas to the compressor due to the shutdown of the C-pad process heaters. Maintenance crews continued to work on correcting the problem with fuel gas to the IWAG compressor. Once corrected 1WAG compressor was brought on line at 2200 hrs and the flare was eliminated. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point March 15, 1997 Time and duration of incident: 04:34 hrs - 19 hrs 26 min Flare Volume: 687 MCF Assist Gas Volume: 3993 MCF This was an unplanned intermitting flaring event which occurred when the 1WAG Injection Gas Compressor at C-pad shutdown due to high temperature in the 3`d stage suction of compressor. Attempt was made to restart, but was unsuccessful. Maintenance crews made every attempt to expedite the start-up of the unit, but repair is taking longer than initially anticipated. Production wells were shut-in across the field in order to mitigate excessive flaring. The Injection compressor is still down at 0600 on the 16`h' due to a gas leak, which was caused by a gasket failure and was identified during an attempt to re-start compressor at 0300 hrs. Once identified that the injection compressor would be down for longer than anticipated additional production was shut-in to eliminate flaring. Maintenance crews are gathering materials to repair the gasket on the 3`d stage suction cylinder and operations is in the process of completion of a safe-out so the unit can be worked on again. Estimation of compressor downtime is unknown at this time, but expectations are to return to service as soon as safely possible.. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point March 7, 1997 Time and duration of incident: 0614 hrs - 1 hr 16 min Flare Volume: 83 MCF Assist Gas Volume: 360 MCF This was unplanned flaring as a result of an unexpected shut down of the C-pad gas injection compressor (IWAG). The circumstances of the shut down were determined and conditions restored to normal. The IWAG compressor was re- started as soon as possible and flaring stopped. • BP EXPLORATION March 13, 1997 State of Alaska Alaska Oil and Gas Conservation Commission 3001 Porcupine Drive Anchorage, AK 99501 Attn. Wendy Mahan: BP Exploration (Alaska) Inc. 900 East Benson Boulevard P.O. Box 196612 Anchorage, Alaska 99519-6612 (907) 561-5111 Attached are the Monthly Producer's Report of Gas Disposition for the month of February 1997 . Should you have any questions, please contact Bob Wilks at (907) 564-5670. Sincerely, ~~~ ~. Paul D. Bly Manager, Volume, Royalty & Severance n. ' ALASKA OIL AND GAS CONSERVATION CONII~lISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition Milne Point BP Exploration (Alaska) Inc. Milne Point February, 1997 u Disposition Volume MCF* 1. Sold Fuel 14,906 2. Reinjected 493,967 3. Flared or vented less than 1 hour 308 4. Flared or vented greater than 1 hour 117 (Supplemental report required--See 20 AAC 25.235) 5. Pilot and Purge 1,876 6. Used for lease operations Fuel 247,436 Assist 18,676 7. Other 'i ras5 TOTAL items 1-7 1~ ~ 777,286 ~.s "~ 8. NGL gas equivalent produced ~ ~ ~.C3 9. Purchased gas 3 10. Transferred from: 11. Transferred to: Remarks: I hereby cert~if/y that th~ej~foregoing is true and correct to the best of my knowled/ge. Si nature Title Date /v *Indicate contribution of each pool to total. Pool Name Code Percent KUPARUK 525100 94.8 SCH. BLUFF 525140 5.2 Official Use Only-:Flaring Authorization>1 hr. 1. Safety MCF 2. Lease MCF 3. Conserv. Purposes MCF Commissioner Date (Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month folowing the month of disposition. Authority 20 AAC 25.235. Form 10-422 Rev. 4/95 SENT BY~BPX-MPOC 3- 8-97 ; 853 ; BPX-MILNE POINT-~ 9075644094;# 7/ 8 : us~u~y~ i ~s~ ~ Milne Point Unit • M hlp Gas Flaring Incident iteport For: Feb /1997 F~rc Nxmc: Flare 1 f IT®pllanned Events greater than l.hour _ ......._..-._._.... ...._...:._---... . . .. ~~ Duration =Volumc(MSCF) = Start Time (hh:mm) Flerc Assist Cause Comment U2/U6/y7 18:47:OU U' : 4 3 69.4 278.5 02/U6/97 21:46:04 01:14 47.6 190.7 Flare Assist Unplanned Events <=1 hour 307.7 1,756.2 E'nplanncd Events > ~ hour 117.1 469.2 Planned Events <=1 hour and not exceedi~tg 5,000 MCF 0.0 0.0 Plac<~ed Events > 1 boar or exec :ding S,OOU MCF 0.0 O.U ITn~retered Assist Gas 10,276.0 TO7CAL FLA1tCD VOLUME 424.7 ] 2,01.4 MSCF 28 '', IIP' i:xplora6on Pam 4 of 4 .......... Milne l+cHnt, Alaska SENT BY-BPX-MPOC 3- 8-9? 853 BPX-MILIVE POINT. 9075644094;# 8/ 8 • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point February 6, 1997 Tlme and duration of Inddent: 1847 hrs - 1 hr 13 min Flare Volume: 69 MCF Assist Gas Volume: 279 MCF -Time end duration of incident: 2146 hrs -1 hr 14 min Flare Volume: 48 MCF Assist Gas Volume: 191 MCF The.:: were unplanned flaring events from the same cause.. The C-5501.6 gas. compressor required unplanned repairs of having to change out cylinder internal valves. The work was coordinated with other field maintenance while production rates were lowered. Additionally, all gas lifted wells were shut in to mitigate flaring for the duration of the gas compressor repairs. ALASKA OIL AND GAS CONSERVATYON COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition Milne Point BP Ex loration (Alaska) Inc. Milne Point Januar 1997 Disposition Volume MCF* 1. Sold Fuel 15,959 2. Reinjected 521,377 3. Flared or vented less than 1 hour 1,019 4. Flared or vented greater than 1 hour (Supplemental report cequi~ed--See 20 AAC 25.235) 3 8 2 5. Pilot and Purge 2,082 6. Used for lease operations Fuel Assist 263,065 16,836 7. Other TOTAL items 1-7 820,720 8. NGL gas equivalent produced 9. Purchased gas 10. Transferred from: 11. Transferred to: Remarks: I hereby certify that the foregoing is true and correct to the best of my knowledge. ~ /~ f ~o Ddc7i.^ao Signature s ,~G,~G~i~"/ Title .%~v/J ysT Date // Form 10-422 Rev. 4/95 *Indicate contribution of each pool to total. Pool Name Code Percent KUPARUK 5 2 510 0 9 5.2 SCH. BLUFF 5 2 514 0 4.8 Official Use Only-Flaring Authorization>l hr. 1. Safety MCF 2. Lease MCF 3. Conserv. Purposes MCF Commissioner Date (Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month folowing the month of disposition. Authority 20 AAC 25.235. 02/09/97 13:30 Milne PointUnit _ l~thly Gas Flaring Incident Report • For: Jan /1997 . Flare Name: Flare 1 np anne vents ess t an or equa to our Duration -Volume (MSCF) Start Time (hh:mm} Flare Assist Cause Comment 01/11/97 20:44:00 01/11/97 22:53:00 01/11/97 23:58:00 01/12/97 00:59:00 01/12/97 06:29:00 01/12/97 20:10:00 01/12/97 20:40:00 01/12/97 21:59:00 01/12/97 22:11:00 01/17/97 08:32:00 01/17/97 09:31:00 01/17/97 09:48:00 01/17/97 10:22:00 O 1 / 17/97 10:44:00 O 1 /22/97 19:06:00 O 1 /22/97 19:28:00 01/22/97 21:30:00 O 1 /22/97 21:47:00 01/22/97 22:07:00 01/22/97 22:17:00 01/22/97 23:02:00 01/23/97 08:45:00 01/23/97 09:06:00 01/23/97 09:19:00 01/23/97 09:41:00 01/23/97 09:47:00 00:16 0.5 2.3 00:22 2.9 9.8 00:17 0.6 2.4 00:16 0.1 0.5 00:16 0.2 0.8 00:20 1.9 6.8 00:20 1.6 5.8 00:16 0.2 0.4 00:19 1.4 5.0 00:58 32.2 112.9 00:14 6.9 24.4 00:27 17.5 61.7 00:08 7.5 26.9 00:01 0.3 1.0 00:09 4.9 28.2 00:02 0.9 6.2 00:15 14.8 75.0 00:13 10.9 64.3 00:08 4.8 30.0 00:43 33.6 189.5 00:13 10.2 56.5 00:15 16.5 76.0 00:09 5.1 89.8 00:11 5.8 86.8 00:04 1.3 84.3 00:58 46.0 384.4 Unplanned event caused ly IWAG compressor shutdown at C pad (electronic ignition problems). 01/23/9710:49:00 00:26 22.1 193.5 01/23/9711:24:00 00:21 19.6 197.2 01/23/9711:55:00 00:20 19.1 174.3 01/23/9712:26:00 00:19 21.8 183.6 01/23/9712:56:00 00:04 3.1 85.5 01/23/9713:13:00 00:02 1.5 13.9 01/24/9714:22:00 00:08 5.8 86.6 01/24/9714:43:00 00:02 2.1 15.3 01/31/9713:59:00 00:01 0.4 1.4 Several restarts were attempted during '' flaring. Ignition system was repaired & compressor RTS with no father incident. BP Exploration ..Page 6 of 7 Milne Point, Alaska o2io9i9~ t3:3o -Milne-Point Unit l~thly Gas Flaring Incident Report • For: Jan /1997 Flare Name: Flare 1 Unplanned Events greater th an 1 hour Duration -Volume (MSCF) Start Time (hh:mm) Flare Assist Cause Comment 01/08/97 02:26:00 01:19 58.3 2.5 Fieldwide production shutdown caused Field restart was delayed until root by LSHH in vent scrubber vessel. cause of shutdown identified. Level control pump for scrubber was repaired & field was brought BOL. 01/08/97 04:20:00 02:40 137.0 77.9 Fieldwide production shutdown caused Flaring while bring field BOL. by LSHH in vent scrubber vessel. 01/08/97 09:33:00 01:42 86.1 85.8 Second full field shutdown due to Returned process conditions to safe LSHH in 1st stage slug catcher vessel. parameters & brought field BOL. 01/17/97 07:19:00 01:11 44.3 154.7 Unplanned repairs required on Big A SI high gor wells to mitigate flaring (C-5501/11A) gas compressor. during repairs. Expedited repairs & RTS w/out incident. 01/24/97 13:14:00 01:01 56.2 382.9 Unplanned flare event caused by IWAG Problem (bad o-ring) identified with compressor shutdown at C pad. carburetor control. Replaced &RTS w/ no further incident. Flare Assist Unplanned Events <= 1 hour 1,018.9 4,755.0 Unplanned Events > 1 hour 381.8 703.9 Planned Events <=1 hour and not exceeding 5,000 MCF 0.0 0.0 Planned Events > 1 hour or exceeding 5,000 MCF 0.0 0.0 Unmetered Assist Gas 11,377.0 TOTAL FLARED VOLUME 1,400.7 16,835.8 MSCF 31 BP Exploration Page 7 of'7 Milne Point, Alaska C~ Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point January 8, 1997 Time and duration of incident: 0226 hrs - 1 hr 19 min Flare Volume: 58 MCF Assist Gas Volume: 3 MCF • Time and duration of incident: 0420 hrs - 2 hr 40 min Flare Volume: 137 MCF Assist Gas Volume: 78 MCF These were unplanned emergency flaring events from the same cause. Afield wide production shutdown was initiated at 0226 from a level safety high high in the vent scurbber vessel. Restarting the field was delayed until the root cause was identified and equipment repaired. The level control pump for the vent scrubber had component failures requiring maintenance repairs prior to returning the field to production. Time and duration of incident: 0933 hrs - 1 hr 42 min Flare Volume: 86 MCF Assist Gas Volume: 86 MCF This event was also unplanned emergency flaring as a result of a second field wide production shut down intiated from the slug catcher vessel level safety high high. Process conditions were restored to safe parameters within the normal operating limits. Field production was gingerly brought back on line in a manner to mitigate potential of experiencing additional process upsets. • • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point January 23,1997 Time and duration of incident: 09:47 hrs - 2 hrs 24 min Flare Volume: 129 MCF Assist Gas Volume: 1,122 MCF This was an unplanned flaring event which occurred when the IWAG injection compressor at C-pad was shut-down due to a problem with the electronic ignition. The compressor was re-started several times during this intermittent flaring event. Once the ignition system was repaired the compressor was returned to normal operation and the flare was eliminated with no further incident. • Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point January 24, 1997 Time and duration of incident: 13:14 hrs - 1 hr 1 min Flare Volume: 56 MCF Assist Gas: 383 MCF This was an unplanned flaring event which occurred when the IWAG Injection Compressor was shut down due to a problem with carburetor control. Replaced bad O-ring in carburetor and returned unit to service. Once injection compressor was returned to service the flare was eliminated. Flaring Incident Report (exceeding 1 hour) BP Exploration -Milne Point January 17~ 1997 r~ u Time and duration of incident: 0719 hrs - 1 hr 11 min Flare Volume: 44 MCF Assist Gas Volume: 155 MCF This was an unplanned flaring event when repairs to the C-5501/11A gas compressor were required. High GOR wells were shut in to mitigate flaring prior to stopping the compressor. The repairs were expedited and the compressor returned to service and shut in production wells brought back on line.