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HomeMy WebLinkAboutBPXA - GC #3g-:~~;W.J7~rG16,".WGIM/.wrm~~'YO,ml~~o~am:~Li/wPL~~.Niri..w/®/M'~r.:~~.mCSf4rLm$~ZA~LaL~i~~~fwYev~m~B~iri.Yes/s®L#~imi.M'~sr~.ads/i%arke/~ii~slYla"irL!/.p'~sr~s~:nBi®Yf.~GO~iI~/ws~gC~~r~~~p/a1w~60"Y~®YS. ~'C.'.v~/.~Ldnrsn AGOCC GaS Dlsposl~ion Files 1998 $~PXq-GC3 x . - s: ~.~.~.m.~rr~srwaaiesi.~i.~i~~~i~i.~iairca®io~ua^~r~.®~.~~s.~r~~~:~rw~rwi®rws~r~ arnmz~~~iarvi~i~iwrr.~rmiavi~a~r®im~armesr~~®werrimiiri.®r.~isri,~~~r~i~~w~~rrarm~ar~.~i.~i~r~i~i.~i~i.~~~i~imt~ai a ' ~` h ' ~ ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION J (Facility Operator Field(s) Month/Year of Disposition GATHERING CENTER 3 BP EXPLORATION ALASKA WESTERN OPERATING AREA-PBU Dec-98 Disposition *Indicate contribution of each pool to total. 1. Sold 0 Pool Name Code Percent 2. Reinjected 0 PRUDHOE 640150 100 3. Flared or vented less than 1 hour 10,584 4. Flared or vented greater than 1 hour 37,431 (Supplemental report required--See 20 AAC 25.235) ""' x°"" :; ~ .. 5. Pilot and Purge 20,677 - ; u .. __ ..i : . 6. Used for lease operations 596,573 i _ ._ a U .~. Utficial Usc Only--Flaring Authoriz~~ti6n > 1 hr. 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner llate Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. Form 10-422 (Revised 4/95) Remarks: I hereby certify that the fors going is true and correct to the best of my knowledge. Signature: ~ J~ ~ Title: SUPERVISOR 11. Transferred to: CCP 26,421,657 7. Other 'r.'1!;`1f1€ ",' 0 TOTAL items 1 - 7 665,265 8. NGL gas equivalent produced 0 9. Purchased gas 0 10. Transferred from: 0 TOTAL LINE 29 AUDIT TRAIL(plus 29A) 258,362,747 TOTAL FROM 8 FACILffIES 258,362,746 9812 FORM 10-422.x1s/FORM 10-422 •~ BP EXPLORATION (ALASKA) INC. y PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT Page 1 DECEMBER, 1998 Unplanned Events less than or equal to 1 hour ~ ~_ DATE TIME = VOLUME DESCRIPTION OF INCIDENT & CAUSE ' ACTION TAKEN TO ELIMINATE CAUSE 12/1/98 0155-0216 73 Not required for unplanned events which Not required for unplanned events whit 12/1/98 0337-0353 56 are less than or equal to 1 hour are less than or equal to 1 hour 12/1 /98 2031-2102 87 12/2/98 1235-1245 104 12/2/98 1555-1617 125 12/2/98 2323-2350 375 12/3/98 0525-0602 208 12/3/98 1737-1807 320 12/4/98 0202-0229 275 12/4/98 2205-2240 210 12/5/98 0953-1028 194 12/5/98 1120-1134 146 12/5/98 2210-2255 500 12/6/98 0238-0330 625 12/7/98 0453-0551 469 12/7/98 0841-0913 174 12/7/98 1644-1714 139 12/7/98 1804-1856 188 12/8/98 1942-2024 1,460 12/10/98 0957-1019 156 12/10/98 1512-1608 208 12/11 /98 1538-1634 313 12/17/98 2224-2304 160 12/18/98 1354-1423 1,108 12/18/98 1451-1541 2,083 12/18/98 1958-2007 63 12/19/98 1427-1503 188 12/21 /98 2015-2035 208 12/25/98 2034-2129 201 12/26/98 1403-1444 168 TOTAL 10,584 BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT DECEMBER, 1998 Unplanned Events greater than 1 hour DATE TIME '- '; VOLUME DESCRIPTION OF=11 12/3/98 0317-0433 625 See Attachments 12/9/98 1842-1952 275 See Attachments 12/10/98 1715-1826 5,966 See Attachments 12/12/98 1112-1720 19,167 See Attachments 12/13/98 0236-2145 5,585 See Attachments 12/14/98 0001-21.15 3,539 See Attachments 12/15/98 0740-1015 592 See Attachments 12/18/98 0800-0958 164 See Attachments 12/30/98 1745-2400 783 See Attachments 12/31/98 0000-0554 735 See Attachments TOTAL 37,431 ACTION TAKEN TO See Attachments See Attachments See Attachments See Attachments See Attachments See Attachments See Attachments See Attachments See Attachments See Attachments Planned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mcf ~ DATE :TIME VOLUME 'DESCRIPTION OF'INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE TOTAL 0 Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf ~ DATE TIME '' VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO'ELIMINATE CAUSE '' TOTAL 0 Unplanned Events < 1 Hour Unplanned Events > 1 Hour Planned Events < 1 hour & not exceeding 5,000 MCF Planned Events > 1 hour and exceeding 5,000 MCF Pilot Purge TOTAL FLARED VOLUME TOTAL...:.: 10,584 37,431 0 0 20,677 68,692 Page 2 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: O3 DeC 98 REPORT NO: 98-4627, TOTAL VOLUME: 1,15$ MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 03:17 TO: 04:33 1 Hrs. 16 Mins. ® ^ ^ ^ 625 MSCF 2. FROM: 05:25 TO: 06:02 0 Hrs. 37 Mins. ® ^ ^ ^ 208 MSCF 3. FROM: 17:37 TO: 1$:07 0 Hrs. 30 Mins• ^ ® ^ ^ 320 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. While bringing production rates up following CCP 1806 repair, FSIM increased causing discharge to flare. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 3 F. 3. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 6°F. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates equaling 20 mmscfd. Wells were choked back starting at 03:40 hours. 2. BPX reduced production rates equaling 20 mmscfd. Wells were choked back starting at 05:28 hours. 3. BPX reduced production rates equaling 30 mmscfd. ARCO reduced production rates equaling 60 mmscfd. Wells were shut-in or choked back starting at 17:45 hours. 4. 5. Rev 6/22/97 • REPORT NO: 9$-4641, BPX FLARE REPORT .. ' PRUDHOE BAY FACILITY: GC-3 DATE: O9 DeC 98 TOTAL VOLUME: 275 MSCF Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: ~ $:42 TO: 19:52 1 Hrs. 1 O Mins. ® ^ ^ ^ 275 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Am bient temperatu re increased by 7°F. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 1 well and choked back 2 wells equaling 50 mmscfd. ARCO reduced production rates and shut-in 1 wells equaling 55 mmscfd. Wells were shut-in or choked back starting at 18:50 hours. 2. 3. 4. 5. Rev 6/22/97 . • REPORT NO: 98-4642,E BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-$ DATE: 1 O DeC 98 TOTAL VOLUME: 6,530 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 09:57 To: 10:19 0 Hrs. 22 Minn. ® ^ ^ ^ 156 MSCF 2. FROM: 15:12 TO: 16:08 0 Hrs. 56 Mins. ® ^ ^ ^ 208 MSCF 3. FROM: 17:15 TO: 18:26 1 Hrs. 11 Mins. ^ ® ^ ^ 5,966 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 3°F. 2. High Gas Transit line pressure due to ramping up rates when the ambient temperature dropped, 3. Asset Area TEG regeneration system shut down because of a low gas alarm in regeneration skid. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 3 wells equaling 35 mmscfd. Wells were shut-in or choked back starting at 10:05 hours. 2. Arco reduced production rates and shut-in 2 wells equaling 50 mmscfd. Wells were shut-in or choked back starting at 15:25 hours. 3. Equipment was restarted at 17:21 hours and 17:51 hrs. Flaring continued until reboiler temperatures were up. Gas cuts had just been started when the 2nd regeneration train was started. 4. 5. Rev 6/22/97 BPX FLARE REPORT PRUDHOE BAY REPORT NO: 98-464$. FACILITY: GC-3 DATE: 12 Dec 98 TOTAL VOLUME: 19,167 MSCF Intermi ttent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 11:1 Z TO: 17:20 6 Hrs. $Mins. ^ ® ^ ^ 19,167 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK: CONTROLLED BLOWDOWN: _ OTHER:_ First Determination of Cause: 1. A PSV (pressure safety valve) on the LPS Compressors came open allowi ng gas to relieve to the flare system. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. While the GC was troubleshooting, production cuts were made. The problem was found to be a frozen sensing line that goes to the PSV Pilot. Production was then cut to absolute minimum until the line was thawed and the PSV was put back in service. 2. 3. 4. 5. Rev 6/22/97 BPX FLARE REPORT PRUDHOE BAY FACILITY: CiC-$ DATE: 13 DeC 98 TIME OF FLARING: DURATION: 1. FROM: 02:36 TO: 21:45 19 Hrs. 9 Mins. 2. FROM: TO: Hrs. Mins. 3. FROM: TO: Hrs. Mins. 4. FROM: TO: Hrs. Mins. 5. FROM: TO: Hrs. Mins. REPORT NO: TOTAL VOLUME: Intermi ttent Black Yes No Smoke? Planned? ^ ® ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ First Determination of Cause: 1. K5500 wet gas compressor shut down on high differantial on the coalessor filters. 2. 3. 4. 5. 98-4645. 5,585 MscF VOLUME 5,585 MscF MSCF MSCF MSCF MSCF OTHER: Action Taken to Stop Flaring: 1. Filters were changed and numerous attempts were made to keep compressor on line with no success. HP gas was shut down and moved from plant to curtail flaring event. 2. 3. 4. 5. I Rev 6/22/97 • . REPORT NO: BPX FLARE REPORT ' PRUDHOE BAY FACILITY: GC-3 DATE: 14 D2C 98 TOTAL VOLUME: Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? 1. FROM: 00:01 TO: 21:15 21 Hrs. 14 Mins. ^ ® ^ ^ 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ 98-465Q, 3,539 MscF VOLUME 3,539 MscF MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK: CONTROLLED SLOWDOWN: _ OTHER: First Determination of Cause: 1. K5500 wet gas compressor shut down on high differantial on the coalessor filters. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Filters were changed and compressor was restarted at 21:15 hrs. HP gas was shut down or moved from the facilities to curtail flaring event while the compressor was s/d. 2. 3. 4. 5. ae~ si2vs~ BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 15 Dec 98 TIME OF FLARING: DURATION: 1. FROM: 07:40 TO: 10:15 2 Hrs. 35 Mins. 2. FROM: TO: Hrs. Mins. 3. FROM: TO: Hrs. Mins. 4. FROM: TO: Hrs. Mins. 5. FROM: TO: Hrs. Mins. CH ECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK: First Determination of Cause: 1. K-5500 Wet Gas Compressor S/D on high differential. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Equipment was restarted at 10:15 hours. 2. 3. 4. 5. Intermittent Yes No ^ ^ ^ ^ ^ ^ ^ ^ REPORT NO: TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ CONTROLLED BLOWDOWN: 98-4652` 592 MscF VOLUME 592 MSCF MSCF MSCF MSCF MSCF OTHER: _ Rev 6/22/97 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-$ DATE: 18 Dec 98 REPORT NO: TOTAL VOLUME: 98-465,. ... 3,418 MscF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 08:00 TO: 09:58 1 Hrs. 58 Mins. ^ ® ^ ^ 164 MSCF 2. FROM: 13:54 TO: 14:23 0 Hrs. 29 Mins. ^ ® ^ ^ 1,108 MSCF 3. FROM: 14:51 TO: 15:41 O Hrs. 50 Mins• ^ ® ^ ^ 2,083 MSCF 4. FROM: 19:58 To: 20:07 0 Hrs. 9 Mins. ^ ® ^ ^ 63 MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEFVALVE: X RUPTUREDISK:_ CONTROLLEDBLOWDOWN:_ OTHER:_ First Determination of Cause: 1. Wet gas K 5500 s/d do to due to low suction compressor. 2. GLT compressor K-3200 shut down because of control/instrumentation failure associated with 13:52hrs. 3. GLT compressor K-3200 shut down because of control/instrumentation failure associated with 14:38hrs. 4. While bringing production rates up following GLT compressor start up , exceeded maximum gas capacity and discharged to flare. 5. Action Taken to Stop Flaring: 1. Compressor restarted 2. No response taken as this was deemed to be of short duration. 3. BPX reduced production rates and shut-in 24 wells equaling 500 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 100mmscfd. Wells were shut-in or choked back starting at 15:30 hours. 4. BPX reduced production rates equaling 130 mmscfd. ARCO reduced production rates equaling 75 mmscfd. Wells were shut-in or choked back starting at 19:30 hours. 5. Rev 6/22/97 REPORT NO: 98-4674 BPX FLARE REPORT ' PRUDHOE BA Y FACILITY: GC-3 DATE: 30 Dec 98 TOTAL VOLUME: 783 MSCF Intermi ttent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 17:45 TO: 24:00 6 Hrs. 15 Mins. ^ ® ^ ^ 7$3 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARElRELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. K-5500 wet gas compressor s/d due to low suction pressure. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Flaring was permitted to continue while GC operations personnel attempted to restart the equipment. 2. 3. 4. 5. Rev 6/22/97 . REPORT NO: BPX FLARE REPORT ' PRUDHOE BAY FACILITY: GC-3 DATE: 31 Dec 98 TOTAL VOLUME: Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? 1. FROM: 00:00 TO: 05:54 5 Hrs. 54 Mins. ^ ® ^ ^ 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ CH ECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK: CONTROLLED BLOWDOWN First Determination of Cause: 1. K-5500 wet gas compressor s/d due to low suction pressure. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Flaring was permitted to continue while GC operations personnel attempted to restart the equipment. 2. 3. 4. 5. 98-4675; .- ~.~ 735 MSCF VOLUME 735 MSCF MSCF MSCF MSCF MSCF OTHER: ~ Rev 6/22/97 RE: GC3 December 1998 flaring event Subject: RE: GC3 December 1998 flaring event Date: Fri, 5 Mar 1999 17:02:14 -0500 From: "PBU, Prod Opt TL" <PBUProdOptTL@BP.com> To: "'Mahan, Wendy (AOGCC)"' <Wendy_Mahan@admin.state.ak.us> CC: "PBU, Prod Opt TL" <PBUProdOptTL@BP.com>, "PBU, NS Res Engineer" <PBUNSResEngineer@BP.com> > Ms. Mahan: > The following reconstructs the Prudhoe Bay Gathering Center 3 Flaring > Event of December 12, 1998 based on operator logs, alarm summaries, and > discussions with operators and facility supervisors. > 1) Gathering Center 3 had shut down High Pressure production overnight to > repair a risk rank 1 Hazop defect on a first stage separator. The repair > was implemented at the beginning of the day shift and was completed by > approximately 1000 on 12/33:~Z•The HP system was 'safed in' between 1000 > and 1030. > 2) Operations staff began reintroducing gas to the HP system between 1030 > and 1130 with HP oil flow starting between 1045 and 1115. > 3) Flare alarms activated at 1112 and operators saw small volumes of gas > flaring. > 4) Operations staff assumed that flaring was sourced in the HP section > (since that section was just starting up) of the plant and troubleshot > that section of the facility. Small flare volume led operators to believe > that a pilot actuated PSV on a 1st stage HP separator had not seated. > Flare volume slowly increased over approximately an hour to the point that > operators recognized the source of the flared gas was elsewhere. The > source of flaring was not immediately located. PCC Controllers shut in > all HP production to GC-3 between 1200 and 1230. Flaring did not stop. > 5) Operations staff troubleshot other sections of the facility, determined > that flaring was sourced in the low pressure section of the facility. > Decision was made to shut down most production at the Gathering Center > (maintaining flow from coldest, wettest wells to avoid freeze protection). > Low Pressure production was cut by 300 NIMSCFD between 1240 and 1315. At > 1340 an additional 100 MMSCFD low pressure production cut was taken at > GC-3 with all remaining GC-3 wells cut to minimum choke setting. Thus, by > 1340 GC-3 production was at minimum rates to maintain facility operation > without a complete plant shut in (flaring rate was cut to 2-5 MMSCFD by > tha t point) > 6) The frozen PSV sensing line was located in an outdoor piperack at 1403. > Warming the line required until 1.720. The PSVs held at that time. > 7) At 1725 PCC Controllers began to re-introduce Low Pressure production > to GC-3. At 1925, PCC controllers began to reintroduce High Pressure > production. > 8) Normal GC-3 production rates were restored overnight. > In summary, BPX flared gas for over an hour at elevated rates at GC-3 > because the source of flaring was not immediately located (operations > staff assumed flaring sourced in an area of the plant that was > re pressuring following a maintenance shutdown). Production cuts were > initiated prior to one hour but did not affect the section of the plant > that was flaring. As soon as the source was located, additional 1 of 2 7/28/99 11:03 AM RE: GC3 December 1998 flaring event > production cuts were made to reduce flaring to a minimum. Production was > shut in until the PSVs were returned to normal service. > Please contact me if you have questions or comments. > Thanks > Kelly Eager > BPX Prudhoe Bay Production OTL > 907-659-4472 > -- > From: Wendy Mahan(SMTP:Wendy Mahan@admin.state.ak.us] > Sent: Thursday, March 04, 1999 1:28 PM > To: pbuprodopttl@bp.com > Subject: GC3 December 1998 flaring event > Mr. French, > I originally sent the following mesage to you on February 12, 1999. > Since I haven't received a response, I just wanted to make sure that you > do indeed receive the message. Please let me know if BPXA intends to > respond to this information request. Thank you. > Mr. French, > I inadvertently Left out a request for information on an additional > flaring event when I spoke to you on February 10th. A PSV event was > reported for December 12, 1998 from 11:12-17:20. At what time were the > initial production cuts made and at what time was production cut to a > minimum? When was the frozen sensing line discovered and how long did > it take to thaw? Thanks. 2 of 2 7/28/99 11:03 AM s ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition GATHERING CENTER 3 BP EXPLORATION ALASKA WESTERN OPERATING AREA-PBU Nov-98 Disposition 1. sold o 2. Reinjected 0 3. Flared or vented less than 1 hour 11,626 4. Flared or vented greater than 1 hour 17,805 (Supplemental report required--See 20 AAC 25.235) 5. Pilot and Purge 17,027 6. Used for lease operations 583,205 7. Other 0 TOTAL items 1 - 7 629,663 8. NGL gas equivalent produced 0 9. Purchased gas 0 10. Transferred from: 0 I i. Transferred to: CCP 24,782,168 I hereby certify that the foregoing is true and correct to the best of my knowledge. Signature: (~.~~-~/~--- 12~p/ll~j Title: SUPERVISOR Form 10-422 (Revised 4/95) ~/ *Indicate contribution of each pool to total. Pool Name Code Percen[ PRUDHOE 640150 100 Off ci:~l Usc Ouly--Flaring Authorization > 1 lii 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner llate Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. 9811 FORM 10-422.xis/FORM 1 D-422 BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT NOVEMBER, 1998 Unplanned Events less than or equal to 1 hour ~ DATE `TIME VOLUME DESCRIPTION OFINCIDENT &' CAUSE ACTION TAKEN TO ELIMINATE CAUSE 11/1/98 0643-0730 160 Not required for unplanned events which Not required for unplanned events whi~ 11/1/98 1210-1300 139 are less than or equal to 1 hour are less than or equal to 1 hour 11 /2/98 0000-0035 292 11 /2/98 0228-0313 375 11 /3/98 0015-0113 403 11 /3/98 0545-0637 243 11 /3/98 2121-2143 139 11 /5/98 1528-1614 554 11 /6/98 0420-0429 188 11/7/98 0343-0358 188 11/7/98 1129-1202 156 11 /12/98 2029-2127 926 11 /13/98 1128-1145 118 11 /13/98 1241-1338 594 11 /13/98 1424-1458 354 11 /14/98 1054-1116 153 11 /16/98 0855-0928 160 11/16/98 1044-1139 319 11 /17/98 0805-0837 167 11 /18/98 2257-2331 300 11 /19/98 0208-0259 470 11 /19/98 1527-1534 88 11 /19/98 2313-2342 350 11 /20/98 2049-2145 730 11 /22/98 1017-1028 115 11 /22/98 1539-1605 76 11 /23/98 0359-0451 550 11 /23/98 0731-0758 125 11 /23/98 1931-2010 250 11 /23/98 2148-2243 160 11 /24/98 2119-2206 125 11 /25/98 0128-0148 350 11 /25/98 0830-0850 108 11 /26/98 1204-1241 192 11/27/98 1015-1100 343 11 /27/98 2037-2051 97 11 /28/98 0113-0206 306 11/28/98 1127-1157 583 11 /28/98 2144-2157 90 Page 1 BP EXPLORATION (ALASKA) INC. . PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT NOVEMBER, 1998 11/29/98 1923-1956 229 11 /29/98 2123-2151 194 11 /30/98 0027-0057 104 11 /30/98 2004-2054 63 TOTAL 11,626 Unplanned Events greater than 1 hour DATE -. TIME ? VOLUME DESCRIPTION OF INCIDENT'& CAUSE' ~~ ACTION TAKCN TO ELIMINATE 11/1/98 0118-0226 567 See Attachments See Attachments 11/1/98 0953-1128 306 See Attachments See Attachments 11/1/98 1428-1539 243 See Attachments See Attachments 11/1/98 1821-1954 625 See Attachments See Attachments 11/1/98 2143-2400 1,000 See Attachments See Attachments 11/2/98 1955-2131 442 See Attachments See Attachments 11/3/98 1751-1930 375 See Attachments See Attachments 11/4/98 0145-0306 675 See Attachments See Attachments 11/6/98 1254-1710 2,667 See Attachments See Attachments 11/12/98 0431-0542 382 See Attachments See Attachments 11/12/98 1403-1516 347 See Attachments See Attachments 11/13/98 1729-1944 1,428 See Attachments See Attachments 11/14/98 0625-0735 486 See Attachments See Attachments 11/14/98 0822-1033 681 See Attachments See Attachments 11/14/98 1600-1728 396 See Attachments See Attachments 11/15/98 0834-1012 604 See Attachments See Attachments 11/16/98 1741-1853 975 See Attachments See Attachments 11/17/98 0507-0648 521 See Attachments See Attachments 11/17/98 1117-1352 156 See Attachments See Attachments 11/19/98 2012-2156 1,300 See Attachments See Attachments 11/21/98 2101-2225 875 See Attachments See Attachments 11/22/98 0102-0235 575 See Attachments See Attachments 11/26/98 0001-0122 486 See Attachments See Attachments 11/26/98 1912-2041 333 See Attachments See Attachments 11/26/98 2141-2305 333 See Attachments See Attachments 11/28/98 0226-0356 444 See Attachments See Attachments 11/29/98 0003-0213 583 See Attachments See Attachments TOTAL 17,805 E Planned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mcf ~ ... DATE TIME VOLUME 'DESCRIPTION OF;INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE Page 2 TOTAL 0 BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT NOVEMBER, 1998 Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf ~ IJATE ?TIME VOLUME < DESCRIPTION OF INCIDENT & CAUSE ACTION TAKfN TO ELIMINATE CAUSE TOTAL 0 Unplanned Events < 1 Hour Unplanned Events > 1 Hour Planned Events < 1 hour & not exceeding 5,000 MCF Planned Events > l hour and exceeding 5,000 MCF Pilot Purge TOTAL FLARED VOLUME TOTAL 11,626 17, 805 0 0 17,027 46,458 Page 3 • ~ REPORT NO: 9$-4573 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 01 Nov 98 TOTAL VOLUME: 1,415 MSCF Intermi ttent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 01:18 TO: 02:26 1 Hrs. $Mins. ^ ® ^ ^ 567 MSCF 2. FROM: 06:43 TO: 07:30 0 Hrs. 47 Mins. ® ^ ^ ^ 160 MSCF 3. FROM: 09:53 TO: 11:28 1 Hrs. 35 Mins. ® ^ ^ ^ 806 MSCF 4. FROM: 12:10 TO: 13:00 O Hrs. 50 Mins. ® ^ ^ ^ 139 MSCF 5. FROM: 14:28 TO: 15:39 1 Hrs. 11 Mins. ® ^ ^ ^ 243 MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. While bringing production rates up following "X" pad corossion repairs, flared HP gas due to high transit gas line pressure . 2. High gas transit line pressure caused by CGF MI compressor #2 S/D. 3. High gas transit line pressure caused by CGF MI compressor #2 S/D. (Same S/D as listed above) 4. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 10°F. 5. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 12°F. Action Taken to Stop Flaring: 1. Arco reduced production rates and shut-in 6 wells equaling 200 mmscfd. Wells were shut-in or choked back starting at 01:30 hours. 2. Equipment was restarted at 11:12 hours. 3. Equipment was restarted at 11:12 hours. 4. BPX reduced production rates and shut-in 7 wells equaling 110 mmscfd. ARCO reduced production rates and shut-in 3 wells equaling 75 mmscfd. Wells were shut-in or choked back starting at 12:15 hours. 5. BPX reduced production rates and shut-in 6 wells equaling 90 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 75 mmscfd. Wells were shut-in or choked back starting at 14:35 hours. ~~ev sr~as~ REPORT NO: 9$-4576 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: O1 NOV 98 TIME OF FLARING: 1. FROM: 18:21 TO: 19:54 2. FROM: 21:43 ro: 24:00 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 1 Hrs. 33 Mins. 2 Hrs. 17 Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ® ^ ® ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 1,625 MscF VOLUME 625 MSCF 1,000 MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 6°F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 6°F. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 3 wells equaling 44 mmscfd. Wells were shut-in or choked back starting at 18:50 hours. 2. BPX reduced production rates and shut-in 2 wells equaling 40 mmscfd. ARCO reduced production rates and shut-in wells equaling 130 mmscfd. Wells were shut-in or choked back starting at 21:45 hours. 3. 4. 5. Rev 6/22/97 REPORT NO: J$-4577 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: O2 NOV 98 TOTAL VOLUME: 1 ~ 109 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 00:00 TO: 00:35 0 Hrs. 35 Mins. ^ ® ^ ^ 292 MSCF 2. FROM: 02:28 To: 03:13 0 Hrs. 45 Mins. ^ ® ^ ^ 375 MSCF 3. FROM: 19:55 TO: 21:31 1 Hrs. 36 Mins. ® ^ ^ ^ 442 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 6°F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 5°F. 3. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 3°F. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 3 wells equaling 44 mmscfd. Wells were shut-in or choked back starting at 00:01 hours. 2. BPX reduced production rates and shut-in 2 wells equaling 30 mmscfd. ARCO reduced production rates and shut-in 3 wells equaling 80 mmscfd. Wells were shut-in or choked back starting at 02:12 hours. 3. BPX reduced production rates and shut-in 2 wells equaling 50 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 50 mmscfd. Wells were shut-in or choked back starting at 19:49 hours. 4. 5. Rev 6/22/97 • REPORT NO: 9$-4579 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 03 Nov 98 TOTAL VOLUME: 1 ~ 16O MSCF Intermittent Black TIM E OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 00:15 To: 01:13 0 Hrs. 58 Mins. ^ ® ^ ^ 403 MSCF 2. FROM: 05:45 To: 06:37 0 Hrs. 52 Mins. ® ^ ^ ^ 243 MSCF 3. FROM: 17:51 TO: 19:30 1 Hrs. 39 Mins. ® ^ ^ ^ 375 MSCF 4. FROM: 21:21 TO: 21:43 0 Hrs. 22 Mins. ® ^ ^ ^ 139 MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 3°F. 3. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 4. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 2 wells equaling 30 mmscfd. ARCO reduced production rates and shut-in 3 wells equaling 60 mmscfd. Wells were shut-in or choked back starting at 00:15 hours. 2. BPX reduced production rates and shut-in 4 wells equaling 50 mmscfd. Wells were shut-in or choked back starting at 05:50 hours. 3. BPX reduced production rates and shut-in 2 wells equaling 25 mmscfd. ARCO reduced production rates and shut-in 3 wells equaling 50 mmscfd. Wells were shut-in or choked back starting at 18:13 hours. 4. Arco reduced production rates and shut-in 3 wells equaling 60 mmscfd. Wells were shut-in or choked back starting at 21:25 hours. 5. Rev 6/22/97 • ~ REPORT NO: BPX FLARE REPORT PRUDHOE BAY 98-4581 Y FACILITY: GC-3 DATE: O4 NOV 98 TOTAL VOLUME: 675 MSCF Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 01:45 TO: 03:06 1 Hrs. 21 Mins. ^ ® ^ ^ 675 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Am bient temperature increased by 3°F. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 3 wells equaling 33 mmscfd. ARCO reduced production rates and shut-in 3 wells equaling 40 mmscfd. Wells were shut-in or choked back starting at 01:54 hours. 2. 3. 4. 5. Rev 6/22/97 . ~ REPORT NO: BPX FLARE REPORT PRUDHOE BAY 98-4583 FACILITY: GC-$ DATE: OB NOV 98 TOTAL VOLUME: 2,$55 MSCF Intermi ttent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 04:20 TO: 04:29 0 Hrs. 9 Mins. ^ ® ^ ^ 188 MSCF 2. FROM: 12:54 TO: 17:10 4 Hrs. 16 Mins. ^ ® ^ ^ 2,667 MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High gas transit line pressure caused by CCP compressor 1878 Tandem S/D problems . 2. Wet gas cpmpressor had to be s/d for lube oil filter change. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates equaling 150 mmscfd. Wells were choked back starting at 04:18 hours. 2. Equipment was restarted at XXXX hours. 3. 4. 5. Rev 6/22/97 . REPORT NO: 9$-4592 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 12 Nov 98 TOTAL VOLUME: 1,655 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 04:31 TO: 05:42 1 Hrs. 11 Mins. ® ^ ^ ^ 382 MSCF 2. FROM: 14:03 TO: 15:16 1 Hrs. 13 Mins. ® ^ ^ ^ 347 MSCF 3. FROM: 20:29 TO: 21:27 0 Hrs. 58 Mins. ® ^ ^ ^ 926 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 5°F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 3. While bringing production rates up the fsim became a high pressure 4. 5. Action Taken to Stop Flaring: 1. Arco reduced production rates and shut-in 5 wells equaling 100 mmscfd. Wells were shut-in or choked back starting at 04:44 hours. 2. BPX reduced production rates and shut-in 2 wells equaling 30 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 44 mmscfd. Wells were shut-in or choked back starting at 14:30 hours. 3. BPX reduced production rates and shut-in 5 wells equaling 87 mmscfd. ARCO reduced production rates and shut-in 8 wells equaling 120 mmscfd. Wells were shut-in or choked back starting at 20:33 hours. 4. 5. ae~ s~2vsa • REPORT NO: 9$-4593 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 13 NOV 98 TOTAL VOLUME: 2,494 MSCF Intermittent Black TIM E OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 11:28 TO: 11:45 0 Hrs. 17 Mins. ^ ® ^ ^ 118 MSCF 2. FROM: 12:41 TO: 13:38 0 Hrs. 57 Mins. ^ ® ^ ^ 594 MSCF 3. FROM: 14:24 TO: 14:58 0 Hrs. 34 Mins. ^ ® ^ ^ 354 MSCF 4. FROM: 17:29 TO: 19:44 2 Hrs. 15 Mins. ® ^ ^ ^ 1,428 MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. GLT compressor K-3300 shut down due to control/instrumentation failure associated with erroneous fire/gas alarms. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 7°F. 3. High gas transit line pressure caused by CCP LS compressor #1804 shutting down while trying to switch inverters. 4. While bringing production rates up following CCP #1804 s/d a high fsim occured. 5. Action Taken to Stop Flaring: 1. Equipment was restarted at 11:37 hours. 2. BPX reduced production rates and shut-in 3 wells equaling 50 mmscfd. Wells were shut-in or choked back starting at 13:03 hours. 3. Arco reduced production rates and shut-in 11 wells equaling 250 mmscfd. Wells were shut-in or choked back starting at 14:30 hours. 4. BPX reduced production rates and shut-in 6 wells equaling 47 mmscfd. ARCO reduced production rates and shut-in 4 wells equaling 88 mmscfd. Wells were shut-in or choked back starting at 18:34 hours. 5. Rev 6/22/97 • ~ REPORT NO: 9$-4595 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 14 Nov 98 TOTAL VOLUME: 1 ,716 MSCF Intermittent Black TIM E OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 06:25 TO: 07:35 1 Hrs. 1 O Mins. ^ ® ^ ^ 486 MSCF 2. FROM: 08:22 TO: 10:33 2 Hrs. 11 Mins. ® ^ ^ ^ 681 MSCF 3. FROM: 10:54 TO: 11:16 O Hrs. 22 Mins. ^ ® ^ ^ 153 MSCF 4. FROM: 16:00 TO: 17:28 1 Hrs. 28 Mins. ® ^ ^ ^ 396 MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High gas transit line pressure caused by too much gas for current ambient air temperature (12'`F). 2. High gas transit line pressure caused by too much gas for current ambient air temperature (12''F). 3. High gas transit line pressure caused by CCP compressor problems due to LS 1804 (swapped inventors). 4. EWE compressor start-up, Arco brought on too much gas rate. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 4 wells equaling 150 mmscfd. ARCO reduced production rates and shut-in 4 wells equaling 50 mmscfd. Wells were shut-in or choked back starting at 06:25 hours. 2. BPX reduced production rates and shut-in 3 wells equaling 45 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 30 mmscfd. Wells were shut-in or choked back starting at 08:57 hours. 3. LS 1804 was loaded at 11:07 hours. 4. Arco reduced production rates and shut-in 3 wells equaling 80 mmscfd. Wells were shut-in or choked back starting at 16:20 hours. 5. I Rev 6/22/97 • ~ REPORT NO: BPX FLARE REPORT ' PRUDHOE BAY FACILITY: GC-$ DATE: 15 NOV 98 TOTAL VOLUME: Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? 1. FROM: 08:34 TO: 10:12 1 Hrs. 38 Mins. ® ^ ^ ^ 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ First Determination of Cause: 1. High gas transit line pressure caused by CCP compressor problems due to LS 1804 (swapped inverters) 2. 3. 4. 5. Action Taken to Stop Flaring: 98-4597 604 MscF VOLUME 604 MscF MSCF MSCF MSCF MSCF OTHER: 1. BPX reduced production rates and shut-in 3 wells equaling 40 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 50 mmscfd. Wells were shut-in or choked back starting at 08:40 hours. 2. 3. 4. 5. Rev 6/22/97 • • REPORT NO: 9$-4599 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 16 Nov 98 TOTAL VOLUME: 1 X4.54. MSCF Intermittent Black TIM E OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 08:55 TO: 09:28 0 Hrs. 33 Mins. ® ^ ^ ^ 160 MSCF 2. FROM: 10:44 TO: 11:39 0 Hrs. 55 Mins. ® ^ ^ ^ 319 MSCF 3. FROM: 17:41 TO: 18:53 1 Hrs. 12 Mins. ^ ^ ^ ^ 975 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High gas transit line pressure caused by too much gas for current ambient air temperature (7"F). 2. High gas transit line pressure caused by too much gas for current ambient air temperature (8*F). 3. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 5°F. 4. 5. Action Taken to Stop Flaring: 1. Arco reduced production rates and shut-in 2 wells equaling 30 mmscfd. Wells were shut-in or choked back starting at 08:57 hours. 2. Arco reduced production rates and shut-in 2 wells equaling 45 mmscfd. Wells were shut-in or choked back starting at 11:04 hours. 3. BPX reduced production rates and shut-in 5 wells equaling 103 mmscfd. ARCO reduced production rates and shut-in 3 wells equaling 95 mmscfd. Wells were shut-in or choked back starting at 17:45 hours. 4. 5. Rev 6/22/97 REPORT NO: 98-4601 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 17 NOV 98 TOTAL VOLUME: 844 MSCF Intermittent Black TIM E OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 05:07 TO: 06:48 1 Hrs. 41 Mins. ® ^ ^ ^ 521 MSCF 2. FROM: 08:05 TO: 0$:37 0 Hrs. 32 Mins. ^ ® ^ ^ 167 MSCF 3. FROM: 11:17 TO: 13:52 2 Hrs. 35 Mins. ® ^ ^ ^ 156 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 4°F. 2. Extended flaring event occurred while awaiting GC operator/maintenance evaluation ("D" Bank 1 rst stage). 3. Extended flaring event occurred while awaiting GC operator/maintenance evaluation ("D" Bank 1 rst stage),popping flare valve intermittently during the troubleshooting. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 4 wells equaling 30 mmscfd. Wells were shut-in or choked back starting at 05:00 hours. 2. BPX reduced production rates and cut back 5 wells equaling 37.6 mmscfd. Wells were choked back starting at 08:26 hours. 3. 4. 5. Aev 6/22/97 REPORT NO: 98-4603 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-$ DATE: 19 Nov 98 TOTAL VOLUME: 2208 MSCF Intermittent Black TIM E OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 02:0$ TO: 02:59 O Hrs. 51 Mins. ® ^ ^ ^ 470 MSCF 2. FROM: 15:27 TO: 15:34 O Hrs. 7 Mins. ^ ® ^ ^ $$ MSCF 3. FROM: 20:12 TO: 21:56 1 Hrs. 44 Mins. ^ ® ^ ^ 1,300 MSCF 4. FROM: 23:13 TO: 23:42 O Hrs. 29 Mins. ^ ® ^ ^ 350 MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 4°F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 3. High gas transit line pressure caused by CCP compressor problems due to blowing snow obscuring suction. 4. High gas transit line pressure caused by CCP compressor problems due to blowing snow obscuring suction. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates equaling 10 mmscfd. ARCO reduced production rates equaling 80 mmscfd. Wells were shut-in or choked back starting at 02:20 hours. 2. BPX reduced production rates equaling 40 mmscfd. Wells were shut-in or choked back starting at 15:28 hours. 3. BPX reduced production rates equaling 50 mmscfd. ARCO reduced production rates equaling 80 mmscfd. Wells were choked back starting at 20:25 hours. 4. BPX reduced production rates equaling 50 mmscfd. Wells were choked back starting at 23:20 hours. 5. Rev 6/22/97 REPORT NO: 9$-4606 BPX FLARE REPORT ' PRUDHOE BAY FACILITY: GC-3 DATE: 21 Nov 98 TOTAL VOLUME: 875 MSCF Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 21:01 TO: 22:25 1 Hrs. 24 Mins. ^ ® ^ ^ $75 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ® ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Am bient temperatu re increased by 5°F. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates equaling 30 mmscfd. ARCO reduced production rates equaling 30 mmscfd. Wells were shut-in or choked back starting at 20:50 hours. 2. 3. 4. 5. Rev 6/22/97 C~ • REPORT NO: J$-4608 1 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 22 Nov 98 TOTAL VOLUME: 766 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 01:02 TO: 02:35 1 Hrs. 33 Mins. ® ^ ^ ^ 575 MSCF 2. FROM: 10:17 TO: 10:28 ~ Hrs. 11 Mins. ^ ® ^ ^ 115 MSCF 3. FROM: 15:39 TO: 16:05 0 Hrs. 26 Mins. ® ^ ^ ^ 76 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 9°F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 3. High gas transit line pressure caused by Arco/BP adjusting well rates 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates equaling 50 mmscfd. ARCO reduced production rates equaling 80 mmscfd. Wells were shut-in or choked back starting at 01:15 hours. 2. BPX reduced production rates equaling 50 mmscfd. Wells were shut-in or choked back starting at 10:17 hours. 3. BPX reduced production rates equaling 25 mmscfd. Wells were shut-in or choked back starting at 1540 hours. 4. 5. Rev 6/22/97 • ~ REPORT NO: 9$-4615 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 26 Nov 98 TIME OF FLARING: DURATION: 1. FROM: 00:01 TO: 01:22 1 Hrs. 21 Mins. 2. FROM: 12:04 TO: 12:41 0 Hrs. 37 Mins. 3. FROM: 19:12 TO: 20:41 1 Hrs. 29 Mins. 4. FROM: 21:41 TO: 23:05 1 Hrs. 24 Mins. 5. FROM: TO: Hrs. Mins. TOTAL VOLUME: Intermittent Black Yes No Smoke? Planned? ® ^ ^ ^ ® ^ ^ ^ ® ^ ^ ^ ® ^ ^ ^ ^ ^ ^ ^ 1,344 MscF VOLUME 486 MSCF 192 MSCF 333 MscF 333 MscF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 2. High gas transit line pressure caused by ARCO increasing rates. 3. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 4. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 3°F. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 2 wells equaling 40 mmscfd. ARCO reduced production rates and shut-in 4 wells equaling 50 mmscfd. Wells were shut-in or choked back starting at 00:38 hours. 2. BPX reduced production rates by choking back 3 wells equaling 40 mmscfd. ARCO reduced production rates and shut-in 1 cycle well equaling 58 mmscfd. Wells were shut-in or choked back starting at 12:20 hours. 3. BPX reduced production rates and shut-in 3 wells equaling 45 mmscfd. ARCO reduced production rates and shut-in 3 wells equaling 45 mmscfd. Wells were shut-in or choked back starting at 19:48 hours. 4. BPX reduced production rates and shut-in 4 wells equaling 50 mmscfd. ARCO reduced production rates and shut-in 4 wells equaling 70 mmscfd. Wells were shut-in or choked back starting at 22:44 hours. 5. Rev 6/22/97 REPORT NO: 9$-4619 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 28 Nov 98 TOTAL VOLUME: 1 ,423 MSCF Intermittent Black TIM E OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME i . FROM: 01:13 TO: 02:06 0 Hrs. 53 Mins. ® ^ ^ ^ 306 MSCF 2. FROM: 02:26 TO: 03:56 1 Hrs. 30 Mins. ® ^ ^ ^ 444 MSCF 3. FROM: 11:27 TO: 11:57 0 Hrs. 30 Mins. ® ^ ^ ^ 58S MSCF 4. FROM: 21 :44 TO: 21:57 0 Hrs. 13 Mins. ^ ® ^ ^ 90 MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER: First Determination of Cause: 1. Transit gas rates more than system can handle. for current ambient air temperature (4*F) 2. Transit gas rates more than system can handle for current ambient air temperature (4"F) 3. High gas transit line pressure caused by CGF due to booster compressor problems. 4. Extended flaring event occurred while awaiting GC operator/maintenance evaluation (troubleshooting "D" Bank Frist Stage). 5. Action Taken to Stop Flaring: 1. Arco reduced production rates and shut-in 3 wells equaling 70 mmscfd. Wells were shut-in or choked back starting at 01:20 hours. 2. BPX reduced production rates and shut-in 1 wells equaling 28 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 37 mmscfd. Wells were shut-in or choked back starting at 01:28 hours. 3. No response taken as this was deemed to be of short duration. 4. BPX switched wells back to Annex. 5. Rev 6/22/97 REPORT NO: 98-4620 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 29 Nov 98 TOTAL VOLUME: 1 ~QQ& MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: QQ:Q3 TO: 02:13 2 Hrs. 1 Q Mins. ® ^ ^ ^ 5$3 MSCF 2. FROM: 19:23 TO: 19:56 Q Hrs. 33 Mins. ^ ® ^ ^ 229 MSCF 3. FROM: 21:23 TO: 21:51 0 Hrs. 28 Mins. ^ ® ^ ^ 194 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 3°F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 3. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 4. 5. Action Taken to Stop Flaring: 1. Arco reduced production rates and shut-in 4 wells equaling 70 mmscfd. Wells were shut-in or choked back starting at 01:00 hours. 2. BPX reduced production rates and shut-in 2 wells equaling 30 mmscfd. Wells were shut-in or choked back starting at 19:25 hours. 3. BPX reduced production rates and shut-in 1 wells equaling 13 mmscfd. Wells were shut-in or choked back starting at 21:30 hours. 4. 5. Rev 6/22/97 SENT BY~BPX~SFETY N/5 ;10- 2-98 13 54 ; 9076594467 ~-~ BP EXPLORATION (ALASKA) INC. P.O. Box 196612, Anchorage AK 99519-6612 REPORT 4F ACGtt3ENTAl , NATt IRA1 rAS RELEASE 907 276 7542;# 1/ 1 DATE: (Zev~stur- toy ~19~r TO: Mr. Blair Wondzell Alaska oil and Gas Conservation Commission 3005 Porcupine Drive Anchorage, AK 99501 FAX: 276-7542 DEaSCftIPTION OF II~,CIDENT 1. Date and Time: cf/ ~ '~ f 9~ ~S~d0 lta~~S 2. Location: Detailed Location: ~~ Prudhoa Bay .Unit ~Q ~ ' ~ -- Pq~ ~ Cj CCe S S rT0 ~,~ . ,_ Fnrijr_ott '_ -,,. Milne Point .:' - ~ Nl~kuk ~ ~~`5S.``^~ o~ . iD _1 "~~~ ~(GS ;;~.~:~.'~ . V _ Ofhcr . 1 M - ~~~ ~t l v~ ~ s-o wt -~,~•: , 0. Vuluniv uu( „alural gas lose: ~~v,'St,,c~. ~ 4. Cause of loss: '6 /yJse•f p RV~-i-v~ ~Ca 1U - 1~~.1.~ GS ,,~'t' l~a~. -. 5. Actions taken and planned to prevent further loss: ~ \'~ ~~ ~{ S 1'~~ d< <~~` `~ I ;~ o ~ ~, ~-~•~(; e~~.r•e n 41y P _1 ~.. [1•Cl.. P~r~~{~r hv~y ,\v~,l, '~ Co~1~t.~ct` 1"I~a~Pc.~1~~_ ~" 6. Equipment or procedural chanyestopreventloss - ~ L``14- 1`~v~``~a `~"`~` w~11 ~ ~-~s~c}ca( from recurring: t'n c~,~ c..r Yv,,,r~., C tiu S ~ . 7. Contact (name and teiQphone number): ~` - ~ m - R e ~Y1`~ hi e ~ j a (~-idl ~~ S ~ i vs ~S ~~v~,ror,n.~~~-• t ~v, sow- ~ a~`~ ~ ~(~'~`~ Signature: ~~ i~~~~ ~ ~~ cc: BPX f~nvironmental Complianco ~~~ . 6PX Volume Accounting Mp 5-4 .,. \ t ~~ r3 FORM fiEV 5/95 ,...,fir.,` ,~;~~. ~?tr~A1~~~'t~~.~, ~'~ BtF+E. .6 ~~ ~ ~ , ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) IMonth/Year of Disposition GATHERING CENTER 3 BP EXPLORATION ALASKA WESTERN OPERATING AREA-PBU Oct-98 Disposition *Indicate contribution of each pool to total. 1. Sold 0 Pool Name Code Percent 2. Reinjected 0 PRUDHOE 640150 100 3. Flared or vented less than 1 hour 10,198 4. Flared or vented greater than 1 hour 10,497 (Supplemental report required--See 20 AAC 25.235) 5. Pilot and Purge 10,772 6. Used for lease operations 555,822 Oflicia] Use Only--Flaring Authorization > 1 hr. 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner llate 11. Transferred to: CCP -2~5 17~,7~2;';: 7. Other 0 TOTAL items 1 - 7 587,289 8. NGL gas equivalent produced 0 9. Purchased gas 0 10. Transferred from: 0 __ must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. Form 10-422 (Revised 4 5) Remarks: Phereby certify that the f regoing is true and correct to the best of my knowledge. Signature: p ~ Title: SUPERVISOR '~ 9810 FORM 10-422.x1slFORM 10-422 BP EXPLORATION (ALASKA) INC. ~, PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT OCTOBER, 1998 Unplanned Events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN'TO ELIMINATE CAUSE `' 10/7/98 1200-1230 174 Not required for unplanned events which Not required for unplanned events whit 10/8/98 0801-0840 313 are less than or equal to 1 hour are less than or equal to 1 hour 10/8/98 1257-1327 321 10/8/98 1818-1829 191 10/9/98 0906-0950 1, 681 10/10/98 0223-0304 510 10/11/98 0313-0348 200 10/11/98 1748-1840 350 10/11 /98 2322-2349 1,875 10/13/98 0341-0411 250 10/13/98 0834-0856 275 10/14/98 1607-1629 153 10/15/98 1535-1623 500 10/23/98 1239-1255 444 10/24/98 0011-0051 833 10/24/98 0628-0726 486 10/24/98 1247-1309 382 10/24/98 1542-1620 375 10/25/98 0548-0610 97 10/26/98 2039-2059 250 10/27/98 0416-0447 538 TOTAL 10,198 Un tanned Events reater than 1 hour • DATE TIME VOLUME " DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO'ELIMINATE :CAUSE 10/4/98 2019-2345 938 See Attachments See Attachments 10/7/98 1349-1455 573 See Attachments See Attachments 10/9/98 1850-2006 1,585 See Attachments See Attachments 10/10/98 1 i02-1212 229 See Attachments See Attachments 10/15/98 0046-0338 625 See Attachments See Attachments 10/15/98 0510-0643 408 See Attachments See Attachments 10/19/98 0349-0533 317 See Attachments See Attachments 10/23/98 1044-1210 608 See Attachments See Attachments 10/24/98 2004-2124 1,111 See Attachments See Attachments 10!26/98 0908-1900 2,249 See Attachments See Attachments 10/28/98 1432-2400 1,181 See Attachments See Attachments 10/29/98 0000-523 673 See Attachments See Attachments TOTAL 10,497 Page 1 Planned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mcf I DATE TIME 'VOLUME' "....DESCRIPTION OF INCIDENT & CAUSE: ACTION TAKEN TO ELIMINATE CAUSE < ~ , BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT OCTOBER, 1998 TOTAL 0 Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf DATE TIME VOLUME " DESCRIPTION OF"WCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE TOTAL 0 Unplanned Events < 1 Hour Unplanned Events > 1 Hour Planned Events < 1 hour & not exceeding 5,000 MCF Planned Events > 1 hour and exceeding 5,000 MCF Pilot Purge TOTAL FLARED VOLUME TOTAL 10,198 10,497 0 0 i 0.772 31,467 Page 2 C_~ . REPORT NO: 98-4529 `- ,, ~ BPX FLARE REPORT ~ . PRUDHOE BAY ~ -- FACILITY: GC-3 DATE: O4 OCt 98 TOTAL VOLUME: 98$ MSCF Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 20:19 TO: 23:45 3 Hrs. 26 Mins. ® ^ ^ ^ 938 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. While bringing GC-2 production rates up following K7000 LPS compressors being put on line. High transit gas line pressures. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. The rate increase was stopped while both BPX and ARCO cut back on higher GOR wells to make room for the lower GOR wells that needed to be brought up to normal rates. 2. 3. 4. 5. Rev 6/22/97 • ~ REPORT NO: 9H-4533 _ BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: O7 OCt 98 TOTAL VOLUME: 747 MSCF Intermi ttent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 12:00 TO: 12:30 O Hrs. 30 Mins. ® ^ ^ ^ 174 MSCF 2. FROM: 13:49 To: 14:55 1 Hrs. 6 Mins. ® ^ ^ ^ 573 MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 4°F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 3°F. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 1 wells equaling 65mmscfd. ARCO reduced production rates and shut-in 7wells equaling 175 mmscfd. Wells were shut-in or choked back starting at 12:00 hours. 2. BPX reduced production rates and shut-in 1 wells equaling 34 mmscfd. ARCO reduced production rates and shut-in 4 wells equaling 125 mmscfd. Wells were shut-in or choked back starting at 13:50 hours. 3. 4. 5. Rev 6/22/97 • ~ REPORT NO: 9$-4536 _ _ BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-$ DATE: 09 Oct 98 TIME OF FLARING: 1. FROM: 09:06 To: 09:50 2. FROM: 18:50 TO: 20:06 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 0 Hrs. 44 Mins. 1 Hrs. 16 Mins. Hrs.. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ® ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 3,266 MscF VOLUME 1,681 MSCF 1,585 MscF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High gas transit line pressure caused by CGF compressor problems due toair leak repair on booster. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 4°F. 3. 4. 5. Action Taken to Stop Flaring: 1. Equipment was restarted at 0945 hours. 2. BPX reduced production rates and shut-in 3 wells equaling 105 mmscfd. ARCO reduced production rates and shut-in 4 wells equaling 60 mmscfd. Wells were shut-in or choked back starting at 18:45 hours. 3. 4. 5. Rev 6/22/97 REPORT NO: 9$-450 BPX FLARE REPORT PRUDHOE BAY FACILITY: CiC-3 DATE: 10 OCt 98 TIME OF FLARING: 1. FROM: 02:23 To: 03:04 2. FROM: 11:02 TO: 12:12 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 0 Hrs. 41 Mins. 1 Hrs. 1 O Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ® ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 7S9 MSCF VOLUME 51 O MSCF 229 MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High gas transit line pressure caused by CGF 1851 refrigeration unit problems due to SDV logic. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 10°F. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates equaling 90 mmscfd. ARCO reduced production rates equaling 90 mmscfd. Wells were shut-in or choked back starting at 02:15 hours. 2. BPX reduced production rates and shut-in 2 wells equaling 111 mmscfd. ARCO reduced production rates and shut-in 4 wells equaling 125mmscfd. Wells were shut-in or choked back starting at 11:02 hours. 3. 4. 5. Rev 6/22/97 C~ BPX FLARE REPORT PRUDHOE BAY t REPORT NO: 9$-4551 _ FACILITY: GC-3 DATE: 15 OCt 98 TOTAL VOLUME: 1,533 MSCF Intermi ttent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 00:46 TO: 03:38 2 Hrs. 52 Mins. ® ^ ^ ^ 625 MSCF 2. FROM: 05:10 TO: 06:43 1 Hrs. 33 Mins. ® ^ ^ ^ 408 MSCF 3. FROM: 15:35 TO: 16:23 0 Hrs. 48 Mins. ^ ® ^ ^ 500 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER: First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 6°F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 6°F. 3. High gas transit line pressure caused by FS#1 compressor #1804 startup. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 1 wells equaling 40 mmscfd. ARCO reduced production rates and shut-in 4 wells equaling 188 mmscfd. Wells were shut-in or choked back starting at 01:15 hours. 2. BPX reduced production rates and shut-in 3 wells equaling 73 mmscfd. 3. BPX reduced production rates and shut-in 6 wells equaling 107 mmscfd. ARCO reduced production rates and shut-in 9 wells equaling 250 mmscfd. Wells were shut-in or choked back starting at 15:27 hours. 4. 5. Rev 6/22/97 REPORT NO: 98_t~rj~j2e _ BPX FLARE REPORT .. ' PRUDHOE BAY - FACILITY: GC-3 DATE: 19 OCt 9H TOTAL VOLUME: 317 MSCF Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME t . FROM: 03:49 To: 05:33 1 Hrs. 44 Mins. ® ^ ^ ^ 317 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ i OTHER:_ First Determination of Cause: 1. High Gas Transit Line pressure due to bringing production rates up following C Slugcatcher & HP Separator S/D, 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Arco reduced production rates and shut-in 3 wells equaling 95 mmscfd. Wells were shut-in or choked back starting at 04:00 hours. 2. 3. 4. 5. Rev 6/22/97 BPX FLARE REPORT PRUDHOE BAY . REPORT NO: 9$-4555 .. FACILITY: GC-3 DATE: 23 OCt 98 TOTAL VOLUME: 1 X052 MSCF Intermi ttent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 10:44 To: 12:10 1 Hrs. 26 Mins. ® ^ ^ ^ 608 MSCF 2. FROM: 12:39 TO: 12:55 0 Hrs. 16 Mins. ^ ® ^ ^ 444 MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK: CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 25°F. 2. K3200 & K3300 GLT compressors tripped to idle at 1239 hrs. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 6 wells equaling 100 mmscfd. ARCO reduced production rates and shut-in 10 wells equaling 240 mmscfd. Wells were shut-in or choked back starting at 1158 hours. 2. BPX reduced production rates and shut-in 14 wells equaling 300 mmscfd. Wells were shut-in or choked back starting at 1240 hours. Also K3200 & K3300 were reloaded at 1250 hrs. 3. 4. 5. Rev 6/22/97 • ~ REPORT NO: 9$-4557 _ ' - B PX FLARE REPORT , _ ' PRUDHOE BAY FACILITY: GC-3 DATE: 24 OCt JH TOTAL VOLUME: 3,187 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 00:1 1 TO: 00:51 0 Hrs. 40 Mins. ^ ® ^ ^ 833 MSCF 2. FROM: 06:28 TO: 07:26 0 Hrs. 58 Mins. ® ^ ^ ^ 486 MSCF 3. FROM: 12:47 TO: 13:09 0 Hrs. 22 Mins. ^ ® ^ ^ 382 MSCF 4. FROM: 15:42 TO: 16:20 0 Hrs. 38 Mins. ® ^ ^ ^ 375 MSCF 5. FROM: 20:04 TO: 21:24 1 Hrs. 20 Mins. ^ ® ^ ^ 1,111 MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. GLT compressor K-3300 shut down due for maint. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 1°F. 3. High gas transit line pressure caused by CCP compressor 1878 S/D problems. 4. High gas transit line pressure caused by CCP compressor 1878 S/D problems. 5. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 5°F. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 6 wells equaling 100 mmscfd. ARCO reduced production rates and shut-in 4 wells equaling 85 mmscfd. Wells were shut-in or choked back starting at 00:11 hours. 2. BPX reduced production rates and shut-in 16 wells equaling 120 mmscfd. ARCO reduced production rates and shut-in 6 wells equaling 50 mmscfd. Wells were shut-in or choked back starting at 0630 hours. 3. BPX reduced production rates equaling 100 mmscfd. Wells were choked back starting at 12:48 hours. CCP restarted 1878 compressor. 4. BPX reduced production rates equaling 100 mmscfd. Wells were choked back starting at 15:45 hours. CCP restarted 1878 compressor. 5. BPX reduced production rates and shut-in 7 wells equaling 120 mmscfd. ARCO reduced production rates and shut-in 6 wells equaling 140 mmscfd. Wells were shut-in or choked back starting at 20:05 hours. Rev 6/22/97 • ~ REPORT NO: 9$-4562 _ . BPX FLARE REPORT ~ _ ' PRUDHOE BAY ~ - - FACILITY: GC-$ DATE: 26 Oct 98 TOTAL VOLUME: 2499 MSCF Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 09;0$ TO: 19:00 9 Hrs. 52 Mins. ^ ® ^ ^ 2,249 MSCF 2. FROM: 20:39 To: 20:59 O Hrs. 20 Mins. ^ ® ^ ^ 250 MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. K5500 Wet Gas Compressor shut down because of a problem associated with low sucti on pressure. 2. High Transit Pressure due to unloading wells. 3. 4. 5. Action Taken to Stop Flaring: 1. Flaring was permitted to continue while GC operations personnel attempted to restart the equipment. 2. Cut well rates on higer GOR wells 3. 4. 5. Rev 6/22/97 • ~ REPORT NO: 98-4568 B PX FLARE REPORT ' PRUDHOE BAY - FACILITY: GC-$ DATE: 28 OCt 9$ TOTAL VOLUME: 1 X181 MSCF Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 14:32 TO: 24:00 9 Hrs. 28 Mins. ^ ® ^ ^ 1,181 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN: OTHER:_ First Determination of Cause: _ 1. K-5500 Wet Gas Compressor S/D while Tech 's were hooking up wires to the suction valve. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Equipment was restarted at 05:18 hours (Thu 29 Oct 98). 2. 3. 4. 5. Nev 6/22/97 . ~ REPORT NO: 9$-4569 ,, ~ B PX FLARE REPORT ,. ' PRUDHOE BAY FACILITY: GC-$ DATE: 29 Oct 98 TOTAL VOLUME: 673 MSCF Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 00:00 TO: 05:23 5 Hrs. 23 Mins. ^ ® ^ ^ 673 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK: CONTROLLED BLOWDOWN:_ O7HER:_ First Determination of Cause: 1. K-5500 Wet Gas Compressor S/D while Tech 's were hooking up wires to the suction valve. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Equipment was restarted at 05:18 hours. 2. 3. 4. 5. Rev 6/22/97 Flare report information ~ ~ M Subject: Flare report information Date: Fri, 8 Jan 1999 19:15:47 -0500 From: "PBU, NS Optimization Engineer" <PBLTNSOptimizationEngineer@bp.com> To: "'wendy mahan"' <wendy_mahan@admin.state.ak.us> CC: "PBU, Prod Opt TL" <PBUProdOptTL@BP.com> Wendy, Per our phone discussion I have received the following information from GC3 regarding the 10/26 and 10/28-29 GC3 flaring events. A key point is highlighted in bold print in the explanation for the 10/26 event. I am sure that we will become much more proficient at troubleshooting and restarting K5500 as operations gains experience with this piece of equipment. Along with that proficiency will come improved estimates for restart timing, thus improving our ability to make the judgment call that a restart is imminent or that additional steps (a full plant shut down is required to completely stop flaring) must be taken to reduce or stop flaring. If you require additional information, please do not hesitate to contact me via email or at 659-4382. Also please respond to this email so that I can be sure it made its way through the BP network to your desk top. Thank you, Hal Tucker 10/26 Reason for flaring: K-5500, wet gas compressor, shutdown. GC3 had several start attempts during the troubleshooting exercise. GC3 ultimately had to abandon a pair of wires and switch to a spare pair running to the position limit switch on the suction SDV. The two things causing the delay in this instance were a wire or pair of wires that generally don't just fail and the compressor is new to GC3 and the operators have little history regarding its operation yet. GC3 also replaced a PLC output card. During this time GC3 felt that they were on the verge of getting it restarted. 10/28-29 Reason for flaring: K-5500, wet gas compressor, shutdown. K-5500 had been S/D due to electrical work on the suction valve. Start-up was attempted but was held out due to an oil injection pressure transmitter fault (PAXX-5220). Controls techs ensured that the transmitter was calibrated and working correctly. After an attempt was made to start the machine with the Aux. lube oil pump in the hand position, a low level in the lube oil vessel (VSP-5500) was encountered. Lube oil was added and the vessel repressured clearing the transmitter fault. Subsequent restart attempts were unsuccessful as the compressor shut down immediately due to low suction pressure. After the suction pressure was increased twice, it was determined that the compressor was trying to load up too quickly causing a shut down due to low 1 of 2 1/11/99 8:13 AM Flare report information suction pressure. Restart was then attempted with the capacity control in local control instead of PLC control. By preventing the machine from loading beyond 10% capacity the machine remained on through the warm up period. After a successful warm up (suction and discharge valves both open) the compressor was slowly loaded. At approximately 96% capacity the capacity control was switched from local to PLC and returned to normal operation. 2 of 2 1/11/99 8:13 AM ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition GATHERING CENTER 3 BP EXPLORATION ALASKA WESTERN OPERATING AREA-PBU Sep-98 • • Disposition 1. Sold ~ 0 J ~ 2. Reinjected ~ ~ ~' ~ ~"~ ~`~ a ~ 0 3. Flared or vented less than 1 hour - ~ ,, 11,432 4. Flared or vented greater than 1 hour ,~{ ~~f2rr~; ; (Supplemental report required--See 20 AAC 25.235) 8,313 5. Pilot and Purge 14,942 6. Used for lease operations 359,356 7. Other 0 TOTAL items 1 - 7 394,043 8. NGL gas equivalent produced 0 9. Purchased gas 0 10, Transferred from: 0 11. Transferred to: CCP 14,936,016 Remarks: I hereby certify that the fore oing is true and correct to the best of my knowledge. a Signature: J~~~ ~g~ Title: SUPERVISOR Form 10-422 (Revised 4/95) *Indicate contribution of each pool to total. Pool Name Code Percent PRUDHOE 640150 100 U17fciul U,e Only--Fla>7n~~ Authorization > 1 hr. 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner Date must pressure of 14.65 Asia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. 9809 FORM 10-422.x1s/FORM 10-422 u BP EXPLORATION (ALASKA) INC. • PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT SEPTEMBER, 1998 Unplanned Events less than or equal to 1 hour ~ DATE TIME VOLUME DESCRIPTION OF INCIDENT &'CAUSE' ACTION TAKEN TO ELIMINATE CAUSE 9/8/98 2334-2351 5,313 Not required for unplanned events which Not required for unplanned events whit 9/12/98 1805-1840 535 are less than or equal to 1 hour are less than or equal to 1 hour 9/14/98 1119-1208 490 9/15/98 0927-1018 425 9/15/98 1042-1134 365 9/16/98 1215-1243 544 9/17/98 0219-0238 198 9/17/98 0910-0941 167 9/17/98 1401-1457 856 9/17/98 1928-2011 926 9/19/98 0656-0751 281 9/19/98 2253-2342 406 9/20/98 0346-0436 700 9/22/98 1637-1656 226 TOTAL 11,432 Unplanned Events greater than 1 hour ~ DATE `TIME VOLUME DESCRIPTION OF LNCIDENT &' CAUSE ACTION: TAKEN TO ELIMINATE :CAUSE `- 9/7/98 2127-2359 1,792 See Attachments See Attachments 9/8/98 1110-1225 2,604 See Attachments See Attachments 9/11/98 0803-1030 375 See Attachments See Attachments 9/16/98 1049-1206 313 See Attachments See Attachments 9/16/98 1619-1749 2,563 See Attachments See Attachments 9/17/98 0557-0710 333 See Attachments See Attachments 9/18/98 1315-1420 333 See Attachments See Attachments TOTAL 8,313 Planned Events Less Than or Equal 1 Hour AND Not Exceeding 5000 Mcf DATE TIME VOLUME ` DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN 70 ELIMINATE CAUSE TOTAL Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf ~~_ DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE TOTAL 0 Page 1 TOTAL Unplanned Events < 1 Hour 11,432 Unplanned Events > 1 Hour 8,313 Planned Events < 1 hour & not 0 exceeding 5,000 MCF Planned Events > 1 hour and 0 exceeding 5,000 MCF Pilot Purge 14,942 . TOTAL FLARED VOLUME 34,687 BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GCS GAS FLARING INCIDENT REPORT SEPTEMBER, 1998 Page 2 C~ • • REPORT NO: 9$-4490 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 07 Sep 98 TOTAL VOLUME: 1,792 MSCF Intermi ttent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 21:27 TO: 23:59 2 Hrs. 32 Mins. ® ^ ^ ^ 1,792 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: _ RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. While bringing production rates up following GC-3 FSO turn around,LPS compressors exceeded maximum gas capacity and discharged to flare. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX stopped bringing production rates up until wells unloaded and flaring was ceased. 2. 3. 4. 5. ae~ sr~vs~ • ~ REPORT NO: 9$-4492 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 TIME OF FLARING: DATE: 08 Sep 98 1. FROM: 11:10 To: 12:25 2. FROM: 23:34 To: 23:51 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 1 Hrs. 15 Mins. 0 Hrs. 17 Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 7917 MSCF VOLUME 2,604 MscF 5,313 MscF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. While bringing production rates up following GC-3 start-up (partial separation), LPS compressors exceeded maximum gas capacity and discharged to flare. 2. Extended flaring event occurred while awaiting GC operator/maintenance evaluation of level indication on A-HP vessel. Stop production resulted 3. 4. 5. Action Taken to Stop Flaring: 1. Equipment was restarted at 11:27 hours (LPS K-7000) . 2. BPX stopped bringing production rates up. Stop production initiated and flaring stopped. 3. 4. 5. Rev 6/22/97 • REPORT NO: BPX FLARE REPORT PRUDHOE BAY 98-4496 FACILITY: GC-3 DATE: 1 1 Sep 9$ TOTAL VOLUME: 375 MSCF Intermittent Black TIME OF FLARING: DURATION:. Yes No Smoke? Planned? VOLUME 1. FROM: 08:03 TO: 10:30 2 Hrs. 27 Mins. ^ ® ^ ^ 375 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: _ RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. K5500 Wet Gas Compressor shutdown because of a problem with the tube oil system. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Equipment was restarted at 10:30 hours. 2. 3. 4. 5. Rev 6/22/97 BPX FLARE REPORT PRUDHOE BAY • REPORT NO: 98-4505 FACILITY: GC-3 DATE: 16 Sep 98 TOTAL VOLUME: 34.20 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 10:49 TO: 12:06 1 Hrs. 17 Mins. ® ^ ^ ^ 313 MSCF 2. FROM: 12:15 TO: 12:43 0 Hrs. 28 Mins. ^ ® ^ ^ 544 MSCF 3. FROM: 16:19 TO: 17:49 1 Hrs. 30 Wins. ^ ® ^ ^ 2,563 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 4°F. 2. K-5500 Wet Gas Compressor S/D due to a suction pressure transmitter malfuction. 3. High gas transit line pressure caused by CGF compressor problems due to governor malfuntion. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 3 wells equaling 60 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 55 mmscfd. Wells were shut-in or choked back starting at 11:00 hours. 2. Equipment was restarted at 12:43 hours. Flare assist gas was used to prevent black smoke. 3. Equipment was restarted at 17:45 hours. 4. 5. Rev 6/22/97 BPX FLARE REPORT PRUDHOE BAY • REPORT NO: 9$-4506. FACILITY: GC-3 DATE: 17 Sep 98 TOTAL VOLUME: 2480 MSCF Intermi ttent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 02:19 To: 02:38 0 Hrs. 19 Mins. ^ ® ^ ^ 198 MSCF 2. FROM: 05:57 TO: 07:10 1 Hrs. 13 Mins. ® ^ ^ ^ 333 MSCF 3. FROM: 09:10 TO: 09:41 0 Hrs. 31 Mins. ® ^ ^ ^ 167 MSCF 4. FROM: 14:01 TO: 14:57 0 Hrs. 56 Mins. ^ ® ^ ^ 856 MSCF 5. FROM: 19:28 TO: 20:11 O Hrs. 43 Mins. ^ ® ^ ^ 926 MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. While bringing production rates up following annex reboiler s/d the gas transit line recieved a high pressure. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 3. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 4. k-5500 Wet Gas Compressor S/D due to high D/P on the tube oil filter. 5. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 4°F. Action Taken to Stop Flaring: 1. Arco reduced production rates and shut-in 4 wells equaling 84 mmscfd. Wells were shut-in or choked back starting at 02:02 hours. 2. BPX reduced production rates and shut-in 2 wells equaling 50 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 55 mmscfd. Wells were shut-in or choked back starting at 06:12 hours. 3. BPX reduced production rates and shut-in 1 wells equaling 35 mmscfd. ARCO reduced production rates and shut-in 1 wells equaling 80 mmscfd. Wells were shut-in or choked back starting at 09:05 hours. 4. Equipment was restarted at 14:57 hours after changing the tube oil filters. (assit gas was turned on to prevent black smoke) 5. BPX reduced production rates and shut-in 11 wells equaling 265 mmscfd. ARCO reduced production rates and shut-in 7 wells equaling 50 mmscfd. Wells were shut-in or choked back starting at 1940 hours. Rev 6/22/97 • • REPORT NO: BPX FLARE REPORT PRUDHOE BAY a 98-4510 FACILITY: GC-3 DATE: 18 Sep 98 TOTAL VOLUME: 333 MSCF Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 13:15 TO: 14:20 1 Hrs. 5 Mins. ® ^ ^ ^ 333 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLEb BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Am bient temperatu re increased by 14°F, also CGF took one of their refrigeration units off line for survey. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 10 wells equaling 310 mmscfd. ARCO reduced production rates and shut-in 12 wells equaling 600 mmscfd. Wells were shut-in or choked back starting at 12:40 hours. 2. 3. 4. 5. Rev 6/22/97 ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition GATHERINGCENTER 3 BP EXPLORATION ALASKA WESTERN OPERATING AREA-PBU Aug-98 Disposition *Indicate contribution of each pool to total. 1. Sold 0 Pool Name Code Percent 2. Reinjected 0 PRUDHOE 540150 100 r _ __ ._ _ _ .. __. _._ 3. Flared or vented less than 1 hour 2,835 4. Flared or vented greater than 1 hour 641 (Suoulemental report reauved--See 20 AAC 25.235) 5. Pilot and Purge 21,914 6. Used for lease operations 471,833 7.Other 0 TOTAL items 1 - 7 497,223 8. NGL gas equivalent produced 0 9. Purchased gas 0 10. Transferred from: 0 11. Transferred to: CCP 19,089,570 I hereby certify that the fo ping is true and correct to the best of my knowledge. Signature: ~~~~'~~ ~ 10 ~L'Title: SUPERVISOR ~/ ll -~---_.--_ Form 10-422 (Revised 4/95) Official Use OnL --Flarin Authorization > I hr. 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner llate Note: All volumes must be corr~ted to pressure of 14.65 psis and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. 9808 FORM 10-422.bsJFORM 10-422 BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GC-3 ` GAS FLARING INCIDENT REPORT AUGUST, 1998 Unplanned Events less than or equal to 1 hour ~ DATE TIME VOLUME DESCRIPTION''OFlNCIDENT & CAUSE ACTION'TAKEN TO ELIMINATE CAUSE 8/1/98 1126-1157 325 Not required for unplanned events which Not required for unplanned events whit 8/2/98 0527-0540 90 are less than or equal to 1 hour are less than or equal to 1 hour 8/2/98 0952-1008 110 8/2/98 1254-1304 70 8/4/98 1728-1738 76 8/7/98 1237-1251 136 8/8/98 1437-1521 733 8/8/98 2253-2312 132 8/9/98 1029-1059 146 8/9/98 2130-2149 132 8/11 /98 0558-0606 56 8/11/98 1922-1929 49 8/13/98 1202-1228 90 8/14/98 1207-1229 657 8/19/98 1803-1809 33 TOTAL 2,835 Un tanned Events reater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 8/5/98 1037-1148 641 See Attachments See Attachments TOTAL 641 Planned Events Less Than or E ual 1 Hour AND Not Exceedin 5000 Mcf DATE' TIME VOLUINE' DESCRIPTION OF'INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE' • TOTAL 0 Planned Events Exceeding 1 Hour OR E; TOTAL Unplanned Events < 1 Hour Unplanned Events > 1 Hour Planned Events < 1 hour & not exceeding 5,000 MCF Planned Events > 1 hour and exceeding 5,000 MCF Pilot Purge TOTAL FLARED VOLUME VOLUME DESCRIPTION OF INCIDENT & CAUSE u TOTAL 2,835 641 0 0 14 25,390 ACTION TAKEN TO ELIMINATE CAUSE Page 1 BPX FLARE REPORT PRUDHOE BAY REPORT NO: 98-4449 FACILITY: GC-3 DATE: 05 Aug 98 TIME OF FLARING: 1. FROM: 1 x:37 To: 11:48 2. FROM: TO: 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 1 Hrs. 11 Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ® ^ ^ ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 641 MSCF VOLUME 641 MSCF MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK: _ CONTROLLED BLOWDOWN: _ OTHER: _ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 5°F. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 1 wells equaling 30 mmscfd. ARCO reduced production rates and shut-in 3 wells equaling 80 mmscfd. Wells were shut-in or choked back starting at 1042 hours. 2. 3. 4. 5. Rev 6/22/97 .. • • ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION (Facility GATHERING CENTER 3 IBP EXPLORATION ALASKA IFVVES (TERN OPERATING AREA-PBUMonth/Year of Dispoi i9ti8on Disposition 1. Sold 0 2. Reinjected 0 3. Flared or vented less than 1 hour 14,183 4. Flared or vented greater than 1 hour (Supplemental report requued-See 20 AAC 25.235) 2,334 5. Pilot and Purge 21,821 6. Used for lease operations 498,178 7.Other 0 TOTAL items 1 - 7 536,516 8. NGL gas equivalent produced 0 9. Purchased gas 0 10. Transferred from: 0 11. Transferred to: CCP 21,112,069 Remarks: I hereby certify that the f ,regoing is true and correct to the best of my knowledge. / F 7 I ~ Title: SUPERVISOR Signature: ,-~~--~~" ~..4 ~, f~ ~r' ~~, j t? ~.. ~~ Form 10.422 (Revised 4/95) *Indicate contribution of each pool to total. Pool Name I Code PRUDHOE I 640150 Percent 100 Official Use Onl --Flarin .Authorization >„ 1 hr. 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner Date Note: All volumes must be corrected to pressure of 14.65 psis and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GC-3 ~ GAS FLARING INCIDENT REPORT JULY, 1998 Unplanned Events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN!TO ELIMINATE CAUSE 7/1/98 2328-2353 175 Not required for unplanned events which Not required for unplanned events whit 7/3/98 0955-1042 416 are less than or equal to 1 hour are less than or equal to 1 hour 7/3/98 1122-1134 42 7/3/98 1330-1356 186 7/4/98 0745-0759 49 7/4/98 1117-1215 604 7/4/98 2136-2211 490 7/5/98 0707-0717 42 • 7/5/98 1011-1017 79 7/6/98 1155-1210 104 7/6/98 1450-1459 63 7/6/98 1838-1914 375 7/6/98 2108-2127 200 7/7/98 0000-0043 300 7/7/98 0336-0433 285 7/7/98 0959-1022 133 7/7/98 1616-1625 31 7/8/98 0026-0053 375 7/8/98 1250-1304 165 7/11/98 0955-1009 797 7/18/98 0617-0640 192 7/23/98 1318-1349 162 7/25/98 1354-1402 56 7/25/98 2003-2056 663 • 7/26/98 7/26/98 0922-0931 0932-1031 94 1,586 7/27/98 1219-1247 1,731 7/27/98 1408-1428 583 7/27/98 1512-1528 45 7/28/98 1124-1147 52 7/28/98 1330-1348 1,009 7/28/98 2252-2342 438 7/29/98 1300-1334 422 7/30/98 0842-0855 78 7/30/98 1457-1521 1,328 7/30/98 2211-2231 833 TOTAL 14,183 Page 1 BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT JULY, 1998 Unplanned Events rester than 1 hour DATE ' 'TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 7/3/98 2136-2237 1,060 See Attachments See Attachments 7/26/98 1255-1411 581 See Attachments See Attachments 7/29/98 0810-0915 693 See Attachments See Attachments TOTAL 2,334 Planned Events Less Than or E ual 1 Hour AND Not Exceedin 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE -°ACTION TAKEN TO ELIMINATE CAUSE TOTAL 0 Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf ~ ~~. .~ DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE TOTAL 0 TOTAL Unplanned Events < 1 Hour 14,183 Unplanned Events > 1 Hour 2,334 Planned Events < 1 hour & not 0 exceeding 5,000 MCF Planned Events > 1 hour and 0 exceeding 5,000 MCF Pilot Purge 1 21 • TOTAL FLARED VOLUME 38,338 Page 2 • • REPORT NO: J$-4385 , B PX FLARE REPORT ' PRUDHOE BAY FACILITY: GC-3 DATE: 03 Ju198 TOTAL VOLUME: 1,704 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 09:55 TO: 10:42 0 Hrs. 47 Mins. ^ ® ^ ^ 416 MSCF 2. FROM: 1 1 :22 TO: 11:34 0 Hrs. 12 Mins. ^ ® ^ ^ 42 MSCF 3. FROM: 13:30 TO: 13:56 0 Hrs. 26 Mins. ^ ® ^ ^ 186 MSCF 4. FROM: 21:36 TO: 22:37 1 Hrs. 1 Mins. ^ ® ^ ^ 1,060 MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 4°F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 3. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 6°F. 4. While bringing production rates up following ARCO compressor maintenance, transit line pressure increased causing HP to discharged to flare. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 2 wells equaling 55 mmscfd. ARCO reduced production rates and shut-in 1 wells equaling 90 mmscfd. Wells were shut-in or choked back starting at 1030 hours. 2. Arco reduced production rates and shut-in 1 wells equaling 30 mmscfd. Wells were shut-in or choked back starting at 1122 hours. 3. BPX reduced production rates and shut-in 2 wells equaling 40 mmscfd. ARCO reduced production rates and shut-in 4 wells equaling 60 mmscfd. Wells were shut-in or choked back starting at 1330 hours. 4. BPX reduced production rates equaling 125 mmscfd. Wells were shut-in or choked back starting at 21:54 hours. 5. Rey srz2is~ BPX FLARE REPORT PRUDHOE BAY FACILITY: CaC-3 DATE: 26 .JUG 98 • REPORT NO: J$-4426 TOTAL VOLUME: 2,261 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 09:22 To: 09:31 O Hrs. 9 Mins. ® ^ ^ ^ 94 MSCF 2. FROM: 09:32 TO: 10:31 O Hrs. 59 Mins. ^ ® ^ ^ 1,586 MSCF 3. FROM: 12:55 TO: 14:11 1 Hrs. 16 Mins. ® ^ ^ ^ 5$1 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 3°F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 4°F. 3. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 1°F. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 3 wells equating 100 mmscfd. Wells were shut-in or choked back starting at 0852 hours. 2. BPX reduced production rates and shut-in 8 wells equaling 190 mmscfd. ARCO reduced production rates and shut-in 6 wells equaling 190 mmscfd. Wells were shut-in or choked back starting at 0852 hours. 3. BPX reduced production rates and shut-in 2 wells equaling 50 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 80 mmscfd. Wells were shut-in or choked back starting at 1330 hours. 4. 5. Rev 6/22/97 • • REPORT NO: J$-4437 ~~ BPX FLARE REPORT PRUDHOE BAY ' FACILITY: GC-3 DATE: 29JUI98 TOTAL VOLUME: 1,115 MSCF Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 08:10 TO: 09:15 1 Hrs. 5 Mins. ® ^ ^ ^ 693 MSCF 2. FROM: 13:00 TO: 13:34 0 Hrs. 34 Mins. ^ ® ^ ^ 422 MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK: _ CONTROLLED SLOWDOWN: _ OTHER: _ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 3°F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 9 wells equaling 165 mmscfd. ARCO reduced production rates and shut-in 5 wells equaling 100 mmscfd. Wells were shut-in or choked back starting at 0815 hours. 2. BPX reduced production rates and shut-in 6 wells equaling 200 mmscfd. Wells were shut-in or choked back starting at 1304 hours. 3. 4. 5. Rev 6/22/97 ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition GATHERING CENTER 3 BP EXPLORATION ALASKA WESTERN OPERATING AREA-PBU Jun-98 • • Disposition 1. Sold 0 2. Reinjected 0 3. Flared or vented less than 1 hour 6,363 4. Flared or vented greater than 1 hour (Supplemental report required--See 20 AAC 25.235) 6,734 5. Pilot and Purge 20,571 6. Used for lease operations 577,923 7.Other 0 TOTAL items 1 - 7 611,591 8. NGL gas equivalent produced 0 9. Purchased gas 0 10. Transferred from: 0 11. Transferred to: CCP 24,752,801 Remarks: I hereby certify/that the foregoing is true and correct to the best of my knowledge. Signatg~./ /~ „~ /,/ ~ ~ // _~J / Title: SUPERVISOR Form 10-422 (Revised•4/95) *Indicate contribuflon of each pool to total. Pool Name Code Percent PRUDHOE 640150 100 Official Use Oni --Flatin Authorization > 1 hr. 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner llate must pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT JUNE, 1998 Unplanned Events less than ore ual to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 6/12/98 1455-1501 42 Not required for unplanned events which Not required for unplanned events whit 6/15/98 1041-1102 146 are less than or equal to 1 hour are less than or equal to 1 hour 6/15/98 2337-2359 153 6/17/98 1439-1506 563 6/17/98 2056-2126 2,042 6/18/98 2009-2028 132 6/19/98 1141-1226 906 6/22/98 1731-1813 613 6/23/98 1419-1508 749 6/24/98 1329-1407 449 6/26/98 1522-1552 438 6/30/98 1244-1301 130 TOTAL 6,363 Un tanned Events reater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELII411NATE'CAUSE 6/3/98 0833-1102 3,622 See Attachments See Attachments 6/15/98 2115-2253 681 See Attachments See Attachments 6/28/98 1840-2045 2,431 See Attachments See Attachments TOTAL 6,734 Planned Events Less Than or E ual 1 Hour AND Not Exceedin 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE TOTAL 0 • Planned Events Exceedin 1 Hour OR Exceedin 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT &' CAUSE ACTION TAKEN TO ELIMINATE CAUSE TOTAL 0 TOTAL Unplanned Events < 1 Hour 6,363 Unplanned Events > 1 Hour 6,734 Planned Events < 1 hour & not 0 exceeding 5,000 MCF Planned Events > 1 hour and 0 exceeding 5,000 MCF Pilot Purge ~4 71 TOTAL FLARED VOLUME 33,668 Page 1 • • REPORT NO: BPX FLARE REPORT PRUDHOE BAY 98-4338 FACILITY: GC-3 DATE: O3 Jun 98 TOTAL VOLUME: $,622 MSCF Intermi ttent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: O$:33 TO: 11:02 2 Hrs. 2Q Mins. ^ ® ^ ^ $,622 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEFVALVE: X RUPTUREDISK:_ CONTROLLEDBLOWDOWN: OTHER:_ First Determination of Cause: _ 1. Sk-18 compressors had to be s/d for safe-out of K307 compressor for blind to be pulled. This was necessary for the safety of the personnel involved. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Equipment was restarted at 11:02 hours. 2. 3. 4. 5. Rev 6/22/97 • REPORT NO: 9$-4347 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 15 Jun 98 TOTAL VOLUME: 980 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 10:41 TO: 11:02 0 Hrs. 21 Mins. ^ ® ^ ^ 146 MSCF 2. FROM: 21:15 TO: 22:53 1 Hrs. 38 Mins. ^ ® ^ ^ 681 MSCF 3. FROM: 23:37 TO: 23:59 0 Hrs. 22 Mins. ^ ® ^ ^ 153 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK: _ CONTROLLED SLOWDOWN: _ OTHER: _ First Determination of Cause: 1. While bringing production rates up following A-Bank start-up, LPS compressors exceeded maximum gas capacity and discharged to flare. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 3°F. 3. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 4. 5. Action Taken to Stop Flaring: 1. Equipment was restarted at 11:00 hours. C-Pad and X-Pad LDF back online. 2. BPX reduced production rates and shut-in 2 wells equaling 40 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 71 mmscfd. Wells were shut-in or choked back starting at 21:20 hours. 3. Arco reduced production rates and shut-in 1 well equaling 80 mmscfd. Wells were shut-in or choked back starting at 23:40hours. 4. 5. Rev 6/22/97 n BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 28 Jun 98 TIME OF FLARING: 1. FROM: 1$:40 TO: 20:45 2. FROM: TO: 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 2 Hrs. 5 Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. • REPORT NO: TOTAL VOLUME: Intermittent Black Yes No Smoke? Planned? ^ ® ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 98-4334 2,431 MscF VOLUME 2,431 MscF MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK: CONTROLLED SLOWDOWN: OTHER: First Determination of Cause: 1. LP compressor shutdown due to a bad vibration probe. Assist gas was added to prevent black smoke. 2. 3. 4. 5. Action Taken to Stop. Flaring: 1. Flaring was permitted to continue while GC operations personnel attempted to repair/restart the equipment. 2. 3. 4. 5. Rev 6/22/97 L ..._ _._ _.. :- •~ GATHERING CENTER 3 ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Operator Field(s) Month/Year of Disposition BP EXPLORATION ALASKA WESTERN OPERATING AREA-PBU May-98 Disposition 1. Sold 0 2. Reinjected 0 • 3. Flared or vented less than 1 hour 6,038 4. Flared or vented greater than 1 hour 33,978 (Supplemental report requved--See 20 AAC 25.235) S. Pilot and Purge 27,667 6. Used for lease operations 577,526 7.Other 0 TOTAL items 1 - 7 645,209 8. NGL gas equivalent produced 0 • 9. Purchased gas 0 10. Transferred from: 0 11. Transferred to: CCP 25,350,465 Remarks: I hereby certify that the/,foregoing is true and correct to the best of my knowledge. Signature: ~~( ~~ ~ (~, j`'~ Title: SUPERVISOR Form 10.422 (Revised 4,/95) *Indicate contribution of each pool to total. Pool Name Code Percent PRUDHOE 640150 100 Official Use Onl --F1arin Authorization >` I hr. 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner llate Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GC-3 .~ - GAS FLARING INCIDENT REPORT MAY, 1998 Unplanned Events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKENTO ELIMINATE CAUSE 5/1/98 1200-1242 242 Not required for unplanned events which Not required for unplanned events whit 5/5/98 1558-1658 792 are less than or equal to 1 hour are less than or equal to 1 hour 5/5/98 1918-1943 208 5/9/98 1627-1717 1,050 5/15/98 0015-0113 604 5/18/98 0925-0955 167 5/19/98 0005-0046 285 • 5/20/98 0519-0555 275 5/21 /98 0811-0826 105 5/21/98 2141-2216 250 5/22/98 0652-0720 156 5/22/98 0827-0906 244 5/22/98 2320-2400 280 5/23/98 0722-0735 90 5/27/98 0116-0214 1,290 TOTAL 6,038 Unplanned Events greater than 1 hour DATE TIME VOLUME DESCRIPTION OE INCIDENT & CAUSE ACTION'TAKEN TO ELIMINATE CAUSE 5/i/98 0001-0400 2,539 See Attachments See Attachments 5/2/98 0600-2238 9,356 See Attachments See Attachments 5/3/98 0200-2208 4,667 See Attachments See Attachments 5/4/98 0001-1800 9,833 See Attachments See Attachments 5/18/98 1731-1913 333 See Attachments See Attachments 5/25/98 1537-1704 7,250 See Attachments See Attachments TOTAL 33,978 Planned Events Less Than or Equal i Hour AND Not Exceeding 5000 Mcf DATE TIME VOLUME DESCRIPTION AF INCIDENT & CAUSE' ACTION TAKEN`TO ELIMINATE CAUSE TOTAL 0 Planned Events Exceeding 1 Hour OR Exceeding 5000 Mcf DATE `TIME VOt,UME DESCRIPTION`OF INCIDENT & CAUSE ACTION TAKEN 70 ELIMINATE CAUSE - TOTAL 0 Page 1 TOTAL Unplanned Events < 1 Hour 6,038 Unplanned Events > 1 Hour 33,978 Planned Events < 1 hour & not 0 exceeding 5,000 MCF Planned Events > 1 hour and 0 exceeding 5,000 MCF Pilot Purge 27.667 • TOTAL FLARED VOLUME 67,683 BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GCS GAS FLARING INCIDENT REPORT MAY, 1998 Page 2 • • REPORT NO: 9$_42$7 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 01 May 98 TOTAL VOLUME: 2781 MSCF Intermi ttent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 00:01 TO: 04:00 3 Hrs. 59 Mins. ® ^ ^ ^ 2,539 MSCF 2. FROM: 12:00 TO: 12:42 0 Hrs. 42 Mins. ® ^ ^ ^ 242 MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN: OTHER:_ First Determination of Cause: _ 1. Sk-18 LP compressor lost suction because of a problem associated with low rates. Assist gas was adde d to prevent black smoke. 2. Sk-18 LP compressor lost suction because of a problem associated with low rates. Assist gas was added to prevent black smoke. 3. 4. 5. Action Taken to Stop Flaring: 1. Flaring is intermittent. GC Operations personnel endever to resolve the problem. 2. Flaring is intermittent. GC Operations personnel endever to resolve the problem. 3. 4. 5. Rev 6/22/97 • ~ REPORT NO: 9$-4290 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: D2 May 98 TIME OF FLARING: 1. FROM: ~6:~~ TO: 22:38 2. FROM: TO: 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 16 Hrs. 38 Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ® ^ ^ ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 9,356 MscF VOLUME 9,356 MscF MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER: First Determination of Cause: 1. Sk-18 LP compressor lost suction because of a problem associated with low rates. Assist gas was added to prevent black smoke. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Flaring is intermittent. GC Operations personnel endever to resolve the problem. 2. 3. 4. 5. Rey srza~s~ • • REPORT NO: 9$-4291 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 03 May 98 TIME OF FLARING: DURATION: 1. FROM: 02:0 TO: 22:08 2~ Hrs. $Mins. 2. FROM: TO: Hrs. Mins. 3. FROM: TO: Hrs. Mins. 4. FROM: TO: Hrs. Mins. 5. FROM: TO: Hrs. Mins. Intermittent Yes No ® ^ ^ ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 4,667 MscF VOLUME 4,667 MSCF MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: _ RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. Sk-18 LP compressor lost suction because of a problem associated with low rates. Assist gas was added to prevent black smoke. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Flaring is intermittent. GC Operations personnel endever to resolve the problem. 2. 3. 4. 5. Rev 6/22/97 • REPORT NO: 9$-4292 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 04 May 98 TIME OF FLARING: DURATION: 1. FROM: 00:01 TO: 18:00 17 Hrs. 59 Mins. 2. FROM: TO: Hrs. Mins. 3. FROM: TO: Hrs. Mins. 4. FROM: TO: Hrs. Mins. 5. FROM: TO: Hrs. Mins. 9,833 MscF VOLUME 9,833 MscF MSCF MSCF MSCF MSCF TOTAL VOLUME: Intermi ttent Black Yes No Smoke? Planned? ® ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ CHECK ONE: FLARE/RELIEFVALVE: X RUPTUREDISK:_ CONTROLLEDBLOWDOWN:_ OTHER: First Determination of Cause: 1. Sk-18 LP compressor lost suction because of a problem associated with low rates. Assist gas was added to prevent black smoke. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Flaring is intermittent. GC Operations personnel endever to resolve the problem. 2. 3. 4. 5. ae~ sr2zrs~ BPX FLARE REPORT PRUDHOE BAY • REPORT NO: 9$-4296 FACILITY: GC-3 DATE: O5 May 98 TOTAL VOLUME: 1 ~QQQ MSCF Intermi ttent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 15:58 TO: 16:58 1 Hrs. Q Mins. ^ ® ^ ^ 792 MSCF 2. FROM: 19:18 TO: 19:43 0 Hrs. 25 Mins. ^ ® ^ ^ .208 MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. While bringing production rates up following F-pad s/d ,high gas transit line pressure occured. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 3°F. 3. 4. 5. Action Taken to Stop Flaring: 1. Arco reduced production rates and shut-in 8 wells equaling 200 mmscfd. Wells were shut-in or choked back starting at 14:09 hours. 2. BPX reduced production rates and shut-in 1 well equaling 25 mmscfd. Well was shut-in or choked back starting at i 9:20 hours. 3. 4. 5. Rev 6/22/97 • ~ REPORT NO: 9$-43`15 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 TIME OF FLARING: DATE: 1$ May 98 1. FROM: 09:25 To: 09:55 2. FROM: 17:31 To: 19:13 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 0 Hrs. 30 Mins. 1 Hrs. 42 Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ® ^ ® ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Btack Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 500 MSCF VOLUME 167 MSCF 333 MscF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. While bringing production rates up following K7001 shutdown for maintenance, LPS compressors exceeded maximum gas capacity and discharged to flare. 2. High D Bank 1st stage separator pressure due to bringing on production after K7001 LPS Compressor start-up. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX stopped bringing production rates up until wells unloaded and flaring was ceased. 2. Optimized production by switching flowlines to different Production Banks and switching a well to GC-1 Annex. 3. 4. 5. Rev 6/22/97 . REPORT NO: J$-4327 B PX FLARE REPORT ' PRUDHOE BAY FACILITY: GC-$ DATE: 25 May 98 TOTAL VOLUME: 7 250 MSCF Intermittent Black TIME OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 15:37 TO: 17:04 1 Hrs. 27 Mins. ^ ® ^ ^ 7,250 MSCF 2. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: 70: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED SLOWDOWN: OTHER:_ First Determination of Cause: 1. High gas transit line pressure caused by CGF compressor problems due to control techs . working on control panel. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 32 wells equaling 528 mmscfd. ARCO reduced production rates and shut-in 19 wells equaling 450 mmscfd. Wells were shut-in or choked back starting at 15:35 hours. 2. 3. 4. 5. Rev &/22/97 ALASKA OII, AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition GATT-IERING CENTER 3 BP EXPLORATION ALASKA WESTERN OPERATING AREA-PBU Apr-98 ~J Disposition 1. Sold 0 2. Reinjected 0 3. Flared or vented less than 1 hour 17,060 4. Flared or vented greater than 1 hour (Supplemental report required-See 20 AAC 25.235) 54,772 5. Pilot and Purge 25,165 6. Used for lease operations 571,225 7.Other 0 TOTAL items 1 - 7 668,222 8. NGL gas equivalent produced 0 9. Purchased gas 0 10. Transferred from: 0 11. Transferred to: CCP 24,299,030 Remarks: I hereby certify that the foregoing is true and correct to the best of my knowledge. Signature: ~`-~/'~~~%!~-t/~--~~-__ S ~ ~V Title: SUPERVISOR Fotm 10-422 (Revised 4/95) *Indicate contribution of each pool to total. Pool Name Code Percent PRUDHOE 640150 100 Official Use Onl --Flatn Authorization >'1 hr. 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner llate Note: All volumes must be corrected to pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GG3 ' GAS FLARING INCIDENT REPORT APRIL, 1998 Unplanned Events less than or equal to 1 hour ~ DATE TIME== VOLUME 'DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 4/1/98 1424-1429 35 Not required for unplanned events which Not required for unplanned events whit 4/4/98 1029-1111 583 are less than or equal to 1 hour are less than or equal to 1 hour 4/6/98 2329-2351 2,078 4/7/98 0747-0811 1,744 4/7/98 0817-0830 90 4/9/98 0847-0908 408 4/9/98 0931-0951 336 4/9/98 1454-1544 799 • 4/9/98 2225-2236 76 4/11 /98 1300-1358 181 4/11 /98 1400-1448 150 4/11 /98 1500-1544 138 4/12/98 1308-1339 431 4/17/98 1655-1723 194 4/22/98 1225-1241 333 4/22/98 1503-1527 500 4/22/98 2312-2318 347 4/24/98 0913-0946 344 4/24/98 1747-1833 7,668 4/27/98 1037-1105 292 4/27/98 1836-1908 333 TOTAL 17,060 Un tanned Events reater than 1 hour • DATE 4/1/98 TIME' 0912-1434 VOLUME DESCRIPTION OF INCIDENT!& CAUSE 2,736 See Attachments ACTION TAKEN TO ELIMINATE'CAUSE See Attachments 4/2/98 1332-1436 667 See Attachments See Attachments 4/7/98 0952-1732 2,616 See Attachments See Attachments 4/23/98 1351-1622 2,307 See Attachments See Attachments 4/23/98 2228-2400 1,278 See Attachments See Attachments 4/24/98 0000-0215 1,875 See Attachments See Attachments 4/24/98 1300-1445 583 See Attachments See Attachments 4/26/98 2115-2342 3,050 See Attachments See Attachments 4/28/98 0322-2400 9,516 See Attachments See Attachments 4/28/98 1224-1333 719 See Attachments See Attachments 4/29/98 0001-2400 13,990 See Attachments See Attachments 4/30/98 0001-0900 5,435 See Attachments See Attachments 4/30/98 1400-2400 10,000 See Attachments See Attachments TOTAL 54,772 Page 1 BP EXPLORATION (ALASKA) INC. PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT Page 2 APRIL, 1998 Planned Events Less Than or Equal 1 Hour AND Not Exceedin 5000 Mcf DATE TIME VOLUME ' DESCRIPTION OF INCIDENT'& CAUSE ACTION TAKEN TO ELIMINATE CAUSE' TOTAL 0 Planned Events Exceedin 1 Hour OR Exceedin 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION'TAKEN TO'Ei.IMINATE CAUSE TOTAL 0 TOTAL Unplanned Events < 1 Hour 17,060 Unplanned Events > 1 Hour 54,772 Planned Events < 1 hour & not 0 exceeding 5,000 MCF Planned Events > 1 hour and 0 exceeding 5,000 MCF Pilot Purge 25,165 TOTAL FLARED VOLUME 96,997 • BPX FLARE REPORT PRUDHOE BAY • REPORT NO: 98-4247 FACILITY: GC-3 DATE: 01 Apr 98 TOTAL VOLUME: 2,771 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 09:12 TO: 14:34 5 Hrs. 22 Mins. ® ^ ^ ^ 2,736 MSCF 2. FROM: 14:24 TO: 14:29 0 Hrs. 5 Mins. ^ ® ^ ^ 35 MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 10°F. 3. 4. 5. Action Taken to Stop Flaring: 1. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 2. BPX reduced production rates and shut-in 1 wells equaling 80 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 50 mmscfd. Wells were shut-in or choked back starting at 1424 hours. 3. 4. 5. I Rev 6/22/97 . • REPORT NO: J$-4248 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-$ TIME OF FLARING: DATE: Q2 Apr 9$ ~ . FROM: 13:32 To: 14:36 2. FROM: TO: 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 1 Hrs. 4 Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ^ ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 667 MSCF VOLUME 667 MSCF MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER: First Determination of Cause: 1. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 2. 3. 4. 5. Rev 6/22/97 . REPORT NO: 98-4254 B PX FLARE REPORT . ' PRUDHOE BAY FACILITY: GC-3 DATE: O7 Apr 98 TOTAL VOLUME: 4,450 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 07:47 TO: 08:11 O Hrs. 24 Mins. ^ ® ^ ^ 1,744 MSCF 2. FROM: 08:17 TO: 08:30 0 Hrs. 13 Mins. ^ ® ^ ^ 90 MSCF 3. FROM: 09:52 TO: 17:32 7 Hrs. 40 Mins. ® ^ ^ ^ 2,616 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. LPS compressor K-7001 shuf down because of a tube oil leak. 2. LPS compressor K-7001 shut down because of a tube oil leak. 3. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 18 wells equaling 250 mmscfd. Wells were shut-in or choked back starting at 0745 hours. 2. BPX reduced production rates and shut-in 18 wells equaling 250 mmscfd. Wells were shut-in or choked back starting at 0745 hours. 3. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 4. 5. Rev 6/22/97 BPX FLARE REPORT PRUDHOE BAY • REPORT NO: 98-4275 FACILITY: GC-3 DATE: 23 Apr 98 TOTAL VOLUME: 3585 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 13:51 TO: 16:22 2 Hrs. 31 Mins. ^ ® ^ ^ 2,307 MSCF 2. FROM: 22:2$ TO: 24:00 1 Hrs. 32 Mins. ^ ® ^ ^ 1,278 MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. GC-3 was s/d because of a fuel gas leak in Sk-19. Depressuring occured for safeout of piping. 2. Extended flaring event occurred while trying to restart plant after shutdown. Assist gas was used to prevent black smoke due to leaking valves. Only one well was on to pressure plant. Attempts to reduce flaring resulted in increased assist gas usage. 3. 4. 5. Action Taken to Stop Flaring: 1. None as this was necessary for the safety of the personnel and plant. 2. Flaring was permitted to continue while GC operations personnel attempted to restart the equipment. 3. 4. 5. Rev 6/22/97 • • REPORT NO: J$-4276 B PX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 24 Apr 98 TOTAL VOLUME: 10,4.70 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 00:00 TO: 02:15 2 Hrs. 15 Mins. ^ ® ^ ^ 1,$75 MSCF 2. FROM: 09:13 TO: 09:46 0 Hrs. 33 Mins. ^ ® ^ ^ 344 MSCF 3. FROM: 13:00 TO: 14:45 1 Hrs. 45 Mins. ^ ® ^ ^ 583 MSCF 4. FROM: 17:47 TO: 1$:33 0 Hrs. 46 Mins. ^ ® ^ ^ 7,668 MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER;_ First Determination of Cause: 1. Extended flaring event occurred while trying to restart plant after shutdown. Assist gas was used to prevent black smoke due to leaking valves. Only one well was on to pressure plant. Attempts to reduce flaring resulted in increased assist gas usage. 2. While bringing production rates up following plant s/d, LPS compressors exceeded maximum gas capacity and discharged to flare. 3. Extended flaring event occurred while depressuring X-pad for divert repair. 4. Gas Process upset shutdown contactors causing all process gas to flare. High pressure shutdown 2 production banks. 5. Action Taken to Stop Flaring: 1. Plant restarted after troubleshooting PLC. 2. BPX stopped bringing production rates up until wells unloaded and flaring was ceased. 3. None as this was necessary for proper safety of all maintenance workers. 4. Equipment was restarted at 18:33 hours. 5. Rev 6/22/97 • • REPORT NO: 98_4,280 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 26 Apr 98 TIME OF FLARING: 1. FROM: 21:15 To: 23:42 2. FROM: TO: 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 2 Hrs. 27 Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ^ ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 3,050 MscF VOLUME 3,050 MSCF MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER: First Determination of Cause: 1. Sk-18 LP compressor shut down because of control/instrumentation failure associated with high vibration and ground fault. Flare assist gas was added to prevent black smoke 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Flaring was permitted to continue while GC operations personnel attempted to restart the equipment. 4 of restarts attempted at 21:19, 21:27, 21:40, and 23:08. 2. 3. 4. 5. Rev 6/22/97 BPX FLARE REPORT PRUDHOE BAY REPORT NO: 9$_42$3 FACILITY: GC-3 DATE: 28 Apr 98 TOTAL VOLUME: 10,235 MSCF Intermi ttent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 03:22 TO: 24:00 20 Hrs. 3$ Mins. ® ^ ^ ^ 9,516 MSCF 2. FROM: 12:24 TO: 13:33 1 Hrs. 9 Mins. ^ ® ^ ^ 719 MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: _ RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. Sk-18 LP compressor lost suction because of a problem associated with low rates. Assist gas was added to prevent black smoke. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 5°F. 3. 4. 5. Action Taken to Stop Flaring: 1. Flaring is intermittent. GC Operations personnel endever to resolve the problem 2. Arco reduced production rates and shut-in 3 wells equaling 70 mmscfd. Wells were shut-in or choked back starting at 12:15 hours. 3. 4. 5. Rev 6/22/97 • • REPORT NO: 98-4285 BPX FLARE REPORT PRUDHOE BAY FACILITY: CaC-3 TIME OF FLARING: DATE: 29 Apr 98 1. FROM: 00:01 To: 24:00 2. FROM: TO: 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 23 Hrs. 59 Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ® ^ ^ ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 13,990 MscF VOLUME 13,990 MscF MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER: First Determination of Cause: 1. Sk-18 LP compressor lost suction because of a problem associated with low rates. Assist gas was added to prevent black smoke. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. Flaring is intermittent. GC Operations personnel endever to resolve the problem. 2. 3. 4. 5. Rev 6/22/97 ~~ BPX FLARE REPORT PRUDHOE BAY FACILITY: Ca C-3 DATE: 3O Apr 98 TIME OF FLARING: DURATION: 1. FROM: 00:01 TO: 09:00 $ Hrs. 59 Mins. 2. FROM: 14:00 TO: 24:00 1 O Hrs. O Mins. 3. FROM: TO: Hrs. Mins. 4. FROM: TO: Hrs. Mins. 5. FROM: TO: Hrs. Mins. Intermittent Yes No ® ^ ® ^ ^ ^ ^ ^ ^ ^ • REPORT NO: TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 98-4286 15,435 MscF VOLUME 5,435 MscF 10,000 MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: _ RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER: First Determination of Cause: 1. Sk-18 LP compressor lost suction because of a problem associated with low rates. Assist gas was added to prevent black smoke. 2. Sk-18 LP compressor lost suction because of a problem associated with low rates. Assist gas was added to prevent black smoke. 3. 4. 5. Action Taken to Stop Flaring: 1. Flaring is intermittent. GC Operations personnel endever to resolve the problem. 2. Flaring is intermittent. GC Operations personnel endever to resolve the problem. 3. 4. 5. I Rev 6/22/97 ALASKA OIL AND GAS CONSERVATION COMMISSION (~.pR -~ ;,~ ~~4 FACILITY REPORT OF PRODUCED GAS DISPOSITION • • Facility Operator Field(s) Month/Year of Disposition ~1~,~1 ~ C~~ ~~ S. ~L'~j~l~`,; ~.4 GATHERING CENTER 3 BP EXPLORATION ALASKA WESTERN OPERATING AREA-PBU Mar-98 Disposition *Indicate contribution of each pool to total. 1. Sold 0 Pool Name Code Percent 2. Reinjected 0 3. Flared or vented less than 1 hour 10,329 4. Flared or vented greater than 1 hour (Supplemental report required-See 20 AAC 25.235) 24,931 5. Pilot and Purge 21,932 6. Used for lease operations 482,090 7.Other 0 TOTAL items 1 - 7 539,282 8. NGL gas equivalent produced 0 9. Purchased gas 0 10. Transferred from: 0 11. Transferred to: CCP 21,621,690 Remarks: I hereby cert_ify$that~the fore oing is true and correct to/the b/est of my knowledge. Signature: J iJ ~~_~ ~~/~/9~ Title: SUPERVISOR Form 10-422 (Revised 4/95) PRUDHOE I 640150 I 100 Official Use Onl --F7atin Authorization >,'d hr. 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner llate Note: All volumes must be corrected to pressure of 14.65 psis and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. BP EXPLORATION (ALASKA) INC. ~' PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT MARCH, 1998 Unplanned Events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT&' CAUSE ACTION TAKEN TO ELIMINATE CAUSE 3/4/98 0009-0047 1,979 Not required for unplanned events which Not required for unplanned events whit 3/7/98 0720-0816 1,389 are less than or equal to 1 hour are less than or equal to 1 hour 3/9/98 1724-1738 486 3/10/98 0023-0039 167 3/10/98 0636-0720 764 3/11 /98 1801-1807 1, 080 3/12/98 2114-2136 1,640 3/14/98 0251-0317 330 • 3/14/98 2205-2216 190 3/17/98 2138-2225 400 3/19/98 1630-1646 109 3/21/98 1306-1356 63 3/22/98 1507-1541 472 3/22/98 1722-1754 347 3/23/98 1308-1352 278 3/25/98 1413-1443 104 3/25/98 1616-1634 188 3/28/98 1700-1730 260 3/31/98. 1546-1610 83 TOTAL 10,329 Un tanned Events rester than 1 hour DATE' TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 3/3/98 1723-1914 12,250 See Attachments See Attachments 3/9/98 1501-1615 1,385 See Attachments See Attachments • 3/10/98 0203-0307 1,094 See Attachments See Attachments 3/10/98 1532-1754 1,100 See Attachments See Attachments 3/19/98 1004-1140 42 See Attachments See Attachments 3/19/98 1200-1458 1,638 See Attachments See Attachments 3/20/98 0902-1006 691 See Attachments See Attachments 3/20/98 1404-1518 802 See Attachments See Attachments 3/20/98 1710-1830 650 See Attachments See Attachments 3/22/98 1226-1612 2,403 See Attachments See Attachments 3/23/98 0930-1220 1,074 See Attachments See Attachments 3/23/98 1620-1732 455 See Attachments See Attachments 3/25/98 1246-1634 508 See Attachments See Attachments 3/28/98 0940-1512 839 See Attachments See Attachments TOTAL 24,931 Page 1 BP EXPLORATION (ALASKA) INC. '' PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT MARCH, 1998 Planned Events Less Than or Equal 1 Hour AND Not Exceedin 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE TOTAL 0 Planned Events Exceeding 1 Hour OR Exceedin 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE TOTAL TOTAL Unplanned Events < 1 Hour 10,329 Unplanned Events > 1 Hour 24,931 Planned Events < 1 hour & not 0 exceeding 5,000 MCF Planned Events > 1 hour and 0 exceeding 5,000 MCF Pilot Purge 21,932 TOTAL FLARED VOLUME 57,192 Page 2 • • ~ REPORT NO: 9$_t~20'J ~- BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-$ DATE: O3 Maf 9H TIME OF FLARING: 1. FROM: 17;23 To: 19:14 2. FROM: TO: 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 1 Hrs. 51 Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ^ ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ® ^ ^ ^ ^ ^ ^ ^ ^ ^ 12,250 MscF VOLUME 12,250 MscF MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER: First Determination of Cause: 1. LPS compressor K-7000 shut down at 1722 hours because of control/instrumentation failure associated with a PLC malfunction. While troubleshooting the cause of K-7000 SD, K-7001 SD at 1740 hours. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and to all wells flowing to the LPS system. Wells were shut-in or choked back starting at 1722 hours. Extended flaring occurred at minimum LP rates in order to provide sufficient LP gas to restart the LPS compressors. At 1914 hours GC3 experienced a total plant stop production. 2. 3. 4. 5. Rev 6/22/97 • • REPORT NO: J$-4211 i B PX FLARE REPORT ' PRUDHOE BAY FACILITY: GC-3 DATE: O9 Mal' 98 TOTAL VOLUME: 1 X871 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 15:01 TO: 16:15 1 Hrs. 14 Mins. ® ^ ^ ^ 1,385 MSCF 2. FROM: 17:24 TO: 17:3$ ~ Hrs. 14 Mins. ^ ® ^ ^ 486 MSCF 3. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. LPS compressor K-7001 quit compressing gas due to a control problem which could not be found. 2. LPS compressor K-7001 quit compressing gas due to a control problem. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 13 wells equaling 150 mmscfd. Wells were shut-in or choked back starting at 15:30 hours. K-7001 was loaded up successfully, but the problem was not found. 2. Rates were not reduced. A faulty card in control panel was replaced and compressor loaded properly. 3. 4. 5. Rev 6/22/97 REPORT NO: 98-4214 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 1 O Mar 98 TOTAL VOLUME: $~ 12rj MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 00:23 TO: 00:39 O Hrs. 16 Mins. ^ ® ^ ^ 167 MSCF 2. FROM: 02:03 TO: 03:07 1 Hrs. 4 Mins. ® ^ ^ ^ 1,094 MSCF 3. FROM: 06:36 TO: 07:20 O Hrs. 44 Mins. ^ ® ^ ^ 764 MSCF 4. FROM: 15:32 TO: 17:54 2 Hrs. 22 Mins. ® ^ ^ ^ 1,1 OO MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN: OTHER:_ First Determination of Cause: 1. High gas transit line pressure caused by CGF compressor 1801 being taken out of service for maint. 2. LPS compressor K-7001 ramped down to mimimun speed because of control/instrumentation failure associated with a faulty transmitter 3. LPS compressor K-7001 ramped down to mimimun speed because of control/instrumentation failure associated with a faulty transmitter 4. While bringing production rates up following GC-3 S/D, the gas transit line pressure went high enough that it resulted in discharging to flare. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 5 wells equaling 144 mmscfd. ARCO reduced production rates and shut-in 5 wells equaling 120 mmscfd. Wells were shut-in or choked back starting at 23:30 hours. 2. BPX reduced production rates by choking back on 23 wells equaling 300 +/- mmscfd. Wells were shut-in or choked back starting at 0211 hours. 3. The faulty transmitter was replaced and K-7001 was ramped backup. 4. Arco reduced production rates and shut-in 8 wells equaling 150 mmscfd. Wells were shut-in or choked back starting at 15:47 hours. 5. Rev 6/22/97 • REPORT NO: 9$_422] BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 19 Mal' 98 TOTAL VOLUME: 1,789 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 10:04 TO: 11:40 1 Hrs. 36 Mins. ® ^ ^ ^ 42 MSCF 2. FROM: 12:00 To: 14:58 2 Hrs. 58 Mins. ® ^ ^ ^ 1,63$ MSCF 3. FROM: 16:30 TO: 16:46 0 Hrs. 16 Mins. ^ ® ^ ^ 109 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 8°F. 2. Skid 18 LP compressors started recycling light gas due to insufficient gas rates (gas rates were cut earlier due to high ambient temperatures). LP flare assist gas was opened to minimize and prevent black smoke flaring. 3. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates and shut-in 3 wells equaling 28 mmscfd. Wells were shut-in or choked back starting at 1004 hours. 2. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 3. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 4. 5. Rev 6/22/97 • REPORT NO: 9$-4230 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-$ DATE: 2O Mar 98 TOTAL VOLUME: 2,143 MSCF Intermittent Black TIM E OF FLARING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 09;02 TO: 10:06 1 Hrs. 4 Mins. ^ ® ^ ^ 69i MSCF 2. FROM: 14:04 TO: 15:18 1 Hrs. 14 Mins. ^ ® ^ ^ 802 MSCF 3. FROM: 17:10 TO: 18:30 1 Hrs. 20 Mins. ^ ^ ^ ^ 650 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER: First Determination of Cause: 1. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 2. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 3. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 4. 5. Action Taken to Stop Flaring: 1. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 2. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 3. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 4. 5. ~ Rev 6/22/97 • REPORT NO: J$-4234 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 22 Mar 98 TOTAL VOLUME: $,222 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 12:26 To: 16:12 3 Hrs. 46 Mins. ^ ® ^ ^ 2,403 MSCF 2. FROM: 15:07 To: 15:41 0 Hrs. 34 Mins. ^ ® ^ ^ 472 MSCF 3. FROM: 17:22 TO: 17:54 0 Hrs. 32 Mins. ^ ® ^ ^ 347 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 2. While bringing production rates up following P7504 Weir water pump repairs, the LPS compressor exceeded maximum gas capacity and discharged to flare. 3. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 4. 5. Action Taken to Stop Flaring: 1. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 2. BPX reduced production rates and choked back 4 wells equaling 40 mmscfd. Wells were choked back starting at 1500 hours. 3. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 4. 5. Rey si2tis~ • REPORT NO: 98-4236. B PX FLARE REPORT ' PRUDHOE BAY FACILITY: GC-3 DATE: 23 Mar 98 TOTAL VOLUME: 1,807 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 09:30 TO: 12:20 2 Hrs. 50 Mins. ^ ® ^ ^ 1,074 MSCF 2. FROM: 13:0$ TO: 13:52 0 Hrs. 44 Mins. ^ ® ^ ^ 278 MSCF 3. FROM: 16:20 TO: 17:32 1 Hrs. 12 Mins. ^ ® ^ ^ 455 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER: First Determination of Cause: 1. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 2. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 3. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 4. 5. Action Taken to Stop Flaring: 1. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 2. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 3. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 4 5 Rev 6/22/97 • • REPORT NO: 98-4238 B PX FLARE REPORT ' PRUDHOE BAY FACILITY: GC-$ DATE: 25 Mar 9H TOTAL VOLUME: 800 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 12:46 TO: 16:34 3 Hrs. 48 Mins. ® ^ ^ ^ 508 MSCF 2. FROM: 14:13 TO: 14:43 0 Hrs. 30 Mins. ^ ® ^ ^ 104 MSCF 3. FROM: 16:16 TO: 16:34 0 Hrs. 18 Mins. ^ ® ^ ^ 188 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 2. While bringing production rates up following GC3 plant shutdown, the LPS compressor exceeded maximum gas capacity and discharged to flare. 3. While bringing production rates up following GC3 plant shutdown, D-bank gas capacity exceeded maximum gas limits as the wells were unloading and discharged to flare. 4. 5. Action Taken to Stop Flaring: 1. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 2. The second LPS compressor was started 1459 hours. 3. The wells unloaded and D-bank gas capacity returned to normal operating limits. 4. 5. ae~ si2zs~ REPORT NO: 0)$_4242 r • • BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 28 Mar 98 TIME OF FLARING: ~ • FROM: 09:40 ro: 15:12 2. FROM: 17:00 To: 17:30 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 5 Hrs. 32 Mins. 0 Hrs. 30 Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ® ^ ® ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ^ ^ ® ^ ^ ^ ^ ^ ^ ^ 1,099 MSCF VOLUME 839 MscF 26O MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER: First Determination of Cause: 1. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 2. Skid 18 LP compressors started recycling light gas due to insufficient gas rates. LP flare assist gas was opened to minimize and prevent black smoke flaring. 3. 4. 5. Action Taken to Stop Flaring: 1. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 2. Gas rates were increased and Skid 18 LP compressor reloaded. The LP flare assist gas was closed. 3. 4. 5. Rev 6/22/97 ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION Facility Operator Field(s) Month/Year of Disposition GATHERING CENTER 3 BP EXPLORATION ALASKA WESTERN OPERATING AREA-PBU Feb-98 • Disposition 1. Sold 0 2. Reinjected 0 3. Flared or vented less than 1 hour 5,119 4. Flared or vented greater than 1 hour (Supplemental report required--See 20 AAC 25.235) 10,633 5. Pilot and Purge 15,822 6. Used for lease operations 523,227 7.Other 0 TOTAL items 1 - 7 554,801 8. NGL gas equivalent produced 0 9. Purchased gas 0 10. Transferred from: 0 11. Transferred to: CCP 19,962,644 Remarks: I hereby certify that the fo~regoin~g is true and correct to the best of my knowledge. Signature: „~~/~%t''~'`-~-.~_ S'" gp Title: SUPERVISOR *Indicate contribution of each pool to total. Pool Name Code Percent PRUDHOE 640150 100 Official Use Onl --Flarin Authotizafion >' 1 hr. 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner llate pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. Form 10-422 (Revised 4195) BP EXPLORATION (ALASKA) INC. • PRUDHOE BAY UNIT - GC-3 GAS FLARING INCIDENT REPORT FEBRUARY, 1998 Unplanned Events less than or equal to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 2/9/98 0750-0759 521 Not required for unplanned events which Not required for unplanned events whit 2/14/98 1943-2013 1,292 are less than or equal to 1 hour are less than or equal to 1 hour 2/24/98 0915-0949 1,771 2/24/98 1236-1307 1,535 TOTAL 5,119 Un tanned Events reater than 1 hour • DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 2!20/98 1151-1318 10,633 See Attachments See Attachments TOTAL 10,633 Planned Events Less Than or Equal 1 Hour AND Not Exceedin 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE TOTAL Planned Events Exceedin 1 Hour OR Exceedin 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE TOTAL TOTAL Unplanned Events < 1 Hour 5,119 Unplanned Events > 1 Hour 10,633 . Planned Events < 1 hour & not 0 exceeding 5,000 MCF Planned Events > 1 hour and 0 exceeding 5,000 MCF Pilot Purge 15.822 TOTAL FLARED VOLUME 31,574 Page 1 REPORT NO: BPX FLARE REPORT PRUDHOE BAY 98-4188 FACILITY: GC-$ DATE: 2O Feb 98 TIME OF FLARING: i . FROM: 11:51 To: 13:18 2. FROM: TO: 3. FROM: TO: 4. FROM: TO: 5. FROM: TO: DURATION: 1 Hrs. 27 Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Hrs. Mins. Intermittent Yes No ^ ^ ^ ^ ^ ^ ^ ^ TOTAL VOLUME: Black Smoke? Planned? ^ ^ ^ ^ ^ ^ ^ ^ ^ ^ 10,633 MscF VOLUME 10,633 MscF MSCF MSCF MSCF MSCF CHECK ONE: FLARE/RELIEF VALVE: RUPTURE DISK: CONTROLLED BLOWDOWN:_ OTHER: First Determination of Cause: 1. Asset Area TEG regeneration system shut down because a low gas alarm from a sump in same skid reboiler is located. 2. 3. 4. 5. Action Taken to Stop Flaring: 1. BPX reduced production rates by choking wells to minimum equaling 240 mmscfd. Wells were shut-in or choked back starting at 11:05 hours. Rates were cut after reboiler shutdown and flaring was started from slugcatchers to prevent shipping wet gas to CGF. 2. 3. 4. 5. Rei 6/22/97 M~ ~`~ ALASKA OIL AND GAS CONSERVATION COMMISSION FACILITY REPORT OF PRODUCED GAS DISPOSITION • (Facility GATHERING CENTER 3 (BP EXPLORATION ALASKA IFWES (TERN OPERATING AREA-PBUMonth/Year of Di Jpos98 n Disposition 1. Sold 0 2. Reinjected 0 3. Flared or vented less than 1 hour 3,320 4. Flared or vented greater than 1 hour (Supplemental report required--See 20 AAC 25.235) 458 5. Pilot and Purge 14,709 6. Used for lease operations 617,586 7.Other 0 TOTAL items 1 - 7 636,073 8. NGL gas equivalent produced 0 9. Purchased gas 0 10. Transferred from: 0 11. Transferred to: CCP 26,688,428 Remarks: I hereby certify that the foregoi is true and correct to the best of my knowledge. Signature: C!~~~'C Title: SUPERVISOR *Indicate contribution of each pool to total. Pool Name Code Percent PRUDHOE 640150 100 Official Use Onl --Flaiin Authotizafion >'1 hr.' 1. Safety MCF 2. Lease Use MCF 3. Conserv. Purposes MCF Commissioner Date pressure of 14.65 psia and to a temperature of 60 degrees F. Report due by the 20th of the month following the month of disposition. Authority 20 AAC 25.235. Form 10-422 (Revised 4/95) BP EXPLORATION (ALASKA) INC. „ ~ PRUDHOE BAY UNIT - GC-3 t GAS FLARING INCIDENT REPORT JANUARY, 1998 Unplanned Events less than ore ual to 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 1/3/98 1006-1044 924 Not required for unplanned events which Not required for unplanned events whit 1/4/98 0952-1016 267 are less than or equal to 1 hour are less than or equal to 1 hour 1/4/98 1504-1530 450 1/16/98 2245-2301 222 1124/98 0729-0737 56 1 /27/98 2304-2329 1,181 1/28/98 1424-1445 220 TOTAL 3,320 • Un tanned Events reater than 1 hour DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN TO ELIMINATE CAUSE 1/4/98 1852-2032 458 See Attachments See Attachments TOTAL 458 Planned Events Less Than or E ual 1 Hour AND Not Exceedin 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTIONTAKEN TO ELIMINATE CAUSE TOTAL 0 Planned Events Exceedin 1 Hour OR Exceedin 5000 Mcf DATE TIME VOLUME DESCRIPTION OF INCIDENT & CAUSE ACTION TAKEN70 ELIMINATE CAUSE TOTAL 0 TOTAL Unplanned Events < 1 Hour 3,320 Unplanned Events > 1 Hour 458 Planned Events < 1 hour & not 0 exceeding 5,000 MCF Planned Events > 1 hour and 0 exceeding 5,000 MCF Pilot Purge 14,709 TOTAL FLARED VOLUME 18,487 Page 1 • REPORT NO: 9$-4143 BPX FLARE REPORT PRUDHOE BAY FACILITY: GC-3 DATE: 04 Jan 98 a TOTAL VOLUME: 1 ,175 MSCF Intermittent Black TIME OF FLA RING: DURATION: Yes No Smoke? Planned? VOLUME 1. FROM: 09:52 TO: 10:16 0 Hrs. 24 Mins. ^ ® ^ ^ 267 MSCF 2. FROM: 15:04 TO: 15:30 0 Hrs. 26 Mins. ^ ® ^ ^ 450 MSCF 3. FROM: 18:52 TO: 20:32 1 Hrs. 40 Mins. ® ^ ^ ^ 458 MSCF 4. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF 5. FROM: TO: Hrs. Mins. ^ ^ ^ ^ MSCF CHECK ONE: FLARE/RELIEF VALVE: X RUPTURE DISK:_ CONTROLLED BLOWDOWN:_ OTHER:_ First Determination of Cause: 1. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 4F. 2. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 2°F. 3. High ambient temperature swings resulted in flaring and required cuts in production. Ambient temperature increased by 6°F. 4. 5. Action Taken to Stop Flaring: 1. BPX stopped bringing production rates up until wells unloaded and flaring was ceased. 2. BPX reduced production rates and shut-in 4 wells equaling 65 mmscfd. ARCO reduced production rates and shut-in 2 wells equaling 50mmscfd. Wells were shut-in or choked back starting at 15:05 hours. 3. BPX reduced production rates and shut-in 7 wells equaling 65 mmscfd. ARCO reduced production rates and shut-in 3 wells equaling 45 mmscfd. Wells were shut-in or choked back starting at 19:15 hours. 4. 5. Rev 6/22/97