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Alaska Oil and Gas Conservation Commission
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HomeMy WebLinkAboutBPXA - ENDICOTTState of Alaska
Alaska Oil & Gas Conservation Commission
1999 Facility Report
Files
File Names Gas Disposition
- Frd;,~fl~~r
..,.ALASKA OIL AND GAS CONSERVATION CONII~lISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Facility Operator Field(s) Month/Year of Disposition
Endicott BP Exploration (Alaska) Endicott 10450 Jan-99
Disposition ~ Volume MCF*
1. Sold
To Fuel
NGL
Badami 17,021
171,844
5,256
2. Reinjected 10,661,318
3. Flared or vented less than 1 hour 439
4. Flared or vented greater than 1 hour
(Supplemental report required--See 20 AAC 25.235) 10,417
5. Pilot and Purge 9,784
6. Used for lease operations Assist
Fuel 23,369
884 443
7. Other
TOTAL items 1-7 11,783,891
8. NGL gas equivalent produced 171,844
9. Purchased gas
10. Transferred from:
11. Transferred to:
I hereby ce ify t t the foregoing is true and correct to the best of
Signature .~, Title/yuvrL~ t ~ ^ Date Z, ,5"
*Indicate contribution of each pool
Pool Name
220100 Code Percent
Official Use Only-Flaring Authorza
1. Safety MCF
2. Lease MCF
3. Conserv. Purpos MCF
Commissioner Date
Note: All volumes must be
corrected to pressure of 14.65
Asia and to a temperature of 60
degrees F. Report due by the
20th of the month folowing the
month of disposition.
Authority 20 AAC 25.235.
Form 10-422
Rev. 4/95
2/8/99
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL N0.202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
January-99
Unplanned Events less than or equal to 1 hour
.~
DATE ' TIME rVOLUME ' iDESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATEGAUSE
TOTAL 457 Not required for unplanned events which Not required for unplanned events which
are less than or equal to 1 hour are less than or equal to 1 hour
Unplanned Events greater than 1 hour
DATE ' TIME VOLUME DESCRIPTION OF' INCIDENT & CAUSE ACTION TAKEN;TO ELIMINATE<:CAUSE
Plant upset; DCS failure, high separator level
1/10/99 18:20-23:50 962 alarm, All SDI wells were shut-in
1 / 11 /99 00:00-01:50 279 Booster compressor shut-down. Restarted compressor
1 /12/99 22:20-23:50 219 Booster compressor shut-down. Restarted compressor
Booster compressor shut-down. Problems
1/13/99 14;30-17:00 1,431 with NGLsystem. Restarted compressor
1/15/99 01:50-04:50 300 ---- - .___,Booster compressor down, cooler froze up. Restarted compressor
,,Propane compressor system problems, NGL
1/18/99 08:20-11:30 282 ~-°._W~.- "~"~ plant upset. Restarted propane compressor
1 /21 /99 12:00-13:50 249'- ~°-"`~°-- --•-----.~..N.~, Booster compressor shut-down. Restarted compressor
1 /27/99 13:00-16:15 744 ~- ~°~--,--- -----~---.--.._ Gas booster compressor fin fans freezing up. Restarted compressor
1 /28/99 00:00-02:30 525 w._----Booster compressor shut-down. Restarted compressor
1 /29/99 13:10-23:10 2,449 ---- --------- ------~.._. Booster compressor Ashut-down. Restarted compressor
....
~
_
- ------- MGC-A Shut-down. Lost power supply due
1 /30/99 20:30-23:50 2,51 to PLC error. ALL wells shut-in.
1 /31 /99 01:40-05:00 902 Booster compressor down, plant upset. Restarted compressor
TOTAL 10,860
Planned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mcf
DATE TIME ' 'VOLUME ' iDESCRIPTION OF INCIDENT & CAUSE 'ACTION TAKENTO ELIMINATECAUSE'
None
TOTAL 0
Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf
~~
DATE TIME': VOLUME ' DESCRIPTION OF.:.INCIDENT & CAUSE ACTION:TAKENTO ELIMINATE CAUSE
None
TOTAL 0
Page 1
2/8/99 BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL N0.202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
January-99
TOTAL EIDR SDN ENDICOTT
Volume flared less than 1 hour 457 18 0 439
Volume flared greater than 10,860 433 10 10,417
1 hour
Pilot Purge 10,199 406 9 9,784
Assist Gas 24.361 970 22 23,369
TOTAL FLARED VOLUME 45,877 1,827 41 44,009
Page 2
ALASKA OIL AND GAS CONSERVATION COL~lISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Facility Operator Field(s) Month/Year of Disposition
Endicott BP Exploration {Alaska) Endicott 10450 Feb-99
Disposition
Volume MCF*
1. Sold
To Fuel
NGL
Badami 15,159
160,792
42 362
2. Reinjected 8,791,886
3. Flared or vented less than 1 hour 5,885
4. Flared or vented greater than 1 hour
(Supplemental report required--See 20 AAC 25.235) 4,655
5. Pilot and Purge 8,527
6. Used for lease operations Assist
Fuel 20,611
718,474
7. Other
TOTAL items 1-7 9,768,351
8. NGL gas equivalent produced 160,792
9. Purchased gas
10. Transferred from:
11. Transferred to:
I herebv c
Signature
that the foregoing is true and correct to the best of
Title /~(L VDL Date
*Indicate contribution of each pool
Pool Name Code Percent
220100
Official Use Only-Flaring Authoriza
1. Safety MCF
2. Lease MCF
3. Conserv. Purpos MCF
Commissioner Date
Note: All volumes must be
corrected to pressure of 14.65
Asia and to a temperature of 60
degrees F. Report due by the
20th of the month folowing the
month of disposition.
Authority 20 AAC 25.235.
Form 10-422
Rev. 4/95
3/5/99
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL N0.202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
February-99
Unplanned Events less than or equal to 1 hour
DATE TIME VOLUME ' DESCRIPTION'OF'INCIDENT'& CAUSE `ACT10N TAKEN TO ELIMWATE CAUSE
TOTAL 6,359 Not required for unplanned events which Not required for unplanned events which
are less than or equal to 1 hour are less than or equal to 1 hour
Unplanned Events greater than 1 hour
DATE TIME VOLUME 'DESCRIPTIONIO~ INCIDENT'& CAUSE 'ACTION TAKEN'T0 ELIMINATE''CAUSE
Both booster compressors shut-down on high Closed louvers, circulated hot glycol until inter-
2/1 /99 0800-1630 733 temp alarms when the inter-coolers hydrated off coolers thawed out.
Booster compressor shut-down unexpectedly Finally able to restart booster compressor, -ooking
2/10/99 1750-1920 303 to cause for shut-down.
MI compressor commissioning upsets. Troubleshoot and tune logic controls on MI
2/17/99 2150-2300 472 compressor
Temperature control valve stuck open to flare Reseated valve.
2/21 /99 2030-0000 967 header.
MI compressor commissioning upsets. Reviewed MI compressor start-up procedures.
2/23/99 1510-0000 1,403 Troubleshoot and tune logic controls
Startup of MGC-B after shut-down caused Review start-up procedures.
2/24/99 0000-0110 236 unexpected process upset
Process upset due to large volume slug off liquid Reviewed 3-phase instability of SDI flowline and
2/24/99 0930-1430 662 from SDI, plant shut-down. standard procedure for well operation at SDI
MI compressor shut-down due to problems with Controls on 1st stage suction reprogrammed
2/28/99 2040-0000 254 1 stage suction.
TOTAL 5,030
Planned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mcf
DATE' TIME ' VOLUME DESCRIPTION'OF»JNCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE ''
None
TOTAL 0
Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf
DATE TIME VOLUME ' DESCRIPTION'OF INCIDENT & CAUSE . :ACTION TAKEN'TO Ei.1M[NATE"CAUSE
None
TOTAL 0
Page 1
3/5/99 BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL N0.202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
February-99
TOTAL EIDR SDN ENDICOTT
Volume flared less than 1 he 6,359 465 9 5,885
Volume flared greater than 5,030 368 7 4,655
1 hour
Pilot Purge 9,212 673 i2 8,527
Assist Gas 22.268 1.627 30 20,611
TOTAL FLARED VOLUME 42,869 3,133 58 39,678
Page 2
ALASKA OIL AND GAS CONSERVATION CONII~lISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Facility Operator Field(s) Month/Year of Disposition
Endicott BP Exploration (Alaska) Endicott 10450 Mar-99
Disposition
Volume MCF*
1. Sold Fuel
NGL
To Badami 16,160
116,520
38,280
2. Reinjected 5,592,020
3. Flared or vented less than 1 hour 9,174
4. Flared or vented greater than 1 hour
(Supplemental report required--See 20 AAC 25.235) 9,660
5. Pilot and Purge 9,202
6. Used for lease operations Assist
Fuel 22,019
571,495
7. Other
TOTAL items 1-7 6,384,530
8. NGL gas equivalent produced 116,520
9. Purchased gas
10. Transferred from:
- 11. Transferred to:
I hereby ce ify t at the foregoing is true and correct to th~e~~be~st~ of
Signature Title ~((. J~k Date YI II 4"{
*Indicate contribution of each pool
Pool Name Code Percent
220100
Official Use Only- Flaring Authoriza
1. Safety MCF
2. Lease MCF
3. Conserv. Purpos MCF
Commissioner Date
Note: All volumes must be
corrected to pressure of 14.65
psia and to a temperature of 60
degrees F. Report due by the
20th of the month folowing the
month of disposition.
Authority 20 AAC 25.235.
Form 10-422
Rev. 4/95
4/6/99
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL N0.202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
March-99
Unplanned Events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
TOTAL 10,168 Not required for unplanned events which Not required for unplanned events which
are less than or equal to 1 hour are less than or equal to 1 hour
Unplanned Events greater than 1 hour
DATE TIME' VOLUME "DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
MI compressor pressure control setpoint was low Adjusted pressure control setpoint accordingly.
03/01 /99 17:10-20:50 1,375 and caused flare valve to open.
Booster compressor S/D for high temp caused by Booster compressor restarted.
high first stage separator pressure, assist gas on
03/01 /99 22:50-00:00 88 for opacity compliance.
Booster compressor SID for high motor temp Booster compressor restarted.
caused by high first stage separator pressure,
03/01 /99 11:50-13:20 81 assist as on for opacity compliance,
Booster compressor S/D due to motor heating up Production cut to lower first stage separator
03/02/99 00;00-01:20 52 because of high first stage separator pressure, pressure, booster compressor restarted,
MI compressor upsets, Attempts start up and Troubleshoot and tune control logic. Adequate
tune control system. Assist gas on for opacity production cut, but flare response lags cuts,
03/03/99 19:20-20:40 196 compliance.
MI compressor upsets, High differential pressure Troubleshoot operating procedures and tune
03/04/99 09:40-11:50 895 across seals caused shutdown. control logic,
MI compressor upsets. Attempts start up and Troubleshoot operating procedures and tune
tune control system, Assist gas on for opacity control logic.
03/04/99 13:50-17:00 266 compliance. Shut down for high temp. in 2nd
Assist gas on for opacity compliance following Troubleshoot operating procedures and tune
03/04/99 17:20-19:00 73 S/D of MI compressor earlier in day. control logic.
MI compressor start up and shut-down for high Troubleshoot operating procedures and tune
differential across seals. Assist gas on for opacity control logic.
03/05/99 15;00-16;00 180 compliance.
Leaking valve in MI compressor skid. Assist gas Identified and fixed leaking valve,
03/08/99 13:20-15:50 254 increased for opacity compliance.
MI compressor start up and shut-down for high Troubleshoot operating procedures and tune
temp in 1st stage discharge. Assist gas on for control logic.
03/08/99 10:30-12:10 194 o aci com liance,
Page 1
4/6/99
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL N0.202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
March-99
Lost "A"-Main when "B"-Main was already down Shut-in all production. Diagnosed and repaired
for upgrades: lost water pump and low pressure anti-surge valve,
booster compressor, Root cause was anti-surge
03/09/99 02:50-05:00 4,004 valve faliure on 1st stage comp.
NGL plant upset, slug of NGL not absorbed in Adjusted NGL plant.
low oil level in stabilizer and sent to flare, Assist
03/11 /99 08:50-10:20 29 gas on for opacity compliance,
03/12/99 10:00-13:20 2 Assist gas on for opacity compliance, Plant stablilzed,
Failed seal buffer pump caused water injection Repaired faulty seal buffer pump. Flare was
pump S/D, triggering plant upset that resulted in CAUSED by sudden loss in production when
booster compressor and NGL reboiler S/D. Assist water injection pump S/D. Booster compressor
03/ 14/99 08:00-09:00 107 gas on for over 1 hour for opacity compliance. and NGL reboiler could not be restarted in less
MI compressor startup and leaking temperature Ceased start-up attempts when problem was
valve. Additional assist gas required to maintain identified. Closed manual block valve. No
03/18/99 09:30-00:00 1,163 opacity compliance. mitigation possible with production cut.
MI compressor temperature control valve Closed block valve after compressor S/D when
03/19/99 00:00-02:50 73 leakin leak was identified.
Booster compressor S/D due to liquid slug into Cut production to mitigate slugging, Restart
03/21 /99 07:20-08:20 37 plant. Assist gas on for opacity, booster compressor.
MI compressor start up and shut-down. Assist Troubleshoot operating procedures and tune
03/23/99 14:10-15:10 31 gas on for opacity compliance. control logic.
Attempted to start up MI compressor. Troubleshoot operating procedures and tune
03/24/99 09:50-12:00 81 control logic,
Temperature control valve leak by in MI Valve identifed and re-seated, Troubleshoot
03/24/99 13:10-16:30 35 compressor, o erating procedures and tune control logic.
MI compressor upsets Troubleshoot operating procedures and tune
03/25/99 11:30-15:50 487 control logic.
MI compressor start-up. Assist gas on for opacity Troubleshoot operating procedures and tune
03/26/99 13:10-15:50 45 compliance. control logic.
Plant upset. First stage separator flare valve Cut production to eliminate flaring. Diagnosed
opened and first stage compressor PSV opened and repaired control problem.
03/31 /99 19:50-21:20 958 to flare due to antisur e valve control problem
TOTAL 10,706
Page 2
4/6/99
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL N0.202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
March-99
Planned Events Less T han or Equal 1 Hour AND Not Exceeding 5000 Mcf
DATE TIME ' VOCUMf DESCRIPTION OF INCIDENT & CAUSE ACTION'TgKEN TO ELIMINATE CAUSE
None
TOTAL 0
Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf
DATE TIME VOLUME ' DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
None.
TOTAL 0
TOTAL' EIDR
Volume flared less than 1 h 10,168 977 SDN
17 ENDICOTT
9,174
Volume flared greater than 10,706 1,029 17 9,660
1 hour
Pilot Purge 10,199 980 17 9,202
Assist Gas 24.404 2.345 40 22,019
TOTAL FLARED VOLUME 55,477 5,331 91 50,055
Page 3
ALASKA OIL AND GAS CONSERVATION CONII~lISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Facility Operator Field(s) Month/Year of Disposition
Endicott BP Exploration (Alaska) Endicott 10450 Apr-99
Disposition
Volume MCF*
1. Sold Fuel
NGL
To Badami 15,605
114,343
55,689
2. Reinjected 5,714,277
3. Flared or vented less than 1 hour 5,332
4. Flared or vented greater than 1 hour
(Supplemental report required--See 20 AAC 25.235) 4,672
5. Pilot and Purge 9,102
6. Used for lease operations Assist
Fuel 21,906
624,187
7. Other
TOTAL items 1-7 6,565,113
8. NGL gas equivalent produced 114,343
9. Purchased gas
10. Transferred from:
11. Transferred to:
I hereby ce ify hat the f regoing is true and correct to the best of
Signature Title I ~UINV~[~X Date
*Indicate contribution of each pool
Pool Name Code Percent
220100
Official Use Only-Flaring Authoxiza
1. Safety MCF
2. Lease MCF
3. Conserv. Purpos MCF
Commissioner Date
Note: All volumes must be
corrected to pressure of 14.65
Asia and to a temperature of 60
degrees F. Report due by the
20th of the month folowing the
month of disposition.
Authority 20 AAC 25.235.
~~~~
Form 10-422
Rev . 4 / 9 5 Alaska OII ~C GaS Cons. Cotrltri}~$!o~'
Anchorage
5/6/99
Page 1
BP EXPLORATION (ALASKA INC.
ADMINISTRATIVE APPROVAL N0.202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
April-99
Unplanned Events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OFJNCIDENT'& CAUSE ACTION TAKEN TO'ELIMINATE CAUSE
TOTAL 5,567 Not required for unplanned events which Not required for unplanned events which
are less than or equal to 1 hour are less than or equal to 1 hour
Unplanned Events greater than 1 hour
DATE. TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE' ` ACTION TAKEN TO'ELIMINATE CAUSE
"A"-Main shut down unexpectedly due to ground Source of ground fault was found and repaired.
fault which tripped control system. "A"-main Not expected to happen again.
depressurized relatively quickly (-40-50 minutes)
but assist gas was needed to maintain
04/01 /99 10:20-15:30 554 compliance with EPA opacity re ulatlons.
Plant processes were in an upset condition Plant processes were stabilized and assist gas was
following full field shut-down. Assist gas was used no longer needed.
04/01 /99 18:50-00:00 14 to maintain compliance with EPA opacity
Start-up of MI compressor. Assist gas was used as Troubleshooting and tuning controls for
necessary to avoid opacity as per EPA commissioning. Flaring necessary to pressurize
04/04/99 09:30-10;50 140 re ulations. com ressor for start-u .
Assist gas was used duing plant upset condition to Plant operation was stablized and assist gas as
04/04/99 13;40-14:50 206 maintain compliance with EPA o aci turned off.
MI compressor was started-up with necessary use Troubleshooting and tuning of controls for
of assist gas to avoid opacity as per EPA commissioning. Flaring was necessary to
04/04/99 16:00-17:50 75 re ulations. ressurize compressor for start-up.
The MI compressor was initiating plant instability Troubleshooting and tuning controls for
which called for use of assist gas to avoid opacity commissioning. Plant operation was stablized
as per EPA regulations. MI compressor was also when MI compressor was depressurized and assist
04/04/99 18:10-20:10 199 shut-down later in this event, as was turned off.
Unstable plant processes necessitated use of Plant processes were stabilized and assist gas was
assist gas to maintain compliance with EPA no longer needed.
04/05/99 14:10-17:10 33 o aci re ulatlons.
Plant in upset condition resulting from ramping up Plant operations stabilized and assist gas was no
production affer TAPS proration. Upset condition l onger needed. Booster compressor was re-
caused booster compressor to shut down started.
unexpectedly requiring assist gas for compliance
04/10/99 17:50-21:10 117 with EPA o aci re ulations.
5/6/99
Page 2
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
April-99
04/15/99 115:00-17:20
04/15/99 119:20-21:00
04/17/99 09:10-10;30
04/ 17/99 13:30-15:10
04/20/99 19:20-00:00
04/26/99 19:50-20:50
TOTAL
MI compressor instability led to flaring and
necessary use of assist gas to avoid opacity, as
131 per EPA re ulations.
Gas lift instability initiated instability in gas
production rate and resulted in compressors
bogging down,
860
"B"-Main shut down unexpectedly due to high
pressure trip. The high pressure resulted from
plant instablity initiated by the "A"-Main shut
2,302 down for u grades on the previous evenin ,
The plant was unstable when bringing wells back
on production following complete shut-down.
Upset condition required use of assist gas to avoid
42 opacity as per EPA re ulations.
MI compressor shut-down led to gas release from
depressurization, but the majority of the flare
event duration was due to extended use of assist
gas as per EPA opacity requirements.
Troubleshooting and tuning controls for
commissioning.
High GOR production was cut, but not quickly
enough to avoid the flare. The maJority of the
flare volume was flared over a span of less than
30 minutes, but depressurization of the high
pressure flare header lengthened duration of the
All wells were shut-in automatically. "B"-Main was
restarted as soon as possible and the wells were
brought back on slowly to promote plant stability.
Plant operations stabilized and assist gas was no
longer needed,
Troubleshooting and tuning controls for
commissioning. The faulty control function was
identified and corrected. Assist gas was used to
mitigate black flare smoke resulting from MI
250 compressor shutdown.
MI compressor shut-down Jed to some gas release Troubleshooting and tuning controls for
from depressurization, but the duration of the commissioning.
flare event was mostly determined by extended
143 use of assist as as per EPA o achy requirements.
,066
Planned Events Less Than or Equal 1 Hour AND Not Exceedina 5000 Mcf
DATE
04/03/99 22:10-22:10
VOLU
113
DESCRIPTION OF INCIDENT. & CAUSE
MI compressor was shut-down voluntarily, but still
depressured via flaring.
.ACTION TAKEN TO ELIMINATE CAUSE
Troubleshooting and tuning of controls for
commissioning. Flaring was necessary to safely
ressurize com ressor when shuttin down.
Flaring was necessary to pressurize the
compression train for start-uo.
04/ 10/99 00:30-00:30
TOTAL
101
214
"B"-Main planned start-up following upgrades
5/6/99
Page 3
BP EXPLORATION (ALASKA INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
April-99
Planned Events Exceed ing 1 Hour OR Exceeding 5000 Mcf
-DATE TIME VOLUME DESCRIPTION OF INCIDENT.'& CAUSE ACTION TAKEN TO ELIMINATE CAUSE
None
TOTAL 0
TOTAL EIDR
Volume flared less than 1 h 5,781 444 SDN
5 ENDICOTT
5,332
Volume flared greater than 5,066 390 ~ 4 4,672
1 hour
Pilot Purge 9,870 759 9 9,102
Assist Gas 23.754 1.827 21 21,906
TOTAL FLARE D VOLUME 44,471 3,420 39 41,012
Re: Endicott Flare Reporting Follow-up
Subject: Re: Endicott Flare Reporting Follow-up
Date: Thu, 08 Apr 1999 11:54:22 -0800
From: Wendy Mahan <Wendy_Mahan@admin.state.ak.us>
Organization: doa-aogcc
To: "McEntyre, Scott R. (END)" <mcentysr2@BP.com>
Mr. McEntyre,
Hi,
I still need detailed explanations of all of the flaring events for both
January and February. Explanations should include descriptions,
including timing, of equipment problems, employees efforts to resolve
the problems and any efforts made to minimize flaring. If no efforts
were made to minimize flaring, please explain why. It may be helpful to
use our current gas disposition regulations, 20 AAC 25.235, as a guide.
Thanks,
Wendy
"McEntyre, Scott R. (END)" wrote:
> Wendy,
> The purposes of this message are to establish electronic communications with
> you and follow-up on our last discussion concerning the Endicott monthly
> flare reports for January and February of this year. I apologize for the
> delay, but the distractions surrounding our current plant upgrade have kept
> everyone here at Endicott extremely busy. Are there any outstanding issues
> we still need to resolve? My notes indicate that you had questions about
> our flaring on January 10th through 31st and throughout February, but I am
> unsure which, if any, have already been addressed.
> Please reply when you have the opportunity.
> Regards,
> Scott R. McEntyre
> Endicott Production Coordinator
> (907) 659-6544
1 of 1 4/8/99 11:55 AM
'99 05~30PM BPX ENDICOTT DEVP
BP EXPLORATION
April 20, 1999
Ms. Wendy Mahan
Oil & Gas Conservation Commission
3001 Porcupine Drive
Anchorage, AK 99501
6F ~XpW-at10n (Alaska) Inc.
900 ~aSt BBnSOn Boulevard
P,O. Box 196612
Anchorage, Alaska 99519.6812
(90~ 561.5111
Subject: Endicott Flate vent Su lament for Janua and Februa of 1999
Dear Ms. Mahan:
P.2i6
In response to your letter of February 16, 1999 the following detail-specific log has been
prepared for Endicott flaring events exceeding one hour in length during January and February
1999. It is our hope that this letter will allay your Concerns and help facilitate a better
understanding of our operations.
As referenced in our letter to the AOGCC dated 8J16/98, an operational improvement to the
Endicott volume accounting methodology went into effect in the second half of last year. It
was acknowledged at the time that this change was likely increase the number of flaring
incidents over one hour.. We would. also like to assure you however that it is our focus at
Endicott, and for BP Arnoco world-wide, to reduce flaring volumes on an ongoing basis. In
1998, Endicott total flaring volume was reduced by 21.5% from 1997 (707.82 to 555.33
mmscf). A further 10% reduction in flare volume has been targeted for i 999 versus the 1998
figures. Endicott is currently on track to deliver the 1999 target with a reduction in first quarter
flare volume of 13% over the comparable period last year in spite of considerable project work
on our facilities during the period.
During the early months of 1999 several large-scale facility projects have been scheduled at
Endicott. These projects include gas handling expansion of the main gas compressor turbines,
commissioning of a new miscible injectant plant and upgrade of the water injection pumps.
During a period such as this process upsets are not uncommon nor unexpected.
Nevertheless, your request for flare event explanations above and beyond the norm is entirely
understandable and we hope the following meets with your satisfaction.
January 1999:
On January 10, 1999, 962 mscf of gas was flayed in the five hour and 30 minute time period
from 18:20 to 23:50. This flare event was caused by lost control to SDI due to a Direct Control
System (DCS) failure which led a high level alarm in the SDI test separator and accompanying
emergency shut-down of all SDI wells. Production was cut when all SDI wells were
automatically shut in for the duration of the event. Plant upsets followed the shut-in of SD1 and
APR 27 '99 05~31PM BPX ENDICOTT DEVP
AOGCC
-Endicott Flare Event Supplement
April 20, 1999
Page 2
P.3i6
added to the flare event. The root cause of the DCS failure has since been identified and
corrected.
A one hour and 50 minute flare event occurred on January 11, 1999, between the hours of
00:00 and 01:50, during which time 279 mscf of gas was flared. This event was caused by the
unexpected shut-down of the booster compressor. When the booster compressor is down, the
low pressure fuel gas is not pressurized enough to re-enter the first stage gas compressor and
must be vented via flaring. Regardless of produced gas rate, the low pressure fuel gas must
be supplied at a near constant pressure in order to ke®p many components of the plant in
operation. for this reason, cutting production of gas is ineff®ctive in minimizing the volume or
duration of a flare event caused by booster compressor shutdown. Assist gas was included in
the reported total flared gas volume because it was used to avoid opacity as per EPA
regulations. The flare event ended when the booster compressor was re-started.
A flare event of one hour and 30 minutes between 22:20 and 23:50 on January 12, 1999,
resulted in the flaring of 219 mscf of gas. This event occurred when the booster compressor
shut down unexpectedly and could not be mitigated by decreasing production of gas, due to
the plant necessity of stable fuel gas pressure, Associated assist gas is included in the
reported total flare volume, as it was used to avoid opacity under EPA regulations. Start-up of
the booster compressor ended the flare event.
On January 13, 1999, a flare event occurred for two hours and 30 minutes from 14:30 to
17:00, during which time 1431 mscf of gas was flared. The causes of this flare event were an
unplanned shut-down of the booster compressor and an increase in assist gas to avoid opacity
during the associated NGL plant upsets. After multiple attempts, the booster compressor was
re-started and the event ended. A decrease in production would not have decreased the
event duration or volume flared, as the gas flared was a combination of temporarily used assist
gas and low pressure fuel gas which is supplied at a steady rate and pressure, regardless of
produced gas volume.
For three hours from 01:50 to 04:50 on January 15, 1999, 300 mscf of gas was flared due to
booster compressor fin fans freezing. A cut in production would not lessen the volume of gas
flared because the flared gas was from the low pressure fuel gas line which is supplied at a
nearly constant. pressure and rate regardless of produced gas rate. The flare ended when the
fin fans were thawed, the booster compressor was re-started, and the low pressure fuel gas
could be pressurized enough to re-enter the main gas compression train,
On January 18, 1999, 525 mscf of gas was flared during the two and one-half hours from
00:00 to 02:30, This event was caused by continued down-time of the booster compressor
that began the previous day. After several attempts, the booster compressor was successfully
re-started, ending the flare event. Cutting production would not have lessened the severity of
this event since the flared gas sources, low pressure fuel gas and associated assist gas for
avoiding opacity, are independent of produced gas rates.
On January 18, 1999, a flare event of three hours and ten minutes from 08:20 to 11:30
resulted in the flaring. of 292 mscf of gas due to propane compressor system difficulties and
accompanying natural gas liquids (NGL) plant upsets. Upsets to the NGL process effectively
cause opacity of flare smoke and mandate use of assist gas as per EPA regulations. The
APR 27 '99 05~31PM BPX ENDICOTT DEVP
AOGCC
Endicott Flare Event Supplement
April 20, 1999
Page 3
P.4i6
cause of this flare event can not be mitigated by decreasing production because the NGL
processing equipment is downstream from most of the gas compression train and the effect of
cutting produced gas is minimal in reducing flare volume and duration. The propane
compressor system is a key component of the NGL system, but is completely independent of
produced gas rates. This event ended when th® propane compressor difficulties were
remedied and the NGL plant was stabilized.
On January 21, 1999, a one hour and 50 minute flare event between 12:00 and 13:50 led to
the release of 249 mscf of gas to the flare. An unplanned booster compressor shut-down was
the cause of this event. Cutting production of gas would not result in minimizing the flare event
volume or duration, because the low pressure fuel gas line was the source of the flared gas.
Assist gas was also added to avoid opacity of flare smoke as per EPA regulations. The event
ended when the booster compressor was re-started.
From 13:00 to 16:15 (three hours and 15 minutes) on January 27, 1999, 744 mscf of gas was
flared when the inter-cooler for the booster compressor froze, in turn causing the booster
comer®ssors to shut-down because of inadequate cooling. During this event, the low pressure
fuel gas was relieved via flaring because the low pressure fuel gas supply can not be
decreased without shutting down many integral components of the plant. Associated assist
gas was also added to the total flared gas volume for its use in avoiding opacity as per EPA
regulations. The flare event ended when the inter-cooler was thawed and the booster
compressor was re-started.
During the ten hours between 13:10 and 23:10 on January 29, 2,449 mscf of gas was flared.
The flare resulted from the relieving of the low pressure fuel gas system while the booster
compressor was shut-down. This was an unplanned shut-down of the booster compressor.
Without a booster compressor, the low pressure fuel gas system cannot enter the main gas
compression trains and must be relieved via flaring. Because the low pressure fuel gas must
be supplied at steady rates and pressures, a cut in production would decrease neither the
duration of the event or volume flared, Assist gas also constituted a significant part of this
flare volume, as it was added to avoid opacity as defined by EPA regulations. The event
ended when the booster compressor was successfully re-started and the assist gas use could
be decreased.
A flare event occurred for three hours and 20 minutes from 23:50 on January 30 to 03:20 on
January 31, during which time 2,618 mscf of gas was flared, This event was caused by de-
pressurisation of the "A"-Main compression train during an emergency shut-down when power
was lost due to PLC failure. The flaring of the speoified volume of gas was necessary to safely
relieve the system pressure during this unplanned shut-down, All production was shut-in as a
direct result, and remained shut-in for the duration of the event. The faulty PLC has since
been identified and corrected.
During the three hour 20 minute time period from 01:40 to Ofi:00 on January 31, 1999, 902
mscf of gas was flared. This flare event resulted from a booster compressor shut-down and
other plant upsets which had carried over from the day before, January 31, 1999. The flare
ended when the booster compressor was re-started and the plant was returned to stable
operation.
APR 27 '99 05~32PM BPX ENDICOTT DEVP
AOGCC
Endicott Flare Event Supplement
Apri120, 1999
Page 4
P.5i6
F 1 -
On February 1, 1999, 733 mscf of gas was flared during an eight hour and 30 minute period
from 08:00 hours until 16:30 hours. The cause of this flare event was a combination of
relieving pressure from the low pressure fuel gas supply system, and the use of assist gas to
avoid opacity of flare smoke as per EPA regulations. The assist gas was necessary because
both booster compressors shut-down unexpectedly with high temperatur® alarms due to
formation of hydrat® plugs in the inter-cooler system. The booster compressors are necessary
to compressing low pressure fuel gas and enable it to re-enter the first stage gas compressors,
so when the booster compressors are down, the low pressure fuel gas line can only be
relieved to the flare. Because the low pressure fuel gas is supplied independently of produced
gas intake, a cut in production would have no effect in minimizing the flare event. The inter-
coolers were thawed as quickly as possible and returned to service. Soon after, the booster
compressor were re-started and the flare event ended. The total volume of flared gas includes
assist gas used to maintain compliance with EPA opacity regulations.
On February 10, 1999, 303 mscf of gas was flared during an one hour, 30 minute event from
17:50 to 19:20. This event was caused by an unplanned shut down of a booster compressor.
The booster compressor shut-down because the "A"-Main gas compression train was backed
down to minimum throughput for maintenance. When the "A°-Main was backed down the
pressure in the first stage separator increased to a level higher than the allowed discharge
pressure of the boost®r compressor, causing the shut-down. Included in the total volume of
flared gas is the gas relieved from the low pressure fuel gas system and the assist gas
necessary to avoid opacity, as per EPA regulations. Reduction in production accompanied the
backing down of "A"-Main prior to the event. The flare event ended when the booster
compressor was re-started.
On February 17, 1999, 472 mscf of gas was flared from 21;50 to 23:00. This one hour and ten
minute flare event was caused by MI compressor commissioning upsets. Under
commissioning circumstances, flaring is necessary to pressurize the compressor for starting,
and again for the compressor to safely de-pressurize when shutting down. Only high pressure
fuel gas and assist gas was flared in this event, so cutting production rates would have had no
effect on the volume or duration of the flare event. During the flare event, the MI compressor
was running, thereby facilitating troubleshooting and tuning of the logic controls as part of the
commissioning process. Assist gas used to comply with EPA opacity regulations is included in
the total flare volume.
On February 21, 1999, 967 mscf of gas was flared during an 2 hour and 30 minute event from
20;30 hours to 23:00. The root cause of this event was the failure of a temperature control
valve on the MI compressor to close properly. Fuel gas leaked past the valve to result in the
flaring event, Once the failed valve was identified, it was manually re-seated to end the flaring.
A replacement valve has since been ordered and will be installed when received. Because the
flared gas was fuel gas which is supplied at steady rates regardless of production rate, a
production cut would not have minimized the duration of the flare or the volume of gas flared.
Assist gas was also used during this event to comply with EPA opacity regulations and is
included in the total flared gas volume.
On February 23, 1999, we experienced an unplanned flare event beginning at 15:10 hours and
continuing through midnight (duration of 13 hours, 50 minutes) during which time 1403 mscf of
APR 27 '99 05~33PM BPX ENDICOTT DEVP
AOGGC
f=ndicott Flare Event Supplement
Apri120.1999
Page 5
P.6i6
gas was flared. This event resulted when "B"-Main gas compression train went down and de-
pressured to the flare. Assist gas was increased during this time in order to avoid opacity as
per EPA regulations. The assist gas remained on until re-pressurizing the Main Gas
Compression Train "B" during start up at 23;40 hours. The majority of this volume was flared
during the de-pressurizing and re-pressurizing of the compression train, two steps necessary
to safely shut down and start up of the compression train.
On February 24, 1999, 236 mscf of gas was flared over the one hour and ten minutes from
midnight to 01:10 hours due to process upsets caused by start-up of "B"-Main gas compressor.
The total volume of flare gas includes the gas required to pressurize the compressor for start-
up and the accompanying assist gas required to maintain EPA opacity regulations. The start-
up procedures were reviewed in an attempt to identify opportunities to minimize the amount of
flare gas needed to start the compressor in the future. No cut in production was performed as
the necessary cuts were made previously when the compression train was shut down.
Additional assist gas that was needed to maintain compliance with EPA opacity regulations is
included in the total flared gas volume.
On February 24, 1898, 662 mscf of gas was flared during the five hour period from 09:30 to
14:30 hours. This flare event was the result of the main gas compressors de-pressurizing
during an unplanned complete plant shut-down. A slug of liquid formed in the SDI tie-line and
triggered a high level alarm in the first stage separator which caused the shut down. All
production was cut as all wells were automatically shut-in during this shutdown. The flare
event ended when the plant was started-up again. The three phase instability of the tie-line
and standard well procedures were reviewed. Assist gas was applied to the flare to comply
with EPA opacity regulations, and is includ®d in the reported total flare volume.
On February 28, 1999, 254 mscf of gas was flared during the three hour and 20 minute period
from 20:40 to midnight. This event resulted from a commissioning run of the MI compressor
when the machine shut down because of problems with first stage suction pressure. The
controls on first stage suction were subsequently reprogrammed and tun®d to solve the
observed problems. Because the gas flared by MI compressor commissioning is supplied at a
steady rate and pressure that is not affected by produced gas off-take, a production cut would
not have reduced the volume or duration of the flare event and thereby was not enacted. The
total flared volume includes additional assist gas needed to comply with EPA opacity
requirements.
We hope that this information has been helpful to you. Please do not hesitate to contact me if
you have questions or if we can provide additional information.
Sinc efy,
Norman Ingram
Field Manager, ndic and Badami
MAS/mas
ALASKA OIL AND GAS CONSERVATION CONII~lISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Facility
Endicott
Disposition
Operator IField(s) IMOnth/Year of Dispositi
BP Exploration (Alaska) Endicott 10450 May-99
Volume MCF*
1. Sold Fuel
NGL
To Badami 16,323
155,175
45 170
2. Reinjected 8,087,493
3. Flared or vented less than 1 hour 3,519
4. Flared or vented greater than 1 hour
(Supplemental report required--See 20 AAC 25.235) 1,605
5. Pilot and Purge 9,630
6. Used for lease operations Assist
Fuel 22,407
805 945
7. Other
TOTAL items 1-7 9,147,267
8. NGL gas equivalent produced 155,175
9. Purchased gas
10. Transferred from:
11. Transferred to:
I hereby certify that the foregoing is true and correct to the best of
ignature ~. %.
Title f/Yt{D~ ~~ Date
*Indicate contribution of each pool
Pool Name
220100 Code Percent
Official Use Only:-Flaring Authoriza
1. Safety MCF
2. Lease MCF
3. Conserv. Purpos MCF
Commissioner Date
Note: All volumes must be
corrected to pressure of 14.65
Asia and to a temperature of 60
degrees F. Report due by the
20th of the month folowing the
month of disposition.
~--,
LL.
Form 10-422
Rev. 4/95
6/4/99
Page 1
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
May-99
Unplanned Events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
TOTAL 3,726 Not required for unplanned events which Not required for unplanned events which
are less than or equal to 1 hour are less than or equal to 1 hour
Unplanned Events greater than 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
MI compressor tripped to recycle several times Troubleshooting and tuning controls for
before finally shutting down. commissioning. Plant operation was stablized
when MI compressor was depressurized and assist
05/02/99 04:50-06:40 665 gas was turned off.
Plant upset condition caused booster compressor Assist gas was returned to normal levels when
shut-down, which necessitated increased use of plant operation was stabilized and opacity was
assist gas to maintain compliance with opacity acceptable. Booster compressors were
regulations. Note: booster compressors needed overhauled and operations were adjusted to help
overhaul to operate at higher gas throughput (C them keep up with upgraded compressors.
05/15/99 20:00-21:00 93 to D upgrde)
Assist gas was increased a very small ammount to Flare reporting computer was changed to not
mitigate flare opacity, but overall purge, pilot, report assist gas to flare unless the PP&A is above
and assist gas remained below limit of 1161 the 1161 mscf/d limit.
05/19/99 17:30-00:00 2 mscf/d, including this long duration release.
Increased assist gas use was necessary to Assist gas was returned to normal levels when
mitigate opacity of flare exhaust, as per EPA plant operation was stabilized and opacity was
regulation. Opacity condition caused by plant acceptable. Booster compressors were
upset. overhauled and operations were adjusted to help
05/21 /99 1 1:00-13:30 50 them keep up with upgraded compressors.
Increased assist gas use was necessary to Assist gas was returned to normal levels when
mitigate opacity of flare exhaust, as per EPA plant operation was stabilized and opacity was
regulation. Opacity condition caused by plant acceptable. Booster compressors were
upset. overhauled and operations were adjusted to help
05/22/99 14:10-16;40 7 them kee u with u railed com ressors.
~s„~ ~v
6/4/99
Page 2
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
May-99
Increased assist gas use was necessary to Assist gas was returned to normal levels when
mitigate opacity of flare exhaust, as per EPA plant operation was stabilized and opacity was
regulation. Opacity condition caused by plant acceptable, Booster compressors were
upset, overhauled and operations were adjusted to help
05/22/99 17:00-18:30 26 them keep up with upgraded compressors.
Increased assist gas use was necessary to Assist gas was returned to normal levels when
mitigate opacity of flare exhaust, as per EPA plant operation was stabilized and opacity was
regulation. Opacity condition caused by plant acceptable. Booster compressors were
upset. overhauled and operations were adjusted to help
05/22/99 19:20-22:20 14 them keep up with upgraded compressors,
Increased assist gas use was necessary to Assist gas was returned to normal levels when
mitigate opacity of flare exhaust, as per EPA plant operation was stabilized and opacity was
regulation. Opacity condition caused by plant acceptable. Booster compressors were
upset. overhauled and operations were adjusted to help
05/23/99 1 1:20-13:00 28 them keep up with upgraded compressors.
Increased assist gas use was necessary to Assist gas was returned to normal levels when
mitigate opacity of flare exhaust, as per EPA' plant operation was stabilized and opacity was
regulation. Opacity condition caused by plant acceptable. Booster compressors were
upset, overhauled and operations were adjusted to help
05/24/99 13:10-14:10 32 them keep up with upgraded compressors,
Plant upset condition and booster compressor Assist gas was returned to normal levels when
overhaul necessitated increased use of assist gas plant operation was stabilized and opacity was
.05/25/99 18:00-20:30 1 10 to avoid opacity as per EPA regulations. acceptable.
Plant upset condition and booster compressor Assist gas was returned to normal levels when
overhaul necessitated increased use of assist gas plant operation was stabilized and opacity was
to avoid opacity as per EPA regulations. acceptable, Booster compressors were
overhauled and operations were adjusted to help
05/25/99 22:40-00:00 86 them keep up with upgraded compressors,
Increased assist gas use was necessary to Assist gas was returned to normal levels when
mitigate opacity of flare exhaust, as per EPA plant operation was stabilized and opacity was
05/26/99 17:40-20:00 93 re ulation. O aci condition caused b lant acce table.
6/4/99
Page 3
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL N0.202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
May-99
5/29/99
4:40-06:00
94 Production slug to the first stage main production
separator caused the booster compressors work
harder and shut down because of high
temperature. Compressors could not be started
for over 1 hour (lockout), Assist gas was used for
opacity compliance. Booster compressors were re-started when lock-
out period was over. Assist gas was returned to
normal levels.
TOTAL 1,700
Planned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mcf
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
TOTAL 0
Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf
DATE TIME VOLUME DESCR1P710N OF INCIDENT & CAUSE
None ACTION TAKEN TO ELIMINATE CAUSE
TOTAL 0
TOTAL EIDR SDN ENDICOTT
Volume flared less than 1 ho 3,726 204 3 3,519
Volume flared greater than 1,700 93 2 1,605
1 hour
Pilot Purge 10,199 560 9 9,630
Assist Gas 23.731 1.302 22 22,407
TOTAL FLARE D VOLUME 39,356 2,159 36 37,161
{ ~ r..
Kw t ~ $ .~c e
~' ~.
Facility
,_ __~A1COtt
ALASKA OIL AND GAS CONSERVATION CONII~lISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Operator Field(s) Month/Year of Disposition
BP Exploration (Alaska) Endicott 10450 Jun-99
Disposition Volume MCF*
1. Sold Fuel
NGL
To Badami 16,067
168,799
15 723
2. Reinjected 10,063,340
3. Flared or vented less than 1 hour 1,457
4. Flared or vented greater than 1 hour
(Supplemental report required--See 20 AAC 25.235) 2,295
5. Pilot and Purge 9,461
6. Used for lease operations Assist
Fuel 22,569
939 108
7. Other
TOTAL items 1-7 11,238,819
8. NGL gas equivalent produced 168,799
9. Purchased gas
10. Transferred from:
11. Transferred to:
I hereby ce ify tha the fore oing is true and correct to the best of
Signature Title /~/~,~~(~, TJ4~ Date ~7I(~IQC
*Indicate contribution of each pool
Pool Name Code Percent
220100
Official Use Only-Flaring Authoriza
1. Safety MCF
2. Lease MCF
3. Conserv. Purpos MCF
Commissioner Date
Note: All volumes must be
corrected to pressure of 14.65
psia and to a temperature of 60
degrees F. Report due by the
20th of the month folowing the
month of disposition.
Form 10-422
Rev. 4/95
7/6/99
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
June-99
Page 1
Unplanned Events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
TOTAL 1,520 Not required for unplanned events which Not required for unplanned events which
are less than or equal to 1 hour are less than or equal to 1 hour
Unplanned Events greater than 1 hour
TIME
06/10/99 111:30-12:50 88
DESCRIPTION OF INCIDENT & CAUSE
Adjusting export rate for TAPS proration initiated
slugging and plant instability which caused a booster
compressor to trip off-line, thereby increasing need for
opacity mitigation with additional assist gas.
Plant upsets due to slugging production from SDI
resulted in a booster compressor shut down, thereby
increasing need for opacity mitigation with additional
ACTION TAKEN TO ELIMINATE CAUSE
The booster compressor was re-started as soon as
possible to eliminate the need for and use of
addtional assist gas.
The booster compressor was re-started as soon as
possible to eliminate the need for and use of
addtional assist gas.
06/17/99 07:10-08:10 38
06/18/99 17:00-18:00 45
06/20/99 10:20-12:30 121
06/20/99 12:50-16:30 481
06/20/99 18:40-19:50 98
06/21/99 07:50-08:50 10
09:10-19:10 315
The MI compressor shut down on a recycle trip and
safely depressurized to flare. This temporarily
increased the need for assist gas to avoid opacity.
Once the compressor and turbine was safely
depressured, the assist gas was turned off. This event
occurred during the commissioning phase of the MI
Pressurization of M! compressor for start-up and tuning MI compressor was started up and tuned. The
to set surge curves resulted in a significant need for booster compressor was then also re-started. Once
additional assist gas to avoid flare smoke opacity (EPA operational stability returned, additional assist gas
regulation). Simultaneous plant upset caused booster was no longer needed. Production cut during this
compressor to go down also. event was not pertinent to minimizing flared volume.
Pressurization of MI compressor for start-up and tuning MI compressor was started up and tuned. The
to set surge curves resulted in a significant need for booster compressor was then also re-started. Once
additional assist gas to avoid flare smoke opacity (EPA operational stability returned, additional assist gas
regulation). Simultaneous plant upset caused booster was no longer needed. Production cut during this
compressor to go down also. event was not pertinent to minimizing flared volume.
Plant upsets due to slugging production from SDI The booster compressor was re-started as soon as
resulted in a booster compressor shut down, thereby possible to eliminate the need for and use of
increasing need for opacity miti ation with additional addtional assist as.
Pressurization of MI compressor for start-up resulted in a Once the MI compressor was started, the additional
significant need for additional assist gas to avoid flare assist gas was no longer needed and was eliminated.
emission opacity (EPA regulation .
The volume flared during this event was almost Once the knock out vessel was blown down, the
completely addtional assist gas that was necessary for additional assist gas was not necessary and turned
opacity mitigation while blowing liquids down from 1st off. The MI compressor operation was adjusted to
sta a knock out vessel for MI com ressor. minimize li uid formation in this vessel.
7/6/99
Page 2
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
June-99
06/22/99 111:00-13:50
I 06/25/99 104:10-05:40
109
1,058
Performance testing of MI compressor increased the
need for additional assist gas to mitigate flare emission
opacity.
MI compressor shut down and depressurized due to
"O"-ring failure in tree cap of MI injection well 2-22.
Additional assist gas was necessary to avoid flare
smoke opacity as per EPA regulation.
MI compressor shut down and depressurized due to
"O"-ring failure in tree cap of MI injection well 2-22.
Additional assist gas was necessary to avoid flare
smoke opacity as per EPA regulation.
06/25/99 06:10-07:20 31
TOTAL 2,394
Planned Events Less Than or Equal 1 Hour AN D Not E
DATE TIME VOLUME DESCRI
TOTAL 0
Planned Events Exceeding 1 Hour OR Exceeding 5000
DATE TIME VOLUME DESCRI
None ~ ~
TOTAL 0
Volume flared less than 1 he
.Volume flared greater than
I1 hour
st Gas
AL FLARED VOLUME
TOTAL EIDR
1,520 ~ 62
2,394 97
9,870 401
23.543 955
37,327 1,515
ling 5000 Mcf
OF INCIDENT & CAUS
OF INCIDENT & CAU
When the performance testing was complete, the
additional assist gas was no longer needed and was
returned to normal levels.
The "O"-ring on well 2-22 was replaced with a new
"O"-ring made of a material better suited to MI
injection service. This change was applied to each
well scheduled for MI injection service. Production
cut not necessary due to proration.
The "O"-ring in well 2-22 was replaced with a new "O"-
ring made of a material better suited to MI injection
service. This change was applied to each well
scheduled for MI injection service. Production cut
not necessary due to proration.
ACTION TAKEN TO ELIMINATE CAUSE
ACTION TAKEN TO ELIMINATE CAUSE
SDN ENDICOTT
1 1,457
2 2,295
8
30
9,461
22,569
35,782
ALASKA OIL AND GAS CONSERVATION CONII~lISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Facility Operator Field(s) Month/Year of Disposition
Endicott BP Exploration (Alaska) Endicott 10450 Jul-99
Disposition
Volume MCF*
1. Sold Fuel
NGL
To Badami 16,126
153,701
69 341
2. Reinjected 10,260,833
3. Flared or vented less than 1 hour 5,730
4. Flared or vented greater than 1 hour
(Supplemental report required--See 20 AAC 25.235) 4,852
5. Pilot and Purge 9,748
6. Used for lease operations Assist
Fuel 23,349
996 921
7. Other
TOTAL items 1-7 11,540,601
8. NGL gas equivalent produced 153,701
9. Purchased gas
10. Transferred from:
11. Transferred to:
I hereby c i t t the fo egoing is true annnd correct to the best of
Signature ~ Title (M,(~/~,`r]~~ Date ~Q
*Indicate contribution of each pool
Pool Name Code Percent
220100
Official Use Only-Flaring Au~horiza
1. Safety MCF
2. Lease MCF
3. Conserv. Purpos MCF
Commissioner Date
Note: All volumes must be
corrected to pressure of 14.65
psia and to a temperature of 60
degrees F. Report due by the
20th of the month folowing the
month of disposition.
psi
Cdt
~'
f~=
~~
~' ~i ?
? ~
a~
rly
CJ ~
~3
::3
..
tv~
~.~ ~.
~"°j ~
... ~
~•~~.
_ .~,
C:.Ca ~*m.
p`-~"
1~~~~
..,~r?
Form 10-422
Rev. 4/95
8/6/1999
Page 1
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICC
Unplanned Events less than ore ual to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
TOTAL 5,996 Not required for unplanned events which Not required for unplanned events which
are less than or equal to 1 hour are less than or equal to 1 hour
Inplanned Events gr
DATE TIME
07/05/99 20:20-23:20
07/10/99 05:20-07:10
07/13/99 100:00-01:20
07/14/99 05:10-06:10
07/14/99 22:40-00:00
07/15/99 02:40-04:20
07/15/99 08:40-09:40
07/15/99 10:30-12:10
07/ 15/99 114:00-15:10
than 1 hour
VOLUME
524
715
193
199
133
39
140
122
36
DESCRIPTION'OF INCIDENT"& CAUSE
Combination of high ambient temperatures and new
operating conditions with MI compressor were resulting in
severe booster compressor problems. Assist gas was
a Ifed as necessary to avoid o aci of flare emissions.
Simultaneous shut down of the MI compressor and
booster compressor necessitated safe depressurization vic
florin and use of assist as to avoid o achy.
The MI compressor tripped to recycle, initiating plant
instability which caused the booster compressor to shut-
down. Assist as was re uired to avoid opac'
The MI compressor shut-down and depresurrized via the
flare, Assist gas was used to avoid opacity as per EPA
re ulation. Cause was an hydraulic leak in the ro one
During start-up of MI compressor and NGL system, the
booster compressor shut-down. Assist gas use was
necessary to avoid opacit .
The booster compressor shut-down during plant instability
resulting from shutting-down the propane compressor to
fix a leak. Assist gas was necessary to maintain
compliance with EPA o acit re ulation.
Due to the control system, the MI compressor was shut-
down and depressurized via flaring. Assist gas was used
to burn the rich MI gas without causing flare opacity, as
per EPA re ulation.
MI compressor was re-started after shutting down while
commissioning new MI injection header to SDI. Assist gas
was used to maintain compliance with opacity regulation
during re-pressurization and start of the compressor.
Plant instability from propane compressor repairs and MI
compressor start-ups caused booster compressor to shut-
down. Assist as was used as needed to avoid opacity.
ACTIONTAKEN TO ELIMINATE CAUSE
The operating conditions were adjusted to mitigate the high
temperature problems with the booster compressor until the
ambient temperature cooled. Assist gas use was eliminated
as soon as ossible.
The MI compressor was safely depressured via flaring, the
booster compressor was re-started and assist gas use was
terminated when o achy cleared.
The MI compressor and injection wellset were adjusted until
the recycle valve and controls could be tuned.
leak was repaired and the MI compressor was returned
service. Assist gas use was terminated as soon as
Booster compressor was re-started when plant operations
were stabiliized. Assist gas was used only as long as
necessary to avoid opacity.
The booster compressor was restarted as soon as possible
while plant operation was stabilizing, Assist gas use was
eliminated as soon as the flare emissions satisfied the
Upon safely depressurizing the MI compressor, the control
system was reset and the compressor was restarted. Assist
gas was used no longer than necessary to maintain with
several attempts the new inter-island MI injection
'er was purged and warmed up. The MI compressor
aced more smoothly once the line was in service.
The plant was stabilized and the booster compressor was re-
started. Assist gas was only used as long as necessary to
avoid mystery.
8/5/i999
Page 2
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
July-99
When MI gas was circulated through the tie line to the The MI compressor was slowly taken out of recycle as the MI
SDI during comission(ng of the line, the MI compressor tie-line to SDI was warmed up and commissioned. Assist gas
tripped to recycle and thereby necessitated flaring of rich use was terminated as soon as allowed by EPA opacity
07/15/99 16:00-17:10 45 MI as. Assist as was necessary for opacity compliance. re ulations.
Assist gas was added to avoid opacity as per EPA Opacity was remedied in the first 50 minutes in which time
regulations for 50 minutes, and then Jeff on inadvertantly the process was adjusted to eliminate cause of opacity.
for the rest of the day. Operations staff were trained to turn set reminder alarm to
07/16/99 12:00-00:00 570 . turn assist as off after 50 minutes.
The MI compressor shut-down and depresurrized via the The MI compressor was safely depressurized before trouble-
flare. Assist gas was used to avoid opacity as per EPA shooting to find and remedy control system that caused the
07/17/99 19:20-21:00 370 re ulation. shut-down
Assist gas was needed to manage opacity when booster Mi compressor operation was adjusted to increase booster
compressor was frequently shutting down due to new compressor stability. Assist gas was used only when needed
07/19/99 17;50-18;50 54 operatin conditions imposed by MI compressor. to miti ate opaci , as per EPA re ulation.
Assist gas was needed to manage opacity when booster MI compressor operation was adjusted to increase booster
compressor was frequently shutting down due to new compressor stability. Assist gas was used only when needed
07/19/99 21:50-00:00 70 operating conditions imposed b MI compressor. to miti ate o aci , as er EPA re ulation.
Booster compressor shut down when starved of gas MI compressor injection rate was lessened to reduce the
during MI compressor performance testing. Assist gas was starvation of booster compressor, to facilitate it's restart.
needed to avoid opacity. Assist gas was used as necessary to avoid opacity, but was
07/20/99 09:00-11:30 111 terminated as soon as ermissible.
Well work on SDI initiated instability in the plant which Booster compressor was re-started when possible until well
caused booster compressor to shut down and assist gas work, and associated instability, was past. Assist gas was
07/30/99 11:20-12:30 94 use to be required for opacity re ulation compliance. used onl when needed to avoid opacity.
Unexpected shut-down of water injection pump required As soon as plant stability was restored, the booster
rapid shut-in of wells, which initiated temporary plant compressor was restarted and the assist gas use was
instability and caused the booster compressor to shut- terminated.
07/31/99 11:50-13:20 391 down. Assist as was used as necessary to avoid opaci
Unexpected shut-down of water injection pump required As soon as plant stability was restored, the booster
rapid shut-in of wells, which initiated temporary plant compressor was restarted and the assist gas use was
instability and caused the booster compressor to shut- terminated.
07/31 /99 13:40-15:00 386 down, Assist gas was used as nedesaar to avoid o acit .
TOTAL 4,192
Planned Events Less Than or Equal 1 Hour AN D Not Exceeding 5000 Mcf
DATE, TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
TOTAL 0
8/5/1999
Page 3
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
July-99
Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
The booster compressors were shut-down for cleaning in The boosters were returned to service as soon as possible
an effort to make them more reliable at high ambient after washing and the assist gas use was discontinued when
temperatures and operating condition with MI no longer needed.
07/10/99 13:00-15:10 885 compressor. Assist as use was the dominant source and
TOTAL 885
TOTAL EIDR SDN ENDICOTT
Volume flared less than 1 h 5,996 259 7 5,730
Volume flared greater than 5,077 219 6 4,852
1 hour
Pilot Purge 10,199 440 11 9,748
Assist Gas 24.430 1.054 27 23,349
TOTAL FLARED VOLUME 45,702 1,972 51 43,679
ALASKA OIL AND GAS CONSERVATION CONII~lISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Facility Operator Field(s) Month/Year of Disposition
Endicott BP Exploration (Alaska) Endicott 10450 Aug-99
Disposition ~ Volume MCF*
1. Sold Fuel
NGL
To Badami 14,437
146,343
125 765
2. Reinjected 9,798,859
3. Flared or vented less than 1 hour 3,231
4. Flared or vented greater than 1 hour
(Supplemental report required--See 20 AAC 25.235) 6,407
5. Pilot and Purge 9,870
6. Used for lease operations Assist
Fuel 23,637
994 246
7. Other
TOTAL items 1-7 11,122,795
8. NGL gas equivalent produced 146,343
9. Purchased gas
10. Transferred from:
11. Transferred to:
I hereby c ify t the for oing is true and correct to the best of
Signature c Title +rVV~ 1~ Date 9 ~~
*Indicate contribution of each pool
Pool Name Code percent
220100
Official Use Only-Flaring Authoriza
1. Safety MCF
2. Lease MCF
3. Conserv. Purpos MCF
Commissioner Date
Note: All volumes must be
corrected to pressure of 14.65
psia and to a temperature of 60
degrees F. Report due by the
20th of the month folowing the
month of disposition.
Form 10-422
Rev. 4/95
9/3/1999
Page 1
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
Unplanned Events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION-0F INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
TOTAL 3,159 Not required for unplanned events which Not required for unplanned events which
are less than or equal to 1 hour are less than or equal to 1 hour
Unplanned Events Greater than 1 hour
DATE
08/01 /S
08/01 /S
ME
DESCRIPTION OF INCIDENT-& CAUSE
The booster compressor shut down due to high ambient
temperatures and required several attempts to restart. Assist gas
was used to maintain opacity compliance.
High ambient temperatures caused the booster compressor to
shut down. Assist gas use was required to maintain opacity
A small amount of assist gas was required to mitigate a small
amount of black flare emissions, to maintain compliance with
opacity regulation. The assist gas valve failed to completely seat
when commanded to close.
MI compressor recycle trips, shut downs, and re-starts caused
some flaring for safe depressurization of the compressor, which
necessitated use of assist caps to avoid flare emission opacity, as
ACTION TAKEN TO ELIMINATE CAUSE
The booster compressor was restarted and assist gas use was
eliminated as soon as possible. Approximately 40% of the
flared volume was assist gas required for opacity compliance.
The booster compressor was restarted and assist gas use was
eliminated as soon as possible.
The majority of the assist gas usage was for the cause of
avoiding flare emission opacity. When the small flow of gas
was discovered, the valve was researted to eliminate
undesired use of assist gas.
The MI compressor control logic was diagnosed and tuned to
promote more stable performance. Assist gas usage was
eliminated as soon as opacity compliance was attained.
The MI compressor was restarted and assist gas use was
eliminated as soon as permitted by opacity regulation.
Cutting gas production does not effect the amount of gas
flared during MI compressor startup.
The assist gas use was eliminated when it was discovered that
it had been flaring unintentionally. It was immediately shut-in.
MI compressor control logic was diagnosed to facilitate more
stable performance. Assist gas usage was eliminated as soon
as opacity compliance was restored.
573
16:00-18:20 I 233
08/03/99 101:50-03:00
08/04/99 119:00-21:40 I 31
08/04/99 22:00-00:00 226
08/04/99 05:50-12:00 21
08/05/99 00:00-01:20 68
08/05/99 10:30-14:20 485
08/07/99 08:30-20:40 2,49
The Mi compressor tripped to recycle, shut down, and was re-
started. Flaring was necessary to safely depressurize the
compressor during the shutdown. Assist gas use was required for
A small plant upset created black flare smoke which
necessitated use of assist gas to maintain compliance with
opacity regulation. Upon eliminating assist gas use, the valve did
not fully seal and a very small amount of assist gas continued to
The MI compressor shut down and depressured safely via flaring.
Assist gas use was necessary to maintain compliance with
A booster compressor shut down due to ambient temperature
swing and plant instability. Assist gas was used to mitigate flare
opacity as per regulation,
Both booster compressors shut down and required major repairs
before they could be restarted. Flared gas included what is
usually handled by the booster compressor and the associated
assist gas as necessary to maintain opacity compliance.
Production was cut to attain plant stability and the assist gas
use was eliminated as soon as permitted by the opacity
The booster compressor that was repaired first was re-started
and the assist gas use was eliminated as soon as opacity was
in compliance. Cutting back on production does not
decrease the volume of gas flared when the booster
9/3/1999
Page 2
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
August-99
The booster compressor shut down due to high ambient The booster compressor was re-started and the assist gas use
temperatures and required several attempts to restart. Assist gas was eliminated as soon as permissible by the opacity
was used to maintain opacity compliance. regulation. Production cuts are not useful in minimizing flaring
08/09/99 08:30-09:40 171 from booster compressor downtime.
MI compressor tripped to recycle, causing partial depressurization The MI compressor operation was stabilized, the cause of
and necessitating usage of assist gas to maintain opacity black flare emissions was eliminated, and assist gas usage
08/11/99 14:40-16:20 92 compliance. was eliminated as soon as permitted by opacity regulation.
A load shed on the main power generators caused the When electircal power was restored, the booster compressor
electrically driven booster compressors to shut down. Assist gas was restarted and assist gas use was eliminated soon after.
was necessary to achieve clean combustion and maintain Approximately 40% of the flared volume was assist gas
08/11/99 08:50-10:30 251 compliance with opacity regulation, required for opacity compliance.
A plant upset required assist gas to be applied to the flare in The assist gas use was eliminated when it was discovered that
order to maintain compliance with opacity regulation. When it had been left on longer than needed to maintain opacity
the root cause of the black smoke was eliminated, the assist gas compliance,
08/12/99 05:20-12:00 540 was not turned off for the duration of the flare event.
The MI compressor tripped to recycle several times and The MI compressor was safely shut-down and depressurized,
eventually shut down, depressurizing safely via flaring. Each plant stability was restored, and assist gas usage was
recycle trip caused instability that necessitated assist gas use to eliminated as soon as permitted by opacity regulation.
08/15/99 13:40-17:10 170 maintain o acity compliance.
The MI compressor was purged, repressurized, and re-started as The MI compressor was restarted and assist gas use was
per normal cold start up procedure. The purge and eliminated as soon as permitted by opacity regulation.
repressurization stages created black smoke necessitated use of
08/16/99 09:00-10;10 214 assist as to maintain compliance with o acity re ulation.
During a day of plant instability, a small amount of assist gas was When plant operation was stabilized, the assist gas use was
used to mitigate small instances of flare emission opacity that eliminated.
08/16/99 14:20-16:30 6 would occur at erratic, intermittant times.
Instability in the MI/NGL systems caused opacity of flare emissions Assist gas use was eliminated immediately following
and necessitated use of assist gas to restore and maintain permission by opacity regulation.
08/16/99 21:00-22:10 33 compliance with the opacity re ulation.
A plant upset required assist gas to be applied to the flare in As soon as opacity compliance permitted, the assist gas
08/17/99 11:10-12:10 38 order to maintain compliance with opacity re ulation. usage was eliminated.
Assist gas use was required to maintain compliance with opacity When the control system accepted the command to
regulation during a very short booster compressor shut down, but decrease use of assist gas, it was eliminated. The fault in the
could not be turned off immediately when permitted; the control control system has since been identified and remedied.
08/20/99 06:50-10:40 358 system rejected the command to eliminate use of assist gas.
The MI compressor tripped to recycle, initiating NGL system The MI compressor was safely and partially depressured.
instability that necessitated assist gas usage to keep flare Once the need ceased to use assist gas to maintain opacity
emissions in compliance with opacity regulation. compliance, however, human error led to a 1.5 hours delay
08/24/99 13:00-16:00 113 in the elimination of assist as usa e.
9/3/1999
Page 3
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
August-99
8/27/99
7:00-13:10
13 The MI compressor tripped to recycle and eventually shut down,
safely depressuring to flare and causing plant instability which
resulted in black smoke emission from the flare. Assist gas was
required to maintain compliance with opacity regulation. The MI comprssor was re-started and the NGL system was
stabilized. Assist gas use was eliminated as soon as permitted
via opacity regulation.
TOTAL 6,533
Planned Events Less Than or Equal 1 Hour A ND Not Exceeding 5000 Mcf
DATE TIME VOLUME.. DESCRIPTION OF INCIDENT & CAUSE
Flaring resultant from required emissions testing on MI compressor
08/29/99 17:00-17:30 180 turbine; Assist as use was not necessary. ACTION TAKEN TO ELIMINATE CAUSE
Emissions testing was completed and stable operation
resumed for the MI compressor.
TOTAL 180
Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE
Deaerator (DA) gas was diverted from booster compressor to
flare instead to experiment with operating conditions to minimize
08/10/99 08:00-10:00 87 overall flaring associated with booster compressor downtime. ACTION TAKEN TO ELIMINATE CAUSE
When sufficient data was collected, the DA gas was re-
routed back to the booster compressor.
TOTAL 87
TOTAL. EIDR SDN ENDICOTT
Volume flared less than 1 3,339 105 3 3,231
Volume flared greater tha 6,620 207 6 6,407
1 hour
Pilot Purge 10,199 319 10 9,870
Assist Gas 24.423 763 23 23,637
TOTAL FLARED VOLUME 44,581 1,394 42 43,145
ALASKA OIL AND GAS CONSERVATION CONII~lISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Facility Operator Field(s) Month/Year of Disposition
Endicott BP Exploration (Alaska) Endicott 10450 Sep-99
Disposition ~ Volume MCF*
1. Sold Fuel
NGL
To Badami 13,537
137,233
98 161
2. Reinjected 9,739,215
3. Flared or vented less than 1 hour 4,400
4. Flared or vented greater than 1 hour
(Supplemental report required--See 20 AAC 25.235) 629
5. Pilot and Purge 9,430
6. Used for lease operations Assist
Fuel 22,507
933 942
7. Other
TOTAL items 1-7 10,959,054
8. NGL gas equivalent produced 137,233
9. Purchased gas
10. Transferred from:
11. Transferred to:
I hereby c ify at the f regoing is true and correct to the best of
Signature Title I,~/~IL~~(~X Date ~0
*Indicate contribution of each pool
Pool Name
220100 Code Percent
Official Use Only-Flaring Authoriza
1. Safety MCF
2. Lease MCF
3. Conserv. Purpos MCF
Commissioner Date
Note: All volumes must be
corrected to pressure of 14.65
psia and to a temperature of 60
degrees F. Report due by the
20th of the month folowing the
month of disposition.
Form 10-422
Rev. 4/95
10/6/1999
Page 1
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
September-99
Unplanned Events less than or equal to 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
TOTAL 4,380 Not required for unplanned events which Not required for unplanned events which
are less than or equal to 1 hour are less than or equal to 1 hour
Unplanned Events greater than 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
A sharp ambient temperature swing resulted in decreased gas Production was cut to match decreased gas handling
handling capacity which necessitated flaring of process gas and capacity. The booster compressor was restarted and assist
assist gas to keep visible emissions within EPA regulation. gas use was eliminated as soon as possible.
09/05/99 16:20-17:20 198 Additional as flared when the booster compressor S/D.
09/11 /99
03:10-07:00
73 Severe plant upset while ramping down production for TAPS
slowdown required use of assist gas to maintain compliance with
EPA opacity regulation. Once prorated production levels were achieved, plant
operation smoothed out and assist gas use was eliminated as
soon as it was no longer needed for opacity compliance
9/20/99
5:20-16:40
9 Severe slugging through SDI inter island tie-line caused booster
compressors to bump flare; assist gas was needed to ensure the
richer gas from the boosters was combusted in compliance with
EPA Opacity regulation, Production was cut to mitigate slugging and eliminate flaring
from the booster compressors. The assist gas use was
eliminated as soon as possible, given compliance with
Opactiy re ulation.
09/21 /99
06:30-07:40
45 B booster compressor shut down when slugging from SDI initiated
instability in the plant. Assist gas was needed to mitigate flare
opacity as per EPA regulation. A booster compressor was restarted and assist gas use was
eliminated as soon as possible.
09/21 /99
20:30-21:30
210 The MI compressor was started up, requiring purge and
pressurization which ncessitated flaring. Assist gas was used as
necessary to maintain compliance with EPA opacity regulations. The MI compressor was started once it was purged and
pressurized. Assist gas was turned off as soon as possible.
09/29/99
16:50-18:00
63 Start-up of propane compressor caused instability and the
boostercompressor shut down; both operations required used of
assist gas to mainain opacity compliance. Troubleshooting of the Propane compressor once it was re-
started facilitated smooth operation. Booster was re-started
and assist gas use was eliminated as soon as possible.
TOTAL 658
Planned Events Less Than or Equal 1 Hour A ND Not Exceeding 5000 Mcf
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
Planned "A"-Main shut down for TAPS slowdown. Compressed Production was cut for slowdown. "A"-Main was re-started
09/11 /99 01:40-01:40 104 gas safely depressured via flaring. following completion of maintence work.
09/28/99
09:50-09:50
121 "Planned" shutdown MI compressor for calibration of
instrumentation for performance diagnoses. Some assist gas use
was necessary to maintain opacity compliance. Flared volume minimized, data gathered from the calibrated
instruments to be used to improve performance of MI
compressor and thereby decrease future flaring.
TOTAL 225
10/6/1999
Page 2
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
September-99
Planned Events Exceeding 1 Hour OR Exceed ing 5000 Mcf
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
TOTAL 0
TOTAL EIDR SDN ENDICOTT
Volume flared less than 1 4,605 202 3 4,400
Volume flared greater tha 658 29 0 629
1 hour
Pilot Purge 9,870 434 6 9,430
Assist Gas 23.556 1.035 14 22,507
TOTAL FLARED VOLUME 38,689 1,700 23 36,966
~~~~
ALASKA OIL AND GAS CONSERVATION CONIl~lISSION
1~OV 1~~~~~ FACILITY REPORT OF PRODUCED GAS DISPOSITION
Facili ~"~`"~~' Field(s) Month/Year of Disposition
~!~at;~(~ Qt~ gt ~~r C~n~. (`0~' I - Aerator
Endicott ~' BP Exploration (Alaska) Endicott 10450 Oct-99
Disposition ~ Volume MCF*
1. Sold Fuel
NGL
To Badami 14,263
164,267
84 078
2. Reinjected 11,702,445
3. Flared or vented less than 1 hour 3,024
4. Flared or vented greater than 1 hour
(Supplemental report required--See 20 AAC 25.235) 2,561
5. Pilot and Purge 10,193
6. Used for lease operations Assist
Fuel 24,138
1 092 144
7. Other
TOTAL items 1-7 13,097,113
8. NGL gas equivalent produced 164,267
9. Purchased gas
10. Transferred from:
11. Transferred to:
I hereby ce >f t t the foregoing is true ands-,ec~otrrect to the best of
Signature Titleiit.~i~ tri!S Date ~(
*Indicate contribution of each pool
Pool Name
220100 Code percent
Official Use Only-Flaring Authoriza
1. Safety MCF
2. Lease MCF
3. Conserv. Purpos MCF
Commissioner Date
Note: All volumes must be
corrected to pressure of 14.65
Asia and to a temperature of 60
degrees F. Report due by the
20th of the month folowing the
month of disposition.
Form 10-422
Rev. 4/95
11/3/1999
Page 1
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
October-99
Unplanned Events less than or equal to 1 hour
DATE '71ME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTIOIJ TAKEN TO ELIMINATE CAUSE
TOTAL 2,252 Not required for unplanned events which Not required for unplanned events which
are less than or equal to 1 hour are less than or equal to 1 hour
Unplanned Events greater than 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO`ELIMINATE CAUSE
The booster compressor shut-down. Use of assist gas was The booster compressor was restarted. Use of assist gas was
10/03/99 12:00-15:00 258 minimized. minimized.
The booster compressor shut-down and assist gas was used to The error was identified and the assist gas use was eliminated.
maintain opacity compliance. Assist gas was inadvertantly leff on
10/06/99 11:00-18:30 65 for ap roximately 6 hours.
Upsets in the NGL system resulted in the MI compressor shutting The MI compressor was re-started once the NGL system was
down and needing to be restarted. Assist gas use was necessary lined out. Assist gas use was eliminated as soon as opacity
10/09/99 16:50-19:10 150 for o achy compliance. compliance would allow.
Logging MI injection well 2-22 caused MI compressor upsets which The logging operation was completed and MGC-"B" was re-
led to assist gas flaring for opacity compliance. Logging also started. Assist gas use was eliminated as soon as opacity was
10/11/99 10:30-14:30 1,029 caused MGC"B" to shut down at 14:00 and depressure via flaring. clear.
The MI compressor shut down while commissioning the MI injection The MI compressor safely depressured via flaring until the next
header to SDI. Assist gas was used as needed to mitigate opacity attempt to re-comission the SDI MI header. Assist gas use
10/26/99 11:00-12:30 189 re ulation. was eliminated as soon as possible.
The MI compressor shut down while commissioning the MI injection The MI compressor safely depressured via flaring until the next
header to SDI. Assist gas was used as needed to mitigate opacity attempt to re-comission the SDI MI header. Assist gas use
10/26/99 13:00-14:00 67 re ulation. was eliminated as soon as possible.
The MI compressor shut down while commissioning the MI injection The MI compressor safely depressured via flaring until the next
header to SDI. Assist gas was used as needed to mitigate opacity attempt to re-comission the SDI MI header. Assist gas use
10/27/99 20:50-21:50 98 re ulation. was eliminated as soon as ossible.
The MI compressor shut down while commissioning the MI Injection The MI compressor safely depressured via flaring until the next
header to SDI. Assist gas was used as needed to mitigate opacity attempt to re-comission the SDI MI header. Assist gas use
10/28/99 12;40-13:40 148 re ulation. was eliminated as soon as possible.
"A" Booster S/D because hydrates formed in the intercooler. Assist Thelouvre control that affects booster compressor intercooler
gas was used as necessary to maintain compliance with opacity temperature was identified to be broken and was fixed. The
regulations. booster compressor was returned to service and assist gas use
10/31 /99 15:00-19:00 558 was eliminated.
. TOTAL 2,562
11/3/1999
Page 2
BP EXPLORATION (ALASIC~,) INC.
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
October-99
Planned Events Less Than or Equal 1 Hour A ND Not Exceeding 5000 Mcf
DATE TIME VOLUME bESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
MI compressor shut-down during performance testing. Assist gas Performance test data was collected and MI compressor was
was used as necessary to maintain compliance with opacity re-started. Assist gas use was eliminated as soon as opacity
10/01/99 14:30-15:00 129 re ulations. re ulation was satisified.
10/02/99
08:20-08:40
209 MI compressor shut-down during performance testing. Assist gas
was used as necessary to maintain compliance with opacity
regulations. Performance test data was collected and MI compressor was
re-started. Assist gas use was eliminated as soon as opacity
re ulation was satisified.
10/02/99
21:10-21:50
160 MI compressor shut-down during performance testing. Assist gas
was used as necessary to maintain compliance with opacity
re ulations. Performance test data was collected and MI compressor was
re-started. Assist gas use was eliminated as soon as opacity
re ulation was satisified.
10/05/99
17:10-17:20
160 MI Compressor was shut-down intentionally for operator training. MI compressor was started up again. Assist gas use was
eliminated when opacity compliance was re-established.
10/05/99
19:40-20:00
115 MI compressor was re-started for operator training, Operators were trained in start-up procedure of MI
compressor in ho es that future flaring would be reduced.
TOTAL 773
Planned Events Exceeding 1 Hour OR Exceed ing 5000 Mcf
DATE.. _ _ TIME VOLUME DESCRIPTION OF INCIDENT.& CAUSE ACTION TAKEN TO ELIMINATE CAUSE
TOTAL 0
TOTAL'
. EIDR SDN ENDICOTT
Volume flared less than 1 3,025 0 _ 1 , 3,024
Volume flared greater tha 2,562 0 1 2,561
1 hr
Pilot Purge 10,199 0 6 10,193
Assist Gas 24,151 0 13 24,138
TOTAL FLARED VOLUME 39,937 0 21 39,916
ALASKA OIL AND GAS CONSERVATION CONIl~IISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Facility Operator Field(s) Month/Year of Disposition
Endicott BP Exploration (Alaska) Endicott 10450 Nov-99
Disposition ~ Volume MCF*
1. Sold
To Fuel
NGL
Badami 14,295
149,889
103 165
2. Reinjected 11,090,740
3. Flared or vented less than 1 hour 6,228
4. Flared or vented greater than 1 hour
(Supplemental report required--See 20 AAC 25.23.5) 3,347
5. Pilot and Purge 9,862
6. Used for lease operations Assist
Fuel 23,200
1 040 684
7. Other
TOTAL items 1-7 12,441,410
8. NGL gas equivalent produced 149,889
9. Purchased gas
10. Transferred from:
11. Transferred to:
I hereby cer ify th t the foregoing is true and correct to
Signature Title i•vVu,`~'~~( Date the best of
LZ
*Indicate contribution of each pool
Pool Name
220100 Code Percent
Official Use Only- Flaring Autnoriza
1. Safety MCF
2. Lease MCF
3. Conserv. Purpos MCF
Commissioner Date
Note: All volumes must be
corrected to pressure of 14.65
psia and to a temperature of 60
degrees F. Report due by the
20th of the month folowing the
month of disposition.
5.:,.
r.':
=:-
Form 10-422
Rev. 4/95
12/6/1999
Page 1
BP EXPLORATION (ALASKA) INC,
ADMINISTRATIVE APPROVAL NO. 202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
November-99
Unplanned Events less than or equal to 1 hour
DATE TIME VOLUME DESCRfPT10N OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE.
TOTAL 6,233 Not required for unplanned events which ~ Not required for unplanned events which
are less than or equal to 1 hour are less than or equal to 1 hour
Un tanned Events reater than 1 hour
'..DATE TIME VOLUME DESCRIPTION OFJNCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
The booster compressor shut down and could not be restarted, Assist gas The booster compressor was restarted. Assist gas use was
11 /Ol /99 13:50-15:50 226 was necessary to ensure compliance with flare emissions opacity eliminated as soon as permitted by opacity re ulation.
The booster compressor shut down because hydrates had formed in the Once the intercooler was thawed out, the booster compressor
intercooler, thereby inhibiting the cooling of the compressors. Assist gas was restarted, Assist gas was eliminated as imediately upon
11 /02/99 19:10-21:20 291 necessary for opacity compliance. meetin opaci compliance,
An attempt to restart the MI compressor was unsuccessful. Flare volume The MI compressor operating parameters were adjusted
due to purging, pressurization, depressurization, of MI compressor. Assist slightly for a greater chance of success on the next re-start
gas was used for the duration of this event to mitigate flare emission attempt. Assist gas use was eliminated as soon as permitted
11 /03/99 13:50-15:10 369 opacity. by flare emission opacity.
A successful attempt at re-starting the MI compressor. Flare gas necessary As soon as the MI compressor was successfully started, the
to purge and pressurize compressor during start-up sequence, Assist gas flaring was no longer necessary. Assist gas use was eliminated
11 /03/99 15:50-16:50 367 use necessary for flare emission opacity compliance. as soon as permitted by opacity regulations.
An attempt to restart the MI compressor was unsuccessful. Flare volume The MI compressor operating parameters were adjusted
due to purging, pressurization, depressurization, of Ml compressor. Assist slightly for a greater chance of success on the next re-start
gas was used for the duration of this event to mitigate flare emission attempt. Assist gas use was eliminated as soon as permitted
11 /04/99 09:40-10:50 116 opacity. by flare emission opacity.
Difflcuftles encountered when restarting the Propane compressor resulted The propane compressor was restarted, the assist gas use was
11 /11 /99 11:50-13:40 14 in assist gas use to facilitate compliance with opacity regulation, no longer needed and was immediately eliminated.
Multiple attempts were made to restart the MI compressor. Booster The flared volumes of gas that were necessary during the start-
compressor shut down during the attempts and did not immediately re- up and shut-down were eliminated when the MI compressor
start. Significant assist gas was used to mitigate flare opacity. was successfully started. The booster compressor was also
11 /11 /99 14:30-21:30 723 successfully restarted and assist gas use was eliminated.
MI compressor start-up attempt and booster compressor downtime. Gas The booster compressor was restarted. The MI compressor
was flared during MI compressor start-up procedure and as assist gas to operating parameters were adjusted slightly for a greater
avoid flare opacity. chance of success on the next re-start attempt. Assist gas use
11 /14/99 09:40-12:30 103 was eliminated as soon as permitted by flare emission opacity.
MI compressor start-up attempt and booster compressor downtime. Gas As soon as the MI compressor was successfully started, the
was flared during MI compressor start-up procedure and as assist gas to flaring was no longer necessary, Assist gas use was eliminated
11 /14/99 15:10-16:20 81 avoid flare opacity. as soon as permitted by opacity regulations.
The MI compressor tripped to recycle because of control system. Assist Refinement of the control system for the MI compressor is
gas was necessary for flare opacity compliance. ongoing, Steps were taken to mitigate re-occurrence of the
reason for tripping to recycle. Assist gas was used only as long
11 /15/99 12:00-13:00 101 as necessar to miti ate flare o aci
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ALASKA OIL AND GAS CONSERVATION CON~lISSION
FACILITY REPORT OF PRODUCED GAS DISPOSITION
Facility Operator Field(s) Month/Year of Disposition
Endicott BP Exploration (Alaska) Endicott 10450 Dec-99
Disposition
Volume MCF*
1. Sold
To Fuel
NGL
Badami 14,590
143,867
0
2. Reinjected 10,964,500
3. Flared or vented less than 1 hour 6,686
4. Flared or vented greater than 1 hour
(Supplemental report required--See 20 AAC 25.235) 5,449
5. Pilot and Purge 10,191
6. Used for lease operations Assist
Fuel 23,742
1,056,433
7. Other
TOTAL items 1-7 12,225,458
8. NGL gas equivalent produced 143,867
9. Purchased gas
10. Transferred from:
11. Transferred to:
I hereby certify that the foregoing is true and correct to the best of
Signature e Title (~g~. Yj~~( Date ~ LOQp
*Indicate contribution of each pool
Pool Name Code Percent
220100
Official Use Only-Flaring Authorize
1. Safety MCF
2. Lease MCF
3. Conserv. Purpos MCF
Commissioner Date
Note: All volumes must be
corrected to pressure of 14.65
Asia and to a temperature of 60
degrees F. Report due by the
20th of the month folowing the
month of disposition.
Authority 20 AAC 25.235.
Form 10-422
Rev. 4/95
1/5/2000
Page 1
BP EXPLORATION (ALASKA) INC.
ADMINISTRATIVE APPROVAL N0.202.4
GAS FLARING INCIDENT REPORT - ENDICOTT
December-99
Unplanned Events less than ore ual to 1 hour
DATE TIME i' VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE
TOTAL 6,691 Not required for unplanned events which Not required for unplanned events which
are less than or equal to 1 hour are less than or equal to 1 hour
Un tanned Events reater than 1 hour
DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION'TAKEN TO ELIMlNATE'CAUSE
An attempt to restart the MI compressor was unsuccessful. Flare volume The MI compressor operating parameters were adjusted
due to purging, pressurization, depressurization, of MI compressor. Assist slightly for a greater chance of success on the next re-start
gas was used for the duration of this event to mitigate flare emission attempt, Assist gas use was eliminated as soon as permitted
12/09/99 04:50-05:50 199 opacity. by flare emission opacity.
An attempt to restart the MI compressor was unsuccessful. Flare volume The MI compressor operating parameters were adjusted
due to purging, pressurization, depressurization, of MI compressor. Assist slightly for a greater chance of success on the next re-start
gas was used for the duration of this event to mitigate flare emission attempt. Assist gas use was eliminated as soon as permitted
12/09/99 06:10-07:40 94 opacity. by flare emission opaci
An attempt to restart the MI compressor was unsuccessful. Flare volume The MI compressor operating parameters were adjusted
due to purging, pressurization, depressurization, of MI compressor. Assist slightly for a greater chance of success on the next re-start
gas was used for the duration of this event to mitigate flare emission attempt. Assist gas use was eliminated as soon as permitted
12/09/99 12:30-14:20 125 opaci by flare emission opaci
An attempt to restart the MI compressor was unsuccessful. Flare volume The MI compressor operating parameters were adjusted
due to purging, pressurization, depressurization, of MI compressor. Assist slightly for a greater chance of success on the next re-start
gas was used for the duration of this event to mitigate flare emission attempt, Assist gas use was eliminated as soon as permitted
12/09/99 15:10-16:10 419 opacity. by flare emission opacity.
An attempt to restart the MI compressor was unsuccessful. Flare volume The MI compressor operating parameters were adjusted
due to purging, pressurization, depressurization, of MI compressor. Assist slightly for a greater chance of success on the next re-start
gas was used for the duration of this event to mitigate flare emission attempt. Assist gas use was eliminated as soon as permitted
12/09/99 19;40-20:50 202 o achy. by flare emission o aci
DCS (Digital Control System) failure prevented the reduction of assist gas Repeated commands to reduce assist gas rate finally.
to normal rates after short period of increased volume. accepted by DCS, Controls system engineer notified of
12/11 /99 11:50-22;50 313 problem with system.
Main gas compressor inlet air filters plugged up with snow during blizzard Crews cleared inlet air filters and MGC's were restarted.
forcing shutdown of entire field. Gas injection well back-flowed into plant
12/30/99 01:50-03:40 384 to provide fuel gas.
Main gas compressor inlet air filters plugged up with snow during blizzard Crews working to clear MGC inlet air filters were unlable to
forcing shutdown of entire field, Gas injection well back-flowed into plant keep up with blizzard. Waiting on weather to abate.
12/30/99 19:20-00:00 1,001 to rovide fuel gas,
Main gas compressor inlet air filters plugged up with snow during blizzard Crews working to clear MGC inlet air filters were unlable to
forcing shutdown of entire field. Gas injection well back-flowed into plant keep up with blizzard. Waiting on weather to abate.
12/31/99 00;00-23:59 2,116 to provide fuel gas.
TOTAL 5,453
0
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